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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:RO)
MONTHYEARML20024J3211994-10-0505 October 1994 LER 94-006-00:on 940909,failure to Perform Slave Relay Test Associated W/One Containment Isolation Valve Due to Improper Work Practices.Reviewed All Slave Relay Test Procedures & Trained All Qualified reviewers.W/941005 Ltr ML20046B5251993-08-0404 August 1993 LER 93-007-00:on 930705,TS Required Surveillance Was Not Performed Because of Inappropriate Action Because of Lack of Attention to Detail.Generated WO 93047633 to Perform Required Surveillance on Unit 1 IPE CA 9010.W/930729 Ltr ML20045H9821993-07-12012 July 1993 LER 93-005-00:on 930612,manual Rt in Unit 1 Occurred Due to Equipment Failure Due to Failure of L-13 Field Cable Between Data Cabinet B & Bulkhead for Undetermined Reasons.Replaced Field cable.W/930709 Ltr ML20045D9681993-06-25025 June 1993 LER 93-006-00:on 930526,discovered That Sample Blower for Radiation Monitor 1 EMF-43B Off & Monitor Declared Inoperable & Ventilation Sys Air Intakes Not Isolated.Caused by Deficient Procedures.Test Procedures Revised ML20045B2811993-06-11011 June 1993 LER 93-004-00:on 930513,both Trains of CR Ventilation Sys Declared Inoperable Due to Equipment Failure.Exact Cause of Failure Could Not Be Determined.Train B Nuclear Svc Water Sys Flow Balance completed.W/930611 Ltr ML20029C2091991-03-21021 March 1991 LER 91-003-00:on 910219,both Trains of Control Room Ventilation Sys Inoperable.Caused by Design Malfunction & Management Deficiency.Temporary Modifications,Removing Automatic Closure Function implemented.W/910321 Ltr ML20028G9561990-09-26026 September 1990 LER 90-025-00:on 900827,Unit 1 Shut Down Because of Unidentified RCS Leakage Exceeding Tech Spec Limits.Caused by Equipment Failure.Procedure AP/1/A/5500/10 Implemented. Valve 1NC-33 Will Be Repacked at Next outage.W/900926 Ltr ML20044A0091990-06-25025 June 1990 LER 90-015-00:on 900524,Tech Spec 3.0.3 Entered Because More than One Power Range Nuclear Instrumentation Channel Exceeded 5% Deviation.Caused by Mgt Deficiency.Boric Acid Added to Coolant sys.W/900625 Ltr ML20043H4991990-06-21021 June 1990 LER 90-012-00:on 900522,loose Matl,Consisting of Masslin Cloths & Stepoff Pad,Discovered in Upper Containment.Caused by Failure to Follow Procedures.Loose Items Removed & Cleanliness Procedures revised.W/900621 Ltr ML20043H2641990-06-20020 June 1990 LER 90-011-00:on 900521,noted That Valve 1RN-69A Auxiliary Feedwater Assured Supply from Train a Nuclear Svc Water Repositioned to Open Position After Start of Pump.Cause Unknown.Pump Shut Down & Valve closed.W/900620 Ltr ML20043F7471990-06-13013 June 1990 LER 90-010-00:on 900427,discovered That Annulus Ventilation & Control Room Ventilation Sys Headers Would Not Operate,As Designed,Under Postulated Operating Conditions. Caused by Design Deficiency.Change submitted.W/900613 Ltr ML20043F5071990-06-11011 June 1990 LER 90-009-00:on 900512,feedwater Isolation Occurred as Result of Steam Generator 1B Reaching hi-hi Level Setpoint of 82% Level.Caused by Inappropriate Action Because of Lack of Attention to Detail.Feedwater Logic reset.W/900611 Ltr ML20043D6541990-05-30030 May 1990 LER 90-007-00:on 881018,during Insp Ice Condenser Basket Found W/Bottom Screws Missing.Caused by Installation Deficiency Because of Improper Matl Selection.Work Request Initiated to Replace Improper screws.W/900530 Ltr ML20043D7121990-05-30030 May 1990 LER 90-006-00:on 900226,discovered Abnormal Degradation on Steel Containment Vessel.Corrosion Caused by Design Deficiency Caused by Unanticipated Environ Interaction. Detailed Insps conducted.W/900529 Ltr ML20043C8041990-05-30030 May 1990 LER 90-008-00:on 900430,radiation Monitor for Contaminated Parts Warehouse Ventilation & Sampler Min Flow Device Declared Inoperable.Caused by Personnel Error.Appropriate Procedures Enhanced to Prevent recurrence.W/900530 Ltr ML20012D1651990-03-19019 March 1990 LER 90-004-00:on 900208,determined That Holes