ML20028H656

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LER 89-010-02:on 890905,leak Occurred on Containment Spray HX 2A After Valve Stroke Timing.Caused by Defective Procedure Due to Incomplete & Ambiguous Info.Gasket Replaced & Piping Analyzed & Returned to svc.W/910117 Ltr
ML20028H656
Person / Time
Site: Mcguire
Issue date: 10/23/1989
From: Mcconnell T, Sipe A
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-010-01, LER-89-10-1, NUDOCS 9101240162
Download: ML20028H656 (13)


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- fluntersville, NC 28078-8985 DUKE POWER January 17, 1991 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555

Subject:

McGuire Nuclear Station Unit 2 Docket No. 50-370 Licensee Event Report 370/89-10-02 Gentlemen:

Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached is Licensee Event Report 370/89-10-2 concerning a leak that occurred on Containment Spray Heat Exchanger 2A after valve stroke timing. This report is being submitted as a Voluntary Report. This event is considered to be of no significance with respect to the health and safety of the public.

Very truly yours, d< M Q T.L. McConnell DVE/ADJ/cbl Attachment >

xc: Mr. S.D. Ebneter Mr. Tim Reed

Administrator, Region II U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Office of-Nuclear Reactor Regulation

.101 Marietta St., NW, Suite 2900 Washington, D.C. 20555 Atlanta, GA 30323 Mr. P.K. Van Doorn INPO Records Center NRC Resident Inspector Suite 1500 McGuire Nuclear Station l- 1100 Circle 75 Parkway Atlanta, GA 30339 M&M Nuclear Consultants 1221 Avenue of the Americas New York, NY 10020 9101240162 891023

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At approximately 1655, a leak was reported in the Auxiliary Building-716' elevation pipe chase. About a minute later level began decreasing in the Refueling Water Storage Tank. After several valve manipulations, CR personnel determined the problem was with NS Heat Exchanger ODO 2A. A-visual inspection at 1900 revealed a leak on the HX at the lower head gasket. CR personnel closed valve 2NS-20A,.NS Pump 2A Suction From Refueling Water Storage Tank Block, which isolated the leak.

Later estimates concluded that approximately 10,000 gallons of water leaked through the gasket. This event is assigned a cause of Procedure Deficiency because of ambiguous and incomplete information concerning stroking of valve 2NS-18A. This event is also assigned a cause of Inappropriate Action because of lack of attention to detail. The gasket was' replaced and the affected ~NS system piping was analyzed and returned to service. Unit 2 was in Mode 5, Cold Shutdown, with the Reactor Coolant system at 305 psi and 139.5 degrees-F, and Residual Heat Removal (ND) Pump 2A in operation. This report is being written as a Voluntary LER.

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Background

The NS system {EIIS: bel is an engineered safety feature which serves to remove thermal energy from the Containment in the event of a Loss Of Coolant Accident (LOCA). It performs this function in conjunction with the Emergency Core Cooling System (ECCS), which cools the Reactor (EIIS:RCT) core by direct injection. After all the ice from the Ice Condenser has melted, the heat removal capability of the spray system will keep the Containment pressure below the design pressure of 15 psig.

The NS system consists of two pumps (EIIS:P] and two heat exchangers (EIIS:HX] in parallel, with associated piping, valves (EIIS:V], and spray headers. These spray headers are located in the upper Containment volume. This system is supplemented with two ND system pumps and two ND heat exchangers in parallel, with associated piping, valves, and individual spray headers. These spray headers are also located in Upper Containment.

The NS HXs are of the shell and tube type with the tubes welded to the tube sheet.

Borated water from either the Refueling Water (EIIS:DAl Storage Tank [EIIS:TK)

(RWST) or the lower compartment of the Containment circulates through the tubes while nuclear service water circulates through the shell side. The spray heat exchangers are designed to assure adequate heat removal capacity from the water during the recirculation mode. The NS HXs were manufactured by Delta Southern.

