Similar Documents at Hatch |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
[Table view] |
Text
. .' . Georgia Power Company 00 invernes Center Parkway -
Post Offse Box 1295 E -
Birmingham, Alabama 35201 p Telaphone 205 877 7279 m
J. T. Dockham. Jr.
Vice President - Nuclear Geoi$tt Potver Hatch Proioct the sout'>em ekt??c system July 9, 1993 Docket No. HL-306 50-321 005007 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Edwin I. Hatch Nuclear Plant Licensee Event Report Instrument Isolation Valve Packing Leak Results in an Automatic Scram Gentlemen:
In accordance with the requirements of 10 CFR 50.73(a)(2)(iv), Georgia-Power Company is submitting the enclosed Licensee Event Report (LER) concerning an instrument isolation valve packing leak which resulted in an.
automatic reactor scram. This event occurred at Plant Hatch - Unit 1.
Should you have any questions in this regard, please contact this office.
Sincerely, N
. T. Beckham, Jr.
JKB/cr
Enclosure:
LER 50-321/1993-012 cc: Georaia-Power Company Mr. H. L. Sumner, General Manager - Nuclear Plant NORMS U.S. Nuclear Reaulatory Commission. Washinaton. D.C.
Mr. K. Jabbour, Licensing Project Manager - Hatch U.S. Nuclear Reaulatory Commission. Reaion Il Mr. S. D. Ebneter, Regional Administrator Mr. L. D. Wert', Senior Resident Inspector - Hatch 9307210210 930709 7A fj PDR ADDCK 05000321 S PDR ,
_. a
m 400 U.5. hJLLLAd kt(niLAidk! LUPfuh510h AFP i 50-0104 p
LICENSEE EVENT REPORT (LER)
FAllLily NAML (1) UULALI hbMbik (2) FW fan PIANT E. I. HATCH, UNIT 1 05000321 1 0F I 9 TilLE (4)
INSTR 1 RENT IS01ATION VALVE PACKING IEAK RESULTS IN AN AUlOMATIC REACIOR SCRAM EVEhI DATE (5) LER h0MBER (6) REFORT DATE (7) OlHER FACILillE5 INVOLVED (8)
MONTH DAY YEAR YEAR SEQ hum REV MONTH DAY VEAR FACILITV NAMES DOCALT huMBER(5) 05000 06 15 93 93 012 00 07 09 93 05000 OPERATING MODE (9) 1 20.402(b) 20.405(c) ^ 50.73(a)(2)(iv) 73.71(b)
POUER -
20.405(a)(1)(1) -
50.36(c)(1) -
50.73(a)(2)(v) -
73.71(c)
LEVEL 100 20.405(a)(1)(ti) 50.36(c)(2) 50.73(a)(2)(vii) OTHER (Specify in 20.405(a)(1)(iii) 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) Abstract below) 20.405(a)(1)(iv) -
50.73(a)(2)(li) -
50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICEN5E E CONTACT FOR Th15 LER (li)
NAME TELEPHONE NUMBER 4REA CODE STEVEN B. TIPPS, MANAGER NUCIEAR SAFETY AND COHPLIANCE, HATCH 912 367-7851 COMPLETE ONE LINE FOR EACH F AILURE DESCRIBED IN THI5 REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC- P0RT CAUSE SYSTEM COMPONENT MANUF C- R PORT TUR ppg X JA ISV D232 YES SUFFLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR SUBMISSION DATE (15)
] YES(If yes, complete EXPECTED SUBMISSION DATE) ] NO AB5 TRACT (16)
On 6/15/93, at 1453 CDT, Unit 1 was in the Run mode at a power level of 2436 CMWT (100 percent of rated thermal power). At that time, an automatic reactor scram and isolation of the inboard Group 2 Primary Containment Isolation System (PCIS) valves occurred due to a false low reactor water level signal. Control rods fully inserted as designed. As expected, actual water level decreased immediately following the scram, reaching a minimum level of 34 inches below instrument zero (124.5 inches above the top of the active fuel). At approximately 10 inches above instrument zero, an actuation of the outboard PCIS occurred on an actual low water level condition. The Reactor Feedwater Pumps (RFPs) responded to the actual low level condition and restored water level. No Emergency Core Cooling Systems actuated as a result of the low water level condition, nor were they required to actuate. Reactor pressure decreased as a result of the scram and was then controlled by the Turbine Bypass Valves at approximately 920 psig. Due to misleading level indications, level increased above the bottom of the Main Steam Lines, resulting in water intrusion into the lines.