Left in Auxiliary Shutdown Panel Could Allow Water Spray Into Cabinet.Cause Unknown.Holes Covered W/Duct Tape & Repaired. W/900319 Ltr ML20011F4261990-02-16016 February 1990 LER 90-002-00:on 900117,hold Down Screws on Sylvania Contactors in Motor Control Ctrs Found Loose.Caused by Mfg Deficiency.Contactor Screws Tightened.All Hold Down Screws Will Be Replaced W/Another type.W/900223 Ltr ML20006D5571990-02-0707 February 1990 LER 90-001-00:on 900108,reactor Trip Occurred Due to Clogged Strainer on Feedwater Pump a Speed Controller.Caused by Water in Oil Sys.Cause for Water Presence in Sys Unknown. Sludge Minimization Attempts pursued.W/900207 Ltr ML20006A8771990-01-21021 January 1990 LER 89-028-00:on 891204,self-initiated Technical Audit Team Personnel Identified Gap Around Control Room Ventilation Air Handling Unit Access Door.Caused by Possible Const/ Installation Deficiency.Door Sys modified.W/900122 Ltr ML19327C2581989-11-13013 November 1989 LER 89-031-00:on 891012,ac Power Supply Fuse Blew Resulting in Automatic Isolation of Four Outside Air Intakes on Ventilation Sys.Caused by Inappropriate Action.Intake Valves Returned to Svc & Tech Spec 3.3.3.1 exited.W/891113 Ltr ML19324C2031989-11-10010 November 1989 LER 89-024-00:on 890908,MSIV Stroke Timing Periodic Test Performed W/O Air Assistance & Three MSIVs Failed to Close within 5 S.Caused by Brass Guide Screws Excessively Tightened.Set Screws Properly set.W/891106 Ltr ML19324C2011989-10-31031 October 1989 LER 88-019-02:on 880719,damper Compartment Flows Did Not Meet Flow Requirements Due to Closure of Some Sys Dampers. Caused by Defective procedure.As-found Measurements Taken While Operating Fans for Damper positions.W/891030 Ltr ML19327B5611989-10-26026 October 1989 LER 89-030-00:on 890714,visual Insp Revealed 3/4 Inch Open Conduit Connection Which Would Have Prevented Successful Leak Test.Cause Unknown.Connection Removed & Hole Sealed. W/891026 Ltr ML19327B4771989-10-23023 October 1989 LER 89-029-00:on 890922,ESF Actuation Occurred When Diesel Generator 1A Started Due to Momentary Undervoltage Condition on Train a 4,160-volt Essential Switchgear.Cause Unknown. Offsite Power Source Returned to Normal svc.W/891023 Ltr ML19327B1511989-10-19019 October 1989 LER 89-026-00:on 890720,both Trains of Control Area Ventilation Sys Inoperable.Caused by Design Deficiency Because of Unanticipated Interaction of Components.Original Check Damper Reinstalled in Fan on Train B.W/891019 Ltr ML19351A4301989-10-18018 October 1989 LER 89-025-00:on 890918,jumper Came Loose & Inadvertently Made Contact W/Sliding Link B-14 Directly Above Link B-15, Resulting in Turbine Driven Feedwater Pump Automatically Starting.Caused by Inappropriate action.W/891018 Ltr ML19325D4991989-10-16016 October 1989 LER 89-027-00:on 890915,preheaters Did Not Start Because Air Flow Permissive Was Not Made & Cross Connect Dampers Were Closed & Tagged & Ventilation Sys Train a Remained Logged Inoperable.Caused by Design deficiency.W/891016 Ltr ML19325C4871989-09-28028 September 1989 LER 89-018-00:on 890829,both Trains of Control Area Ventilation (VC) & Chilled Water (Yc) Sys Declared Inoperable.Caused by Equipment/Failure Malfunction. Refrigerant Added to Vc/Yc chiller.W/890928 Ltr ML20043D7041989-09-25025 September 1989 LER 89-022-01:on 890826,reactor Trip Occurred Due to Failed Universal Board in Solid State Protection Sys Cabinet A. Caused by Equipment/Malfunction.Universal Board Replaced. W/900530 Ltr ML19325C4731989-09-18018 September 1989 LER 89-015-00:on 890722,discovered That Neutral Pressure Was Best That Could Be Achieved in Some Required Sys Configurations.Caused by Design Deficiency Due to Design Oversight.Outside Air Ref Point installed.W/891004 Ltr ML20024F2791983-08-29029 August 1983 LER 83-066/03L-0:on 830817,invalid Alarm Received for Fire Detection Zone Efa 90 Which Would Not Clear.Caused by Unusual Svc Conditions.Detector Cleaned & replaced.W/830829 Ltr ML20024D8101983-07-29029 July 1983 LER 83-050/03L-0:on 830629,control Area