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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
~ I REGULA Y INFORMATION DISTRIBUTIO 'YSTEM (RIDS)
ACCESSION NBR: 8810260019 DOC. DATE: 88/09/30 NOTARIZED: NQ DOCKET 0 FACIL: 50-315 Donald C. Cook Nuclear Power Planti Unit 1> Indiana 5 05000315 AUTH. NAME AUTHOR AFFILIATION GILES'. Indiana Michigan Power Co. (formerly Indiana 5, Michigan Ele SMITHS'. G. Indiana Michigan Power Co. (formerly Indiana, 5,Michigan Ele RECIP. NAME RECIPIENT AFFILIATION
SUBJECT:
Monthly operating rept for Sept 1988 for DC Cook Unit l
W/881007 ltr.
DISTRIBUTION CODE: ZEROED COPIES RECEIVED: LTR TITLE: Monthlg Operating Report (per Tech Specs)
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ENCL g SIZE:
RECIPIENT COPIES RECIP IENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 0 PD3-1 PD 5 5 SCOTTI W 0 INTERNAL: AEOD/DOA 1 2
i 2
AEOD/DSP/TPAB NRR/DLPG/PEB 11 1 1 ARM TECH ADO 1 1 NRR/DOE*/EAB 11 1 1 ~R=i'+)REPi%P 10 1 1 NUDOCS-ABSTRACT RGN3 1
1
~EC F'IL 01 1 EXTERNAL'GSG SIMPSON' 1 1 EG5G WILLIAMS' 1 1 LPDR 1 1 NRC PDR 1 1 NSIC 1 1 TOT*i NUMBER QF COP IES REQUIRED: LTTR 22 ENCL 20
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N.R.C. OPERATING DATA REPORT DOCKET NO. 50-315 DATE 04-Oct-88 COMPLETED BY H. Giles TELEPHONE 616-465-5901 OPERATINQ STATUS
- 1. Unit Name D. C. Cook Unit 1
- 2. Reporting Period SEPT 1988 ,'nates
- 3. Licensed Thermal Power (MWt) 3250
- 4. Name Plate Rating (Gross MWe) 1152
- 5. Design Electrical Rating (Net MWe) 1030
- 6. Maximum Dependable Capacity (GROSS MWe) 1058
- 7. Maximum Dependable Capacity (Net MWe) 1020
- 8. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since Last Report Give Reasons
- 9. Pawer Level To Which Restricted.
If If Any (Net MWe)
- 10. Reasons For Restrictions. Any:
This Mo. Yr. to Date Cumm.
- 11. Hours in Reporting Period 720.0 6575.0 120527.0
- 12. No. of Hrs. Reactor Was Critical 522.3 6324.8 88162.5
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 483.0
- 14. Hours Generator on Line 511.9 8301.9 86539 '
- 15. Unit Reserve Shutdown Hours 0.0 0.0 321.0
- 16. Gross Therm. Energy Qen. (MWH) 1448245 18248448 251245444
- 17. Gross Elect. Energy Gen. (MWH) 457110 5876520 82021190
- 18. Net Elect. Energy Qen. (MWH) 438285 5647052 78878050
- 19. Unit Service Factor 71.1 95. 8 73.0
- 20. Unit Availability Factor 71.1 95. 8 73.0
- 21. Unit Capacity Factor (MDC Net) 59.7 84.2 65.2
- 22. Unit Capacity Factor (DER Net) 59.1 83. 4 63.2
- 23. Unit Forced Outage Rate 28.9 3.6 8.0
- 24. Shutdowns Scheduled over Next Six Months (Type, Date, and Duration)-
C Fe
- 25. If Shut Down At End of Report Period, Estimated Date of Startup-
- 26. Units in Test Status (Prior to Commercial Operation)-
Forcast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COHKKCIAL OPERATION
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I/NITSIIIITI)OWNSANI)POWER RKI)IM1'IONS UNIT NAME D.C. Cook Unit 1 l)ATK Oct. 10 1988 C:f)Mtl+tKI)ItY J. W. Harner RKPOR I MPN III TKLEtIIONE (616) 465-5901 Page: lof 2 I.iecusee (auseh Cnrtei,tive N i. l4tc Knell) Aelinii tit pt) Retwirl 4 Prcvetll Reelulellcc 271 880907 207.6 NA CI PIPEA The Unit shutdown and the reactor coolant sys-
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tem cooled down to Mode 4 due to a calculated leak rate of 0.96 gpm. Upon containment ent an instrument line was found broken between the manual isolation valve and the instrument, QDA-21. The instrument'is the number 2 reac-tor coolant pump shaft seal thermal barrier differential pressure alarm. The failure was due to the pipe vibrating and. rubbing against a structural support creating a fault. The failed section of piping was removed and re-placed with a new one. The piping was then rerouted away from the support, thus preventi further problems or similar damage in the fu-ture. During the nine day outage selected Emergency Core Cooling System motor operated valves were inspected with no problems being identified. Also during this time selected S valves which were found to be a problem on Unit 2 were inspected on Unit 1. These valve were 1-SI-151 East, 1-SI-151 West, 1-SI-166-L and 1-SI-166-L4 which are check valves in the cooldown lines and safety injection lines to the reactor coolant system.
