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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:RO)
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20154L6321998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for McGuire Nuclear Station,Unit 1 ML20153B3741998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236U1601998-07-31031 July 1998 Non-proprietary DPC-NE-2009, DPC W Fuel Transition Rept ML20237B2381998-07-31031 July 1998 Monthly Operating Repts for July 1998 for McGuire Nuclear Station,Units 1 & 2 ML20153B3931998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236P0451998-07-0808 July 1998 Part 21 Rept Re non-conformance & Potential Defect in Component of Nordberg Model FS1316HSC Standby Dg.Caused by Outer Spring Valves Mfg from Matl That Did Not Meet Specifications.Will Furnish Written Rept within 60 Days 1999-09-30
[Table view] |
Text
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- Duke hwer Company I?00]#I5'#000
... McGuire Nuclear Station s- 12700flagen ferry Road.
Huntentille, NC28018 8985
_ DUKEPOWER June 13, 1990
-U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Subject:
McGuire Nuclear Station Units 1 and 2 Docket No. 50-369 Licenree Event Report 369/90-10
~ Gentlemen
-Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached is Licensee Event Report 369/90-10 concerning the Annulus Ventilation and Control Room Ventilation System filter train heaters that were inadequately sized because of a Design Deficiency. This report is being submitted in accordance with 10 CFR 50.73(a)(2)(v) and (a)(2)(1). This event is considered to be of no significance with respect-to the health and safety of the public, j 1
Very truly yours,
- 2. N .I T. cConnell j l
DVE/ADJ/cbl iAttachment j xc: - Mr. S.D. Ebneter American Nuclear Insurers i Administrator, Region II c/o Dottie Sherman, ANI Library
-U.S. Nuclear Regulatory Commission The Exchange, Suit 245 101 Marietta St., NW, Suite 2900 270 Farmington Avenue Atlanta, GA 30323 Farmington, CT 06032
/ INPO Records Center 'Mr. Darl Hood ,
. Suite 1500 U.S. Nuclear Regulatory Commission l 1100 Circle 75 Parkway Office of Nuclear Reactor Regulation-Atlanta, GA 30339 Washington, D.C. 20555 o i M&M Nuclear Consultants Mr. P.K. Van Doorn
'1221 Avenue of the Americas NRC Resident Inspector New York, NY 10020 McGuire Nuclear Station O b
e ,
LER 369/90-10 '
'P:ga 2 .
June 13, 1990 bxc: B.W.'Bline L.G. Bost J.S. Warren R.L. Gill-C.L. Hartzell-(CNS) l R.S. Matheson (ONS) l P.R. Herran S.S. Kilborn (W) l R.E. Lopez-Ibanez ,
y M.A. Mullen L R.O. Sharpe (MNS)
G.B. Swindlehurst 1
K.D. Thomas l H.S. Tuckman L L.E. Weaver >
R.L. Weber I, J.D. Wylie (PSD) ;
J.W. Willis QA Tech. Services.NRC Coordinator (EC 12/55)
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'* The Annulus Ventilation and Control Room Ventilation enev System Filter Train Heaters Were Inadeaustely Sized Because of a Desien Defic <
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Alen Sipe, Chairman, McGuire Safety Review Group COMPLETE ONE LING FOA t ACM CoasPONENT F AfiURt Ot9CRISED n IN TMit AtPORT t13) gNC ORfag pp
' CAUSE SysttM COMPONE NT CAust SylTEM COMPONENT - $N#AC- g R{0 PR S 1 I I I I I I 1 I I I I i 1 I I I I I i 1 MONTM OAv vtAR I I I I I I I SUPPLEMENT AL REPORT lxPECTED (14 1 l0 0l1 9l 0 G No xl vts irrv . c v. turcreo .u...,..
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ffects of In March of 1990, Catawba Nuclear Station personnel were reviewing the eIt potentially degraded grid voltage.(VE) and After reviewing Control theRoomMcGuireVentilation VE and VC (VC) sy under all postulated operating conditions.
system heaters, it was determined they would not operate as designed postulated operating conditions. Unit 2 was in Mode 1 5.(Cold Shutdown) preparing to enter Mode 4 (Hot Shutdown).An Operability Ev (Power Operation) at 100 percent power. Subsequently, Unit 2 VE system and Unit I and Unit 1 and Unit 2 VE and VC systems. However, Unit 1 VE 2 VC systems were determined to be conditionally operable.An emergency Technical S system was determined to be inoperable. change 11, 1990. request Presently, was' the submitte
- 1990. The NRC approved the emergency TS change on May change to Unit 2 is administrative in nature only because it shares After a common that TS The change will only apply until July 16, 1991.. This event document with Unit 1.
time, the NRC will require the Unit I and a Unit 2 TS to read th systems due to design oversight.
