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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML20198H9941997-12-29029 December 1997 SE Supporting Approval of Application Re Long Island Power Authority Aquisition of Long Island Lighting Co,Subject to Discussed Condition ML20197C4771997-01-0303 January 1997 Safety Evaluation Supporting Nine Mile Point Unit 1 Reactor & Turbine Building Blowout Panels ML20197C4541997-01-0202 January 1997 Safety Evaluation Supporting Resolution of Nine Mile Point Reactor/Turbine Building Pressure Relief Panel Outside Design Basis Issue ML20056H4751993-08-27027 August 1993 Safety Evaluation Accepting Licensee Proposal for Continued Insp & Repair of Flaw in Weld Joining HPCS Nozzle Safe to safe-end Extension ML20205R1311988-10-31031 October 1988 Safety Evaluation Supporting Amend 101 to License DPR-63 ML20153F3851987-05-0404 May 1987 SER Accepting Util 870301 & 0407 Requests for Rev to Tech Specs,Modifying MSIV Actuation Control Sys,Per IEEE Std 279 & GDC 21 ML20153F3671987-04-30030 April 1987 Safety Evaluation Accepting Util 870311 Proposed Changes to Tech Spec Tables 2.2.1-1,3.6.1.2-1 & 3.6.3-1 Re MSIV-closure Setpoint ML20238C7121987-04-0808 April 1987 Safety Evaluation Concluding That Facility May Resume Operation W/O Leakage Control Sys But w/post-accident Leakage Mgt ML20153F3511987-02-0707 February 1987 Safety Evaluation Accepting Util Latest Design Mods to MSIV Actuation Control Sys,Per IEEE 279 & GDC 21 ML20238C6501987-02-0505 February 1987 Safety Evaluation Accepting MSIVs for Facility Operation Up to First Refueling,Contingent on Successful Completion of Preoperational Tests & Prototype Testing Program.Briefing for Commissioner Asselstine Re MSIVs & SALP Input Also Encl ML20238C5801987-02-0202 February 1987 Safety Evaluation Concluding That Facility May Resume Startup Testing & Operation for First Operating Cycle W/ Installed Refurbished Msivs.Necessity of Addl Leak Testing to Be Determined After Review of Prototype Test Results ML20238C1331986-10-27027 October 1986 Safety Evaluation Accepting Refurbished MSIVs for Plant Use Up to First Refueling,Contingent on Prototype Test Performance.Conditions Stated ML20238C1161986-10-22022 October 1986 Safety Evaluation Supporting Schedular Exemption from GDC 54 & 55 Re MSIV Operability to Permit Fuel Load.Salp Input Also Encl ML20153F6291986-08-27027 August 1986 Safety Evaluation Concurring W/Applicant 860703 Exemption Request Re Testing of 16 Relief Valves,Per 10CFR50,App J ML20197C0511978-10-27027 October 1978 Safety Evaluation Rept Supporting Amend 1 to CPPR-112 ML20244E2701974-11-15015 November 1974 Suppl 1 to AEC SER Re Licensee Conversion from Provisional OL to full-term OL for Util 1999-06-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
[Table view] |
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f NUCLEAR REGULATORY COMMISSION 5 WASHINGTON, D. C. 20666
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT N0. 101 TO FACILITY OPERATING LICENSE NO. DPR-63 ,
t l NIAGAPA MOHAWK POWER CORPORATION NINE MILE POINT NUCLEAR POWER STATION, UNIT NO. 1 DOCKET NO. 50-200 l INTRODUCTION i
in a letter dated March 7.1988, the licensee requested Technical Specifications i Sections 3.1.2 and 4.1.2 be revised for the liquid poison system to incorporate :
changes reouired by 10 CFR Part 50.67. "Requirements for reduction of risk from :
anticipated transients without scram (AT*ds) events for light-water-cooled :
! nuclear power plants." Specifically, the proposed changes would-(1) delete ;
) Fiqure 3.1.?a; (2) identify the liquid poison system minimum volume requireNnts; i
- (3) incorporate the equivalency equation for detkrmining the concentration of .
I sodium pentaborate solution enriched in the boron-10 isotope; (4) revise Figure !'
j 3.1.2b to allow a lower concentration of sodium pentaborate as a result of
) using the enriched isotope; and (5) revise Technical Specification 4.1.2b to j j incorporate additional surveillance requirements for monitoring the enriched +
! boron-10 isotope concentration. The Pases for Technical Specification Sections ;
l 3.1.2 and 4.1.? would also be revised to incorporate the equivalency equation !
