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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:RO)
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20154L6321998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for McGuire Nuclear Station,Unit 1 ML20153B3741998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236U1601998-07-31031 July 1998 Non-proprietary DPC-NE-2009, DPC W Fuel Transition Rept ML20237B2381998-07-31031 July 1998 Monthly Operating Repts for July 1998 for McGuire Nuclear Station,Units 1 & 2 ML20153B3931998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236P0451998-07-0808 July 1998 Part 21 Rept Re non-conformance & Potential Defect in Component of Nordberg Model FS1316HSC Standby Dg.Caused by Outer Spring Valves Mfg from Matl That Did Not Meet Specifications.Will Furnish Written Rept within 60 Days 1999-09-30
[Table view] |
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11- I Duke Pourt Company T C Mwuxtv l McGuim Nuclear Generation Department lice President b
- 12700 Hagers Fern Road (MG01A) (704)Si5-4300 'l Hunterscille, NC 80i M 985 (704)STS-4803 fax j l
DUPUiPOWEU1 8 July 29, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 ;
Subject:
McGuire Nuclear Station Unit 1 Docket No. 50-369 :
Licensee Event Report 369/93-07 i Problem Investigation Process No.: 1-M93-0625 l t
Gentlemen:
i Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached is Licensee Event Report 369/93-07 concerning a Technical Specification required surveillance not being performed because of an Inappropriate Action. This report is being submitted in accordance with 10 CFR .
50.73 (a) (2) (1). This event is considered to be of no' significance with respect to the health and safety of the public. .
Very truly ytwurs, f NM McMeekin T.C.
TLP/bcb t Attachment xc: Mr. S.D. Ebneter INPO Records Center '
Administrator, Region II Suite 1500 _
U.S. Nuclear Regulatory Commission 1100 Circle 75 Parkway 101 Marietta~St., NW, Suite 2900 Atlanta, GA 30339 Atlanta, GA 30323 j Mr. Victor Nerses Mr. P.K. Van Doorn U.S. Nuclear Regulatory Commission NRC Resident Inspector ;
Office of Nuclear Reactor Regulation McGuire Nuclear Station- l Washington, D.C. 20555 ]
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t bxc: B.L. Walsh R.C. Futrell (CNS) ,
P.R. Herran !
R.C. Norcutt ;
M.E. Patrick (ONS)
G.H. Savage j l G.B. Swindlehurst H.B. Tucker i
R.F. Cole D.B. Cook G.A. Copp [
C.A. Paton l M.E. Pacetti '
P.M. Abraham W.M. Griffin ,
NSRB Support Staff (EC 12-A) i i
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y46 U.S. NUCLEAR REGULATORY APPR g OFg NO 50-0104 ESE
- EUR LICENSEE EVENT REPORT (LER) Ibo
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McGuire Nuclear Station, Unit 1 05000 369 1 OF 6 l TITLE (4) A Technical Specification Required Surveillance Was Not Performed Because Of An Inappropriate Action l'VEprT DATE( 5 ) 1.ER NUMBER (6) REPORT DATE(7i PIUER FACILTTIES INVOLVED (0)
MONTH DAY YEAR YEAR SEqcENTIAL REVISION MON 31 DAY YEAR FACILITY NAMES g NUMBER NUM!iER N/A 05000 j 07 05 93 93 07 0 08 04 93 05000 l
OPERATING UUTS REPORT IS SUBMI'!"TED PURSUANT 'IO RIOU1REMENTS OF 10CFR (Check one or mnre of t he fo11nwing)(11)
MCDE(9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) i lorER 100% 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL (10) 20.405(a)(1)(11) 50.36(c)(2) 50.73(a)(2)(v11) pER 20.405(a)(3)(iii) X 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) AL g
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20.405(a)(1)(iv) 50.73(a)(2)(it) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.7 3( a) (2 )( x )
LICEN ;EE (X)NTACT tVR UTiIS LER(1J )
NAME TFLEPHONE NUMBER Terry L. Pedersen, Manager AREA WDE 704 875-4487 COMI'TJ"I'E ONE LINE FOR EACH COMWENT FAILURE DESCRIIED IN T iIS REPORT (13)
CAUSE SYSTEM COMPONENT MANLTAO'1VRER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS I
I SUPPLFXENTAL REPORT EXPECTED (34) EXPECTED MONTH PAY YEAR SUBMISSION lYES (If yes. complete EXPECTED SUBMISSION DATE) X lNO DATE(15)
ABSTRACT [ Limit to 1400 spaces, i.e. approxinatmly fifteen single-space typewritten lines (16)
On July 5, 1993, the Work Control Specialist in charge of monitoring the McGuire Preventative Maintenance / Periodic Testing (PM/PT) program, discovered that the PM/PT functional verification tests for Reactor Protection (IPE) system Trains A and B, showed the same due date. Technical Specifications (TSs) require that these tests be performed on a frequency of 62 days such that both trains are tested on a staggered basis. The due dates should be 31 days apart for the PM/ pts. Upon investigation, the Specialist discovered the computer program had failed to properly update the PM/ pts after both were performed on May 22, 1993, at the end of Unit 1 EOCOB. Therefore, the required test on one of the IPE trains had not been performed as required on the 31 day stagger. A work order was generated and testing was satisfactorily completed on IPE system Train A at 1200, on July 5, 1993. Unit 1 was in Mode 1 (Power Operation) at 100 percent power at the time the event occurred. This event is assigned a cause of Inappropriate Action because personnel reviewing the computer program did not properly test the part of the program used for updating the PM/ pts. All other such tests were verified to be within TS requirements and appropriate changes will be made to the computer program to ensure proper updating of future PM/ pts.
