ML20054L144
ML20054L144 | |
Person / Time | |
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Site: | Indian Point |
Issue date: | 06/21/1982 |
From: | Otoole J CONSOLIDATED EDISON CO. OF NEW YORK, INC. |
To: | Haynes R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
References | |
NUDOCS 8207070186 | |
Download: ML20054L144 (1) | |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20096H2301992-05-21021 May 1992
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Text
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John D. OToois v<e P esent Consok1ated Edison Company of New York. Inc 4 Irving Place, New York, NY 10003 Tefechone (212) 460 2533 June 21, 1982 l
)
Re:
Indian Point Unit No. 2 2
Docket No. 50-247 1
I t
i Mr. Ronald C. Haynes Regional Administrator - Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King Of Prussia, PA 19406 i
Dear Mr. Haynes:
In accordance wi t'i Technical Specifications 3.13.A.2 and 6.9.2.d, the following rerart regarding an inoperable motor-driven fire pump is being submitted.
On May 20, 1982 at 8:00 AM, No. 12 Fire Pump was removed from service to repair a leaking packing gland.
Subsequently, it was determined that the pump required overhaul and the pump was overhauled.
Following the completion of the
- work, a
post-maintenance test was performed which revealed leaks in the packing material.
The leaks were repaired.
The post-maintenance test was repeated with satisfactory results.
The pump was returned to service at approximately 3:00 PM on May 27, 1982.
Should you or your staff have questions, please contact us.
Sin erely, TY js y cc: Mr. T. Rebelowski, Resident Inspector U. S. Fuclear Regulatory Commission Post Office Box 38 Buchanan, N. Y.
10511 B207070186 820621
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