The cause of the event was a loose packing nut on an instrument isolation valve becoming disengaged during an instrument calibration. This ultimately resulted in depressurization of the sensing line and a false low reactor water level signal. Corrective actions include repairing the valve, checking other similar installations on both units, performing a walkdown of system piping, and analyzing the effect of water in the Main Steam Lines.
mm u.s. muum iu mum umawn ung g g y ows
" LICENSEE EVENT REPORT'(LER)
TEXT CONTINUATION FACILITY*NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE-(3)
YEAR SEQ hum REV PIANI E. I. HATQi, UNIT i 05000321 93 012 00 2 or 9 TEXT PIANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor Energy Industry Identification System '!
Codes are identified in the text as (EIIS Code XX).
DESCRIPTION OF EVENT On 6/15/93, at 1453 CDT, Unit 1 was in the Run mode at a power level of 2436 CMWT (100 percent of rated thermal power). At that time, an automatic reactor scram and automatic isolation of the inboard Group 2 Primary Containment Isolation System (PCIS, EIIS Code JM) valves occurred due to a false low reactor water level signal. >
L Calibration of reactor water level instrument 1B21-N093B was in progress at the time of the scram. 'This level transmitter providesLa trip signal to the Eigh .
- Pressure Coolant Injection System (HPCI, Ells Code BJ) on a high reactor' water
--level condition. The Technical Specifications require the calibration at Lleast once per 18 months. When the'nonlicensed Instrument.& Controls (I&C) technician I performing the calibration attempted to close a 3/8 inch' instrument sensing line isolation valve, the packing nut came off the valve bonnet upon contact with the !
-stem handle. Subsequently, the packing gland and packing material partially came out of the bonnet resulting in a substantial bonnet leak which partially :
depressurized the instrument line.
This instrument line is a variable, or low pressure-leg, serving various level transmitters that provide input to the Reactor Protection System (RPS, EIIS Code JE), the PCIS inboard valves, Reactor Water Level Indicators 1B21-R606A and C, i the "A" subsystem of the Feedwater level Control System (FWLC, EIIS Code JK),.as !
well as other systems. Consequently, when the instrument line depressurized, a ;
false low water level was sensed by these instruments, resulting in the reactor-scram, automatic isolation of the inboard PCIS valves, and a false low level i indication on Main Control Room indicators 1B21-R606A and C. The FWLC. System 'I was in ."B" control at the time and, . therefore,- was not affected by the false - '
signal.
The control rods fully inserted as designed. As expected, immediately following l
.the scram, reactor water level decreased due to void collapse in the. reactor- ,
coolant. The minimum water level reached during the transient was 34 inches below instrument zero (124.5 inches above thel top of the active fuel) before- -
level was' recovered by the Reactor Feedwater Pumps (RFP,.EIIS Code SJ). During' '
the level transient, at approximate 1y'10 inches'above instrument zero, the PCISL received a second automatic. isolation' signal on an actual' low' level condition, i resulting in closurelof the outboard PCIS valves.
