Similar Documents at Hatch |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
[Table view] |
Text
.-
V; , ?
. , ': ' '",k ]GrNdia her b mpany ' ' '
i '
4 - 233 Piedniont Aven,ue n' ,
s
+ :- Alienta. rp orgs 30308 -
, ,.- TeleMiche 404 6266526 .
4 :
Mai!: rig Address. ,
Ptst Ofiice Box 4545 '!
, ! Alianta.Geo'D'a 30302 .
. R. P. Mcdonald - lie souttern electrc s',$lem Executive Vee President i j, Nuctour Operations HL-889
- a. 0498V December'27, 1989 t
i U.S.' Nuclear Regulatory Commission ATTN: Document Control Desk .
Washington, D.C. -20555 l l- PLANT HATCH - UNIT 2 -
NRC DOCKET 50-366 L OPERATING LICENSE NPF-5 ?
LICENSEE EVENT REPORT L EQUIPMENT FAILURE RESULTS IN A
! ~ REACTOR PROTECTION SYSTEM ACTUATION l:
Gentlemen:
-In accordance::with the' requirements of 10 CFR 50.73(a)(2)(iv),
Georgia 1 Power Company is submitting the enclosed Licensee Event- Report (LER) . concerning a reactor: protection system actuation due to ' equipment failure. This event occurred at Plant Hatch - Unit 2.
l -Sincerely, jf. $O H. G. Hairston, III l -t
- JKB/eb
Enclosure:
LER 50-366/1989-09 c: (See next page.)
900104o036 891227 PDR ADOCK 05000366 /
/h i S PDC
.. . . . . - .,-. . . , - i
+
. ;v s :. i
.. y e - i LCicoipih1\)uX?r) k l U.S. Nuclear Regulatory Commission December-27, 1989 i Page Two c: Georcia Power Comoany '
Mr. H. C. Nix, General Manager - Nuclear Plant Mr. J. D. Heidt, Manager Nuclear Engineering and Licensing - Hatch GO-NORMS U.S. Nuclear Reaulatory Commission. Washinaton. D.C. .
Mr. L. P. Crockir, Licensing Project Managir - Hatch
U.S. Nuclear Reaulatory Commission. Reaion II Mr. S. D. Ebneter, Regional Administrator Mr. J. E. Menning . Senior Resident Inspector - Hatch r
l l
l~
1.
l 1
l l
l l
l 0498V 1
~
{t ; j.
alRC Pete MS ..
U.S. NUCLE 1.N LE;ULATORY COWAISSION APPRIVED OMS NO 31040104 LICENSEE EVENT REPORT (LER) '*"'REs estiin FACILITY NAASE 11) DOCKET NUtISER (2) PAGE G3 PLANT HATCH. UNIT 2 01510101013 1 616 1 lOFl01 5 I l
TITLE 441 E0VIPMENT FAltVRE RESULTS IN' A REACTOR PROTECTION SYSTEM ACTUATION l
- EVENT DATE (Si LER NUMBER tt) REPORT DATE (7) - OTHER F ACILITIES INVOLVED lel J MONTH oAv vlAR vEAR -
Of,n uONTs oAv vEAR . F Aciserv Naves DOCnET NUMaeRis>
0l5l0l0l0l l l
~ ~
1l1 2I9 89 8l 9 0l0 l 9 d0 1l 2 2l7 8l 9 0 1 5 10 1 0 1 0 1 1 1
.,,,,,,,,, THIS REPORT IS SueMITTED PUR8UANT TO THE REQUIREMENTS OF 10 CFt15: (Chece one er more of the feitomagt (til MOOE m 4 20 402(b) 20.406te)
} 00J3teH2Hivl 73.711bl R 20 4064eH1HO 90.asteHt) 5033 eH2Hul 73311el 1103 0 1010 20 *ost*H1Hin so 88t*H2n so 78i=H2Hval cf
_ _ _ O7,HE
,, g g g Ah m ,
s s
y{
= * "do 20.4064e H1Hlv)
8033tsH2HvuiHS)
=
s 20.406teH1Hvl 80334aH2H64H S0331eH2Hal LICENSEE CONTACT FOM TMi$ LER (12)
NAME TELEPHONE NUMBER ARE A CODE Steven B. Tipos. Manaaer Nuclear Safety and Compliance. Hatch 9 1 11 2 31 6171-1 718151 1 ;
COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBE 0 IN TMi$ REPORT (13)
CAUSE SYSTEM COMPONENT 'M REP TA LE g my gpgg MA AC- ' REPOR A LE ; ,
N,UFjC.