NRC Form h6 b/92
~
CD FOHM 366A U.S. NUCLER REGUIATORY COMMISSION APPROVED BY OMB NO. 32 f>0-0104 (s/e2) ,
, EXPIRES $/31/9$
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH W IS LICENSEE l' VENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD
- COMMENTS REGARDING BURDEN ESTIMATE TO THE IWFORMATION TEXT CONTINUATION AND RECORDS MANAGEMENT ERANCH (MNBB M4), U.S. NUCLEAR REGULATORY CCX4 MISSION, WASHING 1DN, DC 20555-0001, AND to THE PAPERWORK REDUCTION PROJEcr (3150-0104), CFFICE or nervm m mnm mnw-w n- m en .
FACILITY NAME(1) 90CTEC NUMBER (2) LER NUMBER (6I PAGE(3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 007 0 2 OF 6 EUALUATION:
Background
The Engineered Safety Features Actuation (ESFA) system (EIIS JE) is used to monitor ,
selected plant parameters, determine whether predetermined safety limits are exceeded, and if they are, send signals into logic matrices that look for combinations that would indicate primary or secondary system boundary ruptures. Once the fequired logic is ,
satisfied, the system sends actuation signals to the Engineered Safety Features (ESP) '
components whose function best serves the situation.
The ESFA system consists of two discrete portions of circuitry. The first is an analog portion which is made up of instrumentation monitoring various plant parameters such as Reactor Coolant (NC) system [EIIS:A.B] pressure or Containment pressure. Each parameter r may be monitored by either three or four redundant channels. The second is the digital ;
portion cor.sisting of two redundant logic trains. Each receives input from the analog protection channels and performs the needed logic functions to actuate the necessary ESF components. Each train is equally and independently capable of actuating the ESF components that may.be required.
Technical Specification (TS) surveillance requirements for the automatic trip and interlock logic state that each train be tested at least every 62 days on a staggered test basis. TS definition of a staggered test basis is as follows: ,
A staggered test basis shall consist of;
- a. A test schedule for n systems, subsystems, trains, or other designated .
components obtained by dividing the specified test interval into n equal subintervals, and
- b. The testing of one system, subsystem, train, or other designated component at the beginning of each subinterval.
The TS surveillance would in this case require that one train be tested each 31 days. The '
Preventative Maintenance / Periodic Testing (PM/PT) program allows 25 percent of the test frequency as a grace period for performance of the test. For a 31 day test this would be -
7 days. Therefore, the maximum allowable time to perform the test would be 38 days.
NBC PORM 366A I U.S. NUCLIER REGUIAIDRY COMMISSION APPROVED BY OMB NO. 3150-0104 (5/32) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TV COMPLY WIDI THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COPMENTS REGARDING EURDEN ESTIMATE 30 THE INFORMATION TEXT CONTINUATION AC RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEMt REGULA70RY COMMISFION, WASHINC1DN, DC 20555-0001, AND ,
70 THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE rw MANvem= m wmmm wn mwa-ww vv ?m m .
- FDCILITY KAME (1) DOCKET NUMBER (2) LER NUMBER (6r PAGE(3) r YEAR SEQUENTIAL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 007 0 3 or 6 ,
Description of Event In June of 1992, the Work Management System (WMS) for generating work orders (WOs) electronically was initially placed into service at McGuire. As a part of the system the '
PM/PT WOs were entered and set up to be generated as they are needed. A part of the PM/PT [
program includes the periodiv functional surveillance testing performed on the Reactor .
