LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures RevisedML20045D968 |
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McGuire ![Duke Energy icon.png](/w/images/7/75/Duke_Energy_icon.png) |
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Issue date: |
06/25/1993 |
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From: |
Pedersen T DUKE POWER CO. |
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Shared Package |
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ML20045D964 |
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References |
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LER-93-006, LER-93-6, NUDOCS 9306300264 |
Download: ML20045D968 (6) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:RO)
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20154L6321998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for McGuire Nuclear Station,Unit 1 ML20153B3741998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236U1601998-07-31031 July 1998 Non-proprietary DPC-NE-2009, DPC W Fuel Transition Rept ML20237B2381998-07-31031 July 1998 Monthly Operating Repts for July 1998 for McGuire Nuclear Station,Units 1 & 2 ML20153B3931998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236P0451998-07-0808 July 1998 Part 21 Rept Re non-conformance & Potential Defect in Component of Nordberg Model FS1316HSC Standby Dg.Caused by Outer Spring Valves Mfg from Matl That Did Not Meet Specifications.Will Furnish Written Rept within 60 Days 1999-09-30
[Table view] |
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LICENSEE EVENT REPORT (LER)
FACILITY nex( McGuire Nuclear Station, Unit 1 DOCKET NUMBER (2) PACE (3)
- 05000 369 1 OF 6 TITLE (o) A Failure To Comply With Technical Specification Action Statement occurred Due To A Technically Deficient Procedure.
EYWT DATE(5) LER NUMBER (6) REPORT DATE(7) U mER FACILITIES INVOLVEDf8)
MCTnt DAY YEAR YEAR SEQUENTIAL REVISION NONTH DAY YEAR FACTLTTY NAPER DOCKET NUMBE9(8)
NUMBER N'JMBER 05000 05 26 93 93 06 0 06 25 93 05000 cPERATIpo 5 THTS REPORT TS SUBMTTED PURSUMt M R@UUMDrPS OF 10CFR (Check one or more of the fo110 wino)(11)
MODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 0% 20.405(a)(1)(1) 50.36(c)(1) 50.73(nJt2)(v) 73.11(c)
LEVEL (10) 20.40$(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(v11) OTHER (Specify in 20.405(a)(1)(iii) X 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) Abstract below and in Text) 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)(111) 50.73(a)(2)(x)
LICENSEE QWTACT FOR 'MIIS LER(12)
TELEPflONR NUMBER CAME Terry L. Pedersen, Manager, McGuire Safety Review Group ARr.A cooE 704 875-4487 COMPLE*fE ONE L1hE FOH EACH CUMPONENT FAILUkE DESCRIBED IN THIS RENRr(13)
MANUFACTURER REPORTABLE CAUSE SYSTEM CCEPONENT MANUFACWRER REPORTABLE CAUSE SYSTEM COMPONENT TO NPRDS TO NPRDS EXPECTED MONTH DAY YEAR SUPPLEMENTAL REPORP EXPEcPED(14)
SUBKISSION YES (If yes, complete EXPECTED SULMISSION DATE) X NO DATE(15)
ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines (16)
On May 26, 1993, Operations and Systems Engineering personnel were performing the Unit 1, Train B, Engineered Safety Features (ESP) actuation test in accordance with procedure PT/1/A/4200/09A, ESF Actuation Periodic Test. While in the re-alignment phase of the test, ,
at approximately 1530, Control Room (CR) personnel discovered that the sample blower for radiation monitor (EMF) 1 EMF-43B was off. 1 EMF-43B monitors the B Train Control Room Ventilation System (VC) air intakes. With the sample blower off, 1 EMF-43B is considered inoperable. Terhnical Specification (TS) 3.3.3.1 requires a VC air intake to be isolated .
within one hour if it has an inoperable EMF. Investigation by CR personnel revealed that 1 EMF-43B had been inoperable for approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 52 minutes, without the VC air intake being isolated. Investigation also revealed that the same EMF had been inoperable for approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 35 minutes earlier in the day, during a different portion of the ESF test. Investigation further showed that the A Traia portion of the test had most likely rendered 1 EMF-43A, which monitors the A Train VC intake, inoperable on May 25, 1993.