I I I I I I I I I I I I I I s s i I I l l l 1 I I I I I I I SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY v5AR >
Y ES (19 yes, comprese EXPECTED SUS 44tSSION DA TEI
} NO l l l ,
ASST AACT (Liese so 1400 peces, te., soproeunere'y hersee anpee vece typewntren eness (14)
On 11/29/89, at approximately 1220 CST, Unit 2 was in Cold Shutdown. The Unit 2 Station Service Air Compressors (SSAC, EIIS LF) were being replaced with screw-type air compressors under Design Change Request (DCR)86-356 to improve their rel iability. SSAC "B" and "C" had been replaced with SSAC "C" in service.
Modification activities were still in progress on SSAC "A" and "B". A temporary air compressor had been installed and maintained in a standby condition as a backup to SSAC "C". At approximately 1155 CST, SSAC "C" tripped on loss of system cooling.
Delays were encountered in placing the temporary compressor in service and low system air pressure resulted. The low system air pressure allowed the scram valves to drift open resulting in a discharge of reactor water to the Scram Discharge Volume (SDV ). At approximately 1220 CST a Reactor Protection System (RPS, EIIS Code JC) actuation occurred from an SDV high level condition. The temporary air compressor was successfully placed into service and SSAC "C" returned to service shortly thereaf ter.
The root cause of the event is oquipment failure. SSAC "C" tripped due to a multimeter test lead which disengaged from the multimeter during troubleshooting activities and grounded the cooling water control circuit.
Corrective actions include placing the backup temporary air compressor into service, replacing a blown fuse in the SSAC cooling water system control circuitry and returning SSAC "C" to service.
W
.c , ~ ,
, Form 300 , UA. NUCLEAR LEOULATORY COaAAtestDN
(.PPROVED 0448 NO. 3100 0104 LICENSEE EVENT REPORT (LER) Exna'8 85
- FACILITY NAast {1) DOCKET NUMBER (2) PAGE W PLANT HATCH. UNIT 2 0 15101010131616 1 loFl015 TITLE tel E0VIPMENT FAllVRE RESULTS IN A REACTOR PROTECTION SYSTEM ACTUATION EVENT DATE (5) LIR NUMBER ($1 REPORT DATI (7) OTHER F ACILITIES INVOLVED (St MONTH DAY YEAR YEAR -
n"v*$n' j f,$ MONTH
[' DAY YEAR F ACILIT V N AMES DOCKET NUMBERi41 ol5l0l0l0l l l-III 2I9
~ ~
89 8l 9 0l0l 9 d0 1l 2 2! 7 8! 9 0 1 510 1 0 1 0 1 1 1
' OPERATINO , THIS REPORT is gueulTTED PURSUANT TD THE REQUIREMENTS OF 10 CFR $: (Chere one or more e# the follourvat) (111 , ,
"I #3 4 20 402(D) 20 406tel J 50.734elGHhl 73.71(b)
I POWER 20 405(aH1Hil 50.36teH1) 90.73(alGHul 78.71(en
- ***(aHi Hiit so.8steiGi e0.73<.H2ilv6) OTHE R l$oecify in A6spect 10 0 1010 20.406(eH1H644) 60.731 alt 2Hil 60.73(aH2Hv4HHA) 641 ,
's 's 20.405(aH1Hhl 50.734aH2Hul 60.736elGHvn4Het '
20.406taH1Hul 60.73talGHull to.73teH2Hal LICENSEE CONTACT FOR THis LER (12l NAME TELEPHONE NUMSER ARE A CQDE Steven B. Tipos. Manager Nuclear Safety and Compliance. Hatch 9 1 11 2 31 6171-I 71815l1 '
COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT T E O NPR CAUSE SYSTEM COMPONENT TU ER PR I I I i ! I I I I I I l l I ';
l-' I l l l l l l I i l i I I
$UPPLEMENTAL REPORT EXPECTED 1941 MONTH DAY YEAR
'~~} YEs in ves. co,,oiew exPecreo susuission cares ' } NO l l l ASSTLACT ILimit to 1400 specer. le., ocorommearly torteen smere spece tverwertern kneet (16l On 11/29/89, at approximately 1220 CST, Unit 2 was in Cold Shutdown. The Unit 2 Station Service Air Compressors (SSAC, EIIS LF) were being replaced with screw-type air compressors under Design Change Request (DCR)86-356 to improve their reliability. SSAC "B" and "C" had been replaced with SSAC "C" in service.
