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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
[Table view] |
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HL-1060 000393 April 23, 1990-U.S.- Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 PLANT HATCH - UNIT 2 NRC DOCKET 50-366 OPERATING LICENSE NPF-5 LICENSEE EVENT REPORT INADEQUATE PROCEDURE CAUSES REACTOR SCRAM AND GROUP 11 ISOLATION-Gentlemen:
In accordance with the requirements of_10 CFR 50.73(a)(2)(iv), Georgia Power Company is submitting the enclosed Licensee Event Report (LER) concerning the unanticipated actuation of some -Engine 6 red Safety Features (ESFs). This event occurred at Plant Hatch - Unit 2.
Sincerely, gfk.ff] #
W. G. Hairston, III JJP/ct
Enclosure:
LER 50-366/1990-003 c: (See next page.)
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I Gedrgialinver d U.S. Nuclear Regulatory Commission April 23, 1990 Page Two c: Georaia Powe Company Mr. H. C. Nix, General Manager - Nuclear Plant Mr. J. D. Heidt, Manager Engineering and Licensing - Hatch GO-NORMS U.S. Nuclear Reaulatory Commission. Washinaton. D.C. .;
Mr. L. P. Crocker, Licensing Project Manager - Hatch U.S. Nuclear Reaulatory Commission. Reaion 11 '
Mr. S. D. Ebneter, Regional Administrator Senior Resident Inspector - Hatch I
i 000393 ,
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. APPROVE) OMt NO 3144010s LICENSEE EVENT REPORT (LER) * * *'a' 8 8 '8' '"
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On 3/28/90 at approximately 0815 CST, Unit 2 was in the Run mode at an approximate power level of 2436 CMWT (approximately 100% of rated thermal power). At that time, a plant Instrument and Controls (I&C) technician was valving-in pressure transmitter 2E32-N050 following a routine calibration per procedure 57CP-CAL-103-2S, "ITT Barton Model 764 Differential Pressure Transmitter." Valving-in the pressure transmitter, which shares a common sensing line with Reactor Protection System (RPS) and Primary Containment Isolation System (PCIS) water level transmitters 2B21-N080C and D, caused a pressure perturbation in the sensing line which caused water level transmitters 2821-N080C and D to spike downscale. This resulted in a false low water level signal l being sent to the A2 and B2 trip channels in the RPS and the PCIS. Full scram and i partial Group 11 PCIS isolation signals were generated per design; the unit scrammed and the outboard Group II Primary Containment Isolation Valves (PCIVs) closed.
The cause of this event is an inadequate procedure. Procedure 57CP-CAL-103-2S did l not provide adequate instructions to prevent the pressure perturbation that resulted when pressure transmitter 2E32-N050 was valved-in. Furthermore, the procedure did I
not provide adequate return to service instructions (e.g., open links, install jumpers, lift leads) necessary to prevent a scram and PCIS actuation in the event of a perturbation in the common sensing line.
Corrective actions for this event include changing procedure 57CP-CAL-103-2S to correct these and similar errors, and reviewing and changing, as necessary, comparable Unit I and Unit 2 procedures.
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SUMMARY
OF EVENT On 3/28/90 at approximately 0815 CST, Unit 2 yas in the Run mode at an approximate power level of 2436 CMWT (approximately 100% of rated thermal power). At that time, a plant Instrument and Controls (I&C) technician was valving-in pressure transmitter 2E32-N050 following a routine calibration per procedure 57CP-CAL-103-25 "ITT Barton Model 764 Differential Pressure Transmitter." Valving-in the pressure transmitter, which shares a common sensing line with Reactor Protection System (RPS, EIIS Code JC) and Primary Containment Isolation System (PCIS, EIIS Code JM) water level transmitters 2821-N080C and D, caused a pressure perturbation in the' sensing line which caused water level transmitters 2B21-N080C and D to spike downscale. This resulted in a false low water level signal being sent to the A2 and B2 trip channels in the RPS and PCIS. Full scram and partial (outboard) Group 11 PCIS isolation signals were generated per design; the unit scramed and the outboard Group II Primary Containment Iso 1'ation Valves (PCIVs, EIIS Code BD) closed.
The cause of this event is an inadequate procedure. Procedure 57CP-CAL-103-2S did not provide adequate instructions to prevent the pressure perturbation that resulted when pressure transmitter 2E32-N050 was valved-in. Furthermore, the procedure did not provide adequate return to service instructions (e.g., open links, install jumpers, lift leads) necessary to prevent a scram and PCIS actuation in the event of a perturbation in the common sensing line.