Failure to isolate the VC air intakes with the EMFs inoperablo constitutes a condition prohibited by TSs, and is therefcLe reportable. Unit 1 was in Mode 5, (Cold Shutdown) at the time of the event. This event was caused by a Technically Deficient procedure. Corrective actions will include revising the Unit 1 and Unit 2 test procedures, to prevent reoccurrence.
9306300264 930624 PDR ADOCK 05000369 S PDR
. . LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILf17 NAME(1) DOCKET NUMBER (21 LER NUMBER (6) PACE (3)
, g SEQUENTIAL REVISION.
NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 06 0 2 or 6 EVALUATION:
i Btckground The control Area Ventilation and Air Conditioning (VC) systems [EIIS VI] are designed to maintain the environment in the Control Room (CR) [EIIS NA), Control Room Area, and Switchgear Room within acceptable limits for operation of unit controls, for maintenance and
. testing of the controls as required, and for uninterrupted safe occupancy of the CR during post-accident shutdown. 'Due to these criteria, the systems are designed as an Engineered Safety Feature (ESF) system [EIIS JE) with absolute and carbon filtration in the outside air intakes and equipment redundancies for use as conditions require.
The Radiation Monitoring (EMF) system [EIISSIL) is divided into two functionally separate systems, the process monitoring portion and the area monitoring portion. The procesa monitoring portion provides several functions. Included in these is the ability to provide early warning to station personnel of equipment, component, or system malfunctions or potential radiological hazards within the station during normal operation consistent with the limits of the station Technical Specifications (TS). An additional function is to provide the radiological monitoring functions for the air intakes of the CR and the onsite Technical Support Center. The specific monitoring function for the CR air intake is provided by EMF 43A and 43B for each air intake, reelectively. A high radiation signal on either EMF will alarm [EIIS*RA) in the CR.
The ESF senses selected unit parameters, determines whether or not predetermined safety limits are being exceeded and, if they are, combines the signals into logic matrices sensitive to combinations indicative of primary or secondary system boundary ruptures. Once the required logic combination is completed, the system sends actuation signals to those ESF components whose aggregate function best serves the requirements of the accident. In order to demonstrate the operability of the ESF system, the system is subjected to periodic tests.
An integrated system test is performed when the unit is cooled down and the Residual Heat ,
Removal (ND) system (EIIS BP) is in operation. This test does not introduce flow into the Reactor Coolant (NC) system [EIIS AB) but does demonstrate the operation of the valves, pump circuit breakers [EIIS 52), and automatic circuitry including Diesel Generator (DG) (EIIS DG) ;
starting and the automatic loading of ESF components on the diesels (by simultaneously l simulating a loss of offsite power to the vital busses).
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- . LICENSEE EVENT REPOPI (LER) TEXT CONTINUATION f FActLrry anett) ooerrr uuxars(n t.ER wuxerRis) Pace (3) i .
l YEAR SEQUEfrr1AL REVISION
{ NUMBER NUMBER I
McGuire Nuclear Station, Unit 1 05000 369 3 06 3 or 6 O_
l Dancription of Event l On May 26, 1991 at 1022, Operations (Ops) and Systems Engineering (SE) personnel began the i active porthru of procedure PT/1/A/4200/09A, ESF Actuation Periodic Test. The purpose of this test procedure is to demonstrata the operability of various portions of the ESF circuitry. The entire test requires 5 days of testing divided into several sections.
Procedure Section 12.3, B Train - Safety Injection, Phase A, Phase B, and Blackout Followed by Safety Injection, was begun on May 26, 1993. Procedure PT/1/A/4200/09A is performed by l
simultaneously initiating a manual Snety Injection (Ss) signal, Phase A (St) Containment Isolation signal, Phase B (Sp) Containment Isolation signal, and opening the feeder breaker l
to 1ATD transformer [EIIS XFMR) which causes a B Train Blackout (Bo) signal. Procedure PT/1/7/4200/09A then verifies the automatic system alignments and component actuation to demonstrate that the ESF system 3 performing as expected. Since one of the features of this test is to initiate a loss of power to the essential bus, all components which receive power from this source are de-energized. The system is designed with a sequencer, which will re-apply loads to the essential bus, as required for an Se signal, once the emergency DG is ready to accept loads. This automatic sequencing of loads only applies to the major components which are supplied power from the essential bus.