Reptant It was found tha 1-SI-151 East and 1-SI-151 West both had one 3 4 I: ln)A:d Rcasitn: Helhtiil: Exhibit Ci - Inst suet in)is S: Scltedttleil A-fillriptltenlfailure]Kap4hl) I -Man rial fnt Pteparatinri <<f I>ata O Matulenattcrt ni Tesl 2 Manual Seta tu. Iintty Sheets fni licensee C Rcfucltug 3 Au)outa!le Sc:iattt. Event II.I!RI I'ilc INlIRI G.
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UNITSIIIITIPOWNS AND I>OlTKN kEI)IJC'1'lONS Unit 1 UNITNAgh D.C. Cook pA~ Oct. 10 1988 c.ourlzmi lsV QEPORT NPH AI Page: 2 of 2 leavens
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kel>>>sl 4 Psevcns kec>uscnce 271 broken retaining block stud which were remove (con't) and replaced the new ones. There are 2 of these studs in each valve which hold the clap per assembly in place. The stud materials of 1-SI-166-Ll and 1-SI-166-L4 were in question, thus these studs were removed and replaced with new ones.
Prior to the unit heatup, a steam generator crevice flush of all four steam generators wa performed. The unit was paralleled at 0224 hours0.00259 days <br />0.0622 hours <br />3.703704e-4 weeks <br />8.5232e-5 months <br /> (EDT), brought to 48'4 power and held here for turbine warming prior to overspeed testing.
272 880916 0.5 NA ZZ ZZZZZZ The to reactor power level was reduced from 9'4 and at 1824 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.94032e-4 months <br /> the unit was removed 4'
from parallel for turbine overspeed testing.
The unit was returned to service at 1855 hour0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br /> The unit was returned to its administrative power limit of 90X on 9-17-88.
I': I'inn>I S: Schc>lnlc>I Reason:
A.I'.>Iulpu>ens I'allu>e LIelhul:
I44nnal fxl>ibis f> ~ lns>>ncsii>ns fiu Psel>a>a>lun i>f I)a>a (Fxl>bin)
II Nalulcnance ui Tesl 2.Manual ScAn>. Icons>y Shecss f>>> ILensce I'.Rcfucllul 3.Aul>>u>a!le Sctan>. I!vcns Mcl>>>>s ll.l Rl I'ilc IHUkl!G.
Il kcy4asnsy Res>skll>us 44)>l>cs Ilixl>blnl OI6I I I:Q>c>alus Tsal>>lull Uccuse liaauNnall>>u F-Adn>lnlss>alive (I (ll>esaslu>>al I4sus Ilixl>latuI I:xlnl>ll I San>c Sin>> i.e I sj II) II All>c( II:xl>bh>I
DOCKET 50-315 NO'NIT NAME: D. C. Cook Unit 1 COMPLETED BY: J. W. Harner TELEPHONE: (616) 465-5901 DATE: October 10, 1988 PAGE: 1of1 MONTHLY OPERATING ACTIVITIES - SEPTEMBER 1988 HIGHLIGHTS:
The Unit shutdown and the reactor coolant system cooled down to Mode 4 due to a calculated leak rate of 0.96 gpm. Upon containment entry an instrument line was found broken between the manual isolation valve and the instrument, ADA-21. The instrument is the number 2 reactor coolant pump shaft seal thermal barrier differential pressure alarm. The failure was due to the pipe vibrating and rubbing against a structural support creating a fault. The failed section of piping was removed and replaced with a new one. The piping was then rerouted away from the support, thus preventing further problems or similar damage in the future. During the nine day outage selected Emergency Core Cooling System motor operated valves were inspected with no problems being identified. Also during this time selected SI valves which were found to be a problem on Unit 2 were inspected on Unit 1. These valves were 1-SI-151 East, 1-SI-151 West, 1-SI-166-Ll and 1-SI-166-L4 which are check valves in the cooldown lines and safety injection lines to the reactor coolant system. It was found that 1-SI-151 East and 1-SI-151 West both had one broken retaining block stud which were removed and replaced with new ones. There are 2 of these studs in each valve which hold the clapper assembly in place. The stud materials of 1-SI-166-L1 and 1-SI-166-L4 were in question, thus these studs were removed and replaced with new ones.
