|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:RO)
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20154L6321998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for McGuire Nuclear Station,Unit 1 ML20153B3741998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236U1601998-07-31031 July 1998 Non-proprietary DPC-NE-2009, DPC W Fuel Transition Rept ML20237B2381998-07-31031 July 1998 Monthly Operating Repts for July 1998 for McGuire Nuclear Station,Units 1 & 2 ML20153B3931998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236P0451998-07-0808 July 1998 Part 21 Rept Re non-conformance & Potential Defect in Component of Nordberg Model FS1316HSC Standby Dg.Caused by Outer Spring Valves Mfg from Matl That Did Not Meet Specifications.Will Furnish Written Rept within 60 Days 1999-09-30
[Table view] |
Text
--
3 h r J %* ;n',
' Duke Ibuer Company ' (104) 87.t4000 i McGuireNuclearStation =
, l'O Bas 188 . ,
- Cornelius, N C 280.110488 ,
s DUKEPOWER
. , s November 13, 1989 j
, i U.S. Nuclear Regul'atory Commission Document Control Desk [
-Washington, D.C. 20555
Subject:
McGuire Nuclear Station Units 1 and 2 Docket No. 50-369 Licensee Event Report 369/89-31 L
q:
F Gentlemen: ;
- i. Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached is Licensee Event Report 369/89-31' concerning both trains:of the Control Area' Ventilation. System being declared inoperable because of an inappropriate . action. This report is '
being submitted in accordance with 10 CFR 50.73(a)(2)(i) and (a)(2)(v). .This event is considered to be of no significance with respect to the health and safety -
of the public.
f Very truly yours, f
/*pf-@ M
-T.L. McConnell DVE/ADJ/cbl-Attachment ,
t xc: Mr. S.D. Ebneter American Nuclear Insurers Administrator, Region II c/o Dottie Sherman, ANI Library J
'.U.S. Nuclear Regulatory Commission The Exchange, Suit 245 ,
101 Marietta St., NW, Suite 2900 270 Farmington Avenue Atlanta, GA 30323 Farmington, CT 06032 INPO Records Center Mr. Darl Hood Suite 1500 U.S. Nuclear Regulatory Commission 1100 circle 75 Parkway Office of Nuclear Reactor Regulation Atlanta, GA 30339 Washington, D.C. 20555 M&M Nuclear Consultants Mr. P.K. Van Doorn l 1221 Avenue of the Americas NRC Resident Inspector ,
New York, NY 10020 McGuire Nuclear Station 9911220005 891113 f>
PDR ADOCK0500g9 S
1\ ,
g ..;g s -. :
' ~LER Cover;Lett r L Ppge 2 '.
T ,
i S bxcs'B.W.'Bline y
A.S. Daughtridge J.S. Warren '
i
- R.L. Gill:
'R.M.-Glover 1(CNS) '.
T.D. Curtis (ONS) '
'P.R. Herran',
u4 ,
S.S. Kilborn (W)
R.E. Lopez-Ibanez J.J. Maher '
.R.O. Sharpe.(MNS) 3 JG.B. Swindlehurst s K.D. Thomas 1\L L.E. Weaver R.L. Weber J.D. Wylie (PSD)
J.W. Willis
'QA Tech. Services NRC Coordinator (EC 12/55)
MC-815-04 (20) 1 b
b f
\
t p .. ~ . .,s.
r 1 3, ,
'j u . <uCLla .. .uu,o., C., io.,
1,
, 3i u .aoveo cue no 3 f t=*me e.See i
'.
- UCENSEE EVENT REPORT (LER) i eaciutv =aast m ooCaet Nuesesa ui rnae cui )
McGuire Nuclear Station, Unit 1 o i s l o j o g o j 3 j6 ; 9 i lor 16 I
"'* Technical Specification 3.0.3 Was Entered On Unit 1 And Unit 2 Due To An Inappropriate i
. Action Durine Maintenance On Theespont Control oatt m Area Ventilation Svatem otMan saciutits iNvolvto e
- sveNT oast a ten nummen iei
'ac'ut'***** 00C' t ' Nuwet a'5' I woNr pav vtan vtaa M,4 6 $*g; coNr Dav vtaa )
McGuire Unit 2 01610 i o t o i gg y to l 1
i i i i i e e i 113 81 9 0 is os g o g o, ; g l 11 0.112 8 9 8I9 01311 010 11 1 v.n. ..Po., .u 1n o ,va.uaN, ro ,NS . ou .tm o, i. C,. i ,C . - , o ii
,,,,,,,,,, n , ..
