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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
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{{#Wiki_filter:--
. George Power Com;cny
'Y
- Co invernets Cemer Parctway Post CMice Sex 129s BirrrungNim. Nabama 3s201 Telephone 205 B77-7279 L
J. T. Beckham, Jr. Georgia Power
%ce President Nadear Hatch Profect If+ 50uf'*"' C E!'C V uf'"
May 3, 1993 Docket No. 50-366 HL-3269 005299 U.S. Nuclear Regulatory Commission ATIN: Document Control Desk Washington, D.C. 20555 Edwin I. Hatch Nuclear Plant - Unit 2 Licensee Event Report Personnel Error Results in a Condition Prohibited by the Technical Specifications Gentlemen:
In accordance with the provisions of 10 CFR 50.73(a)(2)(1), Georgia Power Company is submitting the enclosed Licensee Event Report (LER) concerning a personnel error which resulted in a condition prohibited by the Technical Specifications. This event occurred at Plant Hatch - Unit 2.
Sincerely, G wdA
[ J. T. Beckham, Jr [ v JKB/cr
Enclosure:
LER 50-366/1993-003 cc: Georoia Power Company Mr. H. L. Sumner, General Manager - Nuclear Plant NORMS U.S. Nuclear Reculatory Commission. Washinoton. D.C.
Mr. K. Jabbour, Licensing Project Manager - Hatch U.S. Nuclear Regulatory Commission. Reaion 11 Mr. S. D. Ebneter, Regional Administrator Mr. L. D. Wert, Senior Resident Inspector - Hatch sp?
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I EVEhl DATE (5) L E fa hbMbER (6) EEP0kT Call (7) CINER F ALILIIIE5 Ihv0LbED (6)
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STEVEN B. TIPPS. MANAGER NUCLEAR SAFEIY AND COMPLIRJCE, IRTCH 912 367-7851 l LOPPLETE DhE LlhE FOR LACH FAILbkt DESCRIEED lh Th15 kEP0kT (13)
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On 04/07/93 at 0103 CDT, Unit 2 was in the Run mode at a power level of 938 CMWT 3 (38.5% rated thermal power). At that time, licensed shift personnel were l performing Control Rod Drive (CRD) system scram time testing in accordance with Unit 2 Technical Specifications section 4.1.3.2.a which requires the testing to !
be completed prior to exceeding 40% rated thermal power. Per procedure !
34GO-OPS-001-2S, "PIANT STARTUP," reactor power was being maintained below 40% !
in order to comply with the specification. When licensed personnel prepared to j test control rod 26-31, they expected that fully withdrawing the rod might cause j thermal power to increase to a level very close to 40%. Therefore, they slowly >
withdrew the rod a few notches at a time while observing the Average Power Range :
Monitors. The monitors, which have strip chart indication, appeared to indicate l
approximately 40%. By the time the rod had been fully withdrawn, however, the plant's Process Computer indicated that thermal power had actually reached 40.71%, violating the requirement of the specification. Licensed personnel then ,
scrammed the rod, and thermal power decreased to approximately 38.3%. j The root cause of this event is personnel error on the part of the licensed j superintendent of shift. The plant startup procedure stated that the testing should normally be performed at 35% rated thermal power. However, the plant was operated at a higher power level (38.5%) with the result that when rod 26-31 was ,
fully withdrawn, core thermal power increased to 40.71%. t Corrective actions for this event included counseling the licensed superintendent of shift. Also, the plant startup procedure will be revised by ;
7/16/93 to provide improved administrative control of reactor power. :
1
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TEXT CONTINUATION l
FACILITY %AME (1) DDCKET NUMEER (2)- LER NUMBER (5) PAGE (3) f VEAR SEQ hum REV i PIANT E. I. HATCH, UNIT 2 05000366 93 003 00 2 0F 5 l ILAI ?
PIANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor [
Energy Industry Identification System codes are indicated in the text as (EIIS ;
Code XX). '
l I
DESCRIPTION OF EVENT ,
i On 04/07/93 at approximately 0103 CDT, Unit 2 was in the Run mode at a power -
level of 938 CMWT (38.5% rated thermal power). At that time, licensed shift 1 personnel were performing Control Rod Drive (CRD, EIIS Code AA) scram time !
testing per procedures 34GO-OPS-001-2S, " PLANT STARTUP," and 42SV-C11-001-2S, i
" CONTROL ROD SCRAM TESTING." These procedures implement the requirement to perform individual control rod scram time testing per Unit 2 Technical Specifications section 4.1.3.2.a. This specification requires that scram time i testing on all control rods be completed prior to exceeding 40% of rated thermal power. Seven control rods had been tested successfully and operations personnel ;
were preparing to test control rod 26-31. I i
Prior to rod 26-31 being tested, shift personnel recognized the rod as a ,
high-worth rod. Accordingly, they withdrew the rod in stages (rather than ,
continuously) while observing the Average Power Range Monitors (APRMs, EIIS Code !
IG) to ensure that core power did not exceed 40% as indicated by the APRM strip -
chart recorder. As the rod was withdrawn, core power increased as expected, but appeared on the APRM strip chart to remain at approximately 40%. By the time the rod was fully withdrawn, however, the plant's Process Computer (EIIS Code j IO) indicated that thermal power had reached 40.71%. This represented a l condition prohibited by the plant's Technical Specifications since core thermal power rose briefly above 40% before all control rod scram time testing was l complete. ,
Upon discovering that the plant had exceeded 40% thermal power, licensed ;
personnel completed the scram time test on control rod 26-31, and core thermal l power decreased as expected to approximately 38.3% of rated. The Shift i Technical Advisor then initiated a Deficiency Card to document the event in ;
accordance with the plant's administrative control procedures. Subsequently, !
licensed personnel partially inserted one rod group to provide additional margin ,
below 40%, and then successfully completed scram time testing on the rest of the control rods. The total time during which the plant operated above 40% was ,
approximately two minutes.
CAUSE OF EVENT 3
(
The cause of this event was personnel error on the part of the licensed j superintendent of shift. One of the procedures in use at the time, l 34GO-0PS-001-2S, " PLANT STARTUP," contained a note to the effect that control i rod drive scram time testing is normally to be performed when the plant is operating at approximately 35% of rated thermal power in order to avoid the i
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EXPIRES: 4/3D/92 TEXT CONTINUATION FACILITY hAME (1) DOCKET NUMBER (2) LER NUMBER ($) PAGE (3) 1 EAR 5EQ hum REV PIANT E. I. HAIM, INIT 2 05000366 93 003 00 3 0F 5 lEXT possibility of exceeding 40% during testing. However, the plant was operated at a higher power level (38.5%) with the result that the withdrawal of a high worth rod caused core thermal power to exceed 40%.
REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT This event is reportable per 10 CFR 50.73 (a)(2)(i) because the plant entered a condition which was prohibited by the Technical Specifications. Specifically, prior to completion of all control rod scram time testing as required by Unit 2 Technical Specifications section 4.1.3.2.a. core thermal power exceeded 401 for ;
a period of approximately two minutes. l The Control Rod Drive system provides control of reactivity through positioning 1 of control rods. The system consists of 137 cruciform-shaped control rods and !
related hydraulic equipment to move them. The rods contai.n boron or hafnium (
based compounds which absorb neutrons and thus retard the nuclear chain reaction. E all the control rods are fully inserted into the reactor core, !
sufficient ne w ive reactivity is present to shut down the reactor and maintain i it in the shutdown condition under worst case combinations of moderator density j and temperature. Each control rod is supplied with motive force by its own i hydraulic control unit. The scram function of the CRD system normally causes [
rapid, full insertion of all control rods simultaneously; however,-individual control rods may be scrammed one at a time for testing purposes. If the core l has been altered or shut down for 120 days or more, the scram function of all rods is required to be tested prior to ascending to full power operation. The !
purpose of this testing is to ensure that the CRD system is capable of inserting l all control rods within the time constraints assumed in the plant's Final Safety !