Ventilation Sys Train B Declared Inoperable.Caused by Automatic Reset Preheater Overtemp Cutout Switch Failure.Replacement Switch Will Be installed.W/830729 Ltr ML20024D7531983-07-27027 July 1983 LER 83-048/03L-0:on 830624,control Area Ventilation Sys Train B Declared Inoperable Following Low Refrigerant Temp Alarm Trip of Control Room Chiller B.Caused by Cleaning of Condenser tubes.W/830727 Ltr ML20024D7701983-07-27027 July 1983 LER 83-049/03L-0:on 830624,surveillance Compliance Review Revealed Three Time Response Tests Not Performed.Cause Not Stated.Remaining Channels Will Be Tested During Next refueling.W/830727 Ltr ML20024D8951983-07-27027 July 1983 LER 83-047/03L-0:on 830627,discovered That 18-month Insp of Fire Hose Station 180 Not Performed During Nov 1981.Caused by Order Preventing Personnel from Entering Area Due to High Radiation Levels.Procedural Change instituted.W/830727 Ltr ML20024C4091983-06-28028 June 1983 Updated LER 83-002/03X-1:on 830110,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Heat Damage Found at Heat Dissipating Resistor Connections.Caused by Design Defect in Contactor Coil circuit.W/830628 Ltr ML20024C3941983-06-28028 June 1983 LER 83-035/03L-0:on 830515,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable Per Tech Spec 3.4.3.Caused by Blown Fuse in Heater Contactor Control Circuit.Fuse replaced.W/830628 Ltr ML20024C0001983-06-27027 June 1983 LER 83-030/01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules recalibr.W/830627 Ltr ML20023C4691983-05-0505 May 1983 LER 83-017/03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised ML20028E0131983-01-10010 January 1983 LER 82-081/03L-0:on 821211,lower Personnel Airlock Declared Inoperable After Reactor Door Found Partially Closed W/Small Seal Ruptured & Large Seal Inflated.Cause Not Known.Seal Not Designed to Withstand Unrestrained Inflationary Forces ML20028A5301982-11-10010 November 1982 LER 82-073/03L-0:on 820403,during QA Audit of Test Procedures,Incore & Nuclear Instrumentation Sys Correlation Monthly Check Found Not Performed.Caused by Incorrect Test Schedule ML20027D3351982-10-22022 October 1982 LER 82-071/03L-0:on 820922,motor Control Ctr Lemxd Lost Power Causing Temporary Inoperability of Several Essential Sys/Components.Caused by Automatic Trip of Feeder Breaker. Breaker Reset & Closed.Power Restored ML20027B5051982-09-10010 September 1982 LER 82-067/03L-0:on 820813,two Auxiliary Feedwater Pump Turbine Low Suction Pressure Switches Failed to Perform During Functional Test.Caused by Switches Being Out of Calibr,Possibly Due to Instrument Drift or Misadjustment ML20027B5521982-09-0808 September 1982 LER 82-064/03L-0:on 820809,vent Flow Monitor Indicated Zero W/Vent in Operation During Process of Returning to Mode 1. Caused by Out of Calibr Differential Pressure Transmitter Due to Instrument Drift.Transmitter Recalibr ML20052H5831982-05-10010 May 1982 LER 82-027/03L-0:on 820326,one Channel of Position Indication for RCS Power Operated Relief Valves NC-32 & NC-36 Declared Inoperable When Closed Indicator Lights Failed.Caused by Loose Fitting Bulb Due to Crack in Socket ML20052G6791982-05-0707 May 1982 LER 82-030/01T-0:on 820423,diesel Generator 1A Declared Inoperable After Failing to Start for Periodic Test.Caused by Failure of Station Design Change Implementation Program to Control Work on Station Mods ML20052H7421982-05-0707 May 1982 LER 82-031/03L-0:on 820408,boric Acid Transfer Pump a Failed to Perform at Capacity & Declared Inoperable.Caused by Reverse Rotation Due to Improperly Connected Windings. Personnel Counseled & Maint Routine Modified ML20052H7481982-05-0606 May 1982 LER 82-029/03L-0:on 820402,investigation of Power Operated Relief Valve (PORV) & Pressurizer Code Safety Discharge Line High Temp Alarms Revealed Indications of Leakage for PORV NC-34.Cause Undetermined.Valve Will Be Repaired ML20052H6091982-04-30030 April 1982 LER 82-028/03L-0:on 820401,during Mode 1 Operation,Radiation Monitors EMF-31 & EMF-33 Lost Power.Caused by Monitor