IR 05000272/2016002

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Revised Integrated Inspection Report 05000272/2016002 and 05000311/2016002
ML17101A407
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/10/2017
From: Fred Bower
Reactor Projects Branch 3
To: Sena P
Public Service Enterprise Group
Shared Package
ML17097A293 List:
References
IR 2016002
Download: ML17101A407 (59)


Text

UNITED STATES ril 10, 2017

SUBJECT:

SALEM NUCLEAR GENERATING STATION, UNITS 1 AND 2 - REVISED INTEGRATED INSPECTION REPORT 05000272/2016002 AND 05000311/2016002

Dear Mr. Sena:

By letter dated October 24, 2016 (ML16298A161 1), PSEG Nuclear LLC (PSEG), the licensee for Salem Nuclear Generating Station (Salem) Units 1 and 2, contested a Green non-cited violation (NCV) that was documented in the U.S. Nuclear Regulatory Commissions (NRCs) second quarter 2016 Integrated Inspection Report 05000272/2016002 and 05000311/2016002 dated September 22, 2016 (ML16266A224). Specifically, the October 24, 2016, letter requested withdrawal of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, Green NCV 0500311/2016002-02, Failure to Follow Operability Determination Procedure for Unit 2 Baffle-Former Bolts, concerning the failure to follow the operability process as prescribed in OP-AA-108-115, Operability Determinations & Functionality Assessments. The letter stated that PSEG was in full compliance with procedure OP-AA-108-115 when evaluating the baffle former bolt condition discovered at Unit 1 as it applied to Unit 2.

By letter dated November 3, 2016 (ML16308A328), the NRC acknowledged receipt of your letter and informed you that the staff would review your basis for contesting the NCV and provide the results of our evaluation by written response.

The NRC formed an independent panel to review the information you provided, conducted a thorough and detailed review of the information provided in your letter and provided our conclusions by letter dated March 27, 2017 (ML17083B110). After consideration of your bases for contesting the NCV, the NRC concluded that the violation as written could not be supported.

Specifically, the independent review noted different steps within the procedure that could be interpreted to either support or refute PSEGs claim related to the need for direct evidence of a degraded or non-conforming condition. As a result of this potential for differing interpretations of your procedural requirements, the NRC has determined that it was not appropriate to issue a violation for a failure to comply with the procedure. Therefore, the NCV was withdrawn. To correct our records, the Salem Units 1 and 2 second quarter 2016 Integrated Inspection Report (05000272/2016002 and 05000311/2016002) has been revised to remove the NCV previously

Designation in parentheses refers to an Agencywide Documents Access and Management System (ADAMS) accession number. Documents referenced in this letter are publicly-available using the accession number in ADAMS. documented in Section 1R15 and the revised report is being reissued as an enclosure to this letter.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos. 50-272 and 50-311 License Nos. DPR-70 and DPR-75

Enclosure:

REVISED - Inspection Report 05000272/2016002 and 05000311/2016002 w/Attachment: Supplementary Information

REGION I==

Docket Nos. 50-272 and 50-311 License Nos. DPR-70 and DPR-75 Report Nos. 05000272/2016002 and 05000311/2016002 Licensee: PSEG Nuclear LLC (PSEG)

Facility: Salem Nuclear Generating Station, Units 1 and 2 Location: P.O. Box 236 Hancocks Bridge, NJ 08038 Dates: April 1, 2016 through June 30, 2016 Inspectors: P. Finney, Senior Resident Inspector A. Ziedonis, Resident Inspector E. Burket, Emergency Preparedness Specialist G. DiPaolo, Senior Reactor Inspector M. Draxton, Project Engineer J. Kulp, Senior Reactor Inspector M. Modes, Senior Reactor Inspector R. Nimitz, Senior Health Physicist T. OHara, Reactor Engineer D. Orr, Senior Reactor Inspector R. Vadella, Project Engineer J. Poehler, Senior Materials Engineer Approved By: Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects Enclosure

REPORT DETAILS Summary of Plant Status Unit 1 began the inspection period at 100 percent power. The unit was shut down for a refueling outage on April 14.

Unit 2 began the inspection period at 100 percent power. The unit remained at or near 100 percent power until June 28, when the unit tripped due to actuation of the main generator protection system. The unit remained shut down at the end of the inspection period.

1. REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - 1 sample)

.1 Summer Readiness of Offsite and Alternate Alternating Current Power Systems a. Inspection Scope The inspectors reviewed plant features and procedures for the operation and continued availability of the offsite and alternate alternating current (AC) power system to evaluate readiness of the systems prior to seasonal high grid loading on May 31. The inspectors reviewed PSEGs procedures affecting these areas and the communications protocols between the transmission system operator and PSEG. This review focused on changes to the established program and material condition of the offsite and alternate AC power equipment. The inspectors assessed whether PSEG established and implemented appropriate procedures and protocols to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system. The inspectors evaluated the material condition of the associated equipment by interviewing the responsible system manager, reviewing condition reports and open WOs, and walking down portions of the offsite and AC power systems including the 500 kilovolt (kV).

b. Findings No findings were identified.

1R04 Equipment Alignment

.1 Partial System Walkdown (71111.04Q - 4 samples)

a. Inspection Scope The inspectors performed partial walkdowns of the following systems:

  • Unit 1, 1A and 1C 125V direct current (DC) system during 1B 125V DC battery inoperability on April 6
  • Unit 1, Containment penetrations during irradiated fuel moves on April 19
  • Unit 2, Auxiliary building ventilation with damper 2ABV2 failed open on June 16

The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), technical specification(s) (TSs), WOs, notifications (NOTFs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the systems performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies.

The inspectors also reviewed whether PSEG staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.

b. Findings No findings were identified.

.2 Full System Walkdown (71111.04S - 1 sample)

a. Inspection Scope On June 22, 2016, the inspectors performed a complete system walkdown of accessible portions of the Unit 2 safety injection (SI) to verify the existing equipment lineup was correct. The inspectors reviewed operating procedures, surveillance tests, drawings, equipment line-up check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors also reviewed electrical power availability, component lubrication and equipment cooling, hanger and support functionality, and operability of support systems. The inspectors performed field walkdowns of accessible portions of the systems to verify as-built system configuration matched plant documentation, and that system components and support equipment remained operable. The inspectors confirmed that systems and components were aligned correctly, free from interference from temporary services or isolation boundaries, environmentally qualified, and protected from external threats. The inspectors also examined the material condition of the components for degradation and observed operating parameters of equipment to verify that there were no deficiencies.

Additionally, the inspectors reviewed a sample of related notifications and WOs to ensure PSEG appropriately evaluated and resolved any deficiencies.

b. Findings No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns (71111.05Q - 5 samples)

a. Inspection Scope The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that PSEG controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression

equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

  • Unit 2, Spent fuel (SF) and component cooling heat exchangers (HXs) on May 12
  • Unit 2, Boric acid evaporator unit and chemistry area on May 20
  • Unit 2, SW pump bays during 21 SW pump maintenance on June 8
  • Unit 2, Chiller room while protected on June 16 b. Findings No findings were identified.

1R07 Heat Sink Performance (711111.07A - 1 sample)

a. Inspection Scope The inspectors reviewed the 12 SI pump lube oil cooler readiness and availability to perform its safety functions. The inspectors reviewed the design basis for the component and verified PSEGs commitments to NRC Generic Letter 89-13, Service Water Requirements Affecting Safety-Related Equipment. The inspectors performed inspection of the as-found conditions, and discussed the results of previous inspections with PSEG staff. The inspectors verified that PSEG initiated appropriate corrective actions for identified deficiencies. The inspectors also verified that the number of tubes plugged within the HX did not exceed the maximum amount allowed.

b. Findings No findings were identified.