The head gaskets for the NS HXs are Garlock " Blue-Gard", style 3000, which is a suitable compressible gasket for this application. Torque value for the gasket bolts is 150 ft-lbs as required by procedure MP/0/A/7150/069, Containment Spray Heat Exchange Cover Plate Removal. The HXs were preoperationaily hydrostatically pressurized to 345 psig by the manufacturer.

The NS system was preoperationally hydrostatically tested by Duke Power's Construction Department according to established ASME Section III code procedures.

The actual hydrostatic pressure was 284 psig. The normal operating pressure of the NS system is approximately 170 psig.

The primary function of the ND system (EIIS:BP] is to remove heat energy from the Reactor Core and Reactor Coolant (NC) system (EI!9 t AB) during plant cooldown and refueling operations. This system is also used a part of the Safety Injection

-(NI) system (EIIS:BQ} and NS system. As a secottary function, the ND system is used to transfer refueling water between the RWST and the Refueling Canal at the beginning and end of refueling operations. Two taotor-operated valves (ND-1B and ND-2A, NC Loop C Discharge to ND System Isolation) located in series isolate the ND section piping from the NC system.

Description of Event On September 5,1989, at approximately 1600, Performance (PRF) personnel presented CR personnel with a list of valves to be stroke timed. These valves were required l

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0j 2 l3 OF 1l2 ssx1 m em . .w.a. me.ac n. nu emn to be stroke timed before Unit 2 entered Mode 4, Hot Shutdown. Included was valve 2NS-18A, which would be stroked using procedure PT/2/A/4208/02, NS Valve Stroke Timing - Quarterly. Operator A in the Control Room (EIIS:NA] reviewed the portion of the procedure applicable to valve 2NS-18A to ensure all prerequisites were met and to evaluate system conditions before opening the valve. After his review and evaluation were completed, Operator A granted permission to cycle valve 2NS-18A.

The NC system was at 305 psi and 139.5 degrees-F with ND Pump 2B in operation (reference page 10 of 12).

At 1608:59, oCR personnel opened the valve. The valve became fully opened at 1609:10. CR personnel then noticed the level decreasing in the Pressurizer (EIIS:PZR] and the level increasing in the Pressurizer Relief Tank. They also noticed NC system pressure decreasing and KD system pressure decreasing. Valve 2NS-18A was closed at 1610:29 and became fully closed at 1610:39. An operator was sent to check NS Pump 2A for damage. No damage was observed. At 1629, CR personnel opened valve 2NS-20A as allowed by procedure to return to the pre-test valve alignment. Radwaste Chemistry personnel notified CR personnel at approximately 1655, of ilooding in the Auxiliary Building (EIIS:NF] at the 716' elevation pipe chase. Water was coming through Spent Fuel Pool Cooling (KF) system Filter [EIIS:FLT] Pit reach rod holes. At 1656, CR personnel noticed RWST level decreasing and closed valve 2NS-20A. An operator went to the 716' elevation pipe chase to observe the flooding. He then isolated the Spent Fuel Pool Purification system valve which appeared to stop the flooding. Mechanical Maintenance (KNT) personnel removed a cover from the KF system Filter Pit which revealed the pit level decreasing. The Spent Fuel Pool Purification system was then restarted and no leaking was observed. CR personnel then re-opened valve 2NS-20A at 1823 and the pit level began to increase. CR personnel closed valve 2NS-20A at 1830. At 1900, Operator A, now believing the leak was associated with the NS system piping, went to the NS HX 2A room and observed water on the floor. He called the Control Room and had valve 2NS-20A opened. He then noticed water spraying from bottom of the HX

which he suspected as being caused by a ruptured gasket. Valve 2NS-20A was
subsequently closed which stopped the leak. Operator A then returned to the Control Room and submitted Work Request (WR) 139654 to repair the leak on the HX.

i f MNT personnel replaced the HX gasket on September.7, 1989 using WR 139654. The i gasket was torqued to 200 ft-lbs as recommended by Design Engineering (D.E.)

