ML19308D479

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RO-77-88:on 770715,containment Isolation Valve SWV-47 Failed to Close During Quarterly Cycling Procedure SP-370.Caused by Loose Control Wire Connection to Limit Switch.Connection Tightened & Valve Restored to Operable Condition
ML19308D479
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 08/08/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D473 List:
References
NUDOCS 8002280788
Download: ML19308D479 (2)


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EVENT DESCRIPTION O2 l While performing the quarterly valve cycling procedure SP-370, containment isolation 7 89 i

g l valve SW-47 failed to close contrary to Tech-Spec 3.6.3.1.

Redundancy was maint'ained.

7 89 t

Q l with SW-25.

First time occurrence. Maintenance restored operability of SW-47.

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7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION 9

[OT81 l This event was caused by a loose control wire connection to the limit switch. The

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7 89 iG ADDITIONAL FACTORS 002 2802 P8

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SEE ATTACHED SUPPLEMENTARY INFORMATION W.

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PHONE: 813/866-4159 M E.

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SUPPLEMENTARY.INFORMATION im Report No.:

50-302/77-88 2.

-Facility:

Crystal River Unit #3 3.

Report Date:

8 August 1977 4.

Occurrence Date:

15 July 1977 5.

Identification of Occurrence:

Containment isolation valve SW-47 inoperable contrary to Technical Specification 3.6.3.1.

6.

Conditions Prior to Occurrence:

Mode 1 power operation.

7.

Description of Occurrence:

At 0700, while performing the quarterly valve cycling surveillance procedure, SP-370, Nuclear Services Closed Cycle Cooling Valve SW-47 would not close from the Control s.

Room.

Redundant valve SW-25 was manually closed and valve SW-47 was taken out-of-service for maintenance. Maintenance was performed restoring SW-47 operable.

8.

Designation of Apparent Cause:

This event was caused by a loose wire on the limit switch.

9.

Analysis of Occurrence:

There were no safety implications due to this event, as redundant valve SW-25 was utilized for containment isolation.

10.

Corrective Action:

None required as normal maintensace restored operability of SW-47.

11.

Failure Data:

This was the first occurrence of SW-47 failure to operate.

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