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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:RO)
MONTHYEARML20045H9831993-07-16016 July 1993 LER 93-004-00:on 930628,steam Flow/Feed Flow Mismatch Alarm Received for SGs 2,3 & 4,resulting in Manual Reactor Trip.Caused by Failure of Main Feedwater Regulating Valve 2 Tracking/Driver Card.Card replaced.W/930716 Ltr ML20045E5161993-06-28028 June 1993 LER 93-003-00:on 930529,found That Room Temperature Readings Were Not Performed Due to Missed TS Surveillances.Procedure 14001-2 Was Revised & Personnel disciplined.W/930628 Ltr ML20044E7171993-05-18018 May 1993 LER 93-007-00:on 930425,manual Reactor Trip During Low Power Physics Testing Due to Negative Reactivity.Caused by Personnel Error.Reactor Engineer Counseled Re Importance of Attention to detail.W/930518 Ltr ML20044F5741993-05-17017 May 1993 LER 93-006-00:on 930418,safety Injection Initiated During Slave Relay Testing.Caused by Personnel Error.Team Reminded to Request Assistance When Operational Questions Arise.W/ 930517 Ltr ML20029C3571991-03-21021 March 1991 LER 91-006-00:on 910223,failure of Temperature Channel Circuit Card During Ni Surveillance Causes Reactor Trip. Caused by Trip of Protection Channel I Bistables.Loop 1 T-hot NRA Card replaced.W/910321 Ltr ML20029B1431991-02-28028 February 1991 LER 91-003-00:on 910129,Diesel Generator 2A & 2B Experienced Valid Failures During Testing.Cause of Failures Under investigation.K4 Transfer Relays Replaced & Relay Contacts on Diesel Generator 1A tested.W/910228 Ltr ML20029A6821991-02-25025 February 1991 LER 91-002-00:on 910204,during Surveillance Testing of Train B Safeguards Tests Cabinet,Slave Relay Energized,Causing Steam Inlet Valve to turbine-driven Auxiliary Pump to Open. Caused by Personnel Error.Personnel counseled.W/910225 Ltr ML20028G9131990-09-24024 September 1990 LER 90-011-00:on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for analysis.W/900924 Ltr ML20043G4211990-06-15015 June 1990 LER 90-001-01:on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure carefully.W/900615 Ltr ML20043G1421990-06-0505 June 1990 LER 90-007-00:on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV tested.W/900605 Ltr ML20043C3311990-05-29029 May 1990 LER 90-006-00:on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate action.W/900529 Ltr ML20043C3231990-05-27027 May 1990 LER 90-005-00:on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card replaced.W/900529 Ltr ML20042G7431990-05-11011 May 1990 LER 90-004-00:on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs.W/900511 Ltr ML20042G7381990-05-11011 May 1990 LER 90-009-00:on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation signal.W/900511 Ltr ML20042G7321990-05-11011 May 1990 LER 90-010-00:on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals counseled.W/900511 Ltr ML20042E1731990-04-11011 April 1990 LER 90-005-00:on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator counseled.W/900411 Ltr ML20012D8131990-03-23023 March 1990 LER 90-003-00:on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps replaced.W/900323 Ltr ML20012D9991990-03-23023 March 1990 LER 90-004-00:on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2.W/900323 Ltr ML20012D6591990-03-16016 March 1990 LER 90-002-00:on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing performed.W/900316 Ltr ML20011F5501990-02-23023 February 1990 LER 90-001-00:on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch adjusted.W/900223 Ltr ML20042D3571990-01-0202 January 1990 LER 89-019-00:on 891206,discovered That Tech Specs Violated Due to Foreman Approving Measurements of Cell Recorded as 2.10 V on 891122.Caused by Personnel Error & Inadequate Procedure.Foreman counseled.W/900102 Ltr ML19354D7421989-12-22022 December 1989 LER 89-031-00:on 891202,moisture Separator Reheater (MSR) Level Reached High Level Setpoint Giving Turbine/Reactor Trip.Caused by Personnel Error.Actuator Reinstalled W/ Actuator Piston Correctly aligned.W/891222 Ltr ML20011D8811989-12-21021 December 1989 LER 89-020-00:on 891211,power Removed from Radiation Monitor Before Lifting Leads to ESF Actuation Circuits.Caused by Cognitive Personnel Error & Failure to Follow Procedure. Technician Disciplined.Esf Provisions planned.W/891221 Ltr ML20011D4201989-12-19019 December 1989 LER 89-030-00:on 891126,containment Ventilation Isolation Initiated When Remote/Bypass Switch Moved to Remote Position.Caused by Personnel Error & Inadequate