l personnel. The nominal torque for this gasket is 150 ft-lbs. The HX cover to shell clearance was measured at the bolt circle to ensure gasket compression was not being hampered by metal to metal contact. Values measured at 4 points were approximately 0.07 inches. D.E. personnel also performed an Operability Evaluation on September 8, 1989 which concluded that'the portion of the NS system exposed to NC pressure suffered no degradation which would prevent the NS system from being returned to service. However, this portion of the NS system was hydrostatically pressurized to 242 psi, which is 110 percent of the design operating pressure (220 psi). The NRC and Station Management felt it prudent to pressure test the new gasket installation. This test also revealed no resulting degradation. Valve 2NS-19, NS Pump 2A Suction Safety Relief, was independently pressure tested.

During the test, this valve began leaking by and was subsequently repaired.

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pressure gauge 2MNSPG5100, manuf actured by Weschler, range of 0-60 psi; pressure gauge 2MNSPG5120, manufactured by Barton, range of 0'1175 in. W.D.;

pressure switch [EIIS:PS] 2MNSPS5080, manuf actured by Weschle r, range of 0-250 psig and a high setpoint of 197.34 psig increasing; and flow transmitter [ Ells:FT] 2tiNSFT5020, manuf actured t t Weschler.

Pressure gauge 5100 was found damaged and had to be replaced, 11d the high setpoint of pressure switch 5080 was found at 185.9 psig and had to be r u librated. This work was documented on WR 69526.

Conclusion This event has been assigned a cause of Defective Procedure because of incomplete and ambiguous information. Section 12.5 of the NS Valve Timing procedure contains the step to stroke time valve 2NS-18A (reference page 11 of 12). Step 12.5.5, is the step where CR personnel became involved to grant permission to stroke the valve. This step reads " Ensure system conditions have been evaluated by Control Room Senior Reactor Operator (SRO) or Unit Supervisor, and specific permission for stroking 2NS-18A is granted." This step does not give any specific guidance to the CR personnel as to adverse conditions, situations, or valve alignments to be analyzed. It is left up to the CR personnel to ensure everything is satis f actory.

The substeps contained in step 12.5.7 are actually prerequisites which direct attention to the NS system. In step 12.5.7c, a jumper is installed to allow operation of valve 2NS-18A without opening valve 2NI-185A, Containment Sump Line 2A Isolation, but only jumper connections are given and not the valves which are l

affected. Steps 12.5.7d and 12.5.7e focus on conditions necessary to prevent air l

induction into the NS or ND piping. No caution is given which addresses l

intersystem overpressurization (reference page 11 of 12). Steps 12.5.5, 12.5.7d, and 12.5.7e were added to this section on May 22, 1989, as a result of an incident on November 23, 1988 in which air became bound in the Unit 1 ND piping when valve INS-18A, NS Pump 1 Suction from Containment Sump Blo:k, was stroke timed during mid-loop operation (reference LER 369/88-49). Operations personnel aided PRF personnel in the wording of this change.

1 On July 21, 1988, a non-reportable incident (Problem Investigation Report (PIR) 2-M88-0187) occurred involving the stroke timing of valve 2ND-58A, ND HX 2A Outlet to Centrifugal Charging Pump 2A and 2B Block, which overpressurized the Unit 2 Chemical and Volume Control (NV) [EIIS:CB} and NI pumps suction piping to the existing NC system pressure of approximately 325 psig. As a result of this incident, PRF personnel made procedure changes to the valve stroke timing f procedures to ensure that ND system pressure is lower than NV and NI suction pressures when stroking valves ND-58A and NI-136A, ND HX B To Safet/ Injection Pump B. A similar change was made concerning valve FW-27A, FWST To ND Pump Isolation, to protect RWST piping. However, valves NS-18A and NS-1B, NS Pump B From l Containment Sump Block, were overlooked during this review. PRF personnel stated they were concentrating on valves which could allow ND pump discharge pressure into another system.