When the Bo signal was initiated, one of the components which lost power das the sample blower for 1 EMF-43B, Control Room Air Intake Radiation Monitor. This EMF is used to monitor the B Train air intake of the VC system and to warn CR personnel of any increase in the activity level. This warning would allow the CR personnel to isolate the effected air intake. The EMF itself is not safety related, nor does it receive safety power. The power cupply to the EMF is from the battery backed up, non-saf1 sty power supply KXB. Since the sample blower for 1 EMF-43B had no power during the test, the EMF was inoperable. Technical {
Specification 3.3.3.1 requires that with an inoperable EMF in the VC air intake line, to isolate the mted intake line within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. To complete this portion of the test, and J
' to re-align 'J.
- e 'fected systems took approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 25 minutes. The sample blower for 1 EMF-43B wcs restarted at 1157, on May 26, 1993. j
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The next test section to be performed was 12.4, B Train, Blackout. The test section demonstrates the capability of the ESF system to respond to a Bo only condition (a signal !
l where an Se is not generated.) This section is performed by opening circuit breaker ITD-4, I which is the feeder breaker to the 6900v/4160v transformer lATD, which causes a loss of essential power on the B Train. This power loss again caused the sample blower for 1 EMF-43B to stop, making 1 EMF-43B inoperable. Procedure Section 12.4 was completed to the realignment steps in approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 52 minutes. The sample blower to 1 EMF-438 was restarted at 1329, on May 26, 1993, s- i
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. LIChNSEE EVENT REPORT (LER) TEXT CONTINUATIOZ DOCKET NUMEER(2) LER NUMBER (6) PAGE(3t FACILITY NAME g YEAR SEQUENU AL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 '06 4 or 6 O_
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l Control Foom personnel, when realigning the systems ef fected by section 12.4, realized that the TS requirements for 1 EMF-43b had not been met, and immediately restarted the sample blower. However, the failure to isolate the Vc air intakes within the TS required time constitutes operation in a condition prohibited by TS and 1s therefore reportable.
Investigation by CR personnel revealed that the action statement of TS 3.3.3.1 had also been missed during the earlier test section.
Procedure PT/1/A/4200/09A is also divided so that both trains of the ESF system are tested.
A Train testing was completed on May 25, 1993. The A Train of the VC air intake contains 1 EMF-43A which duplicates the function of 1 EMF-43B, but for the opposite train. The equivalent sample flow alarm (EIIS:FA), which provided information about the status of 1 EMF- I 43B, was not functioning during the A Train tnoting. Without this alarm capability, no direct evidence exists as to whether TS 3.3.3.1 was violated. However, objective evidence, based upon the loss of flow indications of related A Train EMFs indicate that the action statement of TS 3.3.3.1 was violated on May 25, 1993, during the A Train test.
Conclusion The cause of this event is a Technically Deficient Procedure. Procedure PT/1/A/4200/09A is deficient in several respects. Procedure PT/1/A/4200/09A does not specifically reference the TS's which are involved in the test. There is a list s' TSo contained under step 6.13 which states, " Operations (OPS) shall review the following, u log in the Tech. Spec. log book as applicable." However, this list does not contain TS , The list under step 6.13 does contain references to TSs 3.11.1.3, 3.11.2.4, and 3.3.3.9 all of which were moved to chapter 16 of the Final Safety Analysis Report in May, 1991. There are no procedural steps which specifically addreos restarting of the 1 EMF-43 sample blowers. Procedure sections 12.1 and 12.3, for the Ss, St, Sp and Bo, (A Train and B Train, respectively) contain steps 12.1.80 and 12.3.80 which read "Have OPS restart EMF sample blowers af ter 1MISV5581 and 1MISV5583 are re-opened." Tt n valves referred to in procedure steps 12.1.80 and 12.3.80, are the Containment Is i xion valves which isolate the flowpath of the EMFs which are sampling the containment atmosphere. These steps are poorly worded, and imply starting only the sample blower that supplies sample flow to the EMFs which sample the containment atmosphere. In the restoration portions of section 12.2 and 12.4, which are the Bo only portions of the test (A Train and B Train, respectively) there are no steps which would direct any EMF sample blowers to be re-started. Lastly, the procedure is deficient in that it takes longer than the TS allowed time to reach the point of restoration. The CR personnel restarted the EMF sample blowers at their earliest opportunity, based "pon the testing activity. However, the CR personnel were able to restart the sa.aple blower within the TS allowed time I case of the j 1 that were performed.
