LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order IssuedML20044D488 |
Person / Time |
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Site: |
Hatch ![Southern Nuclear icon.png](/w/images/1/14/Southern_Nuclear_icon.png) |
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Issue date: |
05/14/1993 |
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From: |
Tipps S GEORGIA POWER CO. |
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To: |
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Shared Package |
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ML20044D485 |
List: |
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References |
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LER-93-004-01, LER-93-4-1, NUDOCS 9305190219 |
Download: ML20044D488 (6) |
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Similar Documents at Hatch |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
[Table view] |
Text
_. _ ._ _
i gru wb U.5. musi ututAva umaian mg ian LICENSEE EVENT REPORT (LER) f J
l tALitaiY nAnt (1) avtAte noneth m na
LEVEL 000 j 20.405(a)(1)(ii) 20.405(a)(1)(iii) 50.36(c)(2) [ 50.73(a)(2)(vii) [DTHER(Specifyin ;
I 50.73(a)(2)(1) _
50.73(a)(2)(viii)(A) Abstract below) l 20.405(a)(1)(iv) -
50.73(a)(2)(ii) - 50.73(a)(2)(viii)(B) !
20.405(a)(1)(v) 50.73(a)(2)(tii) 50.73(a)(2)(x) j
( LICE 45E L C0hTACI FOR Ittl5 LER (li) j hAME TELEPnchE huMBER '
LREA CODE STEVEN B. TIPPS,1% NAGER NUCLEAR SAFEIY AND 00MP11ANCE. HATCH 912 367-7851 COMPLEIE ChE LlhE FOR EALn FAILURE DESCRIBED lh Inl5 REFDLi (13)
CAUSE SYSTEN COMP 0hENT MAkUFAC- P0RT CAU$E SYSTEN COMPONENT P RT TURE pgDS jAjuFAC-E l
1 ,
l SuPFLEMEhlhL REPORT EAFELIED (143 M0hIn DAY 1 EAR I EXPECTED !
SUBMISSION
] YES(If yes, complete EXPECTED SUBMISSION DATE) "i] NO DATE (15) l ABSISALI (16) !
i On 4/14/93, at 0910 CDT, Unit 1 was in the Refuel mode and core reload was in progress with 23 fuel bundles loaded in the core. The "A" division of the {
j Residual Heat Removal (RHR) System was. out of service for maintenance. The "B" l
division of RHR was in operation in the Shutdown Cooling (SDC) mode. At that !
time, while performing a periodic surveillance, a licensed operator found that l RHR-SDC flow was at zero. He then checked the system alignment and found that !
the Low Pressure Coolant Injection valve (valve lEll-F015B), which also l functions as the_SDC discharge valve, was closed, isolating SDC from the reactor i vessel. The operator opened the valve; however, when the valve reached the full i open position, it automatically reclosed. The ID RHR pump was then secured, 'l fuel movement was stopped, and procedure 34AB-Ell-001-lS, " Loss of Shutdown ]
Cooling," was entered. An investigation was subsequently initiated. At 1015 '
CDT, it was determined that the valve had closed due to a blown fuse. The fuse was replaced and the valve was reopened without incident. By 1043 CDT, the RHR system had been filled and vented and SDC had been returned to service. Reactor coolant temperature did not increase during the event The cause of the event was inadvertent grounding of a logic circuit resulting in the circuit fuse actuating. The grounding incident occurred at approximately 0745 CDT during a modification activity not associated with the RHR system.
Corrective actions included replacing the fuse, testing of the SuC pump, returning SDC to service, revising administrative controls, and issuing an operating order.
