IR 05000440/2021013

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Biennial Problem Identification and Resolution Inspection Report 05000440/2021013
ML22005A330
Person / Time
Site: Perry 
Issue date: 01/10/2022
From: Billy Dickson
NRC/RGN-III/DRP/B2
To: Penfield R
Energy Harbor Nuclear Corp
References
IR 2021013
Download: ML22005A330 (13)


Text

SUBJECT:

PERRY NUCLEAR POWER PLANT - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000440/2021013

Dear Mr. Penfield:

On December 14, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Perry Nuclear Power Plant and discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

January 10, 2022 No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Docket No. 05000440 License No. NPF-58

Enclosure:

As stated

Inspection Report

Docket Number:

05000440

License Number:

NPF-58

Report Number:

05000440/2021013

Enterprise Identifier:

I-2021-013-0018

Licensee:

Energy Harbor Nuclear Corp.

Facility:

Perry Nuclear Power Plant

Location:

Perry, OH

Inspection Dates:

November 15, 2021 to December 14, 2021

Inspectors:

V. Meghani, Reactor Inspector

G. O'Dwyer, Reactor Engineer

T. Ospino, Resident Inspector

R. Ruiz, Project Engineer

J. Steffes, Senior Resident Inspector

Approved By:

Billy C. Dickson, Jr., Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Perry Nuclear Power Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the Division I and II emergency diesel generators.

Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.

Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Corrective Action Program Effectiveness:

The inspectors assessed the licensees corrective action program (CAP) and its effectiveness in identifying, prioritizing, evaluating, and correcting problems. Based on the samples reviewed, the team determined that the licensees performance in these areas adequately supported nuclear safety.

Problem Identification:

Overall, the licensee effectively identified issues at a low threshold and correctly entered them into the CAP as required by Fleet procedures. The inspectors determined that the station was generally effective at identifying trends that could potentially impact nuclear safety. The inspectors also performed plant walkdowns of various areas/systems important-to-safety, including the division 1 and division 2 emergency diesel generators (EDGs) and the service water pump house. For the samples reviewed, the inspectors did not identify any regulatory issues of concern in the area of problem identification.

Regarding problem identification, the team identified three examples of the inconsistent use of the repair tag process outlined in procedure NOP-WM-1003, Nuclear Maintenance Notification Initiation and Screening, which could adversely affect the staffs ability to enter issues into the CAP appropriately. These examples included: a known minor leak on a safety-related valve which had a catch-container installed but no repair tag present; a repair tag hanging in the division 2 EDG room for a condition that maintenance staff had already fixed; and a known oil leak on the division 2 EDG starting air compressor that had no repair tag, whereas a nearly identical leak on the division 1 EDG stating air compressor had a repair tag. Although such inconsistencies are not prohibited by procedure under specific circumstances (such as a prevailing desire to preclude the tags from becoming foreign material), if prevalent, such inconsistent use of the repair tag process could result in a situation where staff may fail to enter conditions into the CAP based on assumptions made in the field that an issue may already be known and entered into the CAP when its not.

Problem Prioritization and Evaluation:

In-depth reviews of a risk-informed sampling of condition reports (CRs), work orders (WOs),and causal evaluations were completed, including a 5-year review of CAP issues and trends associated with the division 1 and division 2 EDGs. The inspectors concluded that the licensee generally prioritized and evaluated issues for resolution appropriately commensurate with their safety significance.

Corrective Actions:

The team concluded that the licensee was generally effective in developing corrective actions (CAs) that were appropriately focused on correcting the identified problem and correcting conditions adverse to quality. The team reviewed a sample of CA assignments developed for selected NRC documented violations, selected licensee event reports, licensee self-assessments, and licensee-identified issues. Based on the samples reviewed, the team determined that the licensee adequately implemented corrective actions.

Operating Experience, Self-Assessments and Audits:

The inspectors assessed the effectiveness of the stations processes for the use of operating experience, audits, and self-assessments. Based on the samples reviewed, the team determined that the licensee's performance in these areas adequately supported nuclear safety.