It is apparent that following the initial.depressurization of the instrument i line, the packing partially sealed off the: bonnet leak. As.a consequence, the :
line7 partially repressurized, resulting in the associated level instruments l'
. tracking reactor water level at lower than actual level. Specifically, Reactor Water Level Indicators 1B21-R606A and C indicated a lower than actual level, and :
level instruments IC32-N004A and C, which input to the "A" subsystem of.FWLC ,;
and/or the Main Turbine and the RFP trip system, were also sensing a lower than '!
r , ,
p JetA U.S. NUM.LAR HLUULMUU umbblUN Mt 104 LICENSEE EVENT REPORT (LER)-
TEXT CONTINUATION FACILITY NAME (1)' DOCKET NUMBER (2) LER NUMBER (5) PAGE (3)
VEAR SEQ hum REV PIMI E. I. HAIUI, UNIT 1 05000321 93 012 00 ~3 0F 9 IEXT actual level. The magnitude of this discrepancy between actual-and sensed level varied during the event.
During recon ry of reactor water level, RFP "B" was secured per procedure to-preclude overfilling the reactor vessel. Level continued to increase, and RFP-
"A" and the Main Turbine tripped on a high reactor water level condition. The actual level at the time of the trip was approximately 68 inches:above instrument zero. The trip setpoint is 54 inches. The delay in the trip system
-actuation was due to level instruments 1C32-N004A and C sensing reactor. water-level approximately 14 inches lower than actual due'to the partially depressurized sensing line.
When sensed water level decreased below the high level trip setpoint, RFP "A" was restarted and placed in automatic level control, aligned to the "B" subsystem of the W LC system. The "B" subsystem of WLC is' served by a separate instrument sensing line and, therefore, was not'affected by the failed instrument line. Consequently, WLC was sensing an actual high reactor water -
level condition, resulting in RFP "A" running on minimum flow and not injecting _
into the reactor vessel, i a
Reactor' pressure initially decreased to approximately 757 psig as a result _of ,
the scram and was then controlled by the Turbine Bypass Valves (TBV) at approximately 920 psig.
i Licensed operators, in responding to the event, monitored reactor water level. l They were aware of a problem associated with a "B" level instrument during -
y calibration that ultimately caused the scram. However, the affected instrument line was unknown and, therefore, the impact of the condition on their instrumentation was also unknown. Reactor Water Level Indicators 1B21-R606A and ;
C appeared to be tracking level after the scram, and Reactor Water Level Indicator 1B21-R606B was'off scale high. The high end of the' scale is 60 inches above instrument'zero. -Licensed operators concluded from the displayed-level l indications that the "B" indicator had failed upscale as a result of the failed l sensing line and that the "A" and "C" indicators were accurately displaying l level.
The level instruments that provide input to the WLC System "B" control are served by the same sensing lines that provide input.to the "B" Reactor Water Level Indicator. Consequently,.the operators, questioning the accuracy of the "B" Reactor Vater Level instrumentation, transferred the WLC System from.."B"- y control to "A" control. The RFP was then being controlled by the "A" WLC subsystem and periodically injected. into. the reactor-vessel as a result of the sensed false low water level. Control room personnel believed at this point
.that reactor water level was being maintained.within an acceptable band by the RFP. 'In actuality, reactor water-level was high and continued to increase each time RFP "A" injected.
During this time, support personnel,. in conjunction with some of the shift personnel, were investigating the cause of the scram. At approximately 1520 CDT, they determined that the depressurized instrument sensing line served the i
- . _ _ _ _ _ _ _ - _ _ - - _ _ ______---.____.___________m.u_________.___-._________.____m_____-.m ______.-_a-__m________-u
U.5 Ni.0LLAR KLCAARMI u7Filbh10N - NTMunu WB 10 J150-0104 gun,, Form J0tA (6-89)c 'i LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY.NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) [
~
YEAR SEQ hum REV PIANI E. I.1%IQi, UNIT 1 05000321 93 012 00 4 0F 9 TEXT-
"A" and "C" Reactor Water Level Indicators ~and not the "B" indicator. -
Therefore, they. questioned the accuracy of the "A" and "C" indicators At that l point, the "A" and "C" indicators were displaying a level of approximately 28 ,
inches above instrument zero, but the actual level was approximately 121 inches' above instrument zero, as indicated by the floodup range instrument. .
