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 Issue dateTitleTopic
ML20006G00921 February 1990Special Rept 90-02:on 900122,plant Shutdown Initiated Due to Unidentified Leakage in Rcs.Dose Equivalent Iodine Exceeded Tech Spec Limit.Sampling & Analysis of RCS Continued at 4 H Intervals Until Iodine Decreased to Below Tech Spec LevelsUnidentified leakage
ML20006D6725 February 1990Special Rept 90-01:891228,waste Gas Decay Tank H & Oxygen Monitoring Channels Removed from Svc & Not Returned to Operational Status within 14 Days.Caused by Leakage from Fittings in Tubing.Mod Procedure Developed
ML20040F8362 February 1982Ro:On 820102,while Performing Surveillance on Power Operated Relief Valve Block Valve (RCV-11),discovered Valve Would Not Cycle to Full Closed Position.Cause Not Determined.Valve Closed Manually.Repairs Effected 820128
ML20038B5051 December 1981Ro:On 811106,during Switch from Decay Heat Removal on B Train to a Train,Approx 800 Gallons of Water from Borated Water Storage Tank Overfilled RCS & Spilled Water on Reactor Bldg Floor.Event Not Reportable Per 10CFR20.403(b)(4)
ML20011A90627 October 1981Telecopy Message of Ro:On 811027,notification Was Received That Potential High Energy Pipe Whip &/Or Jet Impingement Could Cause Possible Loss of safety-related Sys &/Or Components.Detailed Rept Will Follow within 14 Days
ML20009F97423 July 1981Ro:On 810722,during Power Escalation Following end-of-cycle Control Rod Withdrawal,Heat Balance Calculations Indicated That All Nuclear Instrumentations 5,6,7 & 8 Were Less Conservative by Amount Exceeding 0.8%
ML19350E20011 June 1981to Special Rept 80-3:on 801016,during Normal Operation,Fuse in Channel RB2 Failed,Giving 2 Out of 3 Condition Required for Actuation of Es Channel B.Caused by Failed Relay in Safeguards Cabinet 5B.Relay Replaced
ML20004G10512 May 1981Ro:On 810508,while Performing Surveillance Procedure SP-187, Auxiliary Bldg Exhaust Ventilation Sys Testing,Discovered That Three Filter Banks Had Been Inoperable Since 810505, Exceeding Tech Spec 3.7.8.1.Plant Shut Down to Hot Standby
ML19340E98012 January 1981Special Rept 80-03:on 801016,during Mode 1 Power Operation, Fuse in Channel RB2 Blew,Actuating Eecs Subsystem.Caused by Failed Relay in Engineering Safeguards Cabinet 5B.Relay Was Replaced & Functionally Tested
ML20049A33230 October 1980Ro:On 801023,reactor Bldg Exhaust Monitor RM-A1 Was Discovered Operating in Degraded Mode.Caused by Maint Action.Reactor Bldg Purge Terminated at Time of Discovery. Detailed Rept Will Follow within 14 DaysTime of Discovery
ML19340C13430 October 1980RO 80-057-01P:on 801029 Reactor Bldg Exhaust Monitor RM-A1 Discovered Operating in Degraded Mode Due to Improper Detector Installation & Valve Lineup.Detailed Rept Follows within 14 Days
ML19338G05916 October 1980Special Rept 80-2:on 800923,discovered That Fire Protection, Deluge & Sprinkler Sys Test Was Not Completed in Required Surveillance Interval.Caused by Misinterpretation.Employee Appointed to Track & Schedule Required Surveillances
ML19337B55526 September 1980Special Rept 80-1:on 800915,during Mode 1 Power Operation, Meteorological Monitoring Instrumentation Channels Were Not Restored to Operability for More than 7 Days.Caused by Const Effort Which Required Relocation of Cables
ML20049A33021 August 1980Ro:On 800821,during Surveillance of Circulating Water Discharge Temp,Temp at Point of Discharge Exceeded 103 F, Contrary to EIS 2.1.2.Cause Not Stated.Detailed Rept to Follow
ML19312D51721 March 1980Supplemental RO 80-014/04L-0:on 800221,single Measured Value of Radioactivity Concentration in Critical Pathway Environ Medium Samples Exceeded Control Station Value.Caused by Coal Slag Pile.Pile Relocation Study Underway
ML19296D3211 February 1980RO-80-004/04L-0:on 800124,seawater Samples Were Collected at Six Sample Stations But Analysis Were Improperly Performed. Caused by Malfunctions of Analysis Equipment.Seawater Samples Were Recollected & Analyzed.No Reportable Activity