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01 2 15 112 ftXY l# meerg spece e regweest, var edamoew NAC Fame D5A s! Oh This event has also been classified as an Inappropriate Action because of a lack of attention to detail. Operator A analyzed the existing system conditions for the possibility of introducing air into the NS or ND system, even though conditions existed to overpressurize the NS piping through valve 2N'D-19, Supply to NC Loop A Control Bypass. As previously stated, the sect. ion of the NS valve timing procedure concerning valve 2NS-18A focused attention on preventing air induction into the NS or ND system. Operator A remembered the November 23, 1988 incident and had received training concerning the prevention of air binding pumps. lie was also aware of the NRC's concern of this type problem. So, when he read the procedure step to evaluate system conditions and the procedure steps concerning air induction, his mind became focused on the air problem and not the potent.lal for overpressurization. He stated he did not remember the July 21, 1988 incident of overpressurizing the NV pumps suction piping. He also stated that someone had told him that valve 2NS-1B had just been cycled several days ago. Knowing that the unit had 'not undergone a mode change, he erroneously assumed conditions had not changed.

In ad,dition, he stated he had been involved in valve timing procedures many times and had developed confidence in the adequacy of this procedure. Also, most CR personnel have developed confidence in periodic test procedures. Since most tests are performed on a periodic basis, most SR0s have been involved with these without incident.

This test was performed on Tuesday, September 5, one day after the Labor Day holiday. Labor Day weekend was a relatively light work weekend because of the decreased number of personnel on site. However, with Unit 2 coming out of an outage, September 5, 1989 proved to be a busy, catch up day. The new Mode 4 date was moved up to September 13, 1989, with still many items and tests to be completed before Mode 4 could be entered. Operator A was responsible for coordinating activities and reviewing numerous periodic test work packages.

Different priorities exist between the Operations group and the PRF group when scheduling performance tests. During an outage, many tests, including valve timing tests, are scheduled during a block of time. It is the responsibility of Performance personnel to complete these tests in that time block, i.e. before entering Mode 4. However, maintenance is also scheduled during this same block of time, and because of various reasons may actually take longer than originally planned. PRF personnel are not able to perform many of their tests until maintenance is complete. Testing then tends to concentrate at the end of the time block after maintenance is comh ete. This presents problems to CR personnel who may have other procedures scheduled or other items that have a higner priority.

Integrated Scheduling personnel have estimated that possibly up ti. 'O percent of outage work is performed on day shift, Monday through Sat.urday. .tation personnel will evaluate the possibility of spreading out the workload to balance day / night refueling outage workload.

The head gasket for NS HX 2A had been rr.;placed in October, 1988 as documented on WR 96042 and procedure MP/0/A/7150/069, Containment Spray Heat Exchanger Cover Plate Gasket Removal, and was torqued to 150 ft-lbs. The NS pumps were then run to ensure there were no leaks. However, after the leaking gasket was removed on September 7, 1989, tint personnel noticed that a section of the gasket approximately l 12 to 15 inches long and 1/8 to 3/16 inches wide (on the outside diameter) was not  !

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compressed because of misalignment during' the October,1988 replacement. A gasket compression check was not documented in WR 96042 and there is no requirement to check gasket compression in the gasket removal procedure, McGuire Engineering Services (HES) personnel stated that because of the HX orientation and gasket cover configuration, it is almost impossible to check alignment (reference page 12 of 12). However, MES personnel have performed a review of the gasket removal procedure and believe that section 11.3 is adequate to ensure proper gasket alignment.

In the Operability Evaluation for the NS system dated September 8,1989, D.E.

personnel stated that a phenomenon called relaxation also contributed to the gasket leak. Relaxation occurs when a bolt loses its initial torque load as a result of )

conditions such as lack of proper bolt lubrication, thermal cycling, vibration, c__

temperature gradients, pressure gradients, and loss of gasket resiliency after compression, and can be as high as 25 percent. Relaxation of initial belt load (150 ft-lbs) resulted in a bolt load that, at best, was marginal and possibly below that required to withstand 305 psi, especially at the area of non-compression.

