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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:RO)
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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Text
Gemga Power Compriy 40 l'wemen Cenw Pahay
. Pon: 0"ce G a 1295 Bemergham. Ata* an.a 35201 To.eproye 2D5 6773122 m
C. K. McCoy Georeiav Power Vce Puscent Nx+c Vo@e Prejed IT Cot,1 hero ehrtT system LCV-0008 Docket No. 50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
VOGTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT S AFETY INJECTION INITIATED DURING SLAVE RELAY TESTING In accordance with the requirements of 10 CFR 50.73, Georgia Power Company submits the enclosed report related to an event which occurred on April 18,1993.
Sincerely, C. K. McCoy
/
/
CKM/NJS
Enclosure:
LER 50-424/1993-006 xc: Georgia Power Company Mr. W. B. Shipman Mr. M. Sheibani NORMS U. S. Nuclear Reculatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. D. S. Ilood, Licensing Project Manager, NRP.
Mr. B. R. Bonser, Senior Resident Inspector, Vogtle P80 0 7. 3
- BP EEE E8Skg4 e .
).
nn 0:4 U.5. N 1 LLAn RLUd M Y n m lbhiUN AryH i GiO4 LICENSEE EVENT REPORT (LER) l I
l iALitiin hAML (1) UULAti hbMets (2) Fw 131 l VOGTE ELECIRIC GDERATING PIANT - UNIT 1 05000424 1l0Fl4 !
IllLE (4)
SAFL'IY IlUECTION INITIATED DURUE SIAVE REIAY TESTUC '
EVEh1 DATE (5) LER huMBER [6) REPCkl DATE (7) OTHER FACILITIES Ihv0LVED (8)
MGkIN DAV VLAR VEAR 5EQ hbM REW m0h1M DAY YEAR FACILITY hAME5 DOCAET h0MBEk(5)
O5000 04 18 93 93 006 00 05 17 93 05000 CPERATlhG IMS nN 15 M M h*M M M WMMBS M M UR [H)
MODE (9) 5 20.402(b) 20.405(c) ^ 50.73(a)(2)(iv)
_ 73.71(b)
POUER 20.405(a)(1)(1) -
50.36(c)(1) -
50.73(a)(2)(v) 73.71(c)
LEVEL 0 20.405(a)(1)(ii) T OTHER (Specify in 50.36(c)(2) 50.73(a)(2)(vii) 20.405(a)(1)(tii) 50.73(a)(2)(1) -
50.73(a)(2)(viii)(A) Abstract below) 20.405(a)(1)(iv) ~~
50.73(a)(2)(ti) 50.73(a)(2)(vi11)(B) Tech. Spec.
20.405(a)(1)(v) 50.73(a)(21(111) 50.73(a)(2)(x) Special Report LICEh5EE C0hlAC1 FOR THis LER (li)
NAME TELEPN0hE huMBER LREA CODE MDIDI SHEIBANI. NUCIIAR SAFEIY AND COMPLIANCE 706 826-3209 COMPLETE Cht LIhE FOR EACH FAILURE DE50RlbED Ih IN15 REP 0kT (13) ,
CAUSE SYSTEN COMP 0hENT MAhurAC- R P0RT CAUSE SYSTEM COMFONENT R PORT TU pgD5 jANUFAC-ggER SUPPLEMENTAL kEPORI EXPECIED (14; M0hTN DAY 1 EAR EXPECTED SUBMISSION
] YES(If yes coniplete EXPECTED SUBMISSION DATE) "E] h0 DATE (15)
AE51RACT (16)
On April 18, 1993, while in cold shutdown, the solid state protection system (SSPS) mode selector switch was taken to " Operate" in order to support slave relay testing. Immediately, the SSPS processed a safety injection (SI) signal due to low pressurizer pressure and low steamline pressure. At the time that the mode selector switch was taken to " Operate," SI actuation should have been blocked. However, due to work in progress that affected the pressurizer pressure instrumentation channels, automatic unblock permissive conditions were present. Control room operators recognized the inadvertent SI signal and responded to reduce injection flow and restore the normal charging system flowpath. Because this actuation had resulted in emergency core cooling system discharge to the RCS, and operators had returned the unit to normal operation, a Notification of Unusual Event was both declared and terminated at 0824 EDT.