Safety Conscious Work Environment:

The team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed a representative cross-section of station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, workers at the Perry plant expressed freedom to raise and enter safety concerns through any of the various avenues available. The team encountered no indications of chilling or retaliation. Finally, all plant personnel interviewed were aware of the Employee Concerns Program (ECP) and expressed a willingness to use it as an avenue to raise concerns, if desired.

The team communicated two observations based on comments received during interviews.

The first observation was regarding a supervisor who expressed a lack of clear understanding concerning the initial categorization of issues as adverse to quality versus Non-adverse to quality. Although this was only one individual, given their position as a supervisor, this lack of clarity may extend to their workgroup. Additionally, a lack of clarity in this area could lead to instances where the Management Review Board is challenged as the barrier to catch potential categorization errors in condition reports. The team did not identify any such instances through its reviews. During its follow-up, the team also learned that plant leadership already knew of this topic, and actions were underway to address the categorization clarification area.

The second observation is related to a theme of comments that the team received throughout many of the interviews regarding workforce staffing levels. Specifically, the team encountered a high percentage of comments regarding workforce staffing levels being notably lower than in the past with the same amount of work existing, resulting in longer hours, more overtime, and lowering morale. Industry operating experience has shown that sustained low workforce morale and resource pressures can reduce the quality of work, which can lead to future events or challenges to regulatory limits. Additionally, such sustained pressures can exacerbate the effect of driving staff out of an organization. During its follow-up, the team recognized that this topic was already known by plant leadership and is a focus area with actions being taken. Although the inspection team did not identify any such instances of regulatory challenges, the Resident Inspectors will continue to track and monitor station performance for any potential impacts on safety margin or regulatory limits.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On December 14, 2021, the inspectors presented the biennial problem identification and resolution inspection results to Rod Penfield, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ATA-2021-4992

Pre-NRC Inspection on Problem Identification & Resolution

04/01/2021

ATL-2018-0166-

ATA-150

CR 2020-08686 will be Included in the Electrical Training

Program for Electrical Safety

2/17/2021

CA-2020-08383-

001

Label the Sewage Pump House Quincy 400 AMP Disconnect

Switch with a Warning Sign

2/16/2020

CA-2020-08383-

2

Replace the Quincy Feed Cable from Pole 9525

2/05/2021

CR-2019-01671

Main Generator/Main Turbine Trip Resulting in a Reactor

Scram

2/25/2019

CR-2019-02529

Request to Use Longer Bolt or Heli Coil to Repair

1B21F0022A Control Air Pack Mounting

03/19/2019

CR-2019-02533

B21-029B Failed Leak Rate Test

03/19/2019

CR-2019-02796

Threads Damaged During Air Blow of "C" inboard MSIV

03/25/2019

CR-2019-02861

Oil Leaking from Outboard MSIV D

03/27/2019

CR-2019-02939

Inboard MSIV 'D' 1B21F0022D Slow Speed Adjustment

Found Damaged

03/29/2019

CR-2019-03273

High Main Generator Casing Liquid Level Requires Manual Trip of Main Turbine

04/07/2019

CR-2019-05852

General Causal Evaluation for Proper Categorization of

Previous CRs and Associated Maintenance Rule Applicability

07/11/2019

CR-2020-00032

Error Identified in USAR Section 9A.4.23.5 (Unit 2 Turbine

Building Fire Hazards Analysis)

01/03/2020

CR-2020-00284

PY-PTI-R50-P0001 Portion Failure Due to E-plan 5-way

Notification Line Not Connecting to All Parties

01/15/2020

CR-2020-00611

Cause Evaluation: Issue identified with the RCIC Turbine

Mechanical Overspeed Trip While Performing Overspeed

Trip Testing

01/26/2020

CR-2020-00622

RCIC Waterleg Pump Vertical Velocity Vibration Reading is

in the Alert Range

01/26/2020

CR-2020-00623

Alarm Wouldn't Clear Div 2 DG

01/26/2020

71152B

Corrective Action

Documents

CR-2020-00843

Combustible Gas Mixing Compressor Tripped on Degraded

Thermal Overloads.