ML19322A51819 October 1979Ro:On 790708,sodium Hydroxide Tank Levels Not Reported Due to Misinterpretation of Reporting Requirements.Detailed Rept Will Follow within 14 Days
ML19322A37118 September 1979RO 79-097-01P:on 790918,reactor Power Exceeded Power Level Cutoff Limit of 92%.Nuclear Instrumentation Calibr & Reactor Power Reduced.Detailed Rept Will Follow within 14 Days
ML19259D04417 August 1979Confirms Ro:On 790817,unplanned Release Occurred of Radioactive Liquid When Turbine Bldg Sump Was Pumped to Settling Pond.Health & Safety of General Public Was Not Affected.Rept Will Be Submitted within 14 Days
ML19261B97027 February 1979RO 79-013/04L-0 on 790223:water Samples Not Obtained for Jan 1979 from Test Wells 1,3 & 4,discharge Canal to North of Ponds & Waste Water Ponds.Omission Due to New Lab Director Not Being Informed of Procedure
ML19308D4807 December 1977RO-77-141E:on 770101-1031,environ Samples LLDs Exceeded ETS Requirements.Possibly Caused by Natural Activity in Sample.Analysis Procedures Being Revised Enlarging Sample Size & Counting Time
ML19308D4758 November 1977RO-77-134E:on 770101-0930,incorrect Procedure Used for Environ Sample Analysis.Caused by Inadequate Procedures, Techniques & Equipment.Procedures Being Revised to Allow Longer Count Times
ML19308D4717 November 1977RO-77-133E:on 770930-1007,air Inhalation Sample Station C41 Gross Beta Activity Exceeded Control Station Activity.Caused Control Station Activity.Caused by Fallout Due to 770919 Nuclear Weapons Test by Peoples Republic of China
ML19308D2603 October 1977RO-77-01:on 770101,wall Crack Discovered in Eight Inch Schedule 40 304 Stainless Steel Bldg Spray Pipe Inside Containment Bldg.Caused by Stress Corrosion Cracking Due to Chlorides & Oxygen.Investigation ContinuingStress corrosion cracking
ML19340A44626 September 1977RO 77-116E:on 770918,unmonitored Radioactive Release to Atmosphere Occurred.Caused by Reactor Bldg Purge Monitor RM-A1 Vacuum Pump & Monitor Alarm Indicator in Control Center Being Inoperable During 2-h & 51 Minute Purge
ML19340A42223 September 1977RO 77-117E:on 770909-10,fish Impingement on Intake Screens Exceeded Tech Specs Limit.Possibly Caused by Oil Barge Leaving Intake Canal During Survey
ML19340A42921 September 1977RO 77-110E:from Jan-May 1977,milk Samples Not Collected or Analyzed from Sample Station C-47.Caused by Assumption That Milk Need Not Be Collected from C-47 Because Milk Was Unavailable at Critical Sample Station C-49 for Comparison
ML19340A43621 September 1977RO 77-111E:on 770101-0731,environ Samples Not Analyzed Using Procedures That Provided LLDs Equal to or Less than Tech Specs Criteria.Caused by Inadequate Techniques,Procedures & Equipment to Achieve Required LLDs
ML19340A44515 September 1977RO 77-108E:on 770830-31,fish Impingement on Intake Screens Exceeded Tech Specs Limit.No Cause Given
ML19340A45215 September 1977RO 77-107E:on 770907,unplanned Radioactive Gas Release to Turbine Bldg Occurred for 12-h & 40 Minutes.Caused by Gas from Makeup Tank Leaking by Valves MUV-142 & MUV-143 to Bldg Via Vent Valve HYV-25 During Maint on Hydrogen Supply Sys
ML19308D48613 September 1977RO-77-106E:on 770830,facility Site Load Found Below 70% Level Specified in Ets.Caused by Reduced Sys Load at Night Coupled W/Necessity of Keeping Other Power Stations in Sys at Base Load
ML19308D46112 September 1977RO-77-105E:on 770901,reactor Bldg Purged Unmonitored Contrary to Ets.Caused by Failure to Ascertain Monitor Operability Prior to Purge Initiation.More Stringent Procedure Adherence Will Be Followed
ML19340A4599 September 1977RO 77-103E:on 770903,unplanned Radioactive Gas Release to Auxiliary Bldg Occurred.Caused by Concentrated Waste Storage Tanks Loop Seals Being Blown.Loop Seals re-established & Sys Mods Initiated to Prevent Future OccurrencesLoop seal