=aos = i . 3. ,
n .. _
. n .laH i _
X to.73teH3Hvl 73.7t les
. 30 44isHtH6) 00 36teHil
,,., 1 iO i 0 . in H.,
.. m _
. n.,an ,
_ g,=,. g. ,.g.,..
.I86 ai 30 4N4aH1Hdel X to 134sIGilil 50 73IsH3H.seiHAl
.nwi.e, ni.i H..n.,
. .in H ,
M 40$leH1H.) to 73 eH3H iil to 73 aH3Hei Litte,stt C.NT ACT FOR THIS LE A Hal TELEPMONE NVutta NLMt amt& CODE Alan Sine. Chairman. McGuire Safety Review Group 71014 R17 l %I -It. I 11 R l9 CoMPLEf t .Nt LINE FOR SACN C0espoNENT pa Lunt otecnitt0.N TM.S REPORf Hal Sv5Tav "$$he m*0{,fata e
Clust Svlitu COMPONtNT "$$'g aC. R$PO Pa$s' CaV56 COMPONENT I l l I I I t i I I l 1 I I 1 l l l 1 1 I I I I l l l l UON7" Dav Vlam ;
SUPPLEMENTAL alPont tartCTto itel SvSvtS$l0N
""" i T] vii m ,. . . ameno suevissio= e4 rri ] a.o oi3 ol 1 91 0
.ser a aCT ,L ,~, . , ao . . . . ....,, a,=,. .u. ,,.-e. mv o si On October 12, 1989, Instrumentation and Electrical (IAE) personnel were performing maintenance on the Chlorine Detectors for the Control Area Ventilation (VC) System.
At 1435, IAE personnel were returning the Chlorine Detectors to service by reconnecting power leads. One of the power leads was accidentally dropped and touched the grounding screw. This caused the AC power supply fuse to' blow, resulting in the automatic isolation of the four outside air intakes on the VC system. This resulted in Units 1 and 2 entering Technical Specification
.(TS) 3.0.3. Operations personnel removed power from the outside air intake valves However, Units 1 and then manually opened the valves, thereby exiting TS 3.0.3.
and 2 then entered TS 3.3.3.1 which requires that two channels of the VC Air Intake Radiation Monitorc be operable. The Radiation Monitors could still detect radiation; however, they could not close the VC system outside air intake valves because the power had been removed. IAE personnel replaced the fuse. The intake valves were returned to service, and TS 3.3.3.1 was exited. Unit 1 and Unit 2 were in Mode 1 (Power Operation) at 100 percent power at the time of this event. This event is assigned a cause of Inappropriate Action because the action taken was accidental. Maintenance Engineering Services (MES) personnel will evaluate adding a terminal strip with sliding links and another fuse for the VC Chlorine Detectors.
l c w una o
g ,. , .,'
- .' a 400lC Poem 20A U S. NUCLEA3 [lIUL1TORV COMMiettose i P' '-
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION oe:ovio ow. No. mo-em emnes sw.
PACILifyNaMS m , DOCRL1 NUMSSR W LE A NUMSI A 103 PAOS (31 l' " a'i " t'.& 7x,*J:
l'~
McGuire Nuclear Station, Unit 1 o js j o j o l o l 3 l 6l 9 8l9 0l 3[1 Oj0 0l2 0F 0l 6 l text u m . = e w aac f.= assmm EVALUATION: i L Background L
There are two independent trains of the VC [EIIS:VI] System which are designed to maintain a habitable environment in the Control Room [EIIS:NA), Control Room Area, and Switchgear Rooms, during normal and accident conditions. Based on these i criteria, the system is designed as an Engineered Safety Features [EIIS:JE] system I with absolute and carbon filtration [EIIS:FLT] in the outside air intakes and with equipment redundancies for use as conditions require. The Control Room is designed to be maintained at a positive pressure of greater than or equal to 0.125 inches water gauge (w.g.), relative to outside atmosphere during an accident to prevent
L Chlorine Detectors [EIIS:DET) monitor the outside air intake structure of the VC system for the presence of chlorine gas. Each train has two intake structures.
Each structure is monitored by one detector and has two redundant isolation valves
[EIIS:ISV). If gas is detected by either detector of the train, the train intake structures will be automatically secured by means of closing four intake isolation valves and a local / remote alarm [EIIS: ALM] will be generated. The major parts of a {
chlorine detector are the electrolyte tank [EIIS:TK] that houses a wick, a blower
[EIIS:BLO) unit, and an electronic unit.
TS 3.0.3 states that when a Limiting Condition of Operation is not met, except as
- provided in associated Action Statements, within one hour action must be initiated to place the affected units in a mode in which the specification does not apply.