Modification activities were still in progress on SSAC "A" and "B". A temporary air compressor had been installed and maintained in a standby condition as a backup to SSAC "C". At approximately 1155 CST, SSAC "C" tripped on loss of system cooling.
Delays were encountered in placing the temporary compressor in service and low system air pressure resulted. The low system air pressure allowed the scram valves to drift open resulting in a discharge of reactor water to the Scram Discharge Volume (SDV). At approximately 1220 CST a Reactor Protection System (RPS, EIIS Code JC) actuation occurred from an SDV high level condition. The temporary air compressor was successfully placed into service and SSAC "C" returned to service shortly thereafter.
The root cause of the event is equipment failure. SSAC "C" tripped due to a multimeter test lead which disengaged from the multimeter during troubleshooting activities and grounded the cooling water control circuit.
- Corrective actions include placing the backup temporary air compressor into service,
, replacing a blown fuse in the SSAC cooling water system control circuitry and returning SSAC "C" to service.
gR,C,,P-m 2
e ,
- m -
mac eerm asea u.s hvettA: ntIutAfony comutessose UC'ENSEE EVENT REPORT (LER) TEXT C3NTINUATION1 ' uenovio ous no mo-om
, exeines: s.wie eAcev a m . oocui muus,n m .t ,ou ,,,, m ,Ao, m
'T' a t' t'#n
' PLANT HATCH,-UNIT 2 Y muu o ls lo lo lo l 3l6 l 6 8l9 -
0'l0l9 -
0l0 0 l2' oF 0 l5 1 em,< ,ww mmm PLANT AND SYSTEM IDENTIFICATION General. Electric - Boiling Water Reactor Energy- Industry Idcutification System codes are identified in the text-as (EIIS Code.XX).
SUMMARY
OF EVENT- I
- 0n ll/29/89,- at approximately 1220 CST, Unit 2 was in Cold Shutdown The Unit 2 Station Service Air Compressors (SSAC, EIIS LF) were being replaced with screw-type air compressors under Design Change Request (DCR)86-356 to improve their reliability. SSAC "B" and "C" had been replaced with SSAC "C" in service.
Modification activities were still in progress on SSAC "A" and "B", A' temporary air compressor had been installed and maintained in a standby condition as a backup to-SSAC "C". At approximately 1155 CST, SSAC "C" tripped on loss of system cooling. Delays were encountered in placing the temporary compressor-in service and' a low system air pressure resulted. The low system air, pressure allowed.the scram valves to drift open _resulting in a discharge of reactor water-to the Scram Discharge Volume (SDV). At approximately 1220 CST a Reactor
-Protection System (RPS, EIIS Code JC) actuation occurred from an SDV high level-condition. The temporary air compressor was successfully placed into service and-SSAC "C" returned to service shortly thereafter.
The root cause of the event is equipment failure. SSAC "C" tripped due to a multimeter test lead which disengaged from the multimeter during trouble shooting activities and grounded the cooling water control circuit.