1R08 In-service Inspection Activities (71111.08 - 1 sample)

a. Inspection Scope Inspectors from the NRC Region I Office, specializing in materials and in-service examination activities, observed portions of PSEGs activities involving baffle bolt examinations and replacements during the Salem Unit 1 spring 2016 refueling outage (1R24). PSEG notified the NRC of problems with baffle bolts in Event Notification 51902, Anomalies Identified during Visual Inspection of Reactor Vessel Internals. During May 17-19, 2016, and June 20-23, 2016, inspectors conducted an inspection of PSEGs evaluation of the baffle bolt ultrasonic testing results and visual examination performed during 1R24. The inspectors reviewed documentation, interviewed personnel, and reviewed video recordings of visual examinations performed during the current and previous refueling outages. The inspectors also observed in-progress baffle bolt replacement activities.

Nondestructive Examination and Welding Activities (Section 02.01)

The inspectors conducted a review of PSEGs implementation of in-service inspection (ISI) program activities for monitoring degradation of the reactor coolant system boundary, risk significant piping and components, and containment systems during Salem Unit 1 refueling outage 1R24. The sample selection was based on the inspection procedure objectives and risk priority of those pressure retaining components in these systems where degradation would result in a significant increase in risk. The inspectors observed in-process nondestructive examination (NDE), reviewed records, and interviewed personnel to verify the following: a) that non-destructive activities were performed in accordance with American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Section XI, 2004 Edition, no Addenda, requirements; b) that indications and defects, if present, were dispositioned in accordance with the ASME Code or an NRC approved alternative; and, c) that relevant indications were compared to previous examinations to determine if any changes occurred.

The inspectors reviewed the ultrasonic testing (UT) procedure used for the examination of the Unit 1 baffle bolts to verify it met the requirements of the ASME Boiler and Pressure Vessel Code and the applicable guidance in the Electric Power Research Institutes Materials Reliability Program (MRP-227 and 228). The inspectors reviewed the UT data records for the examinations performed during the 1R24 refueling outage to verify that activities were performed in accordance with applicable examination procedures.

The inspectors reviewed video from the visual examination of the baffle bolts performed in the current refueling outage (RFO). The inspectors also reviewed video of visual examinations performed during Unit 1 RFOs in 2001, 2013, and 2014 to assess the as-found conditions of the baffle bolts. The inspectors reviewed certifications of the NDE technicians performing the examinations to verify the examinations were performed by qualified individuals in accordance with approved procedures and the results reviewed and evaluated by certified Level III NDE personnel.

The inspectors performed a sample of observations of NDE activities and reviewed records of NDE activities. The review sample consisted of two or three types of NDE activities, including at least one volumetric examination.

ASME Code Required Examinations Salem Unit 1, Liquid Penetrant Report No. PT-16-002, 11-RHRHEX Vessel Support, 4/15/16, (Summary No.205170) [record review]

Salem Unit 1, Liquid Penetrant Report No. PT-16-001, Pipe Lugs 8-RH-2116-10PL-1 through 4, 4/15/16, (Summary No. 263631) [record review]

Salem Unit 1, Liquid Penetrant Report No. PT-16-004, Pipe to Penetration IA, Component 12 SJ-2152-36PS-4, 4/19/16, (Summary No. 263904) [record review]

Salem Unit 1, Liquid Penetrant Report No. PT-16-003, Inlet Nozzle To 11 Charging Pump, Component 6-CV-2111-14R1, 4/15/16, (Summary No. 220757) [record review]

Salem Unit 1, Liquid Penetrant Report No. PT-16-005, Pipe-to-Valve (11CS48)

[record review] Component ID: 8-CS-2114-60, 4/15/16, (Summary No. 56640)

Salem Unit 1, Ultrasonic examination (Summary #006325) Report UT-16-039, Component ID: 1-PZR-20, Pressurizer, shell J weld [Observed]

Component ID: 16-BFN-2111-IRS, Inside Radius Section Ultrasonic Examination, 16-BF-2111, Report UT-16-013, Steam Generator #11, (Summary #204201) [Observed]

Component 4-PRN-1100-IRS, Pressurizer Relief Nozzle, inside Radius Section, Ultrasonic Examination, (Summary #007000), UT-16-031, [Observed]

Observation of Baffle Bolt Replacement Activities The inspectors observed electrical discharge machining activities on a baffle bolt location. The inspectors observed the bolt hole milling activities for a baffle bolt. The inspectors verified that bolt replacement activities were being performed in accordance with approved procedures.

Other Augmented, License Renewal or Industry Initiative Examinations PSEG did not schedule augmented inspections in the outage scope for 1R24.

Review of Relevant Indication(s) Evaluated and Accepted for Continued Service PSEG did not have any originally rejectable indications since the end of their prior outage, which were later accepted for continued use after evaluation.

Modifications, Repairs, or Replacements Consisting of Welding on Pressure Boundary Risk Significant Systems The inspectors reviewed Design Change Package 80092579, Salem Unit 1 - Steam Generator (SG) Bowl Drain Repair, for SGs 11, 12, 13, and 14. This change removed Alloy 600 and associated 82/182 weld material from each SG channel head bowl drain plug to reduce the potential for primary water stress corrosion cracking. The inspectors determined overall whether the modifications were completed in accordance with ASME Section XI as a repair/replacement activity. Specifically, the inspectors reviewed the machining and welding procedures used to complete the modifications, reviewed the training of the machinists, welders and laborers qualified on a mockup of the channel heads, and reviewed the mockup training completed by all craft personnel on the project.

The inspectors reviewed the in-process NDE and the final NDE procedures to determine whether the change was implemented in accordance with ASME Section XI repair/replacement requirements.

PWR Vessel Upper Head Penetration Inspection Activities (Section 02.02)

The Salem Unit 1 reactor pressure vessel head was replaced with an Alloy 690 head in 2005. The inspectors determined that reactor pressure vessel head examinations (per ASME Code Case N-729) were not required during 1R24.

Boric Acid Corrosion Control Inspection Activities (Section 02.03)

The inspectors reviewed the Boric Acid Corrosion Control program and implementing PSEG procedures, and discussed the outage inspections with program engineers. The inspectors also reviewed documentation, corrective action process notifications, including photographic records, of the conditions identified during the plant shutdown.

The inspectors also reviewed a sample of notifications recommending repairs to identified conditions and a sample of boric acid engineering evaluations performed to determine the priority of repair of identified boric acid corrosion on safety significant

piping and components. Boric acid inspections were conducted on safety significant piping and components inside the containment structure during walk downs conducted by PSEG staff with the plant at normal pressure and temperature conditions. The inspectors reviewed a sample of photos and visual inspection records to verify that boric acid leakage was being appropriately identified and non-conforming conditions of boric acid leaks were documented in the CAP with a focus on areas that could cause degradation of safety significant components.

The inspectors verified that potentially more significant boric acid deficiencies were being adequately dispositioned by reviewing a sample of evaluations documented in the following PSEG condition reports: 20682192, 20699859, 20699820, 20699910, 20704139, 20707125, 20712774, 20713572, 20722494, 20682192, 20699859, 20707125, 20722494, 70179375, 20699820, 20704139, 70185980, 20712774, 20713573, 20713572.