EMF-46 Tripping Circuit Breaker Due to Direct Short Across Power bulb.EMF-46 Isolated & EMF-31 & 33 Returned to Svc ML20052G3611982-04-29029 April 1982 LER 82-025/03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency 1994-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20154L6321998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for McGuire Nuclear Station,Unit 1 ML20153B3741998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236U1601998-07-31031 July 1998 Non-proprietary DPC-NE-2009, DPC W Fuel Transition Rept ML20237B2381998-07-31031 July 1998 Monthly Operating Repts for July 1998 for McGuire Nuclear Station,Units 1 & 2 ML20153B3931998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for McGuire Nuclear Station,Units 1 & 2 ML20236P0451998-07-0808 July 1998 Part 21 Rept Re non-conformance & Potential Defect in Component of Nordberg Model FS1316HSC Standby Dg.Caused by Outer Spring Valves Mfg from Matl That Did Not Meet Specifications.Will Furnish Written Rept within 60 Days 1999-09-30
[Table view] |
Text
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. . ' Duke Ibuer Company (IU4P 75-4000 AlcGuire Nuclear Statwn 12:00 llagers l' erry Road fluntersrille NC30784985 DUKE POWER May 30, 1990 U.S. Nuclear Regulatory Commission Document control Desk Washington, D.C. 20555
Subject:
McGuire Nuclear Station Unit 1 Docket No. 50-369 Licensee Event Report 369/89-22-01 Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached is Licensee Event Report 369/89-22-01 concerning a Reactor Trip because of a failed universal board in the Solid State Protection System. This report is being revised and submitted in accordance with 10 CFR 50.73(a)(2)(iv). This event is considered to be of no significance with respect to the health and safety of the public.
Very truly yours, r
ny Iff T.L. McConnell DVE/ADJ/cbl Attachment xc: Mr. S.D. Ebneter American Nuclear Insurers Administrator, Region II c/o Dottie Sherman, ANI Library U.S. Nuclear Regulatory Commission The Exchange, Suit 245 101 Marietta St., NW, Suite 2900 270 Farmington Avenue Atlanta, GA 30323 Farmington, CT 06032 INPO Records Center Mr. Darl Hood Suite 1500 U.S. Nuclear Regulatory Commission 1100 Circle 75 Parkway Office of Nuclear Reactor Regulation Atlanta, GA 30339 Washington, D.C. 20555 M&M Nuclear Consultants Mr. P.K. Van Doorn 1221 Avenue of the Americas NRC Resident Inspector New York, NY 10020 McGuire Nuclear Station 90061100{ noo -
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'Lb369/89-22-01 >
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'bxc ~B.W. Bline L.G. Bost J.S. Warren ,
R.L. Gill R.M. Glover (CNS) y T.D. Curtis (ONS)
P.R. Herran S.S. Kilborn (W)
R.E. Lopez-Ibanez M.A. Mullen !
R.O. Sharpe (MNS)
G.B. Swindlehurst ,
K.D. Thomas M.S. Tuckman L.E. Weaver <
R.L. Weber J.D.-.Wylie (PSD)
J.W. Willis :
i QA Tech. Services NRC Coordinator (EC 12/55)
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LICENSEE EVENT REPORT (LER) ' mate r3um pageglTy esaget qu DOCEST 90VRA9th til PAGE G Nc0uire Nuclear Station, Unit 1 o ls ;o io iol3 6i ; 9 1 loFl 018
''' Reactor '! rip Occurred Because Of A Failed Universal Board In The Solid State Protection System Cabinet Train "A" Evtaff OATS (S) LGR NURSER del . RSPORT Daf t t?) OTHER F ACILifitt INVOLVl0 m)
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Lectassit CONTACT FOR fMIS Lim till NAME TELEPHONE NUMetR
- Rta COD 4 Alan Sipe, Chairman, McGuire Safety Review Group 7; O i 4 8,7 i 5, ,4 , 1, 8 ,3 Cot 8PLif t ONC LINE FOR S ACM COMPONENT f ALLURE DESCRis40 th TMI: Atront H31 CAust $v5ftM . COMPONENT
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~} vis m ,.. w are surerto suewssioN oa rt; Tl No 0 16 0l1 9 10 Au,R AC, w.., a uw ,,a., ... n-m<v rsw ove u ava.nw <-. > ve On August 26, 1989 at 0934, a Unit 1 Reactor Trip occurred because of a Reactor Coolant (NC) low flow signal that is interlocked with a permissive signal which j blocks a Reactor Trip when the unit is less than 48 percent power (P-8 permissive).