Protection (IPE) system [EIIS:JC). The equipment identification numbers for these ;
surveillances are Units 1 and 2 IPE CA 9010 and 9020 for IPE system Trains A and B, respectively. TSs require that these surveillances be performed every 62 days on a staggered basis.
Prior to June of 1992, the WOs were updated manually so that the two trains were kept on a '
staggered schedule 31 days apart. To accomplish this using the WMS program these PM/ pts were entered to be updated as an A type calculation. This should have had the computer recognize the particular equipment number for one of the IPE trains each time it was j entered.as complete, update the program for that PM/PT WO for 62 days, search for the corresponding equipment number for the opposite train, and once found update the. program to ensure that the PM/PT WO for that train was dated for 31 days.
The program was initially checked out by Wcrk Control (WC) personnel and the PM/ pts using the A type calculation appeared to be working properly. No further verification of the program was performed by WC personnel. Routine reviews of the PM/ pts were perforried and the PM/ pts associated with the A type calculation appeared to be updating in a proper manner.
On July 5, 1993, the WC Specialist in charge of monitoring the PM/PT program was performing a routine review of the PM/ pts due for a 7 day window 3 weeks in the future.
This particular printout covered a 7 day window from July 19 to July 25, 1993. During the course of the review the Specialist noted the PM/ pts for Unit 1 IPE Trains A and B had the same due date shown. The Specialist recognized the dates should have been 31 days apart.
Upon further investigation, the Specialist discovered the PM/ pts were performed together on May 22, 1993, at the end of Unit 1 EOC08. '
e ,
Consequently, the PM/PT surveillance for one of the trains should have been performed no !
later than June 29, 1993. Realizing the error, the Specialist generated WO 93047633 to perform the required surveillance on Unit 1 IPE CA 9010 (Train A). The surveillance was begun at 1000, on July 5, 1993 and succensfully completed at.1200, on July 5. ". 9 9 3 .
NRC FORM 3MA U.S. NUCLEAR RECUIAMRY COMMISSION APPROVED BY CMB No. 3150-0104 (5/92) EXPIRES 5/31/95 ESTIMATED BURDEN FER RESPONSE 'IO COMPLY WITH 'THIS
, LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD CO W.ENTS RECARDING BURDEN ESTIMATE TO THE INFOTORTION TEXT CONTINUATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULA'IORY COMMISSION, WASHINGMN, DC 20555-0001, AND .
'IO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE f nP M v N m
- A e w w T"". wh et* T w M nr* MM.
FACILITY NAME(I) DOCKET NUMBER (2) LER NUMBER (61 PAGE(3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER t McGuire Nuclear Station, Unit 1 05000 369 93 007 0 4 Or 6 The Specialist performed a search to determine if any other PM/ pts using the A type calculation had been missed. No others were found to have been missed. Also, work was begun to find the cause for the error in the program and repair it.
Conclusion This event is assigned a cause of Inappropriate Action because of lack of attention to detail. When WC personnel reviewed the WMS computer program for the A type calculation, they did not properly ensure the program updated'PM/ pts to accomplish the required stagger. Subsequent routine reviews of PM/ pts failed to reveal the problem with the ,
program.
When the PM/ pts on IPE Trains A and B were performed together at the end of Unit 1 EOC08 the program updated both for 62 days in the future. The next routine check of these PM/ pts, on July 5, 1993, revealed they had the same due date. The WC Specialist performing the review recognized this was an error and checked the last date the PM/ pts were performed to determine the correct date the 31 day staggered PM/PT should be performed. He consequently discovered the PM/PT should have been performed no later than June 29,1993. Immediate action was taken to generate a WO to perform the test on the available train. The test was completed successfully at 1200, on July 5, 1993.
Subsequently, the WC Specialist verified all other PM/ pts associated with the A type calculation to confirm that no other surveillances had been missed. Also, the WC Specialist notified the appropriate personnel at Catawba and Oconee of the discrepancy.