Procedure.Technician counseled.W/891219 Ltr ML19332E7991989-12-0404 December 1989 LER 89-029-00:on 891105,heater Drain Tank High Level Dump Valve 2LV-4333 Isolated from Heater Drain Tank,Causing Steam & Water to Escape from Packing & Reactor Trip.Caused by Failure to Maintain Steam Generator level.W/891204 Ltr ML19332E6111989-11-30030 November 1989 LER 87-005-06:on 870406,containment Isolation Actuation & Containment Ventilation Isolation Actuation Occurred.Caused by Spurious Signals from High Range Radiation Monitor. Circuit Setpoints to Be increased.W/891130 Ltr ML19327C2651989-11-14014 November 1989 LER 89-028-00:on 891016,while Replacing Faulty Circuit Board,Power Cable & Arcing Occurred at Terminal Connection, Resulting in Containment Ventilation Isolation.Caused by Inadequate Design.Longer Block Screw installed.W/891114 Ltr ML19324C2051989-11-10010 November 1989 LER 88-047-00:on 880614,handswitches for Manual Actuation of Containment & Containment Ventilation Isolation Tested.On 891013,handswitches Disabled.Caused by Test Procedure Error.Procedures Re Manual Actuation revised.W/891110 Ltr ML19327B7341989-11-0303 November 1989 LER 89-027-00:on 891011,automatic Reactor Trip Occurred W/Reactor in Stable Operation at 58% Rated Thermal Power. Caused by Dropped Rod Due to Diode Failure.Diode for Rod K-2 replaced.W/891103 Ltr ML19325E8191989-10-31031 October 1989 LER 88-035-01:on 881113,momentary Loss of Power to Radiation Monitor 1RE-12116 Resulted in Control Room Isolation Actuation.Setpoint Will Be Raised During Next Refueling outage.W/891031 Ltr ML19324B5121989-10-30030 October 1989 LER 89-018-00:on 891002,steam Generator 1 Train a MSIV Failed to Close,Resulting in Automatic Reactor Trip.Caused by Blown Fuse in Control Logic Power Supply.Grounding Corrected & Limit Switch & Fuse replaced.W/891030 Ltr ML19327A8121989-10-13013 October 1989 LER 87-082-01:on 890620,discovered That Reactor Trip Breaker Had Been swapped-out on 871017 W/O Performing Response Time Test for Breaker Being Installed.Caused by Procedural Inadequacy.Procedure revised.W/891013 Ltr 1993-07-16
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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- Gs.o'ge Power Comrwiy 333 P.tdmont Aenae Atenta, Goafgia 303D6
..; inep? vie 404 !4'0 3195
- Maang Add'ent 40 invemess Center Puksay Post O!!ce Dan 1?DS D.munf am, Alabama 35201 Telermone 20$ 660 55B1 t*w scwcrn A c sc. tem W G. Hairston, lit sensor V,ce Presdent Nacteat CWrations ELV-Oll87 December 22, 1989 0179 Docket No. 50-425 U. S. Nuclear Regulatory Commission ATTN: Document Control l'esk Washington, D. C. 20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT LICENSFE EVENT REPORT HEATER DRAIN dNK VALVE REASSEMBLY ERROR LEADS TO TURGi.*!E/ REACTOR TRIP in accordance with 10 CFR 50.73, Georg a Power Company hereby submits the enclosed report relating to an event which occurred on December 2,1989.
Sincerely, at)/f W,.
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G. Hairston, 111 WGH,Ill/NJS/gm
Enclosure:
LER 50-425/1989-031 xc: Georaia Power Company Mr. C. K. McCoy Mr. G. Bockhold, Jr.
Mr. P. D. Rushton Mr. R. M. Odom NORMS U. S. Nuclear Reaulatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. J. B. Hopkins, Licensing Project Manager., NRR Mr. J. F. Rogge, Senior Resident inspector, Vogtle 9001020207 891222 PDR ADOCK 05000425 [621 S PDC
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,. .e n ei i i i On 12-2-89, plant personnel were releasing a clearance on Heater Drain Tank (HDT) high level dump valve 2LV-4334. The high level dump valve for Moisture Separator Reheater (MSR)"D", 2LV-4525, was in a 50% jacked-opened position due to 2LV-4334 being isolated. Upon opening the valve which isolated P.LV-4334, it became evident that 2LV-4334 was not closed. The HDT level decreased and the normal level control valve, 2LV-4332, closed. The isolation valve was reclosed and HDT level rose; however, 2LV-4332 failed to reopen resulting in rising feedwater heater levels and, due to the configuration of 2LV-4525, MSR D level rose as well. At 0341 CST, MSR D level reached the high level setpoint giving a turbine / reactor trip.
The root cause for the event was cognitive personnel error involving reassembly of 2LV-4334. The valve was reassembled such that its position indication showed closed when it was actually full open. For 2LV-4332, the level control sensing lines were discovered to be clogged which resulted in its malfunction.