Unit I was operating in Mode 1, Power Operation, at 100 percent power prior to the i trip. A low.NC flow signal with P-8 permissive caused Reactor Trip Breaker "A" to-trip the unit. The signal was caused by a failed Universal Board in the Solid.
State Protection System (SSPS) cabinet for Train "A". The Turbine Generator automatically tripped because of the Reactor Trip. All systems and equipment responded as expected following the trip with one exception. Operations personnel implemented the Reactor Trip recovery procedure to recover from the transient. At about 1000, Operations personnel made the required notification to the NRC. At 2220, Instrumentation and Electrical personnel discovered the failed Universal Board and replaced it. The SSPS Cabinet was tested after the board was replaced to ensure the train'would operate properly. Unit I was returned to Mode 1, Power Operation, on At. gust 28, 1989 at 1230. This event is assigned a cause of Equipment l' Failure / Malfunction. This event is Nuclear Plant Reliability Data System L reportable. The board will be sent to Westinghouse for repair and failure analysis.
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EVALUATION:
Background
The Solid State Protection System (SSPS) takes digital inputs (voltage /no voltage) from the 7300 Process Control System and nuclear instrument channels [EIIS:CHA]
corresponding to conditions (normal / abnormal) of unit parameters. The system combines these signals in the required logic combination and generates a trip signal (no voltage) to the undervoltage coils of the Reactor [EIIS:RCT] Trip circuit breakers [EIIS:52] when the necessary combination of signals occur. The system also provides annunciator [EIIS: ANN] status lights [EIIS:IL] and computer
[EIIS: CPU) input signals which indicate the condition of biatable input signals, partial trip and full trip functions and the status of the various blocking, i permissive [EIIS:69] and actuation functions. .Bistables actuate at the setpoints j at which a signal would be initiated through the Reactor Protection System (RPS) j
[EIIS:JC]. j Annunciation for Reactor Trips consists of alert. and bistable indication lights
[EIIS:IL] which will light and sometimes flash when a channel in the 7300 Process
~ Control System (PCS) receives a signal that a setpoint has been reached (e.g. low coolant flow). . When logic is satisfied (e.g. two out of three channels in a loop receive a low coolant flow signal) a Reactor Trip is initiated and a first out annunciator that indicates what caused the Reactor Trip (e.g. Lo Flow P-8 Permissive Reactor Trip) will light.
The P-8 permissive interlock [EIIS:IEL] blocks a Reactor Trip from either a single loop loss of coolant flow signal or a Turbine [EIIS:TRB] Trip signal if the unit is
- _ below approximately 48 perce.it of full power.
The Reactor Coolant (NC) System [EIIS: AB) low flow Reactor Trips protect the core j
from departure from nucleate boiling (DNB) in the event of a loss of coolant flow. ,
j An output signal from two out of the three histables in a loop indicates a low flow in that loop. Above P-8 permissive, low flow in any one loop causes a Reactor Trip. Each of the two logic trains, A and B, is capable of opening a separate and independent Reactor Trip breaker, RTA and RTB, respectively.
Technical Specification Action Statement No. 14, Table 3.3-3 states:
"With the number of operable channels one less than the minimum channels
..perable requirement, be in at least Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Cold l Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />; however, one channel may be bypassed 9 for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing per Specification 4.3.2.1, provided the other channel is operable."
Description of Event On August 26, 1989 at 0934, a Reactor Trip signal was received along with a "Lo Flow P-8 Permissive Reactor Trip" first out alarm indication. The reactor was in Mode 1, Power Operation, at 100 percent power with all control systems in automatic prior to the trip. There were no NC low flow alert or bistable indications
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, . LICENSEE EVENT REP 2RT (LER) TEXT CONTINUATION uenovf o oMe No. mo-om EXPints: tt31/3 FActLity esaast tu DoceLit sevaSER m LER NUMeta (en Past (31 YEAR UiNa :
aN n . J McGuire Nuclear Ststion, Unit 1 o js jo j o j o l3 l 6l9 8l9 --
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? 1 L received prior to receiving the Reactor Trip and the first out Reactor Trip l indication. Instrumentation and Electrical (IAE) personnel were testing the RPS I 7300 PCS System in Channel IV with T-ave and delta-T in test. The Events Recorder
[EIIS IQ) had documented that the Reactor Trip Breaker A (RTA) opened 284 milliseconds prior to the opening of Reactor Trip breaker B (RTB).
The Reactor Trip initiated a Turbine Trip. The C Steam Generator (S/G) (EIIS:SG)
Power Operated Relief Valve (PORV) [EIIS:RV), ISV-7, lifted as the S/G pressure reached 1119.3 psig which is within the open setpoint range (1114 psig to 1136 psig). Next, S/G B had a Iow-low level signal which in turn initiated the start of the Auxiliary Feedwater (CA) System [EIIS:BA).