The cause of this event was a personnel error on the part of the control room team for allowing the SSPS to be returned to service when a SI signal would not be blocked. Contributing to this was the large number of activities occurring as restoration of plant systems took place following the refueling. The crew did not fully evaluate the impact of other maintenance activities on this procedure. The team was reminded to request assistance when operational questions arise and/or to take sufficient time for review prior to changes in ;
the configuration of plant systems.
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LICENSEE EVENT REPORT (LER) )
TEXT CONTINUATION ,
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) l YEAR SEQ NUM REV :
V0GI1E ELECIRIC GDUATING PLANT - UNIT 1 05000424 93 006 00 2 or 4 j TEXT i A. REQUIREMENT FOR REPORT f This report is required per 10 CFR 50.73 (a)(2)(iv) because an unplanned. l engineered safety feature (ESF) actuation occurred when a safety injection i (SI) signal resulted in an emergency core cooling system (ECCS) discharge j into the reactor coolant system (RCS). It is also required per Technical !
Specification 3.4.9.3, because residual heat removal (RHR) suction relief. l valves opened to mitigate an RCS pressure transient. :
1 B. UNIT STATUS AT TIME OF EVENT i i
At the time of this event, Unit 1 was in Mode 5 (cold shutdown) at 0 percent l of rated thermal power for a refueling outage. The RCS was solid.with a !
temperature of 120 degrees F and a pressure of 345 psig. Other than that described herein, there was no inoperable equipment which contributed to the occurrence of this event. j i
C. DESCRIPTION OF EVENT j On April 18, 1993, personnel were preparing to perform slave relay testing j per Procedure 14606-1, " Slave Relay K618 Train A Test Safety. Injection." For j this test, the solid state protection system (SSPS) is required to be in !
service. To ensure that no unnecessary. actuation would occur when placing !
the SSPS in service. a control room operator checked the bypass permissives :
light board (BPLB) and found that all required blocks were illuminated l However, two of the three pressurizer pressure channels were also in trip.due !
l to other work that was in progress at the time. As a result, the leetc for j the P-11 safety injection automatic unblock permissive was complete. ;
Therefore, at 0756 EDT, when the operator took the Train A SSPS mode selector !
switch to " Operate," the SSPS processed an SI signal for Train A due to low- i pressurizer pressure and low steamline pressure, conditions which are always [
present during cold shutdown, but normally blocked. Control room operators recognized the inadvertent SI signal and responded to reduce injection flow i and restore the normal charging system flowpath. This action and the-lifting ;
of the residual heat removal (RHR) suction relief valves at approximately {
450 psig, as designed, prevented any serious RCS pressure transient from i occurring. After the required 60-second delay for SI signal processing, the l SI actuation signal was reset, and normal unit operation was restored.
Because this actuation had resulted in ECCS discharge to the RCS and operators had returned the unit to normal operation, a Notification of ,
Unusual Event was both declared and terminated at 0824 EDT, and appropriate !
notifications were completed.
D. CAUSE OF EVENT l The cause of this event was a personnel error on the part of the control room f team for allowing the SSPS to be returned to service when a S1 signal would not be blocked. The control room team, led by the unit shift supervisor I (USS), questioned among themselves the action of placing the SSPS in !
" Operate." The error oc::urred when the crew placed the SSPS switch to ).