Prior to the unit heatup, a steam generator crevice flush of all four steam generators was performed. The unit was paralleled at 0224 hours0.00259 days <br />0.0622 hours <br />3.703704e-4 weeks <br />8.5232e-5 months <br /> (EDT);
brought to 48% power and held here for turbine warming prior to overspeed testing.
The reactor power level was reduced from 485 to 9X and at 1824 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.94032e-4 months <br /> the unit was removed from parallel for turbine overspeed testing. The unit was returned to service at 1855 hours0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br />. The unit was returned to its administrative power limit of 90% on 09-17-88.
An unusual event was declared on 09-22-88 due to a fire in a plastics factory in the village of Stevensvi lie.
DETAILS 9-7-88 At 0440 hrs. a planned unit shutdown and reactor coolant cooldown was commenced due to an elevated reactor coolant leak rate of 0.96 gpm.
The reactor coolant system was cooled down and the unit entered Mode 4 at 1914 hrs.
Following the repairs of the reactor coolant system leak, SG crevice flush, and reactor coolant heat-up the unit entered Mode 3 at 0540 hrs.
The unit entered Mode 2 with a reactor startup at 0447 hrs. The startup was terminated due to criticality not being reached at the conditions calculated, (ECP).
After recalculating an estimated critical rod position (ECP) a reactor startup at 1602 hrs was commenced. The reactor reached criticality at 1629 hrs.
The reactor entered Mode One at 2105 hrs.
The Unit was paralleled at 0224 hours0.00259 days <br />0.0622 hours <br />3.703704e-4 weeks <br />8.5232e-5 months <br /> (EDT) and reactor power was increased to 48K. Reactor power was held at this power level for turbine warming in preparation for a scheduled turbine overspeed test.
Reactor power was reduced to 9X power and the unit was removed from parallel at 1824 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.94032e-4 months <br /> (EDT) to perform the scheduled main turbine overspeed test. The unit was returned to service at 1855 hours0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br />.
The unit reached the 90K administrative power limit at 1133 hrs. and remained there for the remainder of the reporting period.
At 0407 hrs. an unusual event was declared due to a fire in a plastics factory in the local community of Stevensville. The unit exited the unusual event at 0740 hrs after it was determined no hazardous gases existed.
DOCKET NO. 50-315 UNIT NAME ~D. . Cook - Unit No. 1 DATE October 7 1988 COMPLETED BY J. W. Harner TELEPHONE 616 465-5901 PAGE 1 o 1 MAJOR SAFETY-RELATED MAINTENANCE SEPTEMBER 1988 M-1 1-ADA-21 (0'2 reactor coolant pump shaft seal thermal barrier differential pressure alarm). Instrument piping broken due to rubbing against structural member. The broken pipe was replaced with a new one and rerouted to prevent a reoccurance.
M-2 1-HV-AES-2 had an air leak through the charcoal bed which was greater than the technical specification limit due to a damaged damper gasket.
The damper gasket was replaced with a new one and the damper linkage adjusted accordingly.
M-3 1-SI-151 East and West (residual heat removal cooldown lines check valves). Found each valve had 1 broken retaining block stud which was removed and replaced with a new stud.
M-4 1-SI-161-L1 and 1-SI-161-L4 had studs made of questionable materials.
These studs were removed and replaced with new studs.
Indiana Michigan Power Company Cook Nuclear Plant P.O. Box 458 Bridgman, Ml 49106 616 465 5901 RF INDIANA NICHIGAN POWER U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 October 7, 1988 Gentlemen:
Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 1 Technical Specification 6.9.1.10, the attached Monthly Operating Report for the month of September 1988 is submitted.
Sincerely, Plant Manager WGS/jd cc: D. M. Williams, Jr.
M. P. Alexich C. A. Erikson J. J. Markowsky D. A. Timberlake R. F. Kroeger B. L. Jorgensen M. J. Parvin J. R. Sampson E. A. Smarrella Dolly Krieger T. R. Stephens D. S. Climer R. C. Callen D. W. Paul D. R. Mahn S. L. Mall INPO Records Center ANI Nuclear Engineering Department NRC Region III Nuclear Safety EPRI Analysis Center
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