Operations (OPS) Control Room personnel implemented Reactor Trip procedure, EP/1/A/5000/01, Reactor Trip or Safety Injection, and then entered procedure EP/1/A/5000/1.3, Reactor Trip. OPS Control Room personnel then implemented Reactor Trip Recovery procedure OP/1/A/6100/05, Unit Fast Recovery. At 0950, a manual isolati-on of the Feedwater (CF) System [EIIS:SJ) was initiated to conserve i auxiliary steam. At about 1000 the NRC was notified by OPS Control Room personnel i according to procedure RP/0/A/5700/10, NRC Immediate Notification Requirements.
At 1030, Work Request 139505 was submitted to check calibration on th- NC system flov bistables for the RPS. Extensive testing was performed to determine if any of tt.e bistable setpoints had drifted above the required trip setpoint (90 percent),
after testing was complete, it was determined that the bistables had not drifted.
- The flows for all loops were plotted and none of the flows had decreased below the bistable setpoints. This indicated that the trip did not occur because of an input to the 7300 PCS channels.
A meeting was then held between Operations, IAE, Maintenance Engineering Services (MES) and Performance personnel at 1800 to discuss the current findings from troubleshooting the 7300 PCS cabinet [EIIS: CAB]. Former trip reports were reviewed for documented times for Reactor Trip Breakers to trip. A loss of voltage trip is normally somewhere between 60 to 90 milliseconds with an administrative maximum of 100 milliseconds. Based on past Reactor Trips, it was shown that it took about 190 milliseconds to initiate a Reactor Trip on a high negative reactivity rate (i.e.
all contro1~ rods entering the core by gravity). IAE tested the 7300 PCS output signals to the annunciators since no alert or bistable low flow indicationc were received prior to the trip. Normally, if one channel receives a low-flow signal, an alert annunciator will alarm. No problems were found. Therefore, with the lengthy time between Reactor Trip breakers and correct annunciator operation, MES personnel concluded that the problem was probably in the SSPS Train "A" cabinet.
At 1820, Work Request 139510 was submitted to troubleshoot the SSPS Train "A" Cabinet. Train "A" was chosen because RTA opened first or. a loss of voltage signal. RTB opened on a high negative reactivity rate signal.
Procedures IP/0/A/3010/07, Procedure For Troubleshooting The Solid State Protection System (SSPS), and PT/0/A/4601/08A, Solid State Protection System (SSPS) Train A Periodic Test With NC System Pressure Greater Than 1955 psig, were used to troubleshoot the SSPS Train "A" cabinet. Universal boards [EIIS:ECBD] A303, 304, l NIC PORM 3ggA .y,3, cpo 1944 520 541,000H rPMl
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'saa "MM', 27.*.W McGuire Nuclear Station, Unit 1 o ls lo j o j o l 3,l 6l 9 8l9 0l2l2 0l1 0l4 OF 0[8 TexTw .-.. n. sm-wmic=-aw w n 305, 306, and 308 were tested with the SSPS Cabinets' automatic logic test sequencer. This sequencer sends pulses to the circuit boards to check logic state changes. No problems were found. The boards were checked again by manually checking the 'agic states and no problems were found. A visual check of the boards was completad by pulling the boards out of the cabinet, thereby, deenergizing the boards. By procedure when the boards are removed, they are required to have the logic re-checked. When Universal board A303 was checked this time, it failed. All the other boards tested satisfactorily. IAE then tested board A303 again with it failing again. A303 was replaced. Also, by procedure, when a board is replaced the entire cabinet is required to undergo a logic check. All boards checked out satisfactorily.
At 2218, OPS complied with Technical Specification Action Statement No. 14 of Table 3.3-3 since SSPS Train "A" was not returned to service within the required 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> because of troubleshooting. Unit I was in Mode 3, Hot Standby, at the time. At i.
2220, Universal Board A303 in the SSPS Train "A" cabinet was determined to have
. failed and was replaced. At 2230, a follow-up meeting between Operations, IAE, HES, and Performance personnel was held to inform these groups about the failed universal board. At 2240, SSPS Train "A" was returned to service after testing had been completed.
t i On August 28, 1989, at 1230, Unit I was returned to Mode 1, Power Operation.