Corrective actions for this event include changing procedure 57CP-CAL-103-2S to correct these and similar errors, and reviewing and changing, as necessary, comparable Unit 1 and Unit 2 procedures.
DESCRIPTION OF EVENT On 3/28/90 at approximately 0645 CST, Unit 2 was in the Run mode at an approximate power level of 2436 CMWT (approximately 100% of rated thermal power). At that time, a plant I&C technician began'the routine calibration of pressure transmitters 2E32-N050, 2E32-N058, and 2E32-N060 per procedure 57CP-CAL-103-25. These three pressure transmitters are part of the Main Steamline Isolation Valve (MSIV) Leakage Control System (EIIS Code BF). They provide pressure permissive signals to the logic of the MSIV Leakage Control System to allow the system to be actuated by the operator following a design basis loss-of-coolant accident.
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7tKT fr mese apose e #mensmW, ese ensupuW WAC 8 san JEd W (171 At approximately 0815 CST, the technician had completed the calibration of pressure ;
transmitter 2E32-N050 and was returning it to service per the requirements of the calibration procedure. When he valved-in the instrument, a pressure perturbation was created in the instrument's sensing line. This is a connon sensing line shared by several instruments, including water level transmitters 2B21-N080C and D. These instruments provide water level inputs to trip channels A2 and B2, respectively, in the ,
RPS and the PCIS.
The perturbation in the common sensing line caused RPS and PCIS water level transmitters 2B21-N080C and D to spike downscale. When these instruments spiked downscale, they transmitted a false low water level signal to trip units 2B21-N680C and ,
D. The false low water level signal was below the trip units' setpoint of l approximately 12 inches above instrument zero; therefore, the trip units actuated resulting in seal-in trips in the A2 and B2 trip channels of the RPS and the PCIS. The one-out-of-two-taken-twice logic of the RPS was satisfied and the unit scrammed per design. Likewise, the' minimum actuation logic for the outboard Group II PCIS was satisfied and the outboard Group II PCIVs closed per design.
Immediately following the scram, actual reactor water level decreased from void collapse to approximately 23 inches below instrument zero (to approximately 11.8 feet above top of active fuel). This is an expected and normal occurrence and resulted in another full scram signal and a full, i.e., inboard and outboard, Group II PCIS isolation signal on low water level approximately six seconds after receipt of the false low water level signal. All four RPS and PCIS trip channels, A1, A2, B1, and B2, tripped as a result of the actual low water level and the inboard Group II PCIVs closed.
Reactor water level was restored to its normal level of approximately 36 inches above l instrument zero at al. proximately 0852 CST using the Reactor Feedwater Pumps (RFPs, EIIS
- Code SJ ). Neither the High Pressure Coolant Injection (EIIS Code BG) system nor the
! Reactor Core Isolation Cooling (EIIS Code BN) system automatically started or injected i as water level never reached their automatic initiation setpoint of 35 inches below instrument zero (minimum water level during this event was approximately 23 inches below instrument zero). These two systems were not useo in the manual mode during this event because the RFPs were available and sufficient for water level recovery and control. '
Reactor vessel pressure was controlled with the Turbine Bypass Valves (EIIS Code S0).
Consequently, the Safety Relief Yalves (EIIS Code JE) were neither used nor needed during this event. Peak reactor vessel pressure was approximately 985 psig which is l normal operating pressure.
At approximately 0855 CST, the unit was in a stable condition and entering the Hot -
Shutdown mede with reactor water level being maintained at the normal level of approximately 36 inches above instrument zero.
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The cause of this event is a less than adequate procedure. Procedure 57CP-CAL-103-2S did not identify pressure transmitter 2E32-N050 as an instrument sharing a common ,
sent.ing line with RPS and PCIS instruments (" pressure boundary instruments").
Consequently, the !&C technician was not required by the procedure to pressurize the instrument to process (i.e., reactor) pressure before valving it into service. This is required by the procedure for those instruments identified as pressure boundary instruments in order to minimize the disturbance to other instruments on the sensing line. Because the instrument was not pressurized to process pressure (it was at approximately 0 psig when it was valved-in), a large pressure perturbation was created- i in the common sensing line when the instrument isolation valves were opened. This '
caused spiking in the water level transmitters resulting in a scram and a partial Group 11 PCIS isolation.