L l 9305190219 930514
- gDR ADOCK 05000321
. PDR i
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m 3 n2 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION ,
FACILITY EAME (1) DDCKET WUMBER (2) LER NUMBER (5) PAGE (3)
{i tLAR 5tQ hum REW PIANI HAKH, UNIT 1 05000321 93 004 00 2 Dr 6 l TLu i t
PLANT AND SYSTEM IDENTIFICATION l General Electric - Boiling Water Reactor Energy Industry Identification System codes are identified in the text as (EIIS Code XX). j DESCRIPTION OF EVENT l l
On 4/14/93, at 0910 CDT, Unit I was in the Refuel mode and core reload was in l progress with 23 fuel bundles loaded in the core. The "A" division of the l Residual Heat Removal System (RHR, EIIS Code BO) was out of service for i maintenance. The "B" division of RHR was in operation in the Shutdown Cooling (SDC) mode. At that time, while performing periodic surveillance procedure 34GO-OPS-015-lS, " Maintaining Cold Shutdown or Refuel Condition," a licensed !
operator found RHR-SDC flow at zero. He then checked the system alignment and !
found the 1D RHR pump running. However, the Low Pressure Coolant Injection l valve (IEll-F015B), which also functions as the SDC discharge valve, was closed, isolating SDC from the reactor vessel. The operator opened the valve using the valve control switch. However, when the valve reached the full open position it i automatically reclosed, indicating that an automatic closure signal was in l effect in the valve control circuit. !
I The ID RHR pump was then secured, fuel movement was stopped, and procedure l 34AB-E11-001-lS, " Loss of Shutdown Cooling," was entered. Since the "A" [
division of the RHR system was out of service for maintenance, it could not be i aligned to the SDC mode. I Reactor coolant temperature was then monitored every 15 minutes via the Fuel [
Pool Cooling and Cleanup (FPCC) System (EIIS C de DA). The reactor coolant !
temperature is normally monitored by using the .HR heat exchanger inlet temperature. However, with SDC out of service, the heat exchanger inlet temperature would not be indicative of reactor coolant temperature. Therefore, 3 reactor coolant temperature was monitored at the suction of the FPCC system j which was aligned to the reactor cavity to identify any increasing trends in j temperature. j An investigatien was initiated regarding the closing of valve 1 Ell-F015B. At 1015 CDT, it was determined that a blown fuse had caused the valve to close.
Based on subsequent review of the RHR system flow recorder chart, it was concluded that the valve had closed, and the fuse had blown, at approximately 0745 CDT. A periodic check of Emergency Core Cooling Systems (ECCS) status had been performed at approximately 0730 CDT at which time the valve had been found to be open.
The fuse was replaced and the valve was reopened without incident. By 1043 CDT, the RHR system had been filled and vented and SDC returned to service. Within 10 minutes following the return to service of SDC, the RHR heat exchanger inlet temperature returned to its pre-event level of 95 degrees Fahrenheit. It was therefore apparent that reactor coolant temperature did not increase during the event. Since only 23 fuel bundles were in the reactor vessel, the heat load was very low and the reactor coolant temperature was not expected to have increased.
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TEXT CONTINUATION l
i rAtitITY MANE (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) l TEAR 5EO huh kik l
P!.AhT HA101, UNIT 1 05000321 93 004 00 3 0F 6 i TLM ],
CAUSE OF EVENT l I
The cause of the event was inadvertent grounding of a control circuit during implementation of a design modification. During the implementation of the Hardened Vent modification, a panel of a control board had to be removed to gain access to the affected viring. While the panel was being removed, a valve j indicating light terminal on the panel contacted the control board frame, '
grounding the associated circuit. As a result, the circuit fuse actuated and de-energized the circuit. The circuit was part of the Primary Containment l Isolation System (PCIS. EIIS Code JE) logic circuitry and was of a fail-safe j design. Consequently, when the circuit de-energized, a PCIS signal was '
generated resulting in the automatic closure of valve 1E11-F015B. :
t i
A licensed operator passing by the panel at the time of the event saw a spark j when the terminal was grounded. However, it did not appear that there had been [
any effect on the plant. Therefore, he did not feel it necessary to investigate [
further. The contract electricians performing the work also saw the spark but !
took no action, believing that the operator would take any necessary actions.
{
REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT !
This report is required pursuant to 10 CFR 50.73 (a)(2)(iv) in that a blown fuse l
resulted in an unplanned automatic actuation of an Engineered Safety Feature i (ESF). Specifically, the SDC discharge valve (IEll-F015B) also functions as a Primary Containment Isolation System valve. As explained earlier, the fuse ;
actuation resulted in the associated circuit de-energizing. The de-energized !
circuit simulated a PCIS signal to the valve resulting in it automatically closing.