TS 3.3.3.1 states for the VC Outside Air Intake Radiation Monitors [EIIS: MON), EMF 43a and 43b, a minimum of two operable channels [EIIS:CilA] are required. With the number of operable channels less than the minimum requirement, the VC system outside air intakes which contain the inoperable instrumentation must be isolated -
within one' hour.
The Operability Evaluation for PIR 0-M89-0163, Revision 1 dated September 14, 1989 l and expiring February 19, 1990, states:
i In order to achieve acceptable pressure in the Control Room, the doors l [EIIS:DR] in the Control Room were sealed with tape, with the exception of the two doors leading to the Service Building [EIIS:MF], and all four outside air intakes were opened. Based on the test results and the conditions required to achieve the test results, the VC system is Conditionally Operable, with the l conditions of operability being: l l
l - Maintain a tight seal on all the doors in the Control Room. All of the l seams of the Control Room doors (except the two doors leading to the j l Service Building, which are pressure doors) are to be taped. Tape can l subsequently be removed as long as Control Room pressurization l requirements are met.
l l
PMM 306A 'O.8. CP0' 1988*% N'989 000I0
I. 4 -
)
anc
- "w. anna ue wetimuutarony ca io=
lT UCENSEE EVENT REPORT (LER) TEXT CONTINUATION ueaovio ove w. vio.oio6 exemes. swa j, FAOLITY haut He 00CKlf NUMSSR W ggn hygggM141 P408 (31
) v8Ah %'$ h*6 -['1*j2
- h. McGuire Nuclear Station, Unit 1 o lslojolol3l 6l9 8l 9 -
0l 3l 1 -
0l 00 13 OF 0 l6 rixvwm . w =-w w mswon All four outside air intakes are to stay open except when testing pursuant to TS 4.3.3.1. The operating procedure for the VC system is to be modified to specify all four intakes to be open during normal and y
i accident conditions. The operator will be required to reopen all intakes if they are closed due to the radiation monitar detecting. contaminated
! air in the duct.
The doors which are required to be sealed with tape to maintain an acceptable !
pressure in the Control Room have been subsequently sealed with a high quality RTV sealant.
! Description of Event- i
, On August 16, 1989, a monthly Preventative Maintenance (PM) was completed on the VC system OMVCMT5010 Chlorine Detector according to work request 03167A. During this PM, which was to check the electrolyte level for the Chlorine Detector, the proper response was received from the appropriate alarms and valves. However, it was discovered that the blower unit and wick needed replacing. Since the monthly surveillance was required to be completed on August 17, 1989, and the alarms and .
valves operated appropriately, work request 69489 was written to replace the blower '
unit and wick. On October 10, 1989, work request 69489 was signed by Operations personnel for IAE personnel to start work on the OMVCMT5010 Chlorine Detector. IAE personnel were using procedure IP/0/B/3012/14, VC System Chlorine Detectors, to '
perform the maintenance. On October 12, 1989, at 1435, IAE Technician A was reconnecting the power leads according to step 10.7.1 in the Return to Service section of the VC System Chlorine Detectors procedure. While IAE Technician A was trying to place the power lead on the terminal strip using a screw starter or holding screwdriver, the screw and power lead fell from the screw starter and landed on the grounding screw in the terminal strip box. This caused a short to ground to occur, which then blew the AC power supply in-line fuse [EIIS:FU). When this, fuse blew, power was lost to all four Chlorine Detectors. This caused all four VC system outside air intakes to isolate. According to the Condition of Operability for the VC system (Operability Evaluation for PIR 0-M89-0163, Revision 1), Units 1 and 2 then entered TS 3.0.3.
IAE Technician A immediately called the Control Room and notified Operations personnel of what had happened. Operations personnel saw that there was a chlorine detection alarm and by looking at the indications for the valve positions they saw ,
that all four VC system outside air intakes had isolated. j 1
At 1510, Operations personnel removed power from the VC system outside air intake valves and manually opened the valves. This enabled Unit 1 and Unit 2 to exit from
'TS 3.0.3. It also placed Units 1 and 2 under another one hour action statement as required by TS 3.3.3.1. With the intake valves manually opened, EMF 43 would not be l able to perform its intended function of closing the intakes if a radiation alarm ;
occurred. Operations personnel were placed on standby at the breakers for the outside air intake valves, to close the valves in case of a high radiation alarm. )
By 1600, IAE personnel had replaced and functionally tested the in-line fuse, and l Operations personnel had restored power to the VC system Outside Air Intake Valves.
I NIC FOIU 366A *b.$. CNi 108a q ,S w e is.
O .-- ,
.]