. and to remove the reference to the maximum in,iection time and revise the !
! minimum in,iection time. The deviations from 10 CFR Part 50.6?(c)(4) associated i with the Technical Specification changes are identified in an exemption request i dated September 14, 1988. The discussion of the exemption rtyuest is included as !
i part of this Safety Evaluation. l t
I !
EVALVATION l The exemption proposed by the licensee has been reviewed by the staff against i
the requirements of the Anticipated Transient Without Scram (ATWS) rule i
! (10 CFR Part 50.62) and Generic letter No. 85-03 "Clarification of Equivalent i
! Control Capacity for Standby Liouid Control Systems." dated January 28, 1985. -
i The licensee's proposed consideration of the 213-inch diameter vessel size in 6 j detennining an equivalent control capacity will provide a bnron cMtent !
. ecuivalent in control cacacity to 86 gpm of 13 weight percent sodium :
! pentaborate for a 251-inch inside diameter vessel. This meets the intent of j 10 CFR Part 50.62 and is, therefore, acceptable. Granting of this Exemption j orovides iustification for certain of the TS changes identified in the ;
amendment request. j I
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l 1 8S11090455 881031 !
4 PDR ADOCK 03000220 l
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l I The liquid poison system is a backup to the Control Rod Drive System. When a 4 scram signal occurs, the control rods are automatically inserted to bring the reactor to a suberitical condition. In the event the control rods would fail ;
i to insert, the liquid poison system is designed to in.fect a sufficient quantity of soluble boron to bring the reactor to a hot suberitical condition. The liquid noison system at Nine Mile Point tinit 1 (NMP-1) performs the function of the standby liquid control system (SLCS) required by Paragraph (c)(4) of 10 CFR 50.6? which states, in part: ,
"Each boiling water reactor must have a standby liquid control system
- (SLCS) with a minirum ficw capccity and boren content equivalent in control capacity to 86 gallons per minute of 13 weight parcent sodium penta > orate solution."
i Generic letter 85-03, dated January 28, 1985, stated that the equivalent boren '
content could be achieved by increasing the flow rate, or the boron concentrath, i or through boron enrichment. These methods of meeting the requirements of 10 t CFR 50.62 were also evaluated in the staff's review of NEDE-31096-P "Anticipated 1 Transients Without Scran: Ferponse to ATWS Rule 10 CFR 50.62 " (G. Lainas to l
T. Pickens, October 21,1986). The staff's evaluation of NEDE-31096-P also ,
i discussed an equivalency equation which could be used to ensure that the SLCS has a control capacity eouivalent to 86 GPM of 13 weight percent natural sodium :
4 pentaborate solution.
l In its application dated March 7, 1988, the licensee requested that the Technical l Specifications for NMP-1 be revised to incorporata the following ecuivalency h
- equation which was discussed in the sta#f's evaluation.
I O x M251 x Cx E >1 ,
Fi T -~ T3 17"3 -
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]
whera: 0
- expected Liouid Poison tystem flow rate (30 GPM)
M = mass of water in the re6ctor vessel and recirculation :
J system at het rated conoitions (501,500 lbs.)
! C = sodium pentaborate soh ; ion concentration, weight percent t 4 E = boron-10 isotope enrichfient (10.8% for natural boron), [
- atom percent M251 = mass cf water for 251-inch reference plant (628,300 lbs ,
! The licensee has proposed to meet the eouivalency equation by using appropriate l l combinations of solution concentration and boron-10 enrichment. j
! i The licensee has indicated that the enriched boron would be supplied premixed ;
! by its vendor. On April 13, 1088 the licensee supplewented its amendnent i application with a letter comitting to revise the applicable site procedures ,
j to require an isoteoic analysis of the enriched sodium pentaborate to be ,
performed by an independent laboratory. In addition, the licersee's amendment :
} application of Farch 7,198A included surveillance recuirements to verify !
conformance with the equivalency equation any time boron or water is added or f 1 if the solution tenperature drops below the limits specified by Fiqure 3.1.?b, .