Corrective actions include placing the backup temporary air compressor into service, replacing a blown fuse in the SSAC cooling water system control circuitry and returning SSAC "C" to service.
DESCRIPTION OF EVENT On 11/29/89,.at approximately 1220 CST, Unit 2 was nearing the end of a refueling outage and in the Cold Shutdown mode following a Reactor Pressure Vessel tydrostatic test. The Station Service Air system was undergoing modification per DCR 86-356. The SSACs were being replaced with screw-type air compressors to improve the reliability of the system. SSAC 's "B" and "C" had been replaced, functionally tested, and SSAC "C" placed in operation. Modification activities were still in progress on SSAC "A" and "B". A temporary air compressor had been installed and maintained as a backup to the SSAC in service while modification activities were in progress on the other SSAC's. With SSAC "C" returned to service, the temporary air compressor was maintained in a standby condition. 1 N C FOMM 366A - 8'J.S. CP0s 1968-520 389 000 ?t' ,
O ,
JI s j' - ,
s seAC form 356A , U.S. EUCLEAR (.E!ULLTORY COMMIS8 ton LICENSEE EVENT REPORT (LER) TEXT CCNTINUATION anovio oMe No mo-oio4 EXPIRES: 8131/06 FACILITV 8eMRE 14 DOCKET NUMDER (2) LIR NUMOER (Si PAGE (3) vsam .
5' g f6 -
"y*J *,p PLANT HATCH, UNIT 2 o l5 lo l0 lo l 3l616 8]9 -
0 l 0l 9 -
010 0l3 0F 0 l5 TEXT (# mwe spoes 4 reevnest, see aswesamt NRC Form 3EMW (IM
< At the time of the event, troubleshooting activities were in progress on a temperature switch in the closed cooling water system dedicated to the SSAC's. An I&C -technician had installed a multimeter across the. temperature switch. At approximately 1155 CST, one of the multimeter test -leads became disengaged from the multimeter and contacted the system skid. This resulted in grounding the closed cooling water system control circuit, loss of cooling, and, subsequently, a trip of SSAC "C". Involved personnel notified the Unit 2 Shift Supervisor of the loss of SSAC "C". .The Shift Supervisor dispatched a nonlicensed operator to start the temporary air compressor and restore air system pressure. At approximately 1205 CST, the temporary air compressor. was started. Even though the temporary air compressor was running, system air pressure continued to decrease.
At approximately 1215 CST, a licensed operator was dispatched to the temporary air compressor to check for proper operation. The compressor was found to be-operating properly. The operator then went to verify the position of the
. temporary compressor supply line discharge valve. The low system air pressure subsequently allowed the scram inlet and outlet valves to open resulting in a discharge of reactor water into the SDV. At approximately 1220 CST, the SDV. had filled to the trip setpoint level initiating an RPS actuation. No rod movement resulted from the RPS actuation since the control rods were full-in at the time of the event. Shortly thereafter,- the operator found the discharge valve closed and immediately opened it. When air pressure was restored,- the RPS actuation was reset.
By approximately 1252 CST, a blown fuse in SSAC closed cooling water system control circuitry had been replaced and SSAC had been returned to service. The temporary compressor was then returned to standby. <
CAUSE OF THE EVENT The root _ cause of the event was equipment failure. A multimeter test lead became disengaged from the multimeter and contracted the system skid. This resulted in grounding the closed cooling water system control circuit, which caused a loss of cooling to, and subsequent trip of SSAC "C". This equipment failure appears to be an isolated event.
Operations personnel experienced delays in placing the temporary compressor into l service due to a less than fully adequate procedure. Specifically, special purpose procedure 34SP-090889-QX-1-2N-did not adequately address operation of the temporary compressor from the standby mode.
l l
N FORM 'U.S. CPO: 1988 520 589700070
M.
senc feni sesA -
U.S, ( UCLE A) 1RIUt " TORY COMMIS$lON
"* U -
1 ' DdENSEE EVENT REPORT (LER) TEXT CONTINUATION : arraovio oMe No sino-oto -
, EXfifCS S/31/W .
