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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:RO)
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
[Table view] |
Text
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Georgia Pow Comgaany '
~ .6 n.
333 Pecaniont Avenue- '
= . ' ' ' Attanta. Geoga 30308
!T . . -/ .'. -
.. j hubone 404 S26 3195 ..
Mamno Nidress ;
'1
. 40 inverne% center Pa4way _
Pot,t Oftce Box 1295 -
., ! ,v Bamingham, A!atema 35201
' lelephone 205 808-558i'
. February 23, 1990 u mu:"edeve mwn ,
j -J- ' W. G. Hairston, lli ,
Nuclear Operat o,s ,
ELV-01340-0241 Docket No. 50-424 U. S.-Nuclear Regulatory Commission i ATTN: : Document Control Desk ..
Washington,- D. C. 20555 Gentlemen:
V0G'TLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT 1
REACTOR ~ TRIP DUE TO INADVERTENT CLOSURE OF MAIN.
STEAM ISOLATION VALVE In accordance with'10 CFR 50.73, Georgia Power Company hereby submits the i enclosed. report related to'an event which occurred on January 24, 1990.
Sincerely, LU ll W. G. Hairston,'III ,
WGHilII/NJS/gm s
Enclosure:
.LER 50-424/1990-01 1 xc: Georoia Power Company -i Mr. C. K. McCoy Mrs G. Bockhold, Jr.
- Mr.-R. M. Odom Mr P.-D. Rushton 3 NORMS t
7 U. S. Nuclear Reuttlatory (pmmission e
- Mr. S. D. . Ebneter, Reg iornal Administrator H Mr.. D.'B.:Matthews, Director, Project Directorate II-3
'Mr. R. F. Aierlo, ' Senior Resident Inspector u
e 9003060244 900223 'dhs PDR ADOCK 03000424 pel i 1
- R PriC 8# l
<tc . . _ . . .
C mm p U 5. NUCLEA3a LE LULATE.Y COMutsSION 4 '
i d.PPAOYED OM8 NO 2190010s
>; ( " P'"' 8 '
LICENSEE EVENT _ REPORT (LER)
F.CILITY NAMt til DOCH11 NUMGE R (26 PAGE13i
-V0GTLE ELECTRIC GENERATING PLANT - UNIT 1- oIsIo1oIoi4l214 1 loFl 0 l5 TICLE tal REACTOR TRIP DUE TO INADVERTENT CLOSURE OF MAIN STEAM ISOLATION VALVE EVENT DAf f (Si LER NUMBER (61 REPORT DAf t (71 OTHER F ACILITit$ INVOLVED (8)
CONTH . DAY YtAR YEAR IS' O [f,","j MONTH OAY YEAR F ACallT V NAws DOCKE T NUM8t RISI L* '
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NAME TE LEPHONE NUMBER ARI A COOf R. M. ODOM/ NUCLEAR SAFETY AND COMPLIANCE 41014 8121 61-13 12101 1 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBIO IN THit REPORT (131 naPoRta e CAust SYSTEM COMPONtNT Mjjf,AC y qpn CAust SYSTEM COMPONENT "j%^C REPORf y pp A E l
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On 1-24-90, partial stroke testing of a Main Steam Isolation Valve .(MSIV) was in progress. During a previous test, the valve had failed to reopen automatically at the 10% closed position as designed. ' As a result, plant personnel were prepared to install a jumper to reopen the valve if it failed to reopen automatically. The test began and an indicator illuminated at approximate 1y'10%
closed; however, unknown to the personnel involved, there were two . limit switches which were not adjusted to actuate concurrently. Consequently, when the indicator. illuminated, the other limit switch had not yet actuated and it l appeared that the valve would not reopen automatically. The jumper was l installed to initiate valve reopening; however, position indication was lost and the MSIV went fully closed. MSIV closure resulted in a rapid decrease in water level in Steam Generator (SG) #4 to the low-low level setpoint and an automatic reactor trip occurred at 0133 CST.
l An investigation determined that when the jumper was installed, the MSIV control L fuses failed, which caused the valve to close.
L Corrective actions include: a) fuse replacement, b) procedure revision to include a caution that the indicator may light prior to the valve receiving the l.' reopen signal, and, c) limit switch adjustment to obtain concurrent actuation. .
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i A. REQUIREMENT FOR REPORT This report'is required per 10.CFR 50.73 (a)(2)(iv) because an unplanned i actuation of the Reactor Protection System occurred. ,
B. UNIT STATUS AT TIME OF EVENT p,
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' At the time of this event, Unit I was operating in Mode 1 (Power Operation) at 90% of rated thermal: power. Other than that described herein, there was-
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no inoperable equipment which contributed to the occurrence of this event. ,
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C. DESCRIPTION OF EVENT j 1
On 1-24-90, partial stroke testing of Main Steam Isolation Valve (MSIV) j 1HV-3036A was-in progress in accordance with Procedure 14842-1, " Main Steam 1' Isolation Valves Partial Stroke Inservice Test". 'During a previous quarterly test in August 1989, the valve did not automatically reopen as !
designed when it reached the 10% closed position. Electricians had been 1 assigned to the auxiliary relay-panel to assist during the test. Their responsibility was to install a jumper to reopen the valve if it did not-automatically reopen at the 10% closed position. If the valve reopened as a
. result of the jumper, this would. confirm that a failed contact was the.cause of the failure to reopen automatically. The test began and at approximately 10% closed, the blue light indicator came on in the control room but the >
valve continued to close because the limit switch which initiates reopening ;
had not yet actuated. The electricians were advised and they-installed the jumper to initiate valve reopening. As they installed the jumper, position
~ indication was lost and the MSIV continued to the full closed position.
t' Closure of the MSIV resulted in a rapid decrease in water level in Steam Generator (SG) #4. The level decreased to the low-low water level setpoint and an automatic ~ turbine / reactor trip occurred at 0133 CST. The Main Feedwater System isolated-and the Auxiliary Feedwater System actuated as designed. Atmospheric Relief Valve (ARV) 1PV-3030 opened' to control pressure in SG #4. Control room operators responded properly to control SG
. water levels. Steam dump valve ITV-500C indicated not fully closed and g control room operators initiated a Main Steam Line Isolation (MSLI) on the remaining three steam lines to limit the Reactor Coolant System (RCS) cooldown rate.