+ ;
4 OthC Form NSA U g. esVCLED [ElutAtjaV COMMuBB40se f *** '-- LICENSEE EVENT REPORT (LER) TEXT CONTINUAT13N . uPaovio oue no. mo-om ERPIRES. t?31/N l
(
PACiterv NAest on DOCR41NUMDSR80 Lgp NUMG4R ts) PA04 43) a YIaR NMNm UEu*aIn McGuire Nuclear Station, Unit 1 o p jo lo j o l3 l 6l9 8l9 --
0l 3'l1 --
Ol0 o l4 0F 0 16 vexi m . w. .as w mc r asnav nn L
-Operations personnel had'to manually close the valves and then close the breakers h to return the intake valves to their full open position. This allowed Unit 1 and (J
Unit 2 to exit TS 3.3.3.1. i a -
On November 3, 1989, Operations personnel notified the NRC of a single failure that caused both trains of VC to become inoperable. ;
Conclusion-E This' event is assigned a cause of Inappropriate Action because the action taken was accidental. While IAE Technician A was placing the power lead on the terminal, the -;
power' lead fell from the' screw starter and touched ground. This in turn blew the '
120V AC power supply to the chlorine detectors in-line fuse, closing all four VC i
! Loutside air-intakes. The procedure requires the power leads to be removed for testing the Chlorine Detectors. Power cannot be isolated by opening a breaker because of other equipment required to be operable. Lifting power leads to test ~)
unisolable low-voltage equipment'is an accepted industry practice. This event <
occurred while the power leads were being replaced to return the OMVCMT5010 Chlorine Detector to service. I AE Technician A was performing this VC system ;
Chlorine Detectors procedure for the first time as on-the-job training and was not Employee Training and Qualifications System (ETQS) qualified to this task. )
However, the IAE Technician A was performing this procedure under supervisory '
- i. direction. This event will be covered with all IAE crews.
A mitigating circumstance is that the terminal box is small which does not allow personnel to hold the power lead in place while terminating it. The use of a holding screwdriver to place a power lead is standard practice for the IAE section.
MES will evaluate adding a terminal box with sliding links in line with existing wiring and take apprepriate actions as necessary.
The AC power supply to the chlo.-ine detectors in-line fuse was added recently during the Unit 2 End of Cycle 5 Outage according to Nuclear Station Modification (NSM) MG-1-0071. This NSM modified the 125 VDC Auxiliary Control Power System by 1 adding miscellaneous fuses to make the non-essential controls powered from the KXA l Inverter [EIIS:INVT] to power panelboard [EIIS:BD) KXA more reliable. A 5 Amp fuse j was added to protect the Radiation Monitor and Chlorine Monitor circuits for the ;
VC System. If this event had occurred prior to this NSM being implemented several i
, other systems in addition to the VC system would have become inoperable (e.g. I Reactor Building Purge System [EIIS:VA]). MES personnel will evaluate adding another fuse for the Chlorine Detectors circuitry to ensure train separation and redundancy and will take appropriate action as necessary. This event is still being investigated and an addendum will be written with the results of the investigation. l Operations personnel prepared for the possibility of the replacement of this in-line fuse taking over an hour, by securing the four intakes in an open position.
With the intakes secured open, if a high radiation alarm on EMF 43 had occurred, L the outside intake valves could not automatically close. Therefore, TS 3.3.3.1 was L entered because EMF 43 was rendered inoperable. Operations personnel were on
. a . cro, m . - - . !
%' J
v ->
4.
J[* . .
,,, vs. =Uct AmuuuroRv communios.
H}' ,
i.lCENSEE EVENT REPORT (LER) TEXT CONTINUATION uenovio ove ao mo-N ,
IXPIRES $/31/N PAC 8LffV hAhet it) DOCERT NUMB 4R 12) LtR NUMSOR 16) PAGE (3)
" O!.M '. s 7#.#
b McGuire Nuclear Station, Unit 1 olslojojol3lq9 8l 9 0l 0 0l5 0l 3l 1 -- OF 0 l6 TEXT (# mee ausse e mFureef. was 88uimoner MIC Fem M W 07) standby at the outside air intake valve breakers to be ready to close the breakers if a radiation alarm was received.
Both one hour TS Action Statements, TS 3.0.3 and 3.3.3.1, were met.
L A review of the past 12 months using the Operating Experience Program data' base for
. McGuire revealed 9 TS violation events or entry into TS 3.0.3 events with a general cause of Inappropriate Action. -However, there were no TS related events with a cause of accidental Inappropriate Action. Therefore, this event is not considered t recurring.
There have been'two events at McGuire in the past 18 months that documented' .