, F ACILIT Y leAME (1) DOCKET NUMSER 42)
LER NLMBER (4) PAGE(36 YIA" '
__ [n#' .Naa
- PLANT: HATCH, UNIT 2 o l5lololo1 3161 6 al 9 -
0l d 9 -
01 0 01 4 0F glq
( rnxT w- a m m mcinmamm
(.
. REPORTABILITY' ANALYSIS AND SAFETY ASSESSMENT This report is required per 10 CFR 50.73(a)(2)(iv) because this event resulted in an unplanned RPS actuation. Specifically, loss of SSAC f'C" resulted in an
[ unplanned RPS actuation on SDV high level.
'The RPS provides timely ~ protection from the occurrence of conditions that could threaten the integrity of the fuel barriers and the nuclear systen process L barriers and mitigation of the consequences of the unlikely failure of the fuel L barriers or the nuclear system process barriers. One of the initiating signals of an RPS actuation is -SDV high water level. The SDV provides a controlled containment for reactor water discharged from'the control rod mechanisms during a scram. An RPS actuation on SDV. high water level is initiated prior to the volume l> filling to a level in which insufficient capacity would remain in the volume to accommodate a scram.
l l
In the event, RPS functioned as designed. The scram inlet and outlet valves began:
drifting open as expected with station service air system low pressure. Since the l- control rods were full-in, no rods began drifting in as a result of this.
However, -the scram outlet valves drif ting open resulted in reactor water being lL ' directed to the SDV. When the SDV water level reached 57 gallons (the high level 1 trip setpoint), an RPS actuation was initiated. The actuation was a conservative action. -
At the time of the event, all control rods were full-in. Thus, no control rod movement resulted from the actuation. Also, at the time of the event, the unit l was in .the Cold Shutdown mode and, per the Unit 2 Technical Specifications, the SDV- High Level trip instrumentation is not required to be operable during the Cold L. Shutdown mode.
Based on the above information, it is concluded that this event had no adverse impact on nuclear plant safety. Since RPS functioned as designed, the event would
.have had no adverse impact on nuclear plant safety had the event occurred under other operating conditions, i
j l
N *.C FORM 3esA ,
'I' i 7 433
n b:;
NRC Peren MSA . . U.S. NUCLEJ.R REIULATOFY COMMIN400f
. 1.:lCENSEE EVENT REPORT (LER) TEXT CONTINUAT!ON eP*ovto oMe sojiao-oio.
EJRES: S/31/N F ACILITY teAME til. DOCKET NURSkft (2) LER NUMSER ($1 PAGE (31 n*a -
"20!P -
"a*.??
, - PLANT HATCH, UNIT 2 01510 l o l o l 3l6 l 6 8 l9 --
0 l0l9 , 0 10 0 l5 oF 0 -l5 TENT /F#ame spese 4 meutesf, ses ash 8nomer NRC Form m W (17l k
CORRECTIVE ACTIONS :
.LThe temporary air compressor was placed into service and the station service air ,
pressure restored. A blown fuse in the SSAC cooling water system; control circuitry was- replaced-and SSAC "C" was returned to service. -
The RPS actuation was reset.
The temporary . compressor was p1 aced in an. automatic mode of operation. In-this mode, the compressor automatically provides air to the--station service air system upon low system pressure and, thus, no manual actions are required by operating '
personnel. Procedure 34SP-090889-QX-1-2N has been revised to address the automatic mode of operation.
.s
', ADDITIONAL INFORMATION No systems other than RPS and the' Station-Service Air System were affected by this e vent.
No previous events have occurred in which an unplanned engineered safety features actuation occurred as the result of an equipment failure of a multimeter during troubleshooting activities.
L !
1.
l' I
I '
l i
i i
NR FOAM 366A 'U,5. CPos 1988-520-589.00d70 ;
. . . . . . - - . ..- .- -. .- . . . . . -- .-