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nxw- w.e e-.a. .~ mc r- , saw nm p As:the generator tripped off the grid, unit power transferred from the Unit-Auxiliary Transformers (UATs) to the Reserve Auxiliary Transformers.(RATS). .
However, a non-safety related 4160 volt bus, INA04, failed to transfer.and..
;. power was lost to its connected loads. These included the Turbine Plant-Cooling Water (TPCW) pump-#1 discharge valve, air compressors, and condenser vacuum breakers. While attempting to re-connect the loads to other buses, l control room operators found they were. unable to open breaker INA04-09, so this was done locally.
Additional' discrepancies noted were a low flow alarm from the Auxiliary-Component Cooling Water (ACCW) System, and a Service Air System failure to isolate.
D. CAUSE OF EVENT
- 1. A review of the MSIV design revealed that there' are two limit switches ,
which were not adjusted to actuate concurrently. When the blue light
-illuminated as the result of one limit. switch actuating, the other limit I switch had not yet actuated and it appeared that the valve had f ailed to reopen. When the electricians installed the jumper,-the MSIV control power fuses failed, resulting in closure of the MSIV.
- 2. The MSIV closed when its actuator fuses blew. ' Although a simulation of l the event failed to duplicate the blown fuses and MSIV closure, it is our engineering judgement that the Georgia-Power Company electricians inadvertently created a momentary electrical short which led to the blown fuses. - This apparent cognitive personnel error was not the result
, 'of failing to follow approved procedures' or the result-of any unusual characteristics of the work location.-
- 3. The cause of the INA04 bus failure to transfer was due to the failure of the alternate feeder breaker from the RAT to close. This was the result of burnt relay contacts which did not allow an adequate electrical connection. The burnt contacts were due to the relay being out of ,
adjustment.
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- 1. 4. Steam dump valve ITV-5000 closed properly. However, the position ;
indication was faulty due to a limit switch being out of adjustment, t
- 5. The inability of the control room operators to open breaker INA04-09 was j
, due to a faulty.handswitch. An examination'of the handswitch concluded ,
that the failure was an isolated incident. !
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- 6. The cause of the ACCW low flow alarm was a momentary loss of power which !
occurred during load transfer.
- 7. The failure of the Service Air System to isolate will be investigated l during the refueling outage which is scheduled to begin February 23, k 1990.
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E.' ANALYSIS OF EVENT i
The'MSIV went:to its safe (fail close) position upon loss of power when the ;
control power- fuses blew. Main Feedwater isolated and Auxiliary Feedwater !
' actuated as-designed and a normal reactor trip occurred. Control room l
operators responded properly to stabilize SG water levels during the trip l recovery. Based on these considerations, there was no adverse effect on
' plant safety or the health and safety of the public~as a result of this
-F. CORRECTIVE ACTIONS i
' 1. The blown fuses were replaced and Procedures 14842-1 and 14842-2 have' been revised to require that the MSIV control room handswitch be moved to the "open" position upon receipt of blue light indication. This indication ensures that the. valve has actuated and represen_ts completion j of the ' quarterly stroke test. Initiation of the automatic reopening is '
not required to be tested. Additionally, a caution note will be added to the procedure stating that the blue light'may actuate prior to the !
valve receiving the reopen signal. Finally, during the 1990 refueling l outages (Units 1 and 2),. the appropriate limit switches will be adjusted -[
to actuate concurrently.
- 2. The electricians involved have been counseled regarding the necessity of -!'
exercising caution when testing circuits having the potential for causing a reactor trip.
- 3. The relay with the burnt contacts in the RAT feeder breaker has been
- replaced and the new relay has been adjusted to prevent recurrence of this failure, f 4. The steam dump valve limit switches were readjusted. '
- 5. 'The faulty handswitch which resulted in the inability to open breaker INA04-09 has been replaced.
- 6. A design change is being investigated to eliminate the ACCW low flow
':7 alarm as a result of a momentary loss of power. We expect to have a course of action identified by 3-1-90.
- 7. Corrective actions to prevent recurrence of the Service Air System's failure to isolate will be based on the results of the investigation to
, be performed during the refueling outage which is scheduled to begin 2-23-90.
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1 G,' ADDIT 10NAL INFORMATION-7 L1)- Failed Components: 3
.a) 'INA04-09 Handswitch manufactured by Electro Switch Corp, rA.
Model #-32762M-105- d b). INA04 Relay manufactured by Gould Controls l Model # 191921T6-R.2 .
- 2) Previous Similar Events: , I
-LER 50-424/1989-018, dated 10-30-89. q Although this 1989. event progressed similarly following fuse failure,
'there was no personnel involvement, and the corrective actions were not Lapplicable- to- the prevention of the 1-24-90 event.
- 13) Energy Industry Identification System Code:
lc. iMain-Steam System - SB :
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ll Service Air System - LF- -
Main Feedwater System - SJ ,
Reactor: Coolant System - AB 1?
L Auxiliary Feedwater System - BA 4
4160 Non-lE Electrical System - EA Turbine Plant Cooling Water System - KB D Auxiliary Component Cooling Water System - CC ;
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