These reviews verified whether the corrective actions were consistent with the requirements of the ASME Code and Title 10 of the Code of Federal Regulations (10 C)FR Part 50, Appendix B, Criterion XVI. The inspectors reviewed the engineering evaluations associated with these condition reports to verify whether equipment or components wetted or impinged upon by boric acid solutions were properly analyzed for degradation that might impact their function.

Steam Generator Tube Inspection Activities (Section 02.04)

PSEGs Base Eddy Current Test (ECT) program consisted of: (a) 100 percent bobbin probe inspection of straight and U-bend tubes, (b) 50 percent Hot Leg coverage of Top of Tubesheet area with an array probe, (c) 3 tube periphery tube array testing, and various + Point sampling strategies (for U-bend and Dent/Ding inspections) of in-service tubes were completed in each SG. The inspectors reviewed the 1R24 SG tube Degradation Assessment, ECT examination scope and expansion criteria to verify that it met TS requirements, Electric Power Research Institute (EPRI) guidelines, and commitments made to the NRC. The inspectors also verified that the ECT scope included areas of degradation that were known to represent potential ECT challenges such as the top of tube sheet, tube support plates, and U-bends. Upon completion of eddy current (EC) examinations and the evaluation of all data, PSEG staff determined that six tubes required plugging. The affected tubes were plugged during 1R24. The inspectors verified that the affected tubes were properly screened against the in situ screening criteria and that none of the tube indications required in-situ pressure testing.

The inspectors observed portions of the ECT being performed and verified whether:

(1) the appropriate probes were used for identifying the expected types of degradation, (2) calibration requirements were adhered to, and (3) probe travel speed was in accordance with procedural requirements. The inspectors performed a review of the site-specific qualifications for the techniques being used, and verified whether the ECT data analyses were adequately performed per EPRI and PSEG specific guidelines. The inspectors selected a sample of degraded tubes and compared them to the previous outage operational assessment to assess PSEGs prediction capabilities. The inspectors also reviewed a sample of EC data, and verified, through discussion with the data analyst that the analytical techniques used to evaluate the inspection data were adequate. The inspectors further verified that the assumed NDE flaw sizing accuracy was consistent with data from EPRI examination technique specification sheet or applicable performance demonstration. Finally, the inspectors reviewed the qualifications for the EC data collection personnel, a sample of the inspection

supervision personnel qualifications and a sample of the qualifications of staff responsible for interpretation and resolution analysis to determine whether the records were complete.

The inspectors observed a portion of a plug integrity visual examination per procedure 81DP-9RC40, Steam Generator Channel Head Video Inspection, to verify that those tubes that had been previously plugged did not exhibit any leakage. No evidence of plug leakage was identified. Additionally, the inspectors observed a portion of the secondary sludge lancing and foreign object search and retrieval (FOSAR) inspections. No significant foreign materials or quantity of sludge were identified.

During the prior operating cycle previous to the current refueling outage 1R24, the inspectors determined whether leakage from each SG was measured, via sampling of each SG, for the complete prior operating cycle (leakage was not measured).

PSEG staff completed secondary side inspections and sludge lancing of all SGs. The inspectors reviewed the results to determine that no loose parts affecting tube integrity were noted and that other SG related inspections were performed without repairs.

PSEG staff performed a plug integrity visual examination to verify that those tubes that had been previously plugged did not exhibit leakage. From this visual exam, PSEG staff documented excessive boron buildup around tube plug 43-34 in the SG 11 cold leg and initiated CR-2016-29172 to track the evaluation of the condition. PSEG staff also initiated Notification 20726743 to track the condition. PSEG Engineering staff review of the plug concluded that no evidence of plug leakage had occurred. Additionally, secondary sludge lancing and FOSAR inspections were performed in each SG. No foreign materials, which could damage SG tubes, were identified. The inspectors reviewed the PSEG evaluations and information to determine the conclusions were technically supported.

Identification and Resolution of Problems (Section 02.05)

The inspectors reviewed a sample of condition reports, which identified NDE indications, deficiencies and other nonconforming conditions since the previous, 1R23, refueling outage. The inspectors verified that nonconforming conditions were properly identified, characterized, evaluated, corrective actions identified and dispositioned, and appropriately entered into the CAP.

b. Findings Introduction. The inspectors determined the level of degradation of Unit 1 baffle bolts reported to the NRC as a condition not previously analyzed is an issue of concern that warrants additional inspection to determine whether a performance deficiency exists. As a result, the NRC opened a unresolved item (URI).

Description. Additional inspection is warranted to determine whether a performance deficiency exists related to Event Notification 51902, dated May 3, 2016, in which PSEG reported to the NRC that the level of degradation of baffle bolts was a condition not previously analyzed. The baffle bolts secure plates in the reactor core barrel to form a shroud around the fuel core to direct reactor coolant flow upward through the fuel assemblies. In order to determine if a performance deficiency exists, the inspectors will review the results of PSEGs RCE which will be completed at a later date.

(URI 05000272/2016002-01, Baffle-Former Bolts with Identified Anomalies)

1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample)

Quarterly Review of Licensed Operator Requalification Testing and Training a. Inspection Scope The inspectors observed licensed operator simulator training on June 8, 2016, which included a heater drain pump oil leak, a steam generator feed pump trip, and a steam generator tube rupture. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the TS action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a. Inspection Scope The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, and component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance WOs, and maintenance rule (MR) basis documents to ensure that PSEG was identifying and properly evaluating performance problems within the scope of the MR. For each sample selected, the inspectors verified that the SSC was properly scoped into the MR in accordance with 10 CFR 50.65 and verified that the (a)(2)

performance criteria established by PSEG staff was reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors ensured that PSEG staff was identifying and addressing common cause failures that occurred within and across MR system boundaries.

  • Unit 2, 22SW535, unsatisfactory stroke time of SW accumulator supply valve to 22 containment fan cooler unit (CFCU) on May 2
  • Common, MR URI, 05000272;311/2015008-01: Inadequate MR System Performance Criteria Selection, closeout on May 1 b. Findings No findings were identified. Additional inspection results regarding the URI closeout are documented in Section 4OA5.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 5 samples)

a. Inspection Scope The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that PSEG performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that PSEG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When PSEG performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk.

The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the stations probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

  • Unit 1, 11SW223, SW outlet valve to 11 CFCU, failure to close on April 7
  • Unit 1, Reactor core baffle-to-former bolt expanded inspection scope on April 22
  • Unit 2, Appendix R safe shutdown panel failed indication on May 9
  • Unit 2, 2A subcooling margin monitor failure on May 26
  • Unit 2, Yellow risk with one offsite power source unavailable on June 1 b. Findings No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15 - 9 samples)

a. Inspection Scope The inspectors reviewed operability determinations for the following degraded or non-conforming conditions based on the risk significance of the associated components and systems:

  • Unit 1, Corrosion and metal loss identified during inspection of 11 SW header on April 23
  • Unit 1, 1 Emergency control air compressor shutdown on April 27
  • Unit 1, SI thermal relief valve failures on May 2
  • Unit 1, 11 diesel fuel oil storage tank high particulates on May 18
  • Unit 2, IOD of the degraded condition of the baffle-former bolts identified from Unit 1
  • operating experience on April 27
  • Unit 2, 125V DC battery degraded cell post connections on May 2
  • Common, 10 CFR Part 21 issue related to safety-related 4kV breakers on May 16 The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or

system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to PSEGs evaluations to determine whether the components or systems were operable. The inspectors confirmed, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by PSEG.

b. Findings No findings were identified.