Actions to prevent recurrence include discussing this event in maintenance shop meetings, n..plementation of a periodic task to blowdown the level control sensing lines associated with 2LV-4332, and inclusion of this event in operator continuing training.
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A. REQUIREMENT FOR REPORT This report is required per 10 CFR 50.73 (a)(2)hv), since the event
' resulted in an automatic actuation of the Reactu Protection System (RPS),
B. UNIT STATUS AT TIME OF EVENT At the time of this event, Unit 2 was in Mode 1 (Power Operation) at 100% of rated thermal. power. Moisture Separator Drain Tank (MSDT) "D" high level dump valve, 2LV-4525, was in a 50% jacked-opened position to reduce flow to Heater Drain Tank (HDT) "B" since HDT "B" high level dump valve, 2LV-4334, was out of service for maintenance. No other plant equioment was inoperable or otherwise in an off-normal status such that it contriauted to the occurrence of this event.
C. DESCRIP110N OF EVENT On 12-2-89, plant personnel were in the process of releasing a clearance on 2LV-4334 in order to perform post maintenance functional testing on this valve. At approximately 0330 CST, a plant equipment operator (PEO) began opening manual isolation valve 2-1304-U4-052, t1ereby unisolating 2LV-4334.
Due to problems which had been experienced on 11-5-89 (reference LER 425/89-029), when restoring the HDT "A" high level dump valve to service, the activities were being directed by an on-shift operations supervisor (0S05) who was present at the valve with a maintenance supervisor, a maintenance foreman, and an instrumentation and controls foreman. Al so, preparations had been made to establish direct communication with the Unit 2 Control Room; however, communication had not yet been established when the PE0 was directed to open the manual isolation valve.
With the manual isolation valve approximately 10% open, the line started moving and it became evident that 2LV-4334 was not closed even though the local indication showed full closed. This allowed HDT "B" to start dumping to the main condenser. The Control Room observed HDT "B" level decrease and then the normal level control valve (i.e., Heater Drain Pump "B" discharge control valve), 2LV-4332, closed on low level.
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1 The PE0 was directed to reclose the manual isolation valve and HDT *B" level
! started increasing. Main feedwater pump "A" and "B" suction pressure had ;
dropped due to valve 2LV-4332 being closed and the standby condensate pump !
was started to restore suction pressure. As HDT "B" level increased, valve 2LV-4332 failed to reopen. This caused HDT "B" level to go off-scale high !
and the levels in feedwater heater "4B", feedwater heater "5B", MSDT "C", l MSDT *D", and Moisture Separator Reheater (MSR) "D" began to increase as I well. The OSOS then proceeded to 2LV-4332 to attempt to open this valve i using the handwheel. The Support Shift Supervisor similarly proceeded to l 2LV-4525 to attempt to further jack it open. However, before either of l these actions could be accomplished, MSR "D" level reached the high level setpoint causing a turbine trip which resulted in a reactor trip at 0341 CST. !
On the reactor trip, all control rods fully inserted, the Main feedwater System isolated and the Auxiliary feedwater (AFW) System actuated as designed. Control Room operators entered emergency operating Procedure 19000-C, "E-0 Reactor Trip or Safety Injection," and then responded to throttle AFW flow and maintain steam generator water levels. By 0353 CST, the plant had been stabilized in Mode 3 and unit operating Procedure 12006-C, " Unit Cooldown to Cold Shutdown," was entered.
Several abnormalities occurred following the reactor trip but had no impact on the ability to shutdown the reactor and maintain it in a safe shutdown ,
condition. These occurrences included the lifting and reclosing of steam generator atmospheric relief valve 2PV-3020, at a steam line pressure below the lift setpoint; an apparent waterhammer involving feedwater heater "4B";
and the trip of breakers 2NBL1-04 and 2NBL1-13 during the residual transfer of 4160 V switchgear 2NA01. The trip of breakers 2NBL1-04 and 2NBL1-13 resulted in normal lighting not being restored to portions of the Auxiliary Building and the Control Building following completion of the residual transfer of 2NA01. Operators responded to reset these breakers and restore lighting to these areas.
D. CAUSE OF EVENT The maintenance of 2LV-4334 had required the removal of the pneumatic actuator from the valve to allow rebuilding of the actuator in the maintenance shop. Since the valve was not to be removed from the line, the maintenance crew that removed the actuator had match-marked the valve in the open position. A second maintenance crew had rebuilt the actuator and reinstalled it using the maintenance match marks. A third crew had tested the valve operation and reinstalled the position indication to match the actuator piston position.
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0l0 0l4 or 0l6 After the reactor tripped, the maintenance match marks were checked and were found to disagree with the valve position indication by 90 degrees. It was then realized that a reassembly error had occurred in that the actuator piston had been in the closed position when the actuator was reinstalled on the valve which had been match-marked in the open position.