However, DE personnel stated that even with the gasket misalignment and the relaxation phenomenon, 150 ft-lbs was sufficient torque to prevent a gasket leak at normal operating pressure. D.E. has recommended a torque valve of 200 ft-lbs which will be incorporated into the appropriate procedures for an additional margin of safety.

During this incident, approximately 10,000 gallons of water leaked into the Auxiliary Building. About 2,000 gallons entered the NS system from the ND system.

The RWST is located on 760' elevation and the NS HX leak was located at approximately 735' elevation. Therefore, when valve 2NS-20A was opened, water from the RWST gravity fed the HX leak. About 8,000 gallons drained from the RWST.

Relief valve 2NS-19 lifted as required (Design lift pressure is 220 psig).

However, this valve is on a 1 inch line and functions only as a relief for thermal expansion. Therefore, this line was not able to fully relieve the NS piping of the additional pressure. Based on chart recorder trends, about 200 gallons of water passed through this line into the Pressurizer Relief Tank.

A review of the previous year's incidents revealed I similar event. As described earlier, PIR 2-M88-0187 involved stroke timing valve 2ND-58A which overpressurized the Unit 2 NV and NI pumps suction piping to existing NC system pressure of 325 psig. Theretore, this event is recurring.

This event _is Nuclear Plant Reliability Data System (NPRDS) reportable-as an overpressurization event requiring component repair or replacement.

There were no personnel injuries, radiation overexposures, or uncontrolled releases of radioactive material to the environment as a result of this event.

CORRECTIVE ACTIONS:

Immediate: CR personnel closed valve 2NS-18A.

! Subsequent: 1) CR personnel closed valve 2NS-20A.

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2) MNT personnel replaced the gasket on NS HX 2A using WR 139654 on September 7, 1989,
3) PRF personnel successfully performed procedure PT/2/A/4208/01A, NS Pump 2A Performance Test.
4) PRF personnel successfully performed procedure PT/2/A/4208/010A, Train 2A NS HX Heat Balance Test. l
5) DE personnel performed a component by component analysis of the affected portion of the Unit 2 NS system. This analysis is documented in calculations referenced in the resulting operability evaluation.
6) PRF personnel revised procedures PT/1 and 2/A/4208/02, NS Valve Stroke Timing-Quarterly, to require that one'of the following conditions are met before stroke timing valve NS-18A or valve NS-1B: ,

valve ND-1, NC Loop C Discharge To ND Syntem Isolation, and valve ND-2, NC Loop C Discharge To ND System Isolation are closed OR NC system pressure is less than 100 psig.

7) MNT personnel overtorqued the cover bolts on the replaced NS HX 2A gasket to 200 ft-lbs.
8) The affected portion of the NS system was successfully hydrostatically pressurized to 242 psi.
9) Relief valve 2NS-19 was rebuilt by MNT personnel.
10) Operations personnel reviewed this incident with personnel involved and with all Shift Supervisors.
l. 11) MNS personnel checked the integrity and calibration of the affected NS field instrumentation. Pressure gauge 2MNSPG5100 l.

' was replaced and pressure switch 2MNSPS5080 was recalibrated.

12) MES personnel performed a walkdown of the affected portion of the NS system and discovered no visible degradations.
13) WRs 502675, 502676, and 502677 have been written by KNT personnel to remove and-test the following valves to ensure that-no internal degradation has occurred: valve INS-2, NS Pump 1B Suction Safety Relief; valve INS-19, NS Pump 1A Suction Safety Relief; and valve 2NS-2, NS Pump 2B Suction Safety Relief.
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14) MNT personnel have written WRs 502627, 502628, and 502629 to overtorque NS HX 2B and Unit 1 NS HXs main gasket covers to 200 ft-lbs.
15) MES personnel have made changes to procedure MP/0/A/7150/69, Containment Spray Heat Exchanger Cover Plate Gasket Removal and Replacement, which specify a cover plate overtorque value of 200 ft-lbs should leakage occur after the system is pressurized.