In addition, the procedure's return to service instructions for this instrument were less than adequate. Return to service instructions for other pressure boundary instruments contain steps (e.g., open links, lift leads, install jumpers) to prevent Engineered Safety Feature actuations in the event of a disturbance in a common sensing line. The return to service instructions for this instrument did not contain those steps necessary to prevent trips in both the A2 and B2 RPS and PCIS trip channels. As a result, the instrument spiking caused by the pressure perturbation actuated the logic ,
necessary to cause a scram and a partial Group II PCIS isolation. ,
I REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT This report is required per 10 CFR 50.73(a)(2)(iv) because an unplanned actuation of I Engineered Safety Features (ESFs) occurred. Specifically, the RPS actuated on a false low water level signal. The outboard Group II PCIVs of the PCIS, an ESF, closed on the ,
same false low water level signal. Approximately six seconds later, the RPS and PCIS logic systems actuated again and the inboard Group II PCIVs closed, this time on an actual low water level signal as voids collapsed from the scram.
The RPS provides timely protection against the onset and consequences of conditions, such as low water level, that could threaten the integrity of the fuel barriers and the -
nuclear system process barrier. A reactor scram initiated by a low water level condition protects the fuel by reducing the fission heat generation within the core.
The PCIS provides timely protection against the onset and consequences of events involving the potential release of radioactive materials from the fuel and nuclear system process barriers by isolating appropriate lines which penetrate the primary containment. Isolation of Group II PCIVs, initiated by a low water level condition, prevents the escape of radioactive materials from the primary containment through process lines which may have been breached. Additionally, isolation of these process lines conserves reactor coolant inventory if a breach of one of these lines caused the low water level condition,
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010 015 0F 016 innt .- . =ae w ma .nm In the event described in this LER, the RPS and the PCIS actuated and the outboard Group 11 PCIVs closed on a false low water level signal. Although no actual low water level condition existed, these systems functioned as if one did. All automatic functions of these two systems performed per design. Furthermore, when voids collapsed following the scram causing an actual low water level condition (a normal occurrence),
the RPS and PCIS logic actuated again and the inboard Group II PCIVs isolated per design.
Water level was restored to normal using the RFPs. Water level was never less than approximately 11.8 feet above the top of' the active fuel and, in fact, never got low enough to actuate any emergency core cooling systems. Based on this information, it is concluded that this event had no adverse impact on nuclear safety. The above analysis is applicable to all power levels.
CORRECTIVE ACTIONS Procedure 57CP-CAL-103-2S will be changed to require instruments to be pressurized to process pressure before they are valved into service. This will minimize the possibility of adverse system responses which might lead to an ESF actuation, The return to service instructions for pressure transmitter 2E32-N050 also will be changed to include those steps necessary to prevent a scram and PCIS actuation in the event of a disturbance in its sensing line as the instrument is being valved-in. Additionally, the procedure's return to service instructions for other instruments will be reviewed to ensure they are adequate to prevent ESF actuations. Changes will be made as needed. The review will be completed and the changes made before the procedure is used again.
Likewise. Unit 2 procedure 57CP-CAL-104-2S, "ITT Barton Model 763 Pressure Transmitter," and Unit 1 procedures 57CP-CAL-103-lS, "ITT Barton Model 764 Differential Pressure Transmitter," and 57CP-CAL-104-15, "ITT Barton Model 763 Pressure Transmitter," will be changed to require instruments to be pressurized to process '
pressure before they are valved into service. These three procedures' return to service instructions also will be reviewed to ensure they are adequate to prevent ESF actuations and changes will be made as needed. The reviews will be completed and the changes made before the procedures are used again, gag.o.. .v s o.o ....o en sa J.
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ADDITIONAL INFORMATION i
- 1. Previous Similar Events:
There was one similar event in which the reactor scrammed from a false low water r level signal. That event was reported in LER 50-321/1988-002, dated 5/6/88. In i that event,1&C personnel were backfilling the reference leg of pressure transmitter 1C32-N004B as part of corrective maintenance activities. That reference leg is shared by RPS and PCIS water level transmitters 1B21-N080C and ,
D. The action of backfilling the comon reference leg caused level transmitters
- 1B21-N080C and D to transmit a false low water level signal to A2 and B2 trip channels, respectively, of the RPS and PCIS logic. As a result, the reactor scrammed and the outboard Group 11 PCIVs isolated. The corrective actions for that event would not have prevented this event because the causes of the two events are different. The previous event was caused by personnel error whereas :
this event was caused by an inadequate procedure.
- 2. Failed Component Identification:
There were no failed components involved in this event. Pressure transmitter 2E32-N050 was being calibrated as part of routine instrument calibration activities and not as part of corrective maintenance activities.
- 3. Other Affected Equipment:
No systems other than RPS and PCIS were affected by this event.
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