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- - -. -, . - -- = - . - . __ __ _ - . - - - _ . - .
l
. 1 3
- and to verify enrichment by analysis once per operating cycle. The staff finds l i
the proposed surveillance requirements and the licensee's comitment to have an l independent verit{ cation to be adequate assurance that the licuid poison system :
! will meet the requirements of the St.CS required by 10 CFP 50.6?. j With the use of the equivalency equation, the effective rate of boron in.iection
< product of pumping capacity (flow rate), solution l l
concentration, boron (Rintothecorewillbetg1 enrichment,andmixinocapacity. Previously conducted L mixing tests were accepted by the NRC staff and, as a result, boron abing is not '
o a factor in determining equivalency to the ATWS rule. By meeting the equivalency i
equation, the licensee will ensure that sodium pentaborate is iniected at a rate eouivalent to 13 weight percent at 26 GPM. As the rate of infection will be ;
onverned by the eouivalency equation and boron mixing is not a factor, the minimum and maximum in.iection times need not be reviewed by the staff. Therefore, the deletion of the maximum mixino time and the revision to the minimum mixing time !
in the Bases is acceptable. l f
Figure 3.1.2a of the Technical Specifications specified the volume-concentration l
- limits of the liquid poison system. This curve is applicable for natural ;
- (unenrichedi boron. These limits will now be determined by the use of the
- equivalency equation and therefore, deletion of Figure 3.1.2a of the Technical Specifications is acceptable. l 1 l 1 Fioure 3.1.2b of the Technical Specifications specified the minimum allowable 1
solution temperature 'or a specified weight percent of sodium pentaForate in ,
solution. This curve was being revised to include the lower weight -:rcent o' '
sodium pentaborate allowed by the ecuivalency equation. However, the licensee !
did not address the potential for freezinq at the lower terperatures (30*F) !
represented on the new curve, in addition, during a discussion with Mr. Peter j j Francisco of the licensee's staff on June 23 loa 8, Mr. Francisco indicated :
f that the curve was erroneously shifted in the non-conservative direction. !
( Pr. Francisco further indicated that operation with the equivalency equation j with the existing Fioure 3.1.2b would be acceptable. The use of the existinq !
i fioure for the minimum allowable solution temperature would not ha affected by {
- the use of the equivalency equation. Therefore, the staff firds the proposed r
! revision to Fiqure 3.1.2b to be unacceptable and the licensee has aareed that "
- chance will be deleted from the proposed revision to the Technical Specifications. !
! This change did rot alter or affect the action noticed or the staff's initial !
j determination published in the Federal Degister on June 1,1988.
l
} On the basis of the above discussion, the staff finds that the licensee's !
changes to the Technical Specification and the Rases for the liquid poison l 1 system as proposed in fts application of Parch 7, 1988 with the exception as ;
- modified, are acceptable and are consistent with the purpose of 10 CFR Part
1 50.6? for the St.CS. ,
i l !
ENVIRONMENTAL CONSIDEPATION
! This anendment involves a change in the installation or use of the facility l l components located within the restricted areas as defined in 10 CF'l Part 20 and l j changes inspection or surveillance requirerents. The staff has determined that l j this amen &ent involves no sionificant increase in the amounts, and no sicnificant ;
i -
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. - _ . . - - - . - - - - --.._.- - -- . ~ - _ _ - _ - - - - - _ _
- _ _ - _ _= - _ .-- __ ___
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4 change in the types, of any effluents that may be released offsite and that there I is no significant increase in individual or cumulative occupational radiation '
exposure. The Comission has previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public coment on such finding. Accordingly, this 6mendment meets the eligibility ,
criteria for categnrical exclusion set forth in 10 CFR Sec 51.22(c)(9). Pursuant !
to 10 CFR Sec. 51.22(b) no environmental irrpact statement or environmental assessment need be prepared in connection with the issuance of this amendment.
1 CONCLUSION, On the basis of the above evaluation the staff finds that the licensee's proposed exemption from 10 CFR Part 50.62(c)(4) as requested in the submittal dated Septernber 14, 1988 is acceptable. Thereafter, the licensee shall comply t
with the provisions of such rule or renew its request for exemption.
! We have concluded, based on the considerations discussed above, thn: (1)there !
15 reasonable assurance that the health and safety of the public will not be l' endangered by operation in the proposed manner, r.nd (2) such activities will be conducted in compliance with the Comission's regulations and the issuance .
l of these amendments will r.ot be inimical to the corinon defense and security or 1 to the health and safety of the public.
i i Dated: October 31, 1988 1 PRINCIPAL CONTRIBUTOR:
N haughey 4 :
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