Planned: 1) Operations, PRF, and D.E. personnel will review ECCS valves and identify. system conditions allowable for valve stroke timing and produce a McGuire valve reference document for station use.

2). Based on the results of item 2, PRF personnel will upgrade appropriate valve stroke timing procedures.

3) Operations personnel will review existing training to ensure that incidents described in PIRs and LERs are covered with appropriate Operations personnel.
4) MES personnel will change section 9.0 of procedure MP/0/A/7150/69, Containment Spray Heat Exchanger Cover Plate Gasket Removal, to verify no external leakage during subsequent running of appropriate NS pump by PRF personnel after gasket replacement.
5) Integrated Scheduling personnel will facilitate a review to evaluate the possibility of balancing day / night refueling outage workload.
6) Operations Shif t personnel will normally schedule 4 Shif t SR0s at the plant during outage times: 1 Shift Supervisor and 3 Assistant Shift Supervisors. This will spread the work load and-decision making responsibilities over a larger number of knowledgeable individuals, thereby minimizing the work load on the SR0s.

SAF"TY' ANALYSIS:

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The stroke timing test of valve 2NS-18A caused the valve to be either fully or

! partially open for approximately one minute and forty seconds. During this time, approximately 2000 gallons of primary coolant were diverted to the pump suction piping of .NS Train 2A via the in-service train of ND. Control Room indication of coincident decreasing Pressurizer level alerted Operators that a fairly significant leak or rupture had occurred and valve 2NS-18A was immediately closed.

The circumstances surrounding the scenario which occurred were of a nature such that comparison to the FSAR Chapter 15 Safety Analysis is conservatively non-applicable because of the Mode 5 conditions. However, for the purpose of l

classification, Section 15.6 of the FSAR describes Decreases in Reactor Coolant l

Inventory, within which.this event is substsntially bounded by either the "T'nndvertent Openine of a' Pressurizer Safety Valve or Relief" event. o r the ."T.os s

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  1. J.cate rY NAM 4 (1) DOC R i f NUMS E R (21 LE R NUMBE R 46 PAGt (3L

~- "w::w n,n McGuire Nuclear Station, Unit 2 o l5 l o j o j o l 3 j 7l 0 8; 9 __

0l lj o __ 0 2 9 or 1 2 rex 7 m - .-w Nec w., m inin of Coolant Accident." The event which occurred amounts to a momentary loss of primary coolant of a measurable amount, during Mode 5 conditions, which later became radiologically diluted with borated water from an alternate source.

In the event that valve 2NS-18A was unable to close or be closed, valve 2ND-19 was capable of being closed from the Control Room. However, if conditions had progressed to a point indicating the symptoms of a loss of residual heat removal capability, such conditions would be covercd by the symptoms and guidelines of AP/2/A/5500/19, Loss of Residual Heat Removal System, Case IV, Leak ar Rupture of ND system. Case IV directs the securing of ND Pumps, isolation from the NC System, isolation of the leak, and restart of the KD Pumps.

Automatic control associated with charging and letdown, which would have been in service at the time of the event, would have responded to makeup NC inventory based on pressurizer level response. Decreasing pressurizer level would result in modulation of the Centrifugal Charging Pump (CCP) discharge control valve for the usual case of normal charging with one of the CCPs, or by an increase in the Reciprocating Charging Pump (PDP) speed for PDP operation.

An assessment of the consequences of a similar event occurring during power operation is not applicable since the ND System would be out of service and isolated from the NC System.

The cause of the leaking heat exchanger gasket, the cycling of valve 2NS-18A, was corrected unknowingly by reclosing the valve according to the test procedure, which initially also secured the feeding of the system leak. However, exiting the test procedure involved returning valves to a normal lineup position which for valve 2NS-20A was open. This provided an alternate flowpath to the NS Pump suction from the Refueling Water Storage Tank (RWST), an uncontaminated borated water source.