1R18 Plant Modifications (71111.18 - 2 samples)

.2 Permanent Modifications a. Inspection Scope The inspectors reviewed Design Change Package (DCP) 80117136, Salem Unit 1 Baffle to Former Bolt Replacement. This modification documents the replacement of 189 degraded and potentially degraded baffle bolts with a new design baffle bolt made of an improved material. Additionally the modification documented the locations of the replacement bolts and the location of three degraded or potentially degraded bolts which were left in place and are described below. The inspectors also reviewed modification documents (DCP 80117378) associated with the equivalency evaluation of the material change from Type 347 stainless steel to Type 316 stainless steel, and the bolt head design change from a slot to a hex configuration. Thus this inspection involved two samples - 1) the bolting pattern analysis for the replacement bolts, and 2) a review of the bolting material change.

This modification was completed during the spring 2016 refueling outage (1R24) and involved the replacement of 189 baffle bolts out of a total of 832 located in the Unit 1 reactor vessel. PSEG replaced 189 either degraded or potentially degraded baffle bolts as observed by visual indications of missing or protruding bolt heads, missing or broken lock bar, bolts that did not pass ultrasonic testing or bolts that were inaccessible for ultrasonic testing. PSEG did not remove and replace three bolts that were potentially degraded due to difficulties encountered during the removal/replacement process. One bolt had an indication during ultrasonic testing but was not visibly damaged. The second bolt was inaccessible for ultrasonic testing, which would have required replacement.

The third bolt had successfully passed an ultrasonic test but had a visual indication on one of the lock bar welds which may have indicated a crack in the weld.

The inspectors reviewed PSEGs analysis and the Westinghouse minimum bolting analysis and determined that leaving the one degraded and two potentially degraded bolts installed was technically acceptable and that the baffle assembly was functional as a system support component. Details of the NRC assessment of the final configuration of the baffle bolts and the minimum bolting analysis can be found in Section 4OA2 of this report.

b. Findings No findings were identified.

1R19 Post-Maintenance Testing (71111.19 - 9 samples)

a. Inspection Scope The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, and witnessed the test or reviewed test data to verify quality control hold point were performed and checked, and that results adequately demonstrated restoration of the affected safety functions.

  • Unit 1, 13 Station power transformer tap changer did not function in automatic on May 4
  • Unit 1, 12 containment fan cooling unit (CFCU) motor cooler HX failed leak test on May 6
  • Unit 1, Turbine-driven AFW room cooler cycling on May 10
  • Unit 1, Reactor vessel level indication system capillary repair on May 13
  • Unit 2, 24 SW strainer trip on thermal overloads on April 7
  • Unit 2, 24 SG flow channel 1 drop to 93 percent on May 4
  • Unit 2, 21 Chiller thermal expansion valve failure on May 24 b. Findings No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

a. Inspection Scope The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1 maintenance and refueling outage (1R24), conducted April 14 through the end of the quarter. The inspectors reviewed PSEGs development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:

  • Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment out of service
  • Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting
  • Status and configuration of electrical systems and switchyard activities to ensure that TSs were met
  • Impact of outage work on the ability of the operators to operate the SF pool cooling system
  • Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss
  • Activities that could affect reactivity
  • Refueling activities, including fuel handling and fuel receipt inspections
  • Fatigue management
  • Tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block the emergency core cooling system suction strainers, and startup and ascension to full power operation
  • Identification and resolution of problems related to refueling outage activities
  • Foreign Object Search and Retrieval (FOSAR) for missing baffle bolts and locking tabs During this outage, PSEG replaced 189 degraded baffle bolts in the Unit 1 reactor vessel baffle assembly. This emergent project resulted in the extension of the outage schedule from 36 days to 106 days.

b. Findings No findings were identified.

1R22 Surveillance Testing (71111.22 - 5 samples)

a. Inspection Scope The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and PSEG procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

  • Unit 1, Manual SI on April 17
  • Unit 2, 21 RHR In-service Testing on April 1
  • Unit 2, 22SW223, SW outlet valve to 22 CFCU, stroke time in the required evaluation range on May 3

Cornerstone: Emergency Preparedness 1EP6 Drill Evaluation (71114.06 - 1 sample)

Emergency Preparedness Drill Observation a. Inspection Scope The inspectors evaluated the conduct of a routine PSEG emergency drill on June 16 to identify any weaknesses and deficiencies in the classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulator, technical support center, and emergency operations facility to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the drill critique to compare inspector observations with those identified by PSEG staff in order to evaluate PSEGs critique and to verify whether the PSEG staff was properly identifying weaknesses and entering them into the CAP.

b. Findings No findings were identified.

2. RADIATION SAFETY Cornerstones: Occupational and Public Radiation Safety 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01 - 6 samples)

a. Inspection Scope The inspectors reviewed PSEGs performance in assessing and controlling radiological hazards in the workplace. The inspectors used the requirements contained in 10 CFR Part 20, TSs, applicable Regulatory Guides (RGs), and the procedures required by TSs as criteria for determining compliance.

Inspection Planning The inspectors reviewed the PIs for the occupational radiation safety cornerstone, radiation protection (RP) program audits, and reports of operational occurrences in occupational radiation safety since the last inspection.

Radiological Hazard Assessment (1 sample)

The inspectors conducted independent radiation measurements during walk-downs of the facility and reviewed the radiological survey program, air sampling and analysis, continuous air monitor use, recent plant radiation surveys for radiological work activities, and any changes to plant operations since the last inspection to verify survey adequacy of any new radiological hazards for onsite workers or members of the public.

Instructions to Workers (1 sample)

The inspectors reviewed high radiation area work permit controls and use; observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.

The inspectors reviewed several occurrences where a workers electronic personal dosimeter alarmed. The inspectors reviewed PSEGs evaluation of the incidents, documentation in the CAP, and whether compensatory dose evaluations were conducted when appropriate. The inspectors verified follow-up investigations of actual radiological conditions for unexpected radiological hazards were performed.

Contamination and Radioactive Material Control The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material.

Radiological Hazards Control and Work Coverage (1 sample)

The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walk-downs and observation of radiological work activities. The inspectors assessed whether posted surveys; radiation work permits (RWPs); worker radiological briefings and RP job coverage; the use of continuous air monitoring, air sampling, and engineering controls; and dosimetry monitoring were consistent with the present conditions. The inspectors examined the control of highly activated or contaminated materials stored within the SF pools and the posting and physical controls for selected high radiation areas (HRAs), locked high radiation areas (LHRAs) and very high radiation areas (VHRAs) to verify conformance with the occupational PI.

Risk-Significant High Radiation Area and Very High Radiation Area Controls (1 sample)

The inspectors reviewed the procedures and controls for HRAs, VHRAs, and radiological transient areas in the plant.

Radiation Worker Performance and Radiation Protection Technician Proficiency (1 sample)

The inspectors evaluated radiation worker performance with respect to RP work requirements. The inspectors evaluated RP technicians in performance of radiation surveys and in providing radiological job coverage.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with radiation monitoring and exposure control (including operating experience) were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings No findings were identified.

2RS2 Occupational As Low As is Reasonable Achievable Planning and Controls (71124.02 - 3 samples)

a. Inspection Scope The inspectors assessed PSEGs performance with respect to maintaining occupational individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors used the requirements contained in 10 CFR Part 20, applicable RGs, TSs, and procedures required by TSs as criteria for determining compliance.

Inspection Planning The inspectors conducted a review of Salem Station collective dose history and trends; ongoing and planned radiological work activities; previous post-outage ALARA reviews; radiological source term history and trends; and ALARA dose estimating and tracking procedures.