This reassembly error was not recognized when the lever which connects the actuator piston connecting rod to the valve shaft was ) laced back onto the valve shaft since this lever will fit onto the valve s1 aft with the actuator piston in either an open or closed position. Stroking of the valve, after reinstallation of the actuator but with the downstream isolation valve still '
closed, had also failed to reveal the error since the valve ball is free to rotate 360 degrees (i.e., the valve was actually being stroked between the open position and a position 90 degrees beyond open). Therefore, when the downstream isolation valve was opened, 2LV-4334 was actually in a full open position even though its position indication showed full closed. This lead -
to the reactor trip as previously discussed.
The root cause for the reassembly error was cognitive personnel error. The ,
maintenance crew that reinstalled the actuator failed to recognize the need to verify the correct actuator piston position as compared to the valve ball position. The maintenance work order controlling the work on 2LV-4334 contained instructions to use both the vendor valve instruction manual and the vendor actuator instruction manual for performing the work. Subsequent interviews of involved personnel revealed that only the actuator instruction manual was used. The valve instruction manual contains details on determining the correct lever / valve shaft orientation based on fcctory index marks located on these individual parts and therefore should have been used as well.
The failure of the normal level control valve, 2LV-4332, to reopen as HDT "B" level increased also contributed directly to the reactor trip. Had this valve responded properly, the reactor trip would not have occurred.
Flushing of the associated level control sensing lines and pot after the i reactor trip revealed that these lines had become clogged with a gunk type ;
substance. The root cause for the failure of 2LV-4332 was the clogged I sensing lines and a contributing cause was that no preventive maintenance 1 (PM) task presently exists to periodically blow down or otherwise flush thes+ sensing lines.
The cause for steam generator atmospheric relief valve 2PV-3020 opening l below its setpoint and the cause for the trip of breakers 2NBil-04 and 2NBL1-13 is still being investigated.
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i E. ANALYSIS OF EVENT )
On the reactor trip, all control rods were observed to fully insert into the core. Main feedwater isolated and Auxiliary Feedwater actuated as designed. ]
The MSR high level setpoint turbine trip actuated as designed to trip the turbine and protect it from water induction damage. No operator action was ,
required to reclose 2PV-3020. The loss of lighting in portions of the i Auxiliary and Control Buildings was an operator inconvenience which was ,
promptly corrected by resetting bra xers 2NBL1-04 and 2NBL1-13. The
- apparent waterhammer involving feedwater heater "48" resulted in no damage to any safety related equipment. Based on these considerations, there was no adverse effect on plant safety or on the health and safety of the public.
F. CORRECTIVE ACTIONS
- 1. The actuator was removed from 2LV-4334 and reinstalled with the actuator piston correctly aligned with the valve ball position.
- 2. This event, including the need to ensure proper use of vendor manuals when required by maintenance work order instructions and the need to ensure all pertinent information is conveyed to the next maintenance crew, will be discussed in maintenance shop meetings by 2-1-90,
- 3. The level control sensing lines and the pot which provides the normal level control for HDT "B" were flushed with demineralized water and normal operation of 2LV-4332 was restored. A PM task will be implemented by 1-15-90 to provide for a periodic blowdown or flush of level control sensing lines and condensate pots for the Heater Drain Tanks.
- 4. This event, including a discussion of alternative methods of reducing flow to a heater drain tank, will be covered in operator continuing training by 4-1-90.
- 5. A walkdown of secondary piping and components associated with feedwater heater "4B" was performed after the waterhammer occurred. Two pressure indicators and a pin for a pipe hanger were found damaged. No other damage was found.
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- 6. The control circuit for 2PV-3020 will be investigated and calibrated or repaired as required by 12-27-89.
- 7. Engineering will investigate the trip of breakers 2NBL1-04 and 2NBL1-13 by 1-31-90 to determine if any corrective action is required.
G. ADDITIONAL INFORMATION
- 1. Failed Components Identification HDT "B" High Level Dump Valve 2LV-4334 Fisher Controls 12 - Inch Design V100 Vee-Ball Valve with Type 1061 Pneumatic Piston Rotary Actuator.
HDT "B" Normal Level Controls Loop 2LCL-4332 Fisher Controls 14 - Inch Cage Style Level-Trol Model No. 2502-2498.
- 2. Previous Similar Events The event which resulted in a reactor trip on 11-5-89 (reference LER 425/89-029) was similar in that the event was initiated when a HDT high level dump valve was restored to service. However, the root causes for these two events differ in that operator actions were appropriate in responding to the current event.
- 3. Energy Industry Identification System Codes Main Feedwater System - SJ High Pressure Heaters and Moisture Separator Reheater Drains and Vents System - SN
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