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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML20198H9941997-12-29029 December 1997 SE Supporting Approval of Application Re Long Island Power Authority Aquisition of Long Island Lighting Co,Subject to Discussed Condition ML20197C4771997-01-0303 January 1997 Safety Evaluation Supporting Nine Mile Point Unit 1 Reactor & Turbine Building Blowout Panels ML20197C4541997-01-0202 January 1997 Safety Evaluation Supporting Resolution of Nine Mile Point Reactor/Turbine Building Pressure Relief Panel Outside Design Basis Issue ML20056H4751993-08-27027 August 1993 Safety Evaluation Accepting Licensee Proposal for Continued Insp & Repair of Flaw in Weld Joining HPCS Nozzle Safe to safe-end Extension ML20247K2531989-09-11011 September 1989 Safety Evaluation Supporting Amends 123 & 41 to Licenses DPR-61 & NPF-49,respectively ML20247E3761989-09-0707 September 1989 Safety Evaluation Supporting Amends 122,34,143 & 40 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20248C0731989-08-0303 August 1989 Sser Accepting 880601,0909 & 890602 Changes to ATWS Mitigation Sys Actuation Circuitry for Plants ML20246L2571989-06-26026 June 1989 Safety Evaluation Supporting Amends 118,33,142 & 36 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20245J0751989-04-25025 April 1989 Safety Evaluation Supporting Amends 114,30,141 & 33 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20205R1311988-10-31031 October 1988 Safety Evaluation Supporting Amend 101 to License DPR-63 ML20205Q5721988-10-31031 October 1988 SER Re Const Mod & Licensing of Company Facility-1 Cpdf. Licensee Technically Qualified to Modify Existing Facility in Such Way as to Assure Adequate Protection of Common Defense & Security ML20205Q5761988-10-31031 October 1988 SER Re Application for CP for Alchemie Facility-2 Oliver Springs.Licensee Technically Qualified to Construct & Operate Proposed Facility in Such Way as to Assure Adequate Protection for Common Defense & Security ML20205M5731988-10-26026 October 1988 Safety Evaluation Supporting Amends 108,25,134 & 26 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20155G4801988-09-28028 September 1988 Safety Evaluation Supporting Amends 107,23,132 & 24 to Licenses DPR-61,DPR-21,DPR-65 & NPF-24,respectively ML20195G5531988-06-24024 June 1988 Safety Evaluation Accepting Proposed Reracking of Util Spent Fuel Storage Pools from Criticality Standpoint.Enrichment of Fuel to 4.5 Weight % U-235 May Be in Conflict W/ 10CFR51 Table S4 & Should Be Investigated by NRC ML20154H2171988-05-18018 May 1988 Safety Evaluation Accepting Util 880414 Submittal Re Reload Startup Physics Test Program ML20147D9631988-02-25025 February 1988 Safety Evaluation Accepting Util 860404 Evaluation of Environ Qualification of Equipment Considering Superheat Effects of high-energy Line Breaks for Plants,Per IE Info Notice 84-90 ML20147E9261988-02-23023 February 1988 Safety Evaluation Supporting Amends 100,14,125 & 15 to Licenses DPR-61,DPR-21,DPR-65 & NPF-45,respectively ML20236M9631987-11-0606 November 1987 Safety Evaluation Accepting Util Proposed ATWS Mitigating Sys Actuation Circuitry for Facilities,Per 10CFR50.62(c)(1) & Pending Final Resolution of Tech Spec Issue ML20236L2001987-10-30030 October 1987 Safety Evaluation Supporting Amends 11 to Licenses NPF-37 & NPF-66,respectively & Amend 1 to License NPF-72 ML20195G5501987-10-28028 October 1987 Safety Evaluation Accepting Proposed Reracking of Util Spent Fuel Storage Pool.Licensee May Be Required to Perform Addl Analyses to Verify Maint of Required Subcriticality If Staff Boraflex Studies Reveal Gap Development in Subj Boraflex ML20235A7331987-09-18018 September 1987 Safety Evaluation Re Installation of Alternate Rod Injection (ARI) Sys & Adequacy of Plant Reactor Coolant Recirculating Pump Trip (RPT) Sys,In Compliance W/Atws Rule 10CFR50.62. ARI & RPT Acceptable ML20195G5461987-08-21021 August 1987 Safety Evaluation Accepting Proposed Util Tech Specs Change to Increase Max Allowed Enrichment of Reload Fuel to 4.2 Weight % U-235 ML20236Y0221987-07-0808 July 1987 Safety Evaluation Clarifying Determination of Acceptability of Test