-j Consequently, actions were taken to lower level. RFP "A" was secured,.and thef Reactor Water Cleanup System was aligned to the Main Condenser in order to ,
lower level.
The bottom of the reactor. vessel nozz1ss for the Main Steam Lines (MSLs). is at 111 inches above instrument zero. Consequently,.with the reactor water level ;
greater than 111 inches above instrument zero, reactor coolant was entering the MSLs. It is believed that the coolant was then being diverted to the Main. :;
Condenser via the TBVs and MSL drain valves. Procedure 34AB-C71-001-1S, " Scram ;
Procedure," requires that, if reactor water level exceeds 100 inches above-instrument zero, the Main Steam Isolation Valves (MSIVs) should be closed. The' .i purpose for closing the MSIVs is to prevent damage to the lines downstream'of !
the MSIVs and to the Main Turbine if water enters the MSta. During scram '
recovery, licensed management personnel made a conscious decision not to close ,
the MSIVs based on the following factors: 1) The Main Turbine had already tripped; therefore, water could -not enter the Main Turbine. 2) Closing the MSIVs would have complicated' scram recovery in that the normal reactor feedwater and the Main Condenser would be unavailable. 3) At the time the action was .;
considered, reactor water level had been accurately assessed and was decreasing.
At approximately 1550 CDT, the reactor water level had decreased below the bottom of the MSL nozzles, and water was no longer entering the MSLs.
The repair of the packing leak required isolation of the affected instrument ,
header which serves Emergency Core Cooling System (ECCS) instrumentation, as j
-well as the RPS and PCIS instramentation previously mentioned. Consequently, in "
accordance with the Technical Specifications, a Limiting Condition for Operation ,
requiring that Co?.d Shutdown be achieved within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if the condition.is not
-repaired was entered. By 0305 CDT, on 6/16/93, the condition had been repaired,
'the' instrument lins unisolated, and the Limiting Condition for Operation
-terminated. ,
CAUSE OF EVENT The cause of the' event was component failure in that ' a loose packing ' nut became j disengaged from an isstrument isolation valve bonnet during a maintenance activity. As described previously, when the nonlicensed Instrument & Controls: l (16C) technician performing a calibration on level instrument 1B21-N093B began: ,
, to close a 3/8 inch instrument sensing-line isolation' valve, upon contacting the
-stem handle, the packing nut came off of the bonnet. Subsequently, the packing.
. gland'and packing partially cameLout of the bonnet, resulting in a substantial '
bonnet _ leak. 'The associated instrument line serving various level transmitters i which provide input to RPS, PCIS, Reactor Water Level Indicators 1B21-R606A and :
C, the "A" system of the FVLC, as well as other systems, depressurized. . .
Consequently, when the instrument line depressurized, a false low water level :l was' sensed by these instruments. resulting in a reactor scram, automatic ,
RF N
]
- n. ,
t
' FUL F0 V J00A U.5. IRELLAR MLbd.AlWT MFM15blW MVUVLD WW IK) 31JO-OlD4 E (6 4 ). 2 LICENSEE EVENT REPORT (LER) 9 TEXT CONTINUATION ,
FACILITY NAME (1) . DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) ,
b VEAR SEQ NUM REV j 0'1 2 ')
IIANT E. 'I. HATCH, UNIT 1 05000321 93 00 5 0F 9 TEXI
. isolation of the inboard PCIS valves,'and a false low level indication on Main a
Control Room indicators 1B21-R606A and C. The FWLC System was in."B" control at the time of the scram and, therefore, was not initially affected by.the false signal. However, when control was transferred to "A" during scram' recovery, the .)
FWLC System controlled the RFP based on the false ' low water . level' signal, . +
ultimately resulting in the high reactor water level condition.