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l EVALUATION:
Background l VE System The main purpose of the Annulus Ventilation [EIIS:VD) (VE) system is to create and maintain a negative pressure zone in the annulus following a Loss of Coolant Accident (LOCA), to minimize the release of radioact .m material following a LOCA, l and to provide long term fission product removal, n- system supplies two VE trains. Each train consists of a filter package [EH d:FLT), a fan (EIIS: FAN] which draws in approximately 8000. cubic feet per minute (cfm) +/- 10 percent of annulus I air, dampers [EIIS:DMP], instruments, and ductwork. The filter package is designed l to help maintain the offsite radiation dose within the 10CFR100 guidelines which states in part the thyroid and the whole body doses at the exclusion area boundary and the low population zone are not to exceed 300 rem and 25 rem, respectively.
The filter train consists of a moisture eliminator, a preheater, a prefilter, two high efficiency particulate air (IEPA) filters, and a gasketless carbon adsorber j
[EIIS: ADS). Holsture is removed from the incoming annulus air by the moisture i eliminator. The assumed 100 percent relative humidity is reduced to 70 percent or l i; less by the preheater. Large particles are removed by the prefilter; removal of I I radioactive particles or particles which would effect the efficiency of the carbon I adsorber are removed by the IEPA filter and iodine is removed by the carbon adsorber. The reduction in relative humidity to 70 percent or less is necessary in ;
order to ensure the decontamination ef ficiency of 95 percent is maintained in the ;
carbon adsorber.
VC System The Control Room Ventilation System [EIIS:VI] (VC) and the Control Area Chilled Water (EIIS:KM] System (YC) combine to perform the Control Room habitability l function. This background will be restricted to the VC system. Th.e VC system consists of three subsystems. The Control Room [EIIS:NA] subsystem provides a i habitable environment for the main Control Room. The Control Room area subsystem provides heating and cooling for the electrical penetration rooms, battery rooms,
. motor control center (EIIS:MCC] (MCC) rooms, cable rooms, restricted instrument shop, and mechanical equipment room. The switchgear (EIIS:SWGR] subsystem provides heating and cooling for four essential switchgear rooms. The Control Room subsystem has two redundant trains (A and B). These trains are cross connected. I Each train consists of a filter package and an air handling unit (EIIS:AHU] (AHU). l Each filter package includes a preheater [EIIS:HTR], demister/ pre-filter, a IEPA ;
filter, a gasketless charcoal adsorber and one 100 percent capacity outside air pressure filter train (OAPFT) fan. Each AHU contains a water cooling coil and a i I
fan. Both A and B trains share a smoke purge exhaust fan which is provided to remove smoke or noxious gases within the Control Room on demand. The preheater l maintains the air at approximately 70 percent relative humidity or less to assure the efficiency of the carbon adsorber. The demister/ pre-filter removes entrained water droplets (if any) and large particles of dust, etc., from the air stream
'before it reaches the IEPA filter. The IEPA filter then removes dust particles, ,
-smoke, etc. which may be either radioactive or harmful to the efficiency of the l
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i nmn . w awwee mmmin carbon adsorber. The gasketless carbon adsorber adsorbs radioactive iodine. The Control Room temperature sLould be maintained at approximately 75'F in order to assure habitability and proper electrical equipment operation during normal operation. During a LOCA the filter package and associated OAPFT fan of the e related train shall be activated. When the OAPFT fan is actuated, about 2000 CFM of air is drawn through a two stage air heater and the filter package. The filtered air and the remaining Control Room return air then passes through a ;
pre-filter and the Control Room AHU to the Control Room. The outside air makeup pressurizes the Control Room.
Technical Specification 4.6.1.8 states, in part, the VE systems will be demonstrated operable by verifying, that a laboratory analysis of a representative ,
l carbon sample obtained in accordance with Regulatory Position C.6.b. of Regulatory Guide 1.52, Revision 2, March 1978, meets the laboratory testing criteria of the above mentioned Regulatory Position, for a methyl-iodide penetration of less than 1 percent. It is also necessary that the preheaters dissipate 43KW +/- 6.4 KW when l tested in accordance with the American National Standards Institute ANSI N510-1975. 1 The system flow rate shall be maintained at 8000 cfm +/- 10 percent during system operation when tested in accordance with ANSI N510-1975. The VE system shall be
\ operable in Modes 1, 2 (Startup), 3 (Hot Standby), and 4.
