ML19308D470
| ML19308D470 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 08/09/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19308D464 | List: |
| References | |
| NUDOCS 8002280780 | |
| Download: ML19308D470 (2) | |
Text
_.
- g5)g7Eg_$ VENT REPORT
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o AME LCENSE NUMOEA WP YC lFlLlCl Rl Pl 3l l 0 l 0-l-l 0 l 0 l 0 l 0 l 0 l-l 0 l 0 l l 4l 1l1l 1l1l l0l3l 9
14 15 25 2G 30 31 32 CATECORY 77P 5o n DOCKET NUMOEA EVENT OATE AEPOAT catt O 1 CON'T l - l - l d W
l0l5l0l-l0l3l0l2l l 017 l 1 l 5 l7 l 7l l0 l8 l0 19 l 7 l 7 l 7 0 57 00 59 60 61 68 69 74 75 00 EVENT DESCRIPTION Ql During the iserformance of 'the quarterly valve cycling surveillanca procedure SP-370.
I 7 oD 80 03 l valve DHV-41 would n#ot open from the control room contrary to Tech Spec 3.6. 3.1.
l 7 89 00 Ql Redundancy NA as valve DHV-4 remained closed. Second occurrence, refer LER 77-9, l
7 89 80 gl dated 9 February 1977. Maintenance restored operability of DHV-41.
(LER ' 77-89) l 7 U9 80
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7 89 pme SO No't CIDE COMPONENT COCE mat FACnAA VOLATCN 8 Ic IP I LrJ Iv li It lv iw Ix I Ld IAi7 ln in I Luj 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION 0
l Valve DHV-41 would not open due to a shift in the torque switch settSc.
Oo The torcue l'
7 89 00 l switch vas reset to ensure opening of the valve.
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% POWER OTHER STATUS OtSCoVEAY DISCOVERY OCSCRIPTON lEl 1019l0l l NA l
lBl l
NA l
70 9
10 12 13 44 45 46 80 FORM oF ACTNITY CONTENT DELEASEo CFRELEASE[
AMOUNT OF ACTN'"v.
LoCATON OF RELEASE 12
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NA l
l NA 7 8 9
10 11 44 45 00 PERSONNEL EXPOSURES NUMBER TYPE DESCA PTCN 13 l0 l0 l 0 l l Zl l
NA l
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7 89 11 12 13 60-PERSONNEL INJunlES NUMOER DESCRIPTON l0 l0 l 0 l l
NA l*
14 7 89 11 12 80 OFFSITE CONSEQUENCES 15 l NA I
7 09 CO LOSS OR OAMAGE TO FACIUTY TYPE CESCAIPTCN bdl NA l
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7 8D 10 60 PUBUCITY 8I NA l
7 BD 00 ADDITIONAL FACTORS l'
See attached Sucoletentarv Information
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NAME:
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P. Stemrt PHONE: 0 13) 866-4159 CPO A ff I. e. r. 7
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SUPPLEMENTARY INFORMATION
- 1. Ifeport No.:
50-302/77-89
- 2. Facility:
Crystal River Unit #3
- 3. Report Date:
9 August 1977
- 4. Occurrence Date:
15 July 1977
- 5. Identification of Occurrence:
i Containment isolation valve DEV-41 would not open from the control room contrary to Technical Specification 3.6.3.1.
- 6. Conditions Prior to Occurrence:
Mod; 1 power operation.
- 7. Description of Occurrence:
I At 1400, while performing the quarterly cycling of valves surveillance procedure SP-370, 4
Decay Heat Valve DEV-41 would not_ open from the control room. Maintenance was initiated l
and DEV-41 restored operable.
- 8. Designation of Apparent Cause:
The cause of this event was due to a shift of the torque switch setting.
- 9. Analysis of Occurrence:
In the ovent of an Engineering Safeguard actuation, there were minimal safety implica-l tions as a result of this occurrence. The alternate long term cooldown path via the pressurtzer spray system was operable and available, and valve DRV-41 could have been operated at its local station, since it is located outside Containment.
- 10. Corrective Action:
i The torque switch contacts were burnished and the switch reset to ensure opening of the valve.
- 11. Failure Data:
This was the second occurrence of this event. Refer to LER 77-9, dated 9 February 1977.
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