The cause of the high reactor water level condition was the partial
-repressurization of_the instrument sensing line. . Typically,z a sensing line
' failure would result in a total depressurization of the line withouc .
repressurization. -In such a situation, the instrument served by the line would ;l fail upscale or downscale and would not respond-to actual water level. changes, t Such was not the case in this event. It is apparent from a review of the Safety _.
Parameter Display System (SPDS, EIIS Code IQ) graphs that the packing leak j
. partially sealed off after the initial depressurization. The graphs show that.
-sensed level on the "A" and "C" instruments initially-went downscale. The !
graphs show that level was restored and then nominally fluctuated as would be f expected due to.the coolant boil-off and periodic'feedwater: additions. This '
phenomenon, coupled with the "B"
~
indicator being upscale, led the- operators to l conclude that the "A" and "C" indicators were correct and the "B". indicator instrument referenceLline had depressurized causing it to fail upscale. An ;
additional factor affecting.their conclusion was'that they knew a "B"_ level ,
instrument was being calibrated ~at.the time of the event.' The operators- j associated the "B" Reactor Water Level Indicator with the instrument being- . .
calibrated and surmised that a problem with the calibration had caused the "B" Reactor Water Level Indicator to fail upscale. .;
~
REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT- I
+
This report is required pursuant to 10 CFR 50.73(a)(2)(iv) in that it' involved .
j unplanned automatic actuations_of Engineered Safety Features (ESF). 1 Specifically, a false low reactor water level condition resulted in automatic- ;
RPS and.PCIS actuations. Additionally, during the level transient following'the :
scram, an actual low water level condition resulted in the outboard PCIS' valves .)
automatically closing.
The RPS provides timely protection against events that'could potentially result' in damage to the fuel by initiating an automatic scram when appropriate plant -l
-parameters exceed design limits. One of the plant conditions'that would result ]
fin lan automatic RPS actuation is a lowLreactor water level condition. A scram dd
'is initiated in this condition to reduce the heat generation rate of ' the ' fuel to ]
- prevent fuel damage due to the reduced ~ coolant inventory and, thus, reduced v !
cooling capacity. .!
'I In'this event, depressurization of an instrument sensing line resulted in two.
level-instruments, which provide input to RPS .failing-low and initiating a trip ];
in the RPS-logic. As designed, the two inputs were sufficient to trip the
. one-of-two-taken twice RPS logic. All control rods fully inserted as designed.
v
.,__m_ _ , - _ .-
______.--_m-
u.s. hur.wvi RGULAIUkV UmibM w tonesuA ArnGW % N JN-0104 (H9)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3)
TEAR SEQ hum REV PIANT E. I. HATCH, INIT 1 05000321 93 012 00 6 or 9 IEXT The PCIS provides automatic isolation capability of. Primary Containment penetrations to preclude the release of radioactive material and the loss of reactor coolant inventory in the unlikely event of an accident. The system is designed to actuate on a low reactor water level condition. The level instruments that innut to RPS also input to PCIS. Consequently, the false low l level condition raw 'ted in isolation of Group 2 PCIS valves. Only the inboard l valves closed due he false low level condition since only the inboard PCIS l is served by the lecal instruments on the affected instrument sensing line. The
! actual level decrease that followed the scram resulted in an actuation of the outboard PCIS. As a consequence, the outboard Group 2 PCIS valves received an L automatic closure signal. The PCIS valves were confirmed to have closed as L required.