Duration for Performance of Integrated Leak Rate Test at Plant ML20214M3361987-05-22022 May 1987 Safety Evaluation Supporting Util Rept Entitled, Rod Swap Methodology Rept for Startup Physics Testing ML20214M1491987-05-21021 May 1987 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 2.1 (Part 2) Re Established Interface W/Nsss or Vendors of Each Component of Reactor Trip Sys ML20153F3851987-05-0404 May 1987 SER Accepting Util 870301 & 0407 Requests for Rev to Tech Specs,Modifying MSIV Actuation Control Sys,Per IEEE Std 279 & GDC 21 ML20153F3671987-04-30030 April 1987 Safety Evaluation Accepting Util 870311 Proposed Changes to Tech Spec Tables 2.2.1-1,3.6.1.2-1 & 3.6.3-1 Re MSIV-closure Setpoint ML20238C7121987-04-0808 April 1987 Safety Evaluation Concluding That Facility May Resume Operation W/O Leakage Control Sys But w/post-accident Leakage Mgt ML20207R6481987-03-11011 March 1987 Safety Evaluation Supporting Licensee Response to Generic Ltr 83-28,Item 2.1 (Part 1) Equipment Classification.Program Acceptable ML20212J4041987-03-0202 March 1987 Safety Evaluation Re Util 831104 Response to Generic Ltr 83-28,Item 4.5.2, Reactor Trip Sys Reliability,On-Line Testing. Licensee Meets NRC Position ML20212B5671987-02-24024 February 1987 Safety Evaluation Re Util Response to Generic Ltr 83-28,Item 4.5.2, Reactor Trip Reliability On-Line Testing. Response Acceptable ML20211Q2971987-02-18018 February 1987 Safety Evaluation Re Auxiliary Feedwater Sys Reliability (Generic Issue 124) for Prairie Island Units 1 & 2 ML20211G4361987-02-14014 February 1987 Safety Evaluation Supporting Util 831110 Response to Generic Ltr 83-28,Item 4.5.2 Re on-line Testing for Reactor Trip Sys Reliability ML20153F3511987-02-0707 February 1987 Safety Evaluation Accepting Util Latest Design Mods to MSIV Actuation Control Sys,Per IEEE 279 & GDC 21 ML20210T2571987-02-0606 February 1987 SER Re Util 850802 Submittal Describing Design Details of Steam Generator Blowdown & Auxiliary Steam Sys to Detect & Isolate High Energy Line Breaks.Sys Design Acceptable, However,Two Deviations from IEEE-STD-297 Criteria Apparent ML20210R2061987-02-0606 February 1987 Safety Evaluation Supporting Util 850517,0802,0823,1211 & 860429 Submittals Re Environ Effects of High Energy Line Breaks in Auxiliary Steam or Steam Generator Blowdown Sys. Design of Blowdown Sys Acceptable ML20238C6501987-02-0505 February 1987 Safety Evaluation Accepting MSIVs for Facility Operation Up to First Refueling,Contingent on Successful Completion of Preoperational Tests & Prototype Testing Program.Briefing for Commissioner Asselstine Re MSIVs & SALP Input Also Encl ML20238C5801987-02-0202 February 1987 Safety Evaluation Concluding That Facility May Resume Startup Testing & Operation for First Operating Cycle W/ Installed Refurbished Msivs.Necessity of Addl Leak Testing to Be Determined After Review of Prototype Test Results ML20209B1511987-01-28028 January 1987 SER Supporting Util Responses to Generic Ltr 83-28,Item 4.5.2 Re Reactor Trip Sys on-line Testing ML20209C3571987-01-23023 January 1987 SER Supporting Facility Design,Per Generic Ltr 83-28,Item 4.5.2, Reactor Trip Sys Reliability,On-Line Testing ML20209C2151987-01-21021 January 1987 Safety Evaluation Re Auxiliary Feedwater Sys Reliability (Generic Issue 124) at Prairie Island Units 1 & 2.Util Actively Pursuing Improvements in Sys Reliability & Reducing Sys Challenges ML20215E0061986-12-12012 December 1986 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 2.1 (Part 1) Re Equipment Classification of Reactor Trip Sys Components ML20214J9911986-11-24024 November 1986 SER Re Conformance to Generic Ltr 83-28,Item 2.1 (Part 1) on Equipment Classification (Reactor Trip Sys Components) at Selected GE BWR Plants.Part 1 Requirements Met 1999-06-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML18040A3301998-02-28028 February 1998 Rev 0 to Technical Rept 97181-TR-03, EPR Testing of Boat Samples from Core Shroud Vertical Welds V-9 & V-10 at NMP Unit 1. 1999-09-30
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- * * "%,* UNITED STATES NUCLE AR REGULATORY COMMISSION i ,; WASMNQ TON, D. C. 20m 5., . p ENCLOSURE-1 e