Flow was propagated by a static head relative to the pump. Complications in identifying the lean source as the 1[X head gasket resulted in several cyclings of valve 2NS-20A, which over approximately a three-hour period, produced a total spilled volume of roughly 10,000 gallons.

Approximately 14 percent of the Unit 2 Auxiliary Building, involving elevations 733', 716', and 695', became contaminated. This was due to water leaking through ductwork,pt:netrations,andgrains. Thecontamjeationlevels in the NS HX 2A room measured from 180 mead /100 cm to 800 mrad /100cm at the HX where the leak occurreq.

Contamination levgls in the area outside the HX room measured from 1000 dpm/100 cm' to 50 mrad /100 cm'. Airborne activity as a result of this incident did not exceed 25 percent of the maximum permissible concentration as defined in 10CFR20 Appendix F. The water was analyzed to be decayed primary coolant with normal activity containing no noble gases or iodines. Also, the contaminated water was entirely contained within the Auxiliary Building. There was no release of water to the outside environment.

The spilled water cleanup is essentially complete, with a few minor areas remaining.

l This incident did not af fect the health and safety of the public.

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.. LICENSEE EVENT REPORT (LER) TEXT CONTINU ATION in ars em .

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McGuire Nuclear Station, Unit 2 0 l5 l0 l 0 j o l 3 l 7l 0 Bj9 - 0 j 1l0 MO g 2;1g 0 .o F 1l 2 ,

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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION w ovio n.s .o um e exeass see etciury ma.g m occatt mu.een m Lam qu eta se6 ,408 tb

...a " t t.M ." F'M.12 McGuire Nuclear Station. Unit 2 0 l5 l 0 l 0 l 0131710 8l9 -

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. Pg 8 of 37 12.5 valve, Stroke Tiains for 2FSISA - NS Pump 2A Suction free Cont. Suay-

+ Block .

Iaitial/Date. .

TEST PREPAAATION

/ 12.5.1 If valve is administratively control) ,d La its safety position, verify valve is recorded in PT/2/A/4203/01, Performance Special Valve Controlling Procedure and N/A remaining Section 12.5. ,

12.5.2 Record previous valve stroke time PVST .

12.5.3 Record date of last remote position indicator verification:

Date .

12.5.4 Record Reference Stroke Time Range free IWV Data Base

. Range to . ,

TEST METHOD

/ (SRO) 12.5.5- Ensure systes conditions have been evaluated by contro1'

/ Room SRO or Unit Supervisor, and specific permission for stroking 2NS18A is granted.

12.5.6 Required Unit Statust None Record currest operationsi modet .

12.5.7 Verify Prerequisite Systee Condittoas a) NS Pumps 2A and 28 are OTy. i

/

/- b) Verify CT.0 SED or have operatione CI,08E 2N820A

/ IV (NS Pump 2A Suction from TWET Block).

/

c) Place a jumper between 5 6 and 5-7 in 2ATC21 (716,

/ IV 0G54)..

/ (SRC) d) If ND Pump 2A or 23 is operating. _ verify NS Systes is water solid by venting at 2ND94 to prev.at. inducing att into ND pump saction piping. ** M'818%* /# ## P f M -

/ (SRO) e) If ND Pump 2A or '2B is operating, verify NS Pump 2A has been run and Train A filled and vested since last NS dratadown. This will ensure that no air is present in the NS Train to act as an accumulator, and push air / water to ND suction.

I 12.5.8 Record valve initial position: .

/ 12.5.9 If required, have Operations Ct.0SE 2NS18A.

/ IV

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1 [ u 8 44CLE AA Ktentato3Y Comasissiose UCENSEE EVENT REPORT (LER) TEXT CONTINUA (10N Ancove co. o pic.oix

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N N

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