ML19340A40418 August 1977RO 77-95E:on 770728-29,impingement Sampling of Fish Discontinued Due to Excessive Seagrass Load.Caused by Large Influx of Seagrass & Algae That Clogged Intake Screens & Resulted in Removal of Collection Baskets
ML19340A46418 August 1977RO 77-96E:on 770801-02,fish Impingement on Intake Screens Exceeded Tech Specs Limit.Probably Caused by Coal & Oil Barges & Maint Dredge Entering & Exiting Intake Canal During Sampling Period
ML19308D46612 August 1977RO 77-93E:on 770729,probable Unplanned Radioactive Gas Release to Auxiliary Bldg Occurred.Caused by Blown Loop Seal on Waste Evaporator.Loop Seal re-established on Each OccurrenceLoop seal
ML19308D43711 August 1977RO-77-92:on 770717,steam Driven Emergency Pump EFP-2 Experienced Overspeed Trip on Autostart.Caused by Condensation in Steam Supply Preventing Fast Throttle Valve Closing.Drain Sys Modified & Steam Bypass InstalledOverspeed trip
ML19308D43610 August 1977RO-77-91:on 770717,reactor Coolant Dose Equivalent I-131 Level Found Contrary to Tech Specs.Caused by Expected Spikes Following Reactor Trip & Known Leaking Fuel Pins.Reactor Coolant Cleaned Via DemineralizersPower change
ML19308D4709 August 1977RO-77-89:on 770715,valve DHV-41 Failed to Open from Control Room During Cycling Surveillance Procedure.Caused by Shift in Torque Switch Setting.Torque Switch Contacts Burnished & Switch Reset
ML19308D4359 August 1977RO-77-90:on 770715,decay Heat Valve DHV-4 Failed to Open from Control Room During Quarterly Valve Cycling.Cause Not Determined.Corrective Action Will Be Initiated After Engineering Evaluation
ML19317G1928 August 1977RO-77-86:on 770712,SP-511 Acceptance Criteria Not Met by Unit 1 & 2 Batteries While in Mode 1 Operation.Caused by Recording Specific Gravity Prior to Battery Stabilization After Electrolyte Addition
ML19308D4898 August 1977RO-77-87:on 770715,containment Isolation Valve WDV-94 Failed to Operate During Quarterly Cycling Procedure SP-370. Caused by Dirty Limit Switch Contacts.Contacts Cleaned & WDV-94 Operability Restored
ML19308D4798 August 1977RO-77-88:on 770715,containment Isolation Valve SWV-47 Failed to Close During Quarterly Cycling Procedure SP-370.Caused by Loose Control Wire Connection to Limit Switch.Connection Tightened & Valve Restored to Operable Condition
ML19308D5178 August 1977RO-77-85:on 770715,methyl Iodine Removal Efficiency Found Below Tech Specs Requirements During Reactor Bldg Charcoal Filter Bank Testing.Caused by Deteriorated Charcoal Due to Site Flue Gases & Air Pollutants.Charcoal Replaced 770806
ML19317G1835 August 1977Corrected RO-77-83:on 770712,level a Channel Removed from Svc Due to Disagreement Between a & B Level Channels.Caused by Level Indication Transmitter Calibr Shift.Instrument Calibr & Channel Operability Restored
ML19317G1725 August 1977RO-77-82:on 770712,radiation Monitoring Instrumentation Functional Test SP-335 Time Exceeded Tech Spec Specified Limits.Surveillance Schedule Amended to Meet ASME Section XI Requirements & SP-335 Completed
ML19317G1865 August 1977RO-77-83:on 770712,level a Channel Removed from Svc Due to Disagreement Between a & B Level Channels.Caused by Level Indication Transmitter Calibr Shift.Instrument Calibr & Channel Operability Restored
ML19317G1895 August 1977RO-77-84:on 770713,discovered That Unit 3 Not Notified of 770706 Unit 1 & 2 Failure.Caused by Personnel Error.Tests Not Meeting Acceptance Criteria Constitute Inoperability. Personnel Instructed in Tech Spec Requirement Procedures
ML19317G2054 August 1977RO 77-81E:on 770712,discharge Point Temp Exceeded Tech Spec Limits for More than 3-h.Caused by High Intake Temp & High Power Level.Incident Revealed During 770727 Environ Data Review.Temp Increase Notification Requires Prompt Action
ML19317G2133 August 1977RO 77-80E:on 770727,unplanned Radioactive Gas Released to Auxiliary Bldg While in Mode 1 Operation.Caused by Concentrated Waste Storage Tank Blown Loop Seals.Loop Seals re-established & Storage Tank Surveillance IncreasedLoop seal