Radiological Work Planning The inspectors selected the following radiological work activities based on exposure significance for review:

  • RWP 14 , Pressurizer Activities
  • RWP 17, Primary SG Work For each of these activities, the inspectors reviewed: ALARA work activity evaluations; exposure estimates; and exposure reduction requirements.

Verification of Dose Estimates and Exposure Tracking Systems The inspectors reviewed the current annual collective dose estimate; basis methodology; and measures to track, trend, and reduce occupational doses for ongoing work activities.

The inspectors evaluated the adjustment of exposure estimates or re-planning of work.

Source Term Reduction and Control (1 sample)

The inspectors reviewed the current plant radiological source term and historical trend, plans for plant source term reduction, and contingency plans for changes in the source term as the result of changes in plant fuel performance or changes in plant primary chemistry.

The inspectors observed radiological work activities and evaluated the use of shielding and other engineering work controls based on the radiological controls and ALARA plans for those activities.

Radiation Worker Performance (1 sample)

The inspectors observed radiation worker and RP technician performance during radiological work to evaluate worker ALARA performance according to specified work controls and procedures. Workers were interviewed to assess their knowledge and awareness of planned and/or implemented radiological and ALARA work controls.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with ALARA planning and controls were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03 - 3 samples)

a. Inspection Scope The inspectors reviewed the control of in-plant airborne radioactivity and the use of respiratory protection devices in these areas. The inspectors used the requirements in 10 CFR Part 20, RG 8.15, RG 8.25, NUREG/CR-0041, TS, and procedures required by TS as criteria for determining compliance.

Inspection Planning The inspectors reviewed the UFSAR to identify ventilation and radiation monitoring systems associated with airborne radioactivity controls and respiratory protection equipment staged for emergency use. The inspectors also reviewed respiratory protection program procedures and current PIs for unintended internal exposure incidents.

Engineering Controls (1 sample)

The inspectors reviewed operability and use of both permanent and temporary ventilation systems, and the adequacy of airborne radioactivity radiation monitoring in the plant based on location, sensitivity, and alarm set-points.

Use of Respiratory Protection Devices (1 sample)

The inspectors reviewed the adequacy of PSEGs use of respiratory protection devices in the plant to include applicable ALARA evaluations, respiratory protection device certification, respiratory equipment storage, air quality testing records, and individual qualification records.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with the control and mitigation of in-plant airborne radioactivity were identified at an appropriate threshold and addressed by PSEGs CAP.

b. Findings No findings were identified.

2RS4 Occupational Dose Assessment (71124.04 - 2 samples)

a. Inspection Scope The inspectors reviewed the monitoring, assessment, and reporting of occupational dose. The inspectors used the requirements in 10 CFR Part 20, RGs, TSs, and procedures required by TSs as criteria for determining compliance.

Inspection Planning The inspectors reviewed: RP program audits; National Voluntary Laboratory Accreditation Program (NVLAP) dosimetry testing reports; and procedures associated with dosimetry operations.

Source Term Characterization (1 sample)

The inspectors reviewed the plant radiation characterization (including gamma, beta, alpha, and neutron) being monitored. The inspector verified the use of scaling factors to account for hard-to-detect radionuclides in internal dose assessments.

External Dosimetry The inspectors reviewed: dosimetry NVLAP accreditation; onsite storage of dosimeters; the use of correction factors to align electronic personal dosimeter results with NVLAP dosimetry results; dosimetry occurrence reports; and CAP documents for adverse trends related to external dosimetry.

Internal Dosimetry (1 sample)

The inspectors reviewed: internal dosimetry procedures; whole body counter measurement sensitivity and use; adequacy of the program for whole body count monitoring of plant radionuclides or other bioassay technique; adequacy of the program for dose assessments based on air sample monitoring and the use of respiratory protection; and internal dose assessments for any actual internal exposure.

Special Dosimetric Situations The inspectors reviewed external dose monitoring of workers in large dose rate gradient environments.

Problem Identification and Resolution The inspectors evaluated whether problems associated with occupational dose assessment were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings No findings were identified.

2RS5 Radiation Monitoring Instrumentation (71124.05 - 1 sample)

a. Inspection Scope The inspectors reviewed performance in assuring the accuracy and operability of radiation monitoring instruments used to protect occupational workers during plant operations and from postulated accidents. The inspectors used the requirements in 10 CFR Part 20; RGs; applicable industry standards; and procedures required by TSs as criteria for determining compliance.

Inspection Planning The inspectors reviewed: Salem Station UFSAR; RP audits; records of in-service survey instrumentation; and procedures for instrument source checks and calibrations.

Walkdowns and Observations The inspectors checked the calibration and source check status of various portable radiation survey instruments and contamination detection monitors for personnel and equipment.

Calibration and Testing Program The inspectors reviewed the calibration standards used for portable instrument calibrations and response checks to verify that instruments were calibrated by a facility that used National Institute of Science and Technology traceable sources.

Problem Identification and Resolution (1 sample)

The inspectors verified that problems associated with radiation monitoring instrumentation (including failed calibrations) were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings No findings were identified.

Cornerstone: Public Radiation Safety (PS)

2RS7 Radiological Environmental Monitoring Program (71124.07 - 2 samples)

a. Inspection Scope The inspectors reviewed the Radiological Environmental Monitoring Program (REMP) to validate the effectiveness of the radioactive gaseous and liquid effluent release program and implementation of the Groundwater Protection Initiative (GPI). The inspectors used the requirements in 10 CFR Part 20; 40 CFR Part 190; 10 CFR Part 50, Appendix I; TSs; Offsite Dose Calculation Manual (ODCM); Nuclear Energy Institute 07-07; and procedures required by TSs as criteria for determining compliance.

Inspection Planning The inspectors reviewed: Salem and Hope Creek Stations 2015 annual radiological environmental and effluent monitoring reports; REMP program audits; ODCM changes; land use census; UFSAR; and inter-laboratory comparison program results.

Site Inspection (1 sample)

The inspectors walked down various passive dosimeter and air and water sampling locations and reviewed associated calibration and maintenance records. The inspectors observed the sampling of various environmental media as specified in the ODCM and reviewed any anomalous environmental sampling events including assessment of any positive radioactivity results. The inspectors reviewed any changes to the ODCM. The inspectors verified the operability and calibration of the meteorological tower instruments and meteorological data readouts. The inspectors reviewed environmental sample laboratory analysis results, laboratory instrument measurement detection sensitivities, laboratory quality control program audit results, and the inter- and intra-laboratory comparison program results. The inspectors reviewed the groundwater monitoring program as it applies to selected potential leaking SSCs; and 10 CFR 50.75(g) records of leaks, spills, and remediation since the previous inspection.

Groundwater Protection Initiative Implementation The inspectors reviewed: groundwater monitoring results; changes to the Groundwater Protection Initiative (GPI) program since the last inspection; anomalous results or missed groundwater samples; leakage or spill events including entries made into the decommissioning files (10 CFR 50.75 (g)); evaluations of surface water discharges; and PSEGs evaluation of any positive groundwater sample results including appropriate stakeholder notifications and effluent reporting requirements.

Identification and Resolution of Problems (1 sample)

The inspectors evaluated whether problems associated with the REMP were identified at an appropriate threshold and properly addressed in PSEGs CAP.

b. Findings No findings were identified.

4. OTHER ACTIVITIES 4OA1 Performance Indicator Verification (71151)

Unplanned Scrams, Unplanned Power Changes, and Unplanned Scrams with Complications (6 samples)

a. Inspection Scope The inspectors reviewed PSEG submittals for the following Initiating Events Cornerstone PIs for the period of July 1, 2015 through June 30, 2016.