Inappropriate Actions that caused Engineering Safety Features Actuations (ESFA).
Licensee Event Report (LER) 360/88-8 involved Performance personnel performing a valve [EIIS:V] stroke timing test where a power lead inadvertently made contact
.with the electrical circuitry of the Turbine Driven Auxiliary Feedwater Pump. This
' caused.a fuse to blow and an ESFA to occur. LER 369/89-25 involved Performance personnel performing a valve stroke timing test where a jumper placed across a sliding link came loose and inadvertently made contact with another sliding link, thereby, causing a fuse to blow and an ESFA'to occur. Based on the above events the problem of Inappropriate Actions because of dropping power leads or jumpers is considered recurring.
' This event is not Nuclear Plant Reliability Data System (NPRDS) reportable.
There were .no personnel injuries, radiation overexposures, or uncontrolled releases .
of radioactive material as a result of this event. "
- CORRECTIVE ACTIONS:
1 Immediate: 1) Operations personnel removed power to the VC system Outside Air Intake valves and manually opened the valves, thereby, exiting TS 3.0.3 and entering TS 3.3.3.1.
- 2) Operations personnel were placed on standby at the Outside Air Intake valve breakers to close the valves in case of a high ;
radiation alarm. <
Subsequent: 1) IAE personnel replaced and functionally checked the in-line fuse on the Chlorine Detectors.
- 2) Operations personnel returned the VC System Outside Air Intakes to service by restoring power to them and returning them to the full open position thereby exiting TS 3.3.3.1.
Planned: 1) This event will be covered with all IAE crews.
I 2) MES personnel will evaluate aduing a terminal box with sliding L links in line with existing wiring and take appropriate action as necessary.
une row un ***m'""*^"*'
W. .
b'.- Olhc Perut 3084 U $ NUCLEI @ [61ULifoRY COMMtESION i,
LICENSEE EVENT MEPORT (LER) TEXT CONTINUATION ' ue ovio ows No 3+om ;
ExPints t/3 pas i P40luTV haast ni DOCKET NUMBER W LgR NUMSER $ PA06 43) vgAn 8 Q [ , <
"g*y McGuire Nuclear Station, Unit 1 o ls go jo jo l 3l q 9 8l 9 ._
q 3l 1 __
Og 0 0l6 0F 0l&
nmT u . m w ww u am4w nn ;
1
- 3) MES personnel will evaluate adding another fuse for the ,
Chlorine Detectors to have a fuse for each train and will take appropriate action as necessary.
- 4) An addendum will be written on the results of the investigation of the blown fuse causing both trains of VC to become' inoperable.
SAFETY ANALYSIS:
The design requirements of the VC syst.em are to supply filtered air at a controlled temperature and humidity to the Control Room and to pressurize the Control Room to !
prevent inleakage of unfiltered air. The VC system helps ensure that doses to Control Room personnel are As Low As Reasonably Achievable and remain below Code of Federal Regulations, Title 10, Part 50 (10CFR50), Appendix A, Criteria 19 (GDC-19) limits.
1 The TS 4.7.6 requirement specifies that a Control Room positive pressure of greater than.or equal to 0.125 inches v.g. relative to outside atmosphere during system operation must be demonstrated at least once every 18 months. A positive pressure y of 0.05-inches w.g. is-considered sufficient to prevent inleakage in excess of 10 cubic feet / minute, which is the assumed leakage value used for radiation dose ,
calculations in Chapter 15 of the Final Safety Analysis Report (FSAR).
The Operability Evaluation for PIR 0-M89-0163 results showed that both outside air pressurization filter trains were able to pressurize the Control Room greater than the 0.1C5 inches w.g. with all four outside air intakes open. With two intakes open, the Control Room pressure was still positive but less than the required 0.125 inches w.g.
P The principle contaminent contained in air leaking into the Control Room is' assumed to.be Iodine which is very conservatively modeled in dose calculations. Very low amounts of Iodine would be expected to reach the area around the Control Room since this requires passage through either Auxiliary or Turbine Building Ventilation ~
systems or passageways.
Control Room Operator dose would be further reduced by operation of the Auxiliary Building Ventilation system which is not safety related but has been maintained to safety standards. l i- In the event that Control Room atmosphere became unbreathable, self contained I breathing apparatus respirators provided in the Control Room area could be l E employed. Radiation monitors in the Control Room would alert Control Room l personnel of high radiation levels. I
~During this event, Operations personnel had manually opened the VC system outside air. intake valves; therefore, the Control Room pressurization would have been l i maintained had it been necessary. i The health and safety of the public were not affected by this event. l l
l
. _ __ _ _ N "' "I"" ,