Conclusion This event is assigned a cause of Equipment Failure / Malfunction because Universal Board A303 failed. When Universal Board A303 failed, an immediate si dnal was sent ,
to Universal Board A308 confirming a low NC flow signal. This then required an output signal to be sent to trip the Reactor if the P-8 permissive interlock was unblocked. Since the unit was at 100 percent power, the signal was sent to RTA to trip the Reactor. While the Reactor was shutting down, RTB tripped on high negative power rate. ,
Since 1986, there have been 9 failures out of 156 Universal boards in use at the station. This is a 2.0 percent failure rate per year. None of the past Universal board failures have caused a Reactor Trip. The past failed Universal boards were sent to Westinghouse to be repaired. The Universal board is manufactured by Westinghouse Electric Corporation, model number 6056D21 001 and serial number 1206.
MES personnel have contacted Westinghouse personnel about repairing this Universal board. Work Request No. 69501 has been written to send the, Universal. board to Westinghouse for repair. A repair summary has been requested to. document what ~
caused the board to fail.
One anomaly reculting from the Reactor Trip was that S/G B level decreased to 11 percent. Station personnel are continuing to investigate the cause of this level decrease. The CA system automatically started because of the S/G B low-low level signal and was capable of removing the decay heat from the Reactor.
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.= LICENSEE EVENT REPORT (LER) TEXT CONTINUATl3N emovto owe no sm-em EXPIRES: 8'31/W i PACILITY esAass gig Docatt NUtdStR (2) . LER NURAbtR 101 P&Of {3) l vi*a "ELO.P 'l'M.i:
McGuire Nuclear Stat' ion, Unit 1 o ls [o j o lc l3l 6l9 8l9 --
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,0l1 0l 5 or 0l8 ftxT tr mwe ausse a snousev, use asasumut AWIC passe m W (173 A review of the LER data base for the past twelve months prior to this event revealed 2 LERs that described Reactor Trips resulting from equipment failures. l LER 370-89-02 documented a Reactor Trip because of a S/G B Low-Low level following loss of the CF turbine pump (CFPT) 2B. This was a failure of suction pressure switches on the CFPT and a broken air supply line to the Full Load Rejection valve
[EIIS:V) 2CM-420. LER 370/89-03 documented a Reactor Trip because of a low-low- i level in S/G C which was caused.by a failed bellows [EIIS:BE] in the positioner for H the CF regulating valve for S/G C, 2CF-20. The corrective actions for these LERs !
were specific to their events. These events are not similar because the failures l
were on different equipment. Therefore, this event is considered not recurring. '
This event is Nuclear Plant Reliability Data System (NPRDS) reportable. Industry reported to NPRDS seven Universal board failures for boards used in the RPS which were manufactured by Westinghouse Electric Corporation with the model number )
6056D21 G01. Four board failures were caused by faulty integrated circuit chips and three failures were caused by unknown reasons.
There were no personnel injuries, radiation overexposures, or releases of radioactive material as a result of this event.
CORRECTIVE' ACTIONS:
t I. Immediate: 1) OPS personnel implemented procedure EP/1/A/5000/01, Reactor
! . Trip or Safety Injection, and then entered procedure EP/1/A/5000/1.3, Reactor Trip.
- 2) OPS personnel implemented recovery procedure OP/1/A/6100/05, l Unit Fast Recovery.
Subsequent: IAE personnel replaced Universal Board A303 in the SSPS train "A" cabinet.
Planned: 1) MES personnel will send the Universal board to Westinghouse for repair and failure caalysis.
- 2) The McGuire Safety Review Group wi?1 write an addendum to this LER when the repair summary is received from Westinghouse.
1:
SAFETY ANALYSIS:
I An analysis of a decrease in NC System flow rate is presented in Section 15.3,
-Decrease in Reactor Coolant System Flow Rate, of the Final Safety Analysis Report
.(FSAR). If the reactor is at power at the time of the accident, the immediate effect of . loss of coolant flow is a rapid increase in the coolant temperature.
This increase could result in DNB with subsequent fuel damage if the reactor is not tripped promptly. The necessary protection against a partial loss of coolant flow l
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, . LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Aaeaovio on.e no mo-m4 axenes ersue -
PACILITY Isaast us Docetti sfunesa (3) Ltm NURABGR 40) PA00 la viaa " d!,0. 'E*.i;
~McGuire Nuclear Station, Unit 1 o js l o j o j o l 3,l 6l 9 8l9 _
0l2l2 0l1 O j6 oF 0 [8 text nr . ancwam4mm accident is provided by the low primary coolant flow Reactor Trip signal which is actuated in any reactor coolant loop by two out of three low flow-signals. Above Permissive 8, low flow in any loop will actuate a Reactor trip. The analysis of 1 effects and consequences for low NC flow shows that the DNB ratic will not decrease i below the limit value at any_ time during the transient. Thus, no fuel or_ clad damage is predicted, and all epplicable acceptance criteria are met. ..
l The unit responded to the Reactor Trip without any significant problems. All j primary and secondary system parameters were at their approximate no-load value 30 i I
minutes after the trip.