Prior to the event, reactor water level was at the normal level of approximately 37 inches above instrument zero. As expected, immediately following the scram, l actual reactor water level decreased due to void collapse in the reactor I coolant. The RFPs responded to the actual decrease and restored level. The minimum level reached in the transient was 34 inches below instrument zero l (124.5 inches above the top of the active fuel). The initiation setpoint for j HPCI and the Reactor Core Isolation Cooling System (RCIC, EIIS Code BN) is 35 )
inches below instrument zero. Consequently, these systems were not required to !
initiate and did not do so.
l I
Following the restoration of reactor water level, it continued to increase due
]
to RFP injection as discussed previously. The FWLC System is comprised of an "A" and a "B" reactor water level input, either of which can be selected as the reactor water level input to control the system. The "A" reactor water level ,
input is from level transmitter IC32-N004A, which is served by the sensing line J that depressurized in this event. The "B" level input is from 1C32-N004B, which is served by an independent and redundant sensing line. During the latter portion of the scram recovery, the FWLC System was selected to "A" level control, which was receiving a false low water level signal. Consequently, the ,
RFP received a feedwater demand signal and supplied water to the vessel even though actual level was high. The RFP trip system did not function in this event to preclude overfilling the vessel because two of the instruments feeding the two-out-of-three-taken-once logic scheme were sensing the false low level condition.
According to the SPDS graphs, reactor water level peaked at a level of 126 inches above instrument zero. It was estimated that approximately 10,000 gallons of water entered the MSLs for the duration of the overfill condition. A significant quantity of the water most likely vaporized to steam. During this time, the TBVs and the MSL drain valves were open, apparently draining the remaining water to the Main Condenser. Based on the piping configurations of the MSLs, HPCI, and RCIC, and on the postulated fluid flow dynamics, it was concluded that most likely a minimal amount of water entered the HPCI steam supply line and that no water entered the RCIC steam supply line. The HPCI steam supply line is equipped with a steam condensate drain pot that would have drained any water that entered the line.
l i g nr.ma uewggg u.3. mua atuute um>>wn ow4
- LICENSEE EVENT REPORT-(LER)
. TEXT CONTINUATION FACILITY NAME.(1) DOCKET NUMBER (2)- LER NUMBER (5) PAGE (3)
TEAR SEQ hum REV PLANT E. I. HATCH, UNIT 1 05000321 93 012 00 7 or 9 TEXT
]
Prior to restart of the reactor, Ceneral Electric performed an evaluation of the j effects of the water entering the MSLs. Based on this evaluation, no safety concerns existed.
- Ii Reactor pressure was at 985 psig prior to the event. As expected, following the scram, pressure decreased to approximately 757 psig. Following the Main Turbine i trip, the TBVs opened and controlled pressure at approximately.920 psig. y Reactor vessel instrumentation provides monitoring capability of critical vessel )
. parameters and provides the appropriate initiating signals when sensed
. parameters exceed prescribed limits. In this event, an instrument sensing line l depressurized, rendering the instruments served by rhe line incapable of )
accurately monitoring their sensed parameters. The instruments associated with ;
the sensing line and the affect of the condition on the associated ESF are as j follows:
i 1B21-N080A/B: These reactor water level instruments provide ;
an actuation signal to RPS and PCIS on a low reactor water j level condition. Depressurization of the instrument sensing line 'i caused these instruments to sense a false low level condition and generate a trip signal, resulting in an RPS and a PCIS actuation.
1B21-N093B: This reactor water level instrument provides.a trip signal to the HPCI System on a high reactor water !
level condition to preclude overfill of the vessel due to l HPCI injection. The logic for this trip signal is a two-of- j two-taken-once scheme and-is not divisionally redundant.
This design is partly due to the fact that the HPCI System is unique among ESFs in that it is a single train safety ;
system. As such, the system is not designed to be divisionally redundant. Also, the logic scheme precludes a single spurious signal from causing a trip of the system.
As a consequence, the depressurization of the instrument sensing line caused the transmitter to sense a false low water level condition and, given the logic scheme, would .l '
have prevented a trip of the system on an actual high level condition.
