ML19308D479

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RO-77-88:on 770715,containment Isolation Valve SWV-47 Failed to Close During Quarterly Cycling Procedure SP-370.Caused by Loose Control Wire Connection to Limit Switch.Connection Tightened & Valve Restored to Operable Condition
ML19308D479
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 08/08/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D473 List:
References
NUDOCS 8002280788
Download: ML19308D479 (2)


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[OT81 l This event was caused by a loose control wire connection to the limit switch. The

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,g l SEE ATTACHED SUPPLEMENTARY INFORMATION '

  • - M E. W. P'. Stewart [ ,, \ PHONE: 813/866-4159 0

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SUPPLEMENTARY .INFORMATION im Report No.: 50-302/77-88

2. -Facility: Crystal River Unit #3 * *
3. Report Date: 8 August 1977
4. Occurrence Date: 15 July 1977
5. Identification of Occurrence:

Containment isolation valve SW-47 inoperable contrary to Technical Specification 3.6.3.1.

6. Conditions Prior to Occurrence:

Mode 1 power operation.

7. Description of Occurrence:

At 0700, while performing the quarterly valve cycling surveillance procedure, SP-370, Nuclear Services Closed Cycle Cooling Valve SW-47 would not close from the Control s.

Room. Redundant valve SW-25 was manually closed and valve SW-47 was taken out-of-service for maintenance. Maintenance was performed restoring SW-47 operable.

8. Designation of Apparent Cause:

This event was caused by a loose wire on the limit switch.

9. Analysis of Occurrence:

There were no safety implications due to this event, as redundant valve SW-25 was utilized for containment isolation.

10. Corrective Action:

None required as normal maintensace restored operability of SW-47.

11. Failure Data:

This was the first occurrence of SW-47 failure to operate.

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