  • Unit 1 & 2 Unplanned Scrams with Complications To determine the accuracy of the PI data reported during those periods, inspectors used definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspectors reviewed PSEG operator narrative logs, maintenance planning schedules, condition reports, event reports, and NRC integrated IRs to validate the accuracy of the submittals.

b. Findings No findings were identified.

4OA2 Problem Identification and Resolution (71152 - 4 samples)

.1 Routine Review of Problem Identification and Resolution Activities a. Inspection Scope As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify PSEG entered issues into their CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into their CAP and periodically attended condition report screening meetings. The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, PSEG performed an evaluation in accordance with 10 CFR Part 21.

b. Findings No findings were identified.

.2 Semi-Annual Trend Review a. Inspection Scope The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. As part of this review, the inspectors included repetitive or closely-related issues documented by PSEG in the CAP and repetitive or closely-related issues that may have been documented by PSEG outside of the CAP, such as trend reports, PIs, major equipment problem lists, system health reports, MR assessments, and maintenance or CAP backlogs. The inspectors also reviewed PSEG CAP database for the first and second quarters of 2016 to assess notifications written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the inspectors daily condition report review (Section 4OA2.1). The inspectors reviewed the PSEG CAP trending data, conducted under LS-AA-125, to verify that PSEG personnel were appropriately evaluating and trending adverse conditions in accordance with applicable procedures.

a. Findings and Observations No findings were identified.

Equipment Reliability (Steady)

The inspectors documented an adverse trend in either equipment reliability or unplanned entries into TS shutdown limiting conditions for operation (LCO) in each of the previous four semi-annual trend review periods (IRs 05000272; 311/2014003, 2014005, 2015002 and 2015004). In February 2016, in response to PSEGs unplanned LCO performance goal not being met, PSEG performed Common Cause Evaluation (CCE) 70184208, Unplanned Shutdown LCO Goal Not Met. The CCE was completed in April of 2016, with the following results:

  • A trend of data over an 18-month period from August 2014 through January 2016 identified 68 unplanned shutdown LCOs, which far exceeded the station goal of no more than 8 in a 12-month rolling average. PSEGs CCE concluded:

1) 15 LCO entries were attributed to faulty parts; 2) 10 entries were attributed to equipment not being repaired in a timely manner; and 3) more follow up evaluations were warranted:

o Work Group Evaluation (WGE) 70185245, Follow up Evaluation from Unplanned shutdown LCOs, was performed to further evaluate the 10 entries attributed to equipment not being repaired in a timely manner. PSEG attributed the cause to ineffective development and implementation of equipment reliability strategies to ensure reliability until long-term elimination or mitigating actions were in place.

Actions were assigned to develop bridging strategies for Plant Health Committee items and rollout to Station Oversight Committee (SOC) and Management Review Committee (MRC) an expectation that if an unplanned LCO occurs, a causal evaluation should be performed.

The inspectors noted some improvement in the area of unplanned entries into TS LCOs in recent months; specifically, 44 unplanned shutdown LCOs occurred from June 2015 to April 2016, but only seven occurred in the last 3 months of this 10 month period. The inspectors determined that the adverse trend of equipment failures did not constitute a

performance deficiency, because the trend, by itself, did not constitute a violation of any NRC requirement. The inspectors inspected individual equipment failures as ROP baseline inspection samples documented in other sections of this report.

Main Control Room Deficiencies (Steady with recent improvement)

The inspectors noted an adverse trend in main control room deficiencies, as evident by a Red station performance metric dating back to mid-2015, when the station metric was redefined to align with the current industry metric. Specifically, in June of 2016, Unit 1 had 69 and Unit 2 had 45, versus a red performance metric threshold of 16 or more.

However, the inspectors noted recent improvements in this area. Specifically, Unit 1 reduced the backlog from 99 in January 2016 to 69 in June, and Unit 2 reduced the backlog from 73 before the fall 2015 refueling outage to 45 in June 2016.

Untimely Reportability Determinations (Steady)

In Section 4OA2.2 of IR 2015-004, the inspectors identified that past operability determinations were untimely in supporting conclusions of LER reportability in 60 days, and listed multiple examples. In response to a LER 05000311/2016-001-000 being submitted well beyond 60 days from the occurrence of the event (see Sections 4OA2.3 and 4OA7 of this report), PSEG performed a review under apparent cause evaluation (ACE) 70183590, to determine the extent of condition relative to missed or late reports under 10 CFR 50.72 and 50.73. PSEG concluded the following: 1) The execution of CAP does not support timely completion of evaluation products to support 60-day LER submittals; 2) SOC and MRC have a low threshold for requesting reportability reviews; and 3) Salem has a high number of supplemental LERs relative to the industry (four in 2015 versus an industry average of less than one), indicating that CAP does not support timely cause evaluation completion, which require LERs to be supplemented. The inspectors noted that PSEGs conclusion 3 above is consistent with a previously identified trend by the inspectors documented in Section 4OA2.2 of IR 2015002, which listed a steady increase in CAP evaluation products and subsequent trend of CAP products falling behind station timeliness goals. As a result of the ACE listed above, PSEG issued a temporary standing order to develop interim guidance until process improvements and controls were institutionalized for reportability, assigned corrective actions to develop procedure improvements and controls for accompanying reportability reviews, and to develop the appropriate change management plan for process changes to perform reportability reviews. The inspectors did not identify any actual violations of 10 CFR 50.72 or 50.73 during the performance of this inspection. The timeliness of reportability determinations remains a minor adverse trend.

Status Control and Human Performance Events (Improving)

The inspectors previously documented an adverse trend in status control in Section 4OA2.5 of IR 2014005. In December of 2015, Nuclear Oversight identified an adverse trend in status control. In February of 2016, PSEG completed a CCE in response to the adverse trend in plant status control. Additionally, status control was a focus area for the station in 2016. Since that time, the inspectors noted considerable improvement in the area of status control. Specifically, as of June 1, 2016, the station achieved 181 status control event free days. However, in recent months, the inspectors noted several human performance events that were not classified as status control events, though they reflect many of the same behavioral breakdowns in standards and fundamentals. Examples include:

  • April 17: 1B EDG invalid actuation: During the performance of solid state protection system testing in Mode 6 (refueling), the 1B EDG unexpectedly started while an operator in the field was attempting to replace a light bulb on the test box. PSEG performed an investigation and determined that the most likely cause was due to the operators finger bumping the block switch during the bulb replacement, which was enough pressure to allow the test block signal to be momentarily interrupted. PSEG reported this event as a telephone notification under 10 CFR 50.73(a)(1) and (a)(2)(iv)(A) on June 15.
  • April 25: #1 Emergency Compressed Air Compressor trip during leak test -

PSEG performed Quick Human Performance Investigation (QHPI) 70186240 and determined the operator in the control room did not understand the report from the equipment operator in the field, and determined that three-way communication was not used when it should have been.

  • April 19: 22B circulator bypass valve operated in the wrong direction - PSEG performed QHPI 71085972 and determined that an equipment operator did not fully open the 22B circulator outlet valve prior to attempting remote closure of the 22B circulator bypass, which resulted in the bypass valve failing to stroke closed.
  • March 27: Station Blackout (SBO) air compressor tripped - the equipment operator did not follow procedure while testing the SBO air compressor, resulting in a trip of the compressor (20723821).

The inspectors determined that none of the issues above were of more than minor significance, because none of them resulted in a significant plant transient or loss of a mitigating system. The inspectors determined that although the trend in events classified as status control had improved, the behaviors that contributed to them were still present.