Analysis Report (FSAR). The method of test involves fully. withdrawing each control rod one at a time, actuating its scram function, and measuring the time interval between the initiation signal and the completion of rod travel. This =
scram time test was in progress at the time of the event. f In this event, licensed shift personnel were operating the plant at a power level of 38.5% of rated while CRD scram time testing was being conducted, i However, when rod 26-31, which is located near the center of the core, was fully l withdrawn during testing, thermal power rose slightly above the 40% limit, l remaining there for approximately two minutes. When licensed shift personnel -{
observed Process Computer indications that thermal power had exceeded 40%, they .
j scrammed rod 26-31, reducing core thermal power to below 40% of rated. Thus, l I
the brief excursion above 40% rated thermal poser occurred as a result of the scram time testing, not as a result of a normal ascension toward full power !
operation. The plant was in steady state operation below 40% power prior to the ;
event and returned to operat 6n below 40% power as the scram function on rod ;
26-31 was tested. The 401 1 6 .t does not form the basis for any assumption in j the FSAR nor was it chosen to protect any safety limit. Therefore, the plant ;
did not exceed or potentially exceed any safety limit as a result of this event. ;
i The operability of plant equipment was not affected by the event, and the. l ability of the CRD system to pr3 duce a scram was not compromised in any way as !
demonstrated by the fact that all control rods were successfully tested prior to l l
i
% tonn OM u.s. NJR_Um idiaLAW uf%bhWN kt%)n a N 0 31 W-Live (6-89) EXPIRES: 4/30/02 TEXT CONTINUATION FACILITY NAME (1) DOCKET kUMBER (2) LER NUMBER (5) PAGE (3)
TEAR !5EQ hum EEV PIRC E. I. HATCH, UNIT 2 05000366 93 003 00 4 0F 5 IEAT normal ascension to full power operation. Following the event, one rod group was partially inserted into the core, reducing reactor power slightly and providing additional margin between the operating regime and the 40% limit.
Thus, there were no further power excursions above 40% of rated until all control rod scram time testing had been successfully completed.
Based on this analysis, it is concluded that this event had no adverse impact on nuclear safety. The a:falysis is applicable to all plant conditions.
CORRECTIVE ACTIONS Corrective actions for this event included: ,
- 1. Counseling the licensed superintendent of shift. This action is complete.
- 2. Revising procedures 34GO-OPS-001-2S, 34GO-OPS-001-1S, 42SV-C11-001-1S, and 42SV-C11-001-2S to provide improved administrative control of reactor power during CRD scram time testing. This action will be completed by 07/16/93.
t ADDITIONAL INFORMATION
- 1. Other Systems Affected: No plant systems other than the CRD system were affected by this event.
- 2. Failed Components Identification: No failed components contributed to or resulted from this event.
- 3. Previous Similar Events: Events reported in the past two years in which ,
personnel arror resulted in the plant entering a condition which is prohibited by the Technical Specifications are described in the following LERs: -
50-321/1991-32, dated 01/27/92 l 50-321/1992-02, dated 02/06/92 50-321/1992-08, dated 04/20/92 50-321/1992-19, dated 08/04/92
. 50-366/1991-16, dated 06/28/91 .
l 50-366/1991-21, dated 12/04/91 !
50-366/1992-04, dated 04/30/92 50-366/1992-06, dated 06/22/92
{ 50-366/1992-11, dated 08/14/92 50-366/1992-12, dated 08/25/92 50-366/1992-17, dated 10/21/92 50-366/1992-22, dated 12/07/92 50-366/1992-24, dated 12/14/92 50-366/1992-25, dated 12/21/92 P
t
u.s. NWm AnMW uminiA V6MD DE WJ 3nD-lim (E-B,dem a s EXPIRES: 4/30/22 .
LICENSEE EVENT REPORT (LER) 1 TEXT CONTINUATION ;
LER NUMBER (5) PAGE (3) I FACILITY %AME (1) DDCKET WUMBER (2)
VEAR SEO hum kev FIANT E. I. liKIG, INIT 2 05000366 93 003 00 $ OF 5 IEAT ,
Corrective actions which addressed the personnel errors contributing to these events included counseling personnel, reviewing events with licensed personnel in Beginning of Shift Training (BOST), reviewing and revising procedures, issuing an Operations Departmental Directive on the purpose of daily instrument channel checks, training plant personnel on the use of self-verification techniques, removing a licensed individual from duty, f carrying out formal discipline under the Company's Positive Discipline program, and performing management observation of personnel performance in the Main Control Room. Although the event described in this LER involved ;
personnel error, these corrective actions would not have prevented this l event because they pertain to the performance of different activities. .
Also, counseling or training personnel cannot completely eliminate ,
oversights such as the one that caused this event. !
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