ML17334A606
| ML17334A606 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 11/30/1997 |
| From: | Center J INDIANA MICHIGAN POWER CO. |
| To: | |
| Shared Package | |
| ML17334A604 | List: |
| References | |
| NUDOCS 9801140267 | |
| Download: ML17334A606 (3) | |
Text
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DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE PAGE 50 - 316 D.C. Cook Unit 2 January 6, 1998 JF Center 616-697-5098 1 of 1 MONTHLYOPERATING ACTIVITIES-November 1997 HIGHLIGHTS The unit entered this reporting period in Mode 6 at 0% RTP.
The unit exited this reporting period in Mode 5 at 0% RTP..
There were no challenges to the pressurizer safety valves or power operated relief valves.
Gross electrical generation for the month of December was 0 MWh.
DETAILS'0/1 3/97 12/05/97 0500 0938 U2R97 Cycle 11 -12 refueling outage begins.
Entered Mode 5.
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DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE PAGE 50 - 316 D.C. Cook Unit 2 January 6, 1998 JF Center 616-697-5098 1 of1 UNITSHUTDOWNS AND POWER REDUCTIONS - NOVEMBER 1997 METHOD OF SHUTl'ING LICENSEE DURATION DOWN EVENT SYSTEM COMPONENT NO.
DATE TYPE" HOURS REASON2 REACTOR>
REPORT NO.
CODE4 CODE5 CAUSE AND CORRECTIVE ACTION TO PREVENT RECURRENCE 334 101297 S
744.0 N/A N/A N/A The scheduled refueling outage commenced while the unit had been shutdown to resolve design basis questions discovered during the NRC Architect and Engineering (AE)
Inspection.
1 TYPE:
F: Forced S: Scheduled 2 REASON:
A: Equipment Failure (Explain)
B: Maintenance or Test C: Refueling D: Regulatory Restriction E: Operator Training and.
Ucense Examination F: Administrative G: Operational Error (Explain)
H: Other (Explain) 3 METHOD:
1: Manual 2: Manual Scram 3: Automatic Scram 4: Other (Explain) 4 SYSTEM:
Exhibit G - Instructions for preparation of data entry sheets for Licensee Event Report (LER) File (NUREG 0161) 5 COMPONENT:
Exhibit I: Same Source