.3 Annual Sample: Unit 2 Auxiliary Feedwater Loop Response Time Exceeded Technical Specifications a. Inspection Scope The inspectors performed an in-depth review of PSEGs identification, evaluation, and resolution following the discovery that a channel of the 21 AFW pump engineered safety feature actuation system (ESFAS) automatic actuation logic was inoperable.

On November 18, 2015, maintenance personnel compiling test data, collected on October 18, 2015, during the Unit 2 plant shutdown for the fall 2015 refueling outage, determined that the pump instrumentation loop time response exceeded test acceptance criteria. At the time, Unit 2 was shut down in a refueling outage and AFW was not required. The cause of the slow loop response was due to the isolation valve to the 21 AFW pump discharge pressure transmitter (2PA3450) being closed. The pressure transmitter provided input into the pump run-out protection and flow control circuit.

The closed isolation valve caused the pressure transmitter to take longer to sense pump discharge pressure, which resulted in the slow opening of the pump SG flow control valves (valves 23AF21 and 24AF21). PSEGs investigation determined that the condition likely existed since April 20, 2015, following the completion of maintenance on the pressure transmitter. On January 19, 2016, PSEG determined that the condition was reportable to the NRC. PSEG initiated an ACE to determine the cause of the untimely review and evaluation of the surveillance data collected on October 18, 2015,

and a WGE to determine the cause of the improperly positioned isolation valve to pressure transmitter 2PA3450. The inspectors performed an in-depth review of the ACE and WGE and corrective actions associated with the issues documented in Orders 70183590 and 70182519. PSEG submitted Licensee Event Report (LER)

05000311/2016-001-000, AFW Loop Response Time Exceeded TSs, on March 21, 2016, as an operation or condition which was prohibited by the plants TS. The inspectors review of the LER is documented in Section 4OA3.1 of this report. Section 4OA7 documents the enforcement aspects related to the LER.

The inspectors assessed PSEGs problem identification threshold, causal analysis, extent of condition reviews, compensatory actions, and the prioritization and timeliness of corrective actions to determine whether PSEG was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of PSEGs CAP and 10 CFR Part 50, Appendix B.

In addition, the inspectors reviewed documentation associated with this issue, and interviewed engineering and maintenance personnel to assess the effectiveness of the implemented and planned corrective actions.

b. Findings and Observations No findings were identified.

Maintenance personnel compiling 21 AFW pump loop time response test data identified the slow response times for valves 23AF21 and 24AF21, and entered this issue into the CAP as NOTF 20710947. During their review, PSEG identified that the instrument isolation valve for the 21 AFW pump discharge pressure transmitter (2PA3450) was closed versus the required position of open. The improperly positioned valve was promptly placed into the required open position. PSEG entered the improperly positioned valve into the CAP as NOTF 20709417, and performed a prompt investigation and a WGE. The inspectors determined that action taken by PSEG upon discovery of the slow response times for valves 23AF21 and 24AF21 were prompt and appropriate.

The inspectors reviewed Order 70182519, which documented the WGE for instrument isolation valve for 2PA3450 being found in the incorrect position. Although the actual cause of the improperly positioned isolation valve was indeterminate, PSEG concluded that the condition most likely existed since April 20, 2015, when maintenance was last performed on 2PA3450. Corrective actions included plans to install human factors tools (i.e., additional measure devices) on all transmitter isolation valves located in both the Unit 1 and 2 AFW instrumentation panels. The inspectors concluded that PSEGs planned corrective action was appropriate.

The inspectors reviewed the timeline of events from the collection of test data on October 18, 2015, until the submittal of the LER for the condition prohibited by TS related to the slow instrument loop response time for the 21 AFW pump. The inspectors concluded that information was available to PSEG personnel on November 20, 2015, that the condition was potentially reportable when the cause was determined to be due to the incorrectly positioned instrument isolation valve to 2PA3450. However, the required LER was not submitted until March 21, 2016.

The inspectors reviewed PSEGs investigation into the reportability timeliness issue, as documented in Order 70183590. PSEG determined that the cause was due to work tracking assignments not being made to facilitate identification and completion of the

required past operability review in accordance with Engineering standard practice. The normal practice to evaluate issues for potential past operability/reportability is for the SOC to assign a technical evaluation to Engineering to review. In this case an action item was assigned to Engineering versus a technical evaluation. The due dates for action items are allowed to be extended by the assignee whereas, the process of extending technical evaluations has more stringent controls. Therefore, the priority of the action item was not established at the correct threshold by the assigned engineering supervisor. This resulted in extensions of the due date for the past operability/reportability review. PSEGs corrective actions taken or planned included issuance of an Operations standing order, which provided additional interim guidance for performing past operability and reportability reviews, and to develop process improvements and controls for accomplishing past operability and reportability reviews.

The inspectors concluded that the actions taken or planned appeared to appropriately address the reportability timeliness issue. In accordance with IMC 0612, "Power Reactor Inspection Reports," the above timeliness of reportability issue constituted a violation of minor significance that is not subject to enforcement action in accordance with the Enforcement Policy.

As discussed in Order 70183590, PSEG recognized that the SOC inappropriately assigned an action item versus the more appropriate technical evaluation to Engineering for the past operability/reportability review. The inspectors observed that actions taken by PSEG did not directly address the shortfall of the SOC in this case.

The inspectors noted that there was a low level assignment for the SOC to evaluate for a human performance crew clock reset; however, the clock reset was determined to not be necessary. The inspectors noted that the other actions taken or planned discussed above appeared to be adequate to address the inappropriate extensions of past operability and reportability reviews.

In NRC Inspection Report 05000272, 05000311/2015004, dated February 10, 2016, a problem identification and resolution adverse trend was documented related to past operability determinations being untimely in supporting conclusions of LER reportability within sixty days. The inspectors concluded that the untimely past operability and reportability review of the failed 21 AFW pump instrument loop time response test as an additional example of the adverse trend identified in NRC IR 05000272, 05000311/2015004 and updated in Section 4OA2.2 of this report. At the end of this inspection period, PSEG had not entered this adverse trend into their CAP.

.4 Annual Sample: Struthers-Dunn Relay Failures in Safety-Related Applications a. Inspection Scope The inspectors performed an in-depth review of PSEGs ACE and corrective actions associated with NOTF 20681569 related to a 21 containment spray (CS) pump failure to start. The 21 CS pump failed to start on October 2, 2015, during post-maintenance testing following scheduled maintenance. The 21 CS pump failure to start was investigated by PSEG during subsequent troubleshooting. Additionally, a failure modes and causal table determined the most likely cause for the failure to start was from a starting relay high contact resistance. PSEG postulated that contact contamination created a high resistance condition that was subsequently cleared due to the wiping action of the relay contact. The starting relay was a Struthers-Dunn Model 219BBX-240 and was replaced. The failed relay was sent for failure analysis to an offsite laboratory.

The lab was unable to repeat the high resistance contact operation that was observed at Salem. The lab functional testing did not yield any deficiencies or failure mechanisms.

The inspectors assessed PSEGs problem identification threshold, causal analyses, technical analyses, extent of condition reviews, and the prioritization and timeliness of corrective actions to determine whether PSEG was appropriately identifying, characterizing, and correcting problems associated with this issue. The inspectors reviewed the circumstances of this relay failure issue to ascertain the appropriateness of corrective actions. The inspectors also assessed PSEGs corrective actions to prevent recurrence. The inspectors compared the actions taken to the requirements of PSEGs CAP and 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action. In addition, the inspectors reviewed documentation associated with this issue, including condition reports, and interviewed engineering personnel to assess the effectiveness of the planned and implemented corrective actions.

b. Findings and Observations No findings were identified.