2/04/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2020-01878

Potential Past Operability Concerns with Combustible Gas

Mixing Compressor B

11/01/2019

CR-2020-02630

Drawing 302-730 has an Incorrect "Fails Open" Annotation

for Solenoid Control Valve 0G50F057 (Seal Water to Floor

Drain Filtrate Pump)

03/25/2020

CR-2020-02939

Perry 3 Minute Audible Test Not Performed Per County

Request

04/06/2020

CR-2020-03062

Emergency Notification System Phone (Red Phone) is not

Working

04/10/2020

CR-2020-03770

Div 2 DG Fuel Oil Press Low Alarm

04/28/2020

CR-2020-04340

MS-C-20-05-07: Record Copy of Work Order Missing

Signature for Submitting As-Built Drawings

05/18/2020

CR-2020-04341

MS-C-20-05-07: Record Copy of Work Order Missing

Signature for Document Verification

05/18/2020

CR-2020-04439

MS-C-20-05-07: Procedure Approval Form Administrative

Discrepancies - Maintenance

05/21/2020

CR-2020-04440

Review of 21 completed Procedure Approval Form Record

Packages (Quality Records) Identified Discrepancies

05/18/2020

CR-2020-04686

Received Aux. Building and Steam Tunnel Cooling HVAC

Trouble

05/30/2020

CR-2020-04955

Concrete Spalling and Leakage in Emergency Service Water

Pump House, 586' Elevation

06/09/2020

CR-2020-06467

ERO Drill - Unplanned Controller Injects Performed During

the 8/12/2020 Dry Run Drill

08/12/2020

CR-2020-06471

ERO-Drill: Timeliness of General Emergency Classification

During 8/12/2020 Dry Run Drill

08/12/2020

CR-2020-07230

NRC EPlan Drill - Objective F.18 Met with Comments due to

Shortfalls in Rigor Regarding Communication Standards.

09/15/2020

CR-2020-07231

Cause Evaluation: NRC EPlan Drill Objective F6 for Dose

Assessment, Not Met

09/16/2020

CR-2020-08383

General Causal Evaluation for Live Electrical Cable Identified

During Work being Performed

10/28/2020

CR-2020-08383-

ATA-01

Threat Assessment of Outbuildings for Safety Issues

03/19/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2020-09635

(MPFF) - Combustible Gas Mixing Compressor Suction

Valve Would Not Reopen Following Compressor Start

2/22/2020

CR-2021-01124

Inconsequential Latent Error Identified in Control Blade

Lifetime Monitoring Software

2/19/2021

CR-2021-01197

Weekly E-Plan Pager Test Did Not Call the Control Room

Shift Manager Notification Device

2/22/2021

CR-2021-01650

(MPFF) - RWCU Pump A and B Failed During 1R18

03/09/2021

CR-2021-01724

Monthly 5 Way Communication Test - Lake County

Equipment Deficiency Identified

03/10/2021

CR-2021-01759

Leakage Rate of 1B21F0028B Outboard MSIV Steam Line B

Exceeds Acceptance Criteria in SVI-B21-T9000

03/12/2021

CR-2021-01759

Leakage Rate Of 1B21F0028B Outboard MSIV Steam Line B

Exceeds Acceptance Criteria In SVI-B21-T9000

03/12/2021

CR-2021-02036

Chain Fall with Incorrect (Short) Pull Chain Rigged to the

Reactor Dry Tube Strong Back

03/20/2021

CR-2021-02292

Second MSIV Accumulator Supply Leaking During ISLT

03/27/2021

CR-2021-02297

SVI-B21-T9000 Step 5.3.5 Acceptance Criteria Not Met

03/27/2021

CR-2021-02894

Cause Evaluation: Reactor Water Cleanup System (RWCU)