l
.i Technical Specification 4.7.6 states, in part, the two independent VC systems will be demonstrated operable by verifying that a laboratory analysis of a representative carbon sample obtained in accordance with Regulatory Position C.6.b of Regulatory Guide 1.52 Revision 2 March 1978, meets the laboratory testing criteria of Regulatory Position C.6.a of Regulatory Guide 1.52, Revision 2, March 1978, for a methyl-iodide penetration of less than 1 percent. Also, the system flow rate shall.be maintained at 2000 cfm +/- 10 percent during system operation when tested in accordance with ANSI N510-1975. The heaters shall dissipate 10 KW
+/- 1.0 KW when tested in accordance with ANSI N510-1975. The VC system shall be operable in all modes. ,
1 Description of Event In mid-March of 1990, Catawba Nuclear Station personnel performed a review of their HVAC systems. They discovered the VE and VC system preheaters were not conservatively sized for .all postulated operating modes. This discovery prompted a i study by Design Engineering (DE) which determined the same problem existed at l McGuire Nuclear Station (HNS). On April 27, 1990, Problem Investigation Report (PIR) 0-M90-0122 was submitted. DE responded by performing Operability Evaluations on both VE and VC systems. The Operability Evaluation was performed using Lne following conditions: a postulated degraded grid voltage scenario with a degraded switchyard voltage, a LOCA, and a loss of one main step-up transformer (EIIS:XFMR]
with automatic-bus transfer to the remaining main step-up transformer. On May 3, 1990, based on test performance data, it was determined Unit 2 VE and Unit 1 and 2 VC systems were conditionally operable with restricted flow rate and heater dissipation tolerances. An additional condition on Unit 2 VE, required monitoring and maintaining a minimum grid voltage,
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The performance limits placed on the two systems require tighter restrictions than the current Technical Specification (TS) while still complying with the TS requirements.
The Unit 1 VE system, however, was determined to b inoperable by DE due to the i inability of the preheaters to dissipate enough heat during the postulated degraded grid voltage condition to limit the air flow to a relative humidity of 70 percent or less as required by design.
Concurrently, Unit I was in a refueling outage and preparing to change from Mode 5 to Mode 4. TS 4.6.1.8 requires the VE system to be operable in Mode 1, Mode 2, Mode 3, and Mode 4. The options available to the MNS for operability of the Unit 1 VE system included operating the system at reduced flowrates and compensatory surveillance, re-designing the power distribution system, resizing the preheaters I at a higher wattage capacity or requesting an emergency TS change. The first option could potentially violate the minimum time requirements to obtain a negative
' pressure due to the tight flow restrictions; the second option would' require adding i
- another transformer; the third option would be dependent on replacement parts. The second and third options would also require reanalyzing the MNS electrical system
-) . which would require a change to the diesel generator (EIIS:D0] rating. All three F options would mean a delay of undetermined length in restarting Unit 1. Therefore, 1 I on May 9, 1990, a request was made to the NRC requesting an emergency Technical Specification revision. The request was revised and supplemented on May 10, 1990.
The proposed revision would change the testing standard for the VE system carbon to another more restrictive standard. This standard is used for systems that do not utilize heaters to control relative humidity. Revising this carbon adsorption test method assures the VE system carbon adsorber maintains a 95 percent or greater decontamination efficiency under all anticipated operating conditions, without the use of heaters'. As a result of the change in the test method, it was allowable to relax the requirements for the system heater dissipation test. The NRC staff-reviewed the proposed revision and determined the use of the more restrictive test standard as a supplement to Regulatory Guide 1.52 provided adequate compensation for the postulated low voltage condition to the VE system. It also provided ,
reasonable assurance the carbon efficiency would be maintained such that potential l on-site and off-site doses would not be increased relative to the efficiency and doses associated with existing TS requirements. The proposed revision was approved by the NRC on May 11, 1990.
Conclusion This event is assigned a cause of Design Deficiency because of unanticipated interaction of systems due to design oversight. The VE and VC filter train l preheaters were not conservatively sized for a postulated degraded grid voltage scenario with the following conditions: a degraded switchyard voltage, a LOCA, and a loss of one main step-up transformer with automatic bus transfer to the remaining main step-up transformer.
DE personnel were able to compensate with minimum voltage and restrictive flow rates for Unit 2 VE and Unit I and 2 VC systems for the postulated degraded grid voltage scenario, thus allowing conditional operability. However, Unit i VE system
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experienced difficulties that could not readily be overcome. The test data used in the evaluation revealed the Unit 1 preheater dissipation measurements were smaller l than that of Unit 2. With a smaller wattage dissipation, the Unit 1 preheater I would have required a higher minimum voltage than that required on Unit 2. It was therefore determined Unit I switchyard would be unable to supply the needed voltage i during a degraded grid voltage condition. The lower preheater capacity would (
potentially allow air flow with a higher humidity (greater than 70 percent) to pass through the carbon adsorber. This higher humidity could degrade the ,
decontamination efficiency of the carbon adsorber, allowing for less iodine removal '
during an accident situation. Lowering the air flow to the heaters to compensate f for diminished preheater capacity would put too great a restriction on the system.. ;
The VE system could potentially violate the required TS minimum time limits. In order to overcome the degraded decontamination efficiency of the carbon adsorbers, i and return the air flow to its normal operating parameters, it was necessary to i supplement the test standard currently used with a more restrictive testing standard, which in this case is American Society for Testing and Mat' erials (ASTM) ,
3803-86, Test Method A. This method is utilized for systems that do not utilize l heaters for humidity reduction. Using this method would ensure the system filter decontamination efficiency would be maintained at 95 percent or greater under all
\ operating modes without the use of the VE system heaters. The method requires
/ testing carbon samples at 30 degrees-C and at a relative humidity of 95 percent.