1C32-N004A,C: These level transmitters do not perform an ESF function; they provide a level signal.to level indicators 1B21-R606A and C in the Main Control Room, to the FWLC System (1C32-N004A only), and to the Main Turbine and RFP trip system. The affect of the sensing line failure on this instrumentation was previously discussed. i 1B21-N095A: This instrument is a level transmitter and performs two functions. First, it provides a trip signal to the RCIC System (a non-ESF) on a high reactor water level condition to preclude overfill of the vessel due to RCIC injection. The logic for this trip signal is a two-of-l j
m
' ~
s ,
cl .
we, tonn Jam u.s. nutuAR KLuuLMUMI umlMlUN , M muvtpUpB NDdlW-WD4 l (6-89) e ' EXPIRES: 4/30/92 LICENSEE EVENT REPORT-(LER)- i TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER:(2). LER NUMBER (5)- PAGE (3)
YEAR SEQ hum REV PLANT E. I. IIAIGI, UNIT 1 05000321 93 0'1 2 00' 8 0F 9 !
TEXT:
a f
two-taken-once scheme-and is_not divisionally redundant. ,
This' design is_ partly due'to'the fact that.the RCIC System- r is a single. train system.. As such, the system.is'not ,
designed totbe.divisionally redundant. Also, the' logic .l scheme precludes a single spurious signal from causing a
~
i trip of the RCIC System. As a consequence, the depressurization .
of the ' instrument s(7 sing line caused the transmitter: to sense a false low water level condition and, given the.logiefscheme,. :
would have prevented a trip of the system on an actual high level . n-i condition.
1 The second function of this transmitter,is to provide a permissive signal to.the Automatic Depressurization System !
on a low reactor water level condition. The sensing line failure in this event would have caused.the permissive ;
signal to be generated at a higher than required level. :
Consequently, the failure would not affect the ability of' f ADS to-function in an accident. Furthermore, the other inputs required to initiate.the. system would preclude i
. premature initiation of the system. 1 Based on the above information, it is concluded that this event had no adverse impact on' nuclear safety. This assessment applies to all operating conditions. l J
CORRECTIVE ACTIONS >
. . t The packing for isolation valve 1B21-N093B-IV-1 was re-installed and the packing'
~'
- nut torqued.
The packing nuts for instrument valves in Unit I were checked. Twenty-three packing nuts were found to be less than snug. The nuts were subsequently-tightened.
?
During the next Unit 2 Refueling outage, the[ Unit 2 instrument packing nuts of' ,
the type involved in this event will be checked for proper tightness.
l A walkdown of the HSLs; downstream of:the MSIVs was performed and no signs of
- damage were identified.
u
- General Electr.ic performed an evaluation of.the water'in the MSLs. '
i c
. ADDITIONAL INFORMATION '
No systems other than those previously identified ~in this' report were affected.
.by thisl event.
,e I
4
?
P
't .
l J004 U.5. WW Kt.blLAILMT LANTilbblLM Artm J UIM
. LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION ~
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER.(5) PAGE (3)
YEAR SEQ NUM REV PLANT E. I. HATCH, UNIT 1 05000321 93 012 00 9 0F 9 TEXT-
.One similar event occurred within.the past 2 years in which a pressure perturbation on an instrument sensing line resulted.in.an automatic reactor-scram.' This event was addressed in the LER 50-321/91-17, dated 10/9/91. In-this event, a hand-held instrument fell and struck'a sensing line drain valve
~
, stem handle. The impact of the fall.resulted,in the valve partially. opening and the sensing line completely depressurizing. Corrective actions for this event-included counseling. personnel and issuing a plant-wide directive. These actions had no bearing on the condition of the packing' nut and, therefore, could not have' prevented this event.
Failed Component Information:
Master Parts List Number: 1B21-N093B-IV-1 Manufacturer: Dragon Valve, Inc.
Model Number: 60N
. Type: Instrument Manifold Valve Manufacturer Code: -D232 EIIS System Code: JA EIIS Component Code: ISV
-Reportable to NPRDS: Yes Root Cause Code: X c
.