l As Main Steam [EIIS:SB] pressure for S/G C reached 1119.3 psig, PORV ISV-7 lifted '
because the S/G pressure entered the open setpoint range (1114 psig to 1136 psig) for valve ISV-7. S/G A, B, and D PORVs did not actuate, although S/G A, B, and D pressures entered the open setpoint range. None of the S/G pressures exceeded their respective open setpoint ranges. Main Steam pressure did not reach the main steam code safety valve lift setpoints and the valves were not challenged. NC system pressure did not reach the Pressurizer [EIIS:PZR] PORV or Pressurizer Code Safety valve lif t setpoints and the valves were not challenged. Adequate core
' cooling was maintained throughout this transient, and the NC System boundary was not challenged. Emergency power and emergency core cooling were not required in l ,i this event and were not actuated.
l
{ The health and safety of the public were not affected by this incident.
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McGuire Nuclear Station, Unit 1 o ls [o jo j o l3l 6l9 8l9 0l 2 l2 -
0l1 0}7 or 0 18 text = - . w. .sm anc a - me w on ADDITIONAL INFORMATION:
Sequence Of Events 0A0 - Operator Aid Computer Printout TRI - Transient / Reactor Trip Investigation Report SSL - Unit 1 Shift Supervisor's Logbook SEL - Unit 1 Shift Engineer's Logbook REL - Unit 1 Reactor Engineer's Logbook PR - Personnel Recollection WR - Work Request Section 1 Date Tin.e Event 8/26/89 09:33:54 A Reactor Trip was received on a first out alarm "Lo Flow P-8 i Permissive Reactor Trip." (OAC.TRI,SEL,SSL) 09:34:01 A Reactor Trip initiated a Turbine Trip. (OAC,TRI) 09:34:17 S/G C PORV ISV-7 lifted as S/G pressure reached 1119.3 psig;
! thereby, entering the Open Setpoint Range for valve ISV-7.
(OAC,TRI) 09:34:22 S/G B Low-Low Level signal caused the CA system to start.
. (TRI)
'09:50:10 A manual feedwater isolation was initiated to conserve auxiliary steam. (TRI) l
, .i l
OPS Control Room personnel implemented the Reactor Trip l
recovery procedures. (TR1,PR)
N1000 OPS Control Room personnel made the required notification to the NRC. (SEL,PR)
L
! 1030 Work Request No. 139505 was submitted to check calibration on the riC sy-tem flow bistables for RPS. (WR) l 1800 - A meeting was held to discuss the results of the !
l- 1930 troubleshooting findings and what further testing should be pe rformed. (PR) 1820- Work Request 139510 was submitted to troubleshoot the SSPS Train "A" Cabinet. (WR) 2218 SSPS Train "A" was not returned to service yithin two hours of commencing testing; therefore, OPS complied with Technical Specification Action Statement No. 14. (SSL) i pone sena ev.s. cro, me.uo uv voon ;
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UCENSEE EVENT REPORT (LER) TEXT CENTINUATCN emovio om omm-o*
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McGuire Nuclear Sta't' ion, Unit 1 olstolcjol3,l6l9 8l9 -
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2220 The Universal Board in the SSPS Train "A" cabinet was found failed and was replaced. (PR,SEL) 2230 A follow-up meeting was held to inform station groups of the l
. failed board. (PR,SEL) {
t.
2240 SSPS Train "A" was back in-service with testing completed. .
(SSL) l t
8/28/89 1230 Unit I was returned to Mode 1 Power Operat.on.
SUPPLEMENTAL INFORMATION: ,
The following information addresses Planned Corrective Action Number 2, to submit t the results of 'the failure summary analysis performed by Westinghouse on Universal Board l A303. j MES personnel sent Universal Board A303 to Westinghouse. On February 12, 1990, MES personnel received a Repair Report from Westinghouse on the item. Westinghouse i ceported that after the universal board was received, it was inspected on January
! 31, 1990 with no visible damage or defects noted. The universal board was then sent for testing on Febra ry 5, 1990. During this test, two component failures were noted. The component failures were on CR29 and CR23 diodes. The CR29 diode is only associated with demultiplexing and could not have contributed to the ,
Reactor Trip. However, the CR23 diode is tied directly to an output signal which generates the Reactor Trip signal by de-energizit.y the Reactor Trip Breaker Undervoltage Coil. Consequently, the failure of the CF23 diode caused the Reactor t to trip. To cause a Reactor Trip. CF23 diode would have to have been electrically I
l shorted out. It could not be determined how CF23 became shorted. ,
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'U.S. GPO: 1988 530-389 UNh g gg, y
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