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- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME(1) DOCEYT NUMBER (2) LER NUMPER(6I PAGE(3)
YEAR SEQUEFTIAL REVISION NUMBER NUMBER McGuire Nuclear Station, Unit 1 05000 369 93 06 0 5 or 6 3 ~
While discussing this event with Ops procedure personnel, it appeared that under certain scenarios of loss of power events, the operability of 1 EMF-43A(B) could be in quastion. The operebility of 1 EMF-43A(B), and all other TS required EMFs, during loss of power events, will be evaluateo by Ops procedure writers.
i A search of the Operating Experience Program data base for the proceding 24 months revealed another report, LER 370/92-02, which deals with an ESF actuation while performing procedure PT/2/A/4200/09A, ESF Actuation Periodic Test, due to a technically deficient proceduro.
Therefore, this event is considered to be recurring. The corrective actions of LER 370/92-02 were specific to that technical deficiency, and would not have prevented this event.
This event is not reportable to the Nuclear Plant Reliability Data System (IIPRDS ) .
L There were no personnel injuries, radiation overexposures, or uncontrolled releases of radioactive material as a result of this event.
CORRECTIVE ACTIONS:
Immediato: 1) Ops personnel restarted 1 EMF-43B sample blower.
Subsequent: 1) None.
Planned: 1) SE personnel will add a step to procedure PT/1/A/4200/09A to isolate the the VC air intake of the train being tested prior to the test being performed.
- 2) SE personnel will add a step to procedure PT/2/A/4200/09A, to isolate the f VC air intake of the Train being tested, prior to the test being performed.
- 3) SE personnel will perform a comprehensive review of the components which are actuated by procedure PT/1/A/4200/09A, and compare this information against the TS to find and correct any other technical deficiencies.
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- 4) SE personnel will perform a comprehensive review of the components which gI, are actuated by procedure PT/2/A/4200/09A, and compare this information y , against the TS to find and correct any other technical deficiencies.
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- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILI[Y NM2(1) DOCPTT NUMBERg LER NUMBER (6) PAGE(3)
YEAR SEQUENTIAL RINISION NWEER N WDEH McGuire Nuclear Station, Unit 1 05000 369 93 06 0 6 or 6
- 5) Ops personnel will evaluate the need to rearrange the steps in procedures AP/l & 2/A/5500/07, Loss Of Electrical Power, to ensure the EMF sample blowers are restarted under all possible scenarios.
- 6) Ops personnel will evaluate the need to add steps to the plant Emergency Procedures to ensure that EMF sample blowers are restarted af ter a loss of power has occurred.
SAFETY ANALYSIS:
The requirement to isolate a VC air intake which has an inoperable EMF is based on limitirig the CR dose during accident situations. The TS action statement assumes that if a VC air intake were not isolated, when its corresponding EMF is '.noperable, the dose to the CR personnel may exceed the General Design Criteria (GDC) 19 limits. The thought is that this may occur due to the CR personnel not taking any action to isolate the air intake if its activity levels were to increase, since the inoperab3e EMF would provide no warning to the CR personnel. PIR 0-M91-0060 was written to address concerns with the VC air intakes. The specific purpose of this PIR is to consider the effect of having the VC air intakes open during accident scenarios. Calculation MCC-1227.00-00-50, which was performed in response PlR 0-M91-0060, states that the dose of CR personnel would not exceed the GDC-19 limits with the intake lef t open, therefore, this event is not considered to be significant. The health and safety of the public were not effected by this event.
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