SAFETY EVALL'ATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION MS!V CHANGE TO WYE-PATTERN GLOBE VALVES SUPPORTING AMENDMENT NO-----TO FACILITY OPERATING LICENSE NO.-----
NIAGARA M0 HAWK POWER CORFORATION NINE MILE POINT-UNIT 2 DOCKET NO:50-410
1.0 INTRODUCTION
Cy letter dated March 11, 1987 The Niagara Mohawk Power Corporation (NMPC, licensee) requested changes to the Technical Specifications for Nine Mile Foint Unit #2. These changes are required due to the changing cf the Main Steam Isolation Valves (M51Ys) from hydraulic actuated ball valve to air-operated Wye-pattern globe valves. By letters dated March 16 April 2, and April 28, 1987, NMPC provided additional infertnation as requested by the staff. Changes to the M31Y-closure trip setpoints in the Technical Specifications are required due to the valve change.
2.0 _ EVALUATION The M51V Wye-pattern gicbe valves function in a similar e.anner as the M51V ball valves. The new valves will close in 3 to 5 seconds in accordance with existino technical specifications. The new valves will also be actuated on the same safety related signals as presently used. NMPC has reviewed the effect on overpressurization protection analysis, LOCA analyses and transient and accident analyses due to the MS!V change to Wye-pattern globe valves. The results of the NMPC review are evaluated below.
8809070248 000010 PDR FOIA KUDLICKOO-356 PDR v o y ty r T ~
2 2.1 OvefpressurizationProtection The worst case overpressurization transient, MS!V closure with flux scram, was not affected since failure of direct position scram was assumed in the analysis. Therefore, the proposeci HSIV closure trip setpoint change in the Technical Specifications from " <6% closed" to " <8% closed" and allewable value change from " (7% closed" to "<12% closed" in RPS instrumentation setpoints have no impact on the overpressurization protection analysis.
2.2 Loss of Coolant Accident (LOCA)
The change in MS!V closure characteristics, resulting from the installation of the Vye pattern glove valves, has a negligible effect on the ECCS performance analyses as shown in Table 1. The change to Wye pattern globe valves would cause less than . degree F increase in the peak clad tenerature (PCT) for the most limiting large break and less than 2 degrees F increase for small breaks. Therefore, the acceptance criteria for emergency core cooling systems for light water nuclear power reactors as contained in 10CFR50.46 are satisfied with the globe valves in operation. The modeling of steam flow during MSIV closure remains unchanged from that is described in NE00-19329, page B-9, and has been previously found to be acceptable by the staf f.
In addition to reanalyzing the worst case breaks, the licensee assessed the impact of the change on other postulated breaks. For a recirculation line, feedwater line, or ECCS line break, MSIV closure is conservatively assumed to occur on low-low-low water level (Level 1). A scram would be expected to have already occurred on Low water level (Level 3). Thus, changing the HSly position scram setpoint has no effect on the ECCS performance analyses for these breaks since it was not utilized in these analyses.
1
3 For a steamline break inside the containment, the scram will occur on high dryvell, pressure before MSIV closure occurs. The MS!Y position scram setpoint is not used for the ECCS systen response. For steamline break outside the containeent, the analysis conservatively starts with the water level at the scram trigger point, Low water level (Level 3).
Realistically, a scran is likely tn occur earlier due to MSIV closure on high steam line flow, but this input has been conservatively omitted in the analysis. Thus, the analysis is unaffected by the MS!V position scram setpoint change.
2.3 ANTICIPATED OPERATICN OCCURRENCES The proposed change to the MSIV closure setpoint necessitated by the valve char.ge has been evaluated with respect to the transtant and accident analyses contained in the FSAR. Loss of air or nitrogen, manual closure of all MSIVs pressure regulator controller failure, and other transients and accidents were considered for any significant effect on the margin of sa fety.