Containment Isolation Valves (Penetration (P132)) Issues

04/14/2021

CR-2021-04817

REMP Fish Samples Lost During Transit to Offsite Vendor

06/21/2021

CR-2021-05006

Document ANS Siren L17 Out of Service

06/29/2021

CR-2021-05033

Service Water Building Intake REMP Location # 34 Water

Sampling Pump is Malfunctioning

06/30/2021

CR-2021-05353

General Cause Evaluation for CR-2021-05353, Cycle 18

Maintenance Rule Periodic Assessment Report Identifies

Potential Adverse Trend

07/13/2021

CR-2021-

054082021

DBAI POV Inspection: RCIC Steam Supply Isolation Valves

Questionable Calculation Justification

09/17/2021

CR-2021-05435

Addition - 2021 DBAI POV Inspection: JOG Classification of

RCIC Steam Supply Isolation Valves

07/16/2021

CR-2021-05580

Site Projects Exceeded Annual Dose Budget

07/22/2021

CR-2021-06362

Rad-Cal Standard for Calibrator Verification is Broken

08/23/2021

CR-2021-06976

EPLAN Drill, Near Miss with Incorrect Pager Message for

Unusual Event

09/15/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2021-07221

Hi Fuel Oil Filter Differential Pressure for Division 2 Diesel

Generator

09/26/2021

CR-2021-07223

Div 2 DG Lube Oil Strainer High DP Alarm Coming in During

DG Run

09/26/2021

Corrective Action

Documents

Resulting from

Inspection

CR-2021-09144

NRC Identified: Div 1 DG High Crankcase Pressure Trip

Valve, 1R43N0711A, Leaking from Sensing Line

2/02/2021

Commitment

Change notice

21-023

Closed Commitment L02393 and Changed TS Bases to

Remove Requirement to Restore Leakage Within 25 SCFH

When MSL Leakage Rate Exceeds 100 SCFH

Commitment

L02393

If the Leakage Rate on Any Main Steam Line Exceeds 100

SCFH, the Leakage Rate Will Be Restored to Within 25

SCFH When Tested at > = PA

OE-2020-0072-1

OE468879R20200310 Auxiliary Feedwater System Declared

Inoperable Due to Check Valve Leakage

OE-2020-0255-1

OE485135R20200918 Error in Basis for Emergency Action

Levels for Fission Product Barrier Containment

Radiation/Reactor Coolant System Activity Thresholds

Miscellaneous

OE-2020-0272-1

NRC IN 20-02, Flex Diesel Generator Operational

Challenges

NOBP-LP-2003

Employee Concerns Program

NOBP-LP-2013

Safety Conscious Work Environment Review Team

NOP-LP-2001

Corrective Action Program

NOP-WM-0001

Work Management Process

Procedures

NOP-WM-1003

Nuclear Maintenance Notification Initiation and Screening

ATA-2020-10929

Attached is the Self-Assessment for the 2020 Drill from

8/12/2020

08/12/2020

ATL-2021-0467-

ATA-01

Assessment of Current Primary Strategic Chemistry Plan

07/29/2021

ATL-2021-0521-

ATA-02

Assessment of Emergent Scope of Last Three Refueling

Outages R16, R17 and R18

08/26/2021

Self-Assessments

CR-2020-06562-

ATA-01

Engineering Change Package (ECP) Product Quality

10/22/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

MS-C-20-01-13

Audit: Design Control/Engineering Programs/ASME

03/05/2020

MS-C-20-03-01

Fleet Oversight Audit Report: Audit Area: Operations Audit

03/01/2020

MS-C-20-05-07

Maintenance/Work Management Quality Assurance Audit

6/30/2020

MS-C-20-11-24

Audit: Emergency Preparedness

2/04/2020

MS-C-21-08-03

Quality Assurance Audit Report for Radiation

Protection/Radwaste

09/23/2021

MS-C-21-09-22

21

Quality Assurance Audit Report; Corrective Action Program

10/11/2021

Work Order 200700044

Repair Oil Leak from Shaft Seal on Engine Driven Jacket

Water Coolant Pump

11/22/2016

Work Order 200784128

In 1R18, 1B21-F028B was Found to be Leaking 52.2 SLM

(110.6 SCFH)

04/01/2021

Work Order 200848877

1B21-F0028B Passed on April 1, 2021

04/01/2021

Work Order 200858837

Repair Oil Leak on Air Dryer Tower Pressure Gauge

07/09/2021

Work Orders

Work Order 200868755

Repair Fuel Oil Leak on Diesel Generator Engine Fuel Oil

Pump Mechanical Seal

11/21/2021