,t 'The current method, Regulatory Position C.6.a of Regulatory Guide 1.52, Revision 2, l March 1978, is used for systems that use heaters for humidity reduction. It i requires testing carbon samples at 80 degrees-C at 70 percent relative humidity. j Even though-the heaters are not being credited for using this test method, they would still be in operation. While in operation, even under postulated degraded voltage conditions, the relative humidity would not exceed approximately 85 i percent. As a result of the test method change, it would also be allowable to l relax the VE system heater power dissipation specification. The specification was l 43 KW +/- 6.4 KW. This value would be changed to 43 KW + 6.4 KW/-17.5 KW, With I the heater capacity degraded by 17.5KW during a degraded voltage condition, the air entering the carbon filter would be approximately 85 percent relative humidity.
This humidity is well below the 95 percent relative humidity specified by the proposed Method A test criteria. This reduced humidity adds conservatism to the VE system operation under the new TS.
To implement these changes and ensure Unit I would not be delayed from entering I Mode 4, an emergency TS change was requested. The NRC approved the change request with the stipulation that after July 16, 1991 both Unit 1 and Unit 2 TS would read the same.
Since the TS change is limited in duration on Unit 2 VE and operating Unit 1 and 2 VC systems under restrictive conditions is not desirable, DE personnel are ,
currently studying alternatives that can be employed to allow operation of the systems under all postulated operatinF modes.
A review of the Operating Experience Program Data Base for McGuire over the l previous twenty-four months reveals three events with a cause of Design Deficiency associated with the VE system filter train preheaters. Therefore this event is s considered recurring. LER 369/89-17 documented an event where the VE system was av.5. CPW 14 9 5b -)d9 011'
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determined inoperable because wiring for the filter unit preheater did not meet ]~,
environmental qualification requirements. LER 369/89-27 documented an event. where
.s the VE system was inoperable due to the preheater_not starting as a result of the I
" differential pressure air flow permissive not being made. Non-reportable PIR -
l 2-M89-0332 documented that aluminum lugs used to terminate Corrective copper VE filter actions as a i preheater wiring were purchased and installed incorrectly. j result of these events would not have prevented this event from occurring, As s result of other events involving Ventilation System problems caused by Design
' Deficiency in general, this can be considered to be a recurring problem.
This event is not reportable to the Nuclear Plant Reliability Data System (NPRDS).
There were no personnel injuries, radiation overexposures, or uncontrolled releases t of radioactive materials as a result of this event.
CORRECTIVE ACTIONS:
Immediate: None Subsequent: 1) An Emergency Technical Specification change was requested by.
MNS for Unit 1 VE system on May 9,1990 and approved by the NRC l
)
on May 11, 1990. ,,
Planned: 1) Design Engineering is studying alternatives to alleviate the
' problem associated with the VE and VC system filter train preheaters.
- 2) The McGuire Safety Review Group will follow up with an addendum once Design Engineering has completed their study on the VE and VC system filter train preheaters.
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SAFETY ANALYSIS: l VE is only assumed to The VE and VC systems are accident mitigation systems.
function following a LOCA and is actuated by a containment Hi-Hi pressure signal of
-3'psig.
VC is assumed to function post accident (not just LOCA) and is actuated by an Engineered Safety Feature signal. The Technical Specifications are still met and thefassumptions made in any previous accident' analysis in the Final Safety This conditionally operable status Analysis Report are obviously satisfied.Thus, the consequences of accidents and irvolves no new failure modes.
malfunctions of equipment important to safety are not increased. Since these l systems are not accident initiators,Since the probability of accidents is not increased no new failure modes are created, the and no new accidents are created.
probability of malfunctions of equipment important to safety is not increased and Since no modification to the plant has been made, no new malfunctions are created.
the fission product barriers are not degraded. The assumptions made in any .
accident analysis are preserved and no safety limits, setpoints, or limiting safety system settings have been changed. Therefore, the margin of safety defined in the bases to the Technical Specifications is not reduced.
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-The VE and VC systems have not been challenged under the conditions set forth in l the postulated grid voltage scenario.
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< -During the time of this event, neither VE or VC systems were required to perform '
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~ their safety functions. !
The health and safety of the public were not affected by this event. !
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