The impact of a delayed scran signal due to the new MSIV closure-trip switch setroint on transients has been evaluated. The new setpoint corresponds to an analytical limit cf '85% MSIV open" insteet of the previous '90 P41V open." Two transients which take credit for this scram function are the manual closure of all main steam isolation valves (direct scram event) and the pressure regulator centroller failure (open event).
Of the two events, the manual closure is more limiting. The transient results are more sensitive (limiting) to differences in the allewable range of the Technical Specifications (3 to 5 sec.) speed of MSiv closure (which isn't being changed by this Technica! Specification change) than due to a small scram delay resulting from the setpoint change. Tiie proposed change to the Main Steam Isolation Valve-Closure setpoint was evaluated by reanalyzing the manual closure of all main steam isolation valves transient and there was no change in the critical power ratio (CPR) operating limit.
4 Another event affected by the setpoint change is load tejection without turbine bypass. This event was also reanalyzed. The change in MCPR, as showninTable1,isinsignificant(muchlessthan0.01).
The remaining existing FSAR transient analyses are based upon an analytical model that bounds the closure characteristics (flow area versus time) of either the ball or globe valves. The Wye pattern globe valves have a 10 psi higher pressure differential when full open, than the bal!
valves, due to frictional flow losses, Sensitivity studies. performed by l
GE based upon information from a number of plants have shown that the l larger aP across the steamline volume produces milder transient rNponse.
Larger steam line AP has a dampening effect on the pressure wave ,
following a closure of turbine stop or control valves. Thus, since the previous analyses are based upon a model which conservatively simulates ;
the Wye pattern valve characteristics, there is no significar,t impact on the other pressurization transients due to the HSIV change.
3.0 CONCLUSION
The preposed change to the HSIV closure setpoint in Technical Specification Table 2.2.1-1 necessitated by the HSIV change was evaluated against affected transient and accident analyses and the proposed change l
has been shown not to involve a significant increase in the probability or consequences of an accident previously evaluated. Table 3.6.1.2-1 has been changed to alter the valve designation to provide consistent notation forthetypeofvalveinstalled,e.g.,anair-operated (A0V) valve. Table 3.6.3-1 has also been changed to alter the valve designation to provide consistent notation. These changes are administrative only. For the reasons discussed in the evaluation, we find the proposed changes in Technical Specification Tables 2.2.1-1, 3.6.1.2-1, and 3.6.3-1 are acceptable.
I i
5 We have concluded, based on the considerations discussed above, that: (1) there is reasonable assurance tha- the health and safety of the public will not' be endangered by operation in the proposed manner, and (2) sucn activities will be conducted in compliance with the Comission's regulations, and issuance of this crendment will not be inimical to the I comon defense and security or to the health and safety of the public.
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6 TABLE 1 COMPARISON OF LOCA ANALYSIS BALL WYE Operating Limit (1) CPR 1.28 1.28 Limiting Transient (1)6 CPR 0.22 <0.22(2)
Safety Limit MCPR 1.06 1.06 Peak-VesselPressure(psi) 1268 1268 Allow >1e Pressure (psi) 1375 1375 Large Break PCT ( F) 1921 1922 g Small Break PCT ( F) 1522 1524 Allowable PCT (*F) 2200 2200 I
(1) Load rejection without bypass Section 15.2.2 (2) Slightly less due to 10 psi higher a P across Y valves COMPARISON OF TRANSIENT ANALYSIS l
BAlu WYE l
Operating Limit CPR 1.28 1.28 HSIV Closure Event (l' 4)
(15.2.4)(3) A CFFs 0.01 <0.01 Safety Limit MCPR 1.06 1.06 Peak Vessel Pressure (psi) 1268 1271 Allowable Pressure (psi) 1375 1375 (1) Only event affected by setpoint change (2) LoadrejectionwithoutbypassSection15.2usingODYNOptionA (3) Slightly less due to 10 psi higher a P across Wye type valves (4) No change in Limiting Transient
. .I ENCLOSURE 2
, SALP EVALUATION - NMPC Functional Areas
- 1. Management Involvement The submittal required additional information to permit approval Rating: Category 2
- 2. Resolution of Technical Issues The initial submittal showed insufficient understanding of the technical l issues involved.
Rating: Category 2
- 3. Responsiveness to NRC Initiatives Responses to questions were fully acceptable,
.: ting: Category 2
_a