The purpose of the Primary Containment Isolation System is to provide timely I protection against the onset and consequences of events involving the potenticl release of radioactive materials from the fuel and nuclear system process l barriers by isolating approprir.te lines which penetrate Primary Containment. .
Additionally, isolation of thu lines acts to conserve reactor water inventory if ,
a breach in the line is causing a loss of reactor coolant. The PCIS logic is of i' a fail-safe design such that on loss of power to the logic a PCIS isolation signal is generated. In this event, a fuse actuation resulted in the de-energization of a portion of the Croup 2 PCIS logic. As a result, PCIs valve 1E11-F015B automatically closed as designed. Other PCIS valves received signals ;
to close; however, with the plant in a refueling outage, most of these valves !
vere already closed prior to the event. The Safety Parameter Display System j (SPDS, EIIS Code IQ) was out of service for maintenance at the time of the event i and, therefore, could not be used to confirm valve actuations.
l The purpose of the Shutdown Cooling mode of the RHR system is to provide {
adequate cooling to the reactor core while the reactor is shutdown in order to ;
reduce the reactor coolant temperature to and/or maintain it below 212 degrees Fahrenheit. In this event, Shutdown Cooling flow was interrupted for 1 1
i l
9
3 f
! . % Form JtM U.5. NRLhi EtWLAW kmh5Wh WrM W Opb NJalW-Q04 '
(6-89) - EXPIRES: 4/30/W I LICENSEE EVENT REPORT (LER) :
TEXT CONTINUATION i .
}
l FAClLITY NAME (1) DLKET NUMBER (2) LER WUMBER (5) PAGE (3)
VEAR SEQ hum REW l
l >
l PUNT 1%TW. WIT 1 05000321 93 004 00 4 or 6 '
TEU I l approximately three hours. At the I f.me of the eveni only 23 fuel bundles were l loaded in the reactor and it had Laen thirty days since the core was last )
critical. Consequently, the decay heat load in the vessel was extremely low and l the temporary interruption of SDC flow did not result in an increase in the- l temperature of the reactor coolant. i i i j Even if the event had occurred under the most limiting plant conditions, the i l
interruption of SDC flow would have been discovered with ample time available i for taking the necessary actions to maintain the core covered and adequately l cooled. The worst case scenario for a loss of SDC is postulated to occur with the reactor core fully loaded and the vessel head de-tensioned or removed at the f earliest possible point after the reactor is shutdorn. The earliest point at which this condition could exist is approximately 2.5 days after the reactor is :
shutdown. At this point in time, the decay heat load would be approximately 37 l million BTU /hr. With this heat load, following an interruption of SDC and ;
evruming a c nservative initial coolant temper:ture of 150 degrees Fahrenheit, !
tne bulk reactor coolant temperature would tsach 212 degrees Fahrenheit in 1.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> at which point boiling would commence. The decay heat load is not ,
sufficient to cause a departure from nucleate boiling and core cuverage is ;
sufficient to prevent fuel cladding damage Once bulk boiling begins, it would (
take 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> for reactor water level to decrease to the top of the active fuel '
with no makaup. This assumes that prior to the event reactor water is at a ;
level of 195.4 inches above the top of the active fuel. This is also a conservative assumption since the level would actually be at the vessel head ;
flange which is 364.2 inches above the top of the active fuel. '
With bulk boiling in progress, it is assumed that the steam generated is vented l to the refueling floor. Refueling floor personnel would notice water vapor j rising from the reactor vessel cavity prior to the onset of boiling and would '
notify the Control Room. Additional assurance that the interruption of shutdown i cooling would be identified early in the event is described as follows. At 190.4 inches above the top of active fuel, a reactor water low level annanciator will alarm. A reactor scram signal and a group 2 PCIS signal will actuate at !