An investigation was performed to determine the problem with the A type calculation used by the program. It was concluded as a result of the investigation that the calculation had never recognized the existence of the associated PM/PT when one of the PM/ pts was updated. It had only updated the PM/PT entered for the 62 day cycle. Since the PM/ pts involved had always been done on time, until Unit 1 EOC08 forced them tc be performed together, the program had appeared to stagger the due dates properly. Appropriate changes will be implemented to the computer program to resolve the discrepancy. No other problems were found to have occurred as a result of the discrepancy.
A review of the Operating Experience Program (OEP) Data Base for twenty-four months prior to this event revealed no events attributed to a cause of Inappropriate Action resulting in a TS violation involving the IPE system. Also, no other events occurred involving the WMS program or inadequate testing of the WMS program. Therefore, this event is not i
l NRC FORM 36fA U.S. NUCLEAR REGUIAERY COMMISSION APPROVED BY OMB NO. 3150-0104
($/92) .
EXPIRES 5/31/95 l
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j l
ESTINATED BURDEN PER RESPONSE 'IO COMPLY WITH 'TilI5 i LICENSEE EVENT REPORT (LER) INIVRMATION COLLECTION REQUEST: 50.0 ERS. FORWARD 1 COMMENTS REGARDING BUPDEN ESTIMATE TO THE INFORMATION TEXT CONTINUATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. FUCLEAR '
REGULAMRY COMMISSION, WASHINGmN, DC 205S5-0001. AND W THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE I nr Frxerrvm yxn emm wamrtwme y ?m m _ i FACILITY NAME(1) DOCTET NUMBER (2) LER NUMBER (6) PAGE(3) l l
nM SEQUENTIAL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 007 0 5 OF 6 P
considered recurring.
i This event is not Nuclear Plant Reliability Data system (NPRDS) reportable.
There were no personnel injuries, radiation overexposures, or uncontrolled releases of radioactive material as a result of"tnis event.
i CORRECTIVE ACTIONS:
Immediate: 1) WC personnel generated WO 93047633 to perform the required surveillance on Unit 1 IPE CA 9010 (Train A).
- 2) Instrumentation And Electrical personnel successfully perfcrmed the PM/PT on Unit 1 IPE CA 9010. :
i
- 3) WC personnel performed a search to determine if any other PM/ pts using ;
the A type calculation had been missed.
- 4) WC personnel notified appropriate personnel at Catawba and Oconee of the discrepancy.
Subcoquent: 1) WC personnel performed an investigation to determine the cause for the error in the WMS A type calculation for PM/ pts.
- 2) WC personnel manually checked the stagger on all A type calculations and verified proper scheduling of the associated PM/ pts.
Planned: 1) WC personnel will r:take appropriate changes to the WMS computer program and verify that the A type calculation program will properly update PM/ pts on a staggered basis.
___m_ . _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . . _ . _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _
3mc FORM 366A U.S. NUCLEAR RECULA'ILRY CCPDGSSION 5
APPROVED BY OMB No. 3150-0104 (5/C2), , EXPIRES $/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH-THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INTDRFJLTION TEXT CONTINUATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND
'IU THE PAPERWORK REDUCTION PRN'ECT (3150-0104), OFTICE or erwacev m pyn m yrw wr etrywm ne m e3_
FACILITY NAME(1) DOCKET NUMBER (2) LER NUMBER (61 PAGE(3) i YEAR SEQUENTIAL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 007 0 6 OF 6 EAFETY ANALYSIS:
The event described in this LER is technical in nature in that it deals with the failure i
to perform a portion of a surveillance requirement. The TS surveillance requirements for the automatic trip and interlock logic state that each train be tested at least every 62 ,
days on a staggered test basis. The portion of the surveillance not performed was the testing of one train Ec the beginning of the subinterval (31 days). Since the testing performed upon discovery of the problem found no inoperable equipment or circuitry, and l since the equipment history of this equipment and circuitry shows no failures in past tests, this equipment is not considered to have been past inoperable. There is no evidence to suggest that the equipment would not have actuated as required during an ,
accident.
1 To render the entire ESFA system inoperable, multiple failures of components would have had to occur. During the time when the portion of the surveillance was missed until the portion of the surveillance was performed, there were no conditions or combinations of conditions that would have required the ESFA system to actuate. There were also no conditions or combinations of conditions which would have been aided by the use of the ESFA system. Therefore, the health and safety of the public were not affected as a result of this event.
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