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LICENSEE EVENT REPORT (LER) l TEXT CONTINUATION i FACILITT NAME f3) DOCKET NUMBER (2) LER NUMBER (b) PAGE (3)
YEAR SEQ hum REV ;
VDGI1E ELECIPJC GmTRATING PIANI - INIT 1 05000424 93 006 00 3 0F 4 -
TEXT f operate even though they had not resolved their initial concern or completed f a full assessment of current plant conditions. There were no unusual !
characteristics of the work loca cion that contributed to the occurrence of ;
this error by the Georgia Power Company personnel involved. .
i Contributing to the cause of this event was the large number of activities {'
which were occurring as restoration of plant systems took place following the refueling. l Also contributing to the cause of this event was a procedure which was not !
written to be performed under the plant conditions that existed when the SSPS ,
was returned to service. Procedure 13503-1, " Reactor Control Solid State ;
Protection System," did not provide the information that the BPLB indications ;
may not reflect all necessary blocking conditions. This procedure directed i operators to ensure that the pressurizer low pressure SI signal and the steamline low pressure SI signal were blocked. Handswitch designations are provided to ensure the blocks are initiated if necessary. Operators use !
block status light indicatiens to verify that the block is in effect. When ;
the SSPS is in " Test," the status lights will illuminate when their associated block switches are placed in block, even if plant conditions are :
above P-ll (or process inputs are tripped, simulating conditions above'P-11). l If actual P-11 conditions are not met when the SSPS is placed in " Operate," !
the block is removed. Additionally, if the SSPS logic is met for an SI i condition, an SI would result when the SSPS is taken to " Operate," as occurred on April 18, 1993, because P-11 will automatically unblock the l actuation signal. The operating procedure in use did not provide adequate l precautionary guidance to the operators to warn them of the potentially misleading indications, and it did not provide other guidance to ensure that l P-11 conditions were met and the SI signals were appropriately blocked. .
E. ANALYSIS OF EVENT I The SI signal was not valid since no condition requiring an SI existed. !
Additionally, operators responded properly to divert the Train A charging l pump flowpath from the RCS. This action and the lifting of the residual heat ;
removal (RHR) suction relief valves at approximately 450 psig, as designed, !
prevented any serious RCS pressure transient from occurring. The Train B j SSPS was out of service due to work in progress, and the SI pumps were inoperable in accordance with the Technical Specifications. The Train A RHR l system was in the shutdown cooling mode of operation. Consequently, only the l Train A centrifugal charging pump injected water into the RCS. Therefore, no excessive pressure condition occurred in the RCS. This event could not have j occurred while the unit was at power because the SSPS must already be ;
operable prior to resuming power operations and because RCS pressure remains ;
above 2000 psig during power operations. Based on these considerations, -!
there has been no adverse effect on plant safety or on the health and safety l of the public as a result of this event. j 1
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u.s. uwm eanum w.n>im g ,nuA ungggpix LICENSEE EVENT REPORT (IZR)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3)
VEAR 5EQ hum REW V0GIE ELICIRIC GDDATING PIANT - LWIT 1 05000424 93 006 00 4 0F 4 lEXl F. CORRECTIVE ACTIONS i
- 1. The team was reminded to request assistance when operational questions arise and/or to take sufficient time for review prior to changes in the configuration of plant systems.
- 2. A caution was added to Procedure 13503-1 to warn operators of the potential for an SI when taking the SSPS to " Operate."
- 3. By July 1,1993 Procedures 13503-1 and 13503-2 will be further enhanced to require verification that conditions within the SSPS are established to permit blocking of the SI signal.
- 4. The details of this event will be reviewed as a " Lesson Learned" in licensed operator requalification training.
G. ADDITIONAL INFORMATION
- 1. Failed Components None t
- 2. Previous Similar Events ,
LER 50-425/1992-004, dated May 11,1992.
Corrective actions from this earlier LER addressed specific solutions that were not applicable for the prevention of the April 18, 1993, SI event.
- 3. Energy Industry Identification System Code Solid State Protection System - JG Reactor Coolant System - AB .
120 Volt AC 1E Power System - ED Safety Injection System - BQ Main Steam System - SB
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