, 170.7 inches above the top of active fuel. At 123.4 inches above the top of l active fuel, the Standby Gas Treatment System will start. At 57.4 inches above y the top of active fuel, a group 1 PCIS signal will actuate and the Diesel l Generators and Core Spray pumps will start and automatically inject into the
! vessel thereby terminating the event. These actuations will result in 4 l indications and alarms in the Control Room. Even if the operators did not
! notice tl.a numerous indications and alarms, the condition wculd be detected l during performance of surveillance procedure 34GO-OPS-015-1P long before the i reactor water level decreased to the top of the active fuel. The procedure is
- performed every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. If the loss of SDC occurred immediately after performance of the surveillance, then the event would progress for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />
- before the surveillance would be performed again. Bulk boiling would be in l progress; however, the reactor water level would be 122.4 inches above the top i of the active fuel. At least one division of the Core Sprsv System (CS, EIIS l Code BM) and the Control Rod Drive Systes (CRD, EIIS Code AA) would be available
- for adding coolant to the reactor vessel. Either of these systems could be aligned to inject to the reactor vessel, restoring reactor water level and j cooling br reactor core.
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TEAR 5EQ h0M REV l
] PLANT 1RTW, INIT 1 05000321 93 004 00 5 0F 6 ,
a TEu ,
i In this event, had the heat load in the reactor vessel at the time the event was
- discovered warranted immediate mitigating actions, the 1 Ell-F015B valve could i have been manually opened in a minimal amount of time, thus returning SDC to q service. The automatic closure signal to the valve would not have prevented the valve from being manually opened. i 1
Additionally, during the event, the ID RHR pump ran at shutoff head and no flow {
conditions for approximately 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Ine pump was secured after it was ,
determined that valve lEll-F015B could not be maintained open using the renote control switch. When SDC was placed back into service, the pump flow and !
discharge pressure were checked and found to be acceptable. Pump vibration was -
j i checked and found to be acceptable. Also, the IB RHR pump was available had the 1D pump been damaged during the event. i j Based on the above analysis, it is concluded that this event had no adverse l
+
impact on nuclear safety. This assessment considers the worst case initial plant conditions and therefore envelopes all other plant conditions.
CORRECTIVE ACTIONS i !
The fuse was replaced, valve lEll-F015B was opened, and the SDC mode of the RHR l system was placed into service. ;
i A plant-wide directive was issued on this event informing plant personnel of the i
, possible consequences of grounding incidents and the need to aggressively l investigate each grounding incident to determine the effects on plant operation.
j' An operability check and a vibration check were satisfactorily performed on the 1D RHR pump.
)
j Administrative controls will be reviewed and revised as necessary to ensure that ;
j SDC flow and reactor coolant temperature are checked at a frequency commensurate ,
q with the decay heat load in the reactor vessel. :
i ADDITIONAL INFORMATION l
i No systems other than those previously addressed in the report were affected by ,
this event. t N
f
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EXP13ES: 4/30/02
. TEXT CONTINUATION rAC-ILITY hAME (1) DDCKET NUMBER (2) LER hUMBER (5) PAGE (3)
TEAR SEQ hum REV PIANT HATCH, UNIT 1 05000321 93 004 00 6 DF 6 IEAT No events have occurred in the previous two years which resulted in a loss of MIR-SDC capability. Eight events have occurred in the previous two years in which a fuse actuation resulted in the automatic actuation of an Engineered Safety Feature. These events were addressed in the following reports:
50-321/91-16, dated 9/30/91, 50-321/91-21, dated 10/25/91, 50-321/91-23, dated 11/12/91, 50-321/92-16, dated 7/10/92, 50-366/91-10, dated 5/13/91, 50-366/91-11, dated 5/15/91, 50-366/92-02, dated 2/19/92, and 50-366/92-18, dated 10/26/92.
Corrective actions for these events included replacing the actuated fuse, returning the applicable system to service, counseling personnel, training personnel, performing a design review of the fuse application, performing a check of the applicable circuit for faults, and evaluating the usage of different types of jumpers. These corrective actions could not have prevented the event addressed by this report because of the unique circumstances involved in this event. Specifically, in this event, electricians were having to remove a valve light indication panel in order to access wiring. In moving the panel out of its frame, a valve indicating light terminal on the panel contacted the panel fr.me, grc unding the circuit. The corrective actions from the previous events could not have prevented this event.
No failed components resulted from or contributed to this event.
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