The Struthers-Dunn relays in critical applications were all replaced in 1996 and 1997 during extended unit shutdowns. From about 2000 to 2015, Salem experienced Struthers-Dunn relay failures in critical applications at about one MR functional failure per year. In May 2013, after a Struthers-Dunn relay failure associated with the 15 containment fan cooling unit (CFCU), PSEG developed extensive corrective actions to revise preventive maintenance (PM) templates and determine an appropriate replacement periodicity. An accelerated testing program was a corrective action and completed in March 2014 to determine the number of relay operations when the contacts gold flashing began to wear away exposing the silver base. Exposing the silver contact base leads to a corrosion condition called sulfidation creating a high resistance between relay contacts. Offsite laboratory analysis of previous Struthers-Dunn relays had identified worn gold flashing and sulfidation.

PSEG determined from the accelerated relay testing program that Struthers-Dunn relays in CFCU applications should be replaced every 10 years. The CFCUs have more frequent equipment on/off cycles compared to other critical Struthers-Dunn applications.

PSEG determined all other Struthers-Dunn relay replacements should be replaced at 20 years. PSEG established the 20 year replacement interval based on 400 relay operations for the equipment considered. However, the inspectors noted that for some relay applications, major gold flashing wear or wiping resulting in areas of exposed silver was observed from the accelerated failure testing results at just 350 relay operations.

PSEG generated notification 20734284 in response to the inspectors observation for resolution and to reevaluate the intended 20 year replacement periodicity.

The corrective action due dates for the final PM templates are due in August 2016.

PSEG accelerated and completed the Struthers-Dunn relay replacements in all CFCU applications. The inspectors noted that if PSEG finalizes a 20 year replacement for non-CFCU applications, considering that all Struthers-Dunn relays were replaced in 1996 to 1997, then all Struthers-Dunn relays would now or in the near term require replacement. PSEG initiated notification 20734280 in response to the inspectors observation for resolution.

.5 Annual Sample: Unexpected Number of Degraded Baffle-Former Bolts Discovered in the Unit 1 Reactor Pressure Vessel a. Inspection Scope The inspectors performed an in-depth review of PSEGs technical evaluation and corrective actions associated with NOTF 20726264 for baffle-former (baffle) bolts found with indications of degradation during the spring 2016 Salem Unit 1 24th refueling outage (1R24). PSEG performed ultrasonic examinations of the baffle bolts in accordance with their procedures in response to recent industry operating experience and 1R24 visual examination results indicating 18 visually damaged baffle bolts. After an unexpected number of degraded baffle bolts were discovered, PSEG staff entered the issue into their corrective action program as NOTF 20727538 and reported the issue to the NRC as Event Notification No. 51902 on May 3, 2016, because the as-found number and location of degraded bolts, which were mainly concentrated in three of the eight baffle assemblies, represented an unanalyzed condition. PSEG staff completed corrective actions to replace 189 of 192 potentially degraded baffle bolts on Unit 1. As documented in Section 1R18, PSEG did not remove and replace three bolts that were potentially degraded due to difficulties encountered during the removal/replacement process.

The baffle bolts help secure vertical plates (also referred to as baffle plates) inside the reactor vessel, which then forms a structure surrounding the reactor fuel assemblies to orient the fuel and to direct coolant flow through the core. A sufficient number of baffle bolts are required to remain intact to secure the baffle plates in place so as to not affect control rod insertion or impede emergency core cooling flow during postulated accident conditions. Bolt heads that separate and are no longer held in place by bolt lock-tabs can also become a loose parts concern.

The inspectors assessed whether PSEG acceptable baffle bolt pattern analysis for Unit 1 was completed in accordance with the NRC-approved methodology and provided appropriate structural margin for the next cycle of operation to ensure the Unit 1 baffle plates will remain in place during both normal operation and limiting postulated accident conditions. The inspectors also assessed whether PSEGs evaluations of the baffle bolts installed in Salem Unit 2 were technically sufficient to conclude the Unit 2 baffle assembly will perform as intended until the next planned refueling outage, at which time PSEG plans to examine the bolts. The inspectors reviewed PSEGs procedures for determining the functionality and operability of degraded systems, components and structures as they relate to Unit 2. Additionally, the inspectors interviewed PSEG engineering personnel and contractor staff to discuss the results of PSEGs technical evaluations and to assess the effectiveness of the implemented and planned corrective actions.

The inspectors assessed PSEGs problem identification threshold, cause analyses, extent of condition, compensatory actions, and the prioritization and timeliness of PSEGs corrective actions to determine whether PSEG staff were properly identifying, characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to PSEGs corrective action program, operability determination process, and the requirements of 10 CFR Part 50, Appendix B. The inspectors observed portions of baffle bolt replacement activities at Unit 1 and reviewed the final visual examination of the baffle bolts and plates once the work was completed.

b. Findings and Observations No findings were identified.

The NRC responded to the initial discovery of an unexpected number of baffle bolts found degraded at Salem Unit 1 by implementing a comprehensive inspection plan consisting of various baseline inspection samples to assess the extent of the issue and to determine the necessary NRC actions. A previously planned ISI sample (Refer to Section 1R08) was expanded to include a review of the capability of the NDE techniques for ultrasonically testing (UT) the baffle bolts, to evaluate the UT results, and to observe a portion of bolt replacement activities on-site. Two permanent modification samples (Refer to Section 1R18) were conducted to review the design change package and evaluations associated with the new, replacement baffle bolts, and to review the PSEG design change package documenting the as-left baffle bolting pattern in Unit 1. NRC resident inspectors reviewed PSEGs foreign material controls and loose parts analysis (Refer to Section 1R20) to address the potential for missing bolt heads and concluded it would not impact safe operation of the plant.

NRC Region I based inspectors, accompanied by an expert from the NRC Office of Nuclear Reactor Regulation, completed this annual problem identification and resolution inspection sample, to verify that PSEGs evaluations and corrective action to replace Unit 1 baffle bolts were completed in accordance with NRC approved methodology to support a conclusion that the Unit 1 baffle assembly meets the plant design basis. The inspectors also reviewed the adequacy of PSEGs technical evaluations completed to determine whether there is a reasonable expectation the Unit 2 baffle assembly will perform as intended during the current operating cycle.

At the completion of this inspection, PSEGs conduct of a RCE to determine the causes of the failure of the baffle bolts in Unit 1 was ongoing. The inspectors determined PSEGs RCE will not be completed until after laboratory tests and analyses, planned for fall 2016, are performed on a sample of the bolts removed from Unit 1. PSEGs technical evaluation discussed the cause of the degraded baffle bolts as primarily due to Irradiation Assisted Stress Corrosion Cracking (IASCC). This determination was based on industry operating experience related to baffle bolt failure in both foreign and domestic plants, is a known degradation mechanism and the operational and physical characteristics of both Salem plants indicate that they are susceptible to this mechanism.

The inspectors reviewed PSEGs technical evaluation and the supporting operating experience related to baffle bolt failures at other plants. IASCC is a cracking mechanism that occurs over a long period of time when susceptible metals are exposed to neutron radiation from the reactor core and stresses as part of normal design and operation.

The inspectors determined PSEG identified the likely cause of the baffle bolt degradation and their plans to complete a RCE when additional metallurgical information was available was appropriate.

Following identification of the degraded baffle bolts on Unit 1, PSEGs immediate corrective action was to analyze the as-found condition and begin replacing bolts that either had visual indications of bolt failure (protruding bolt head for example), did not pass UT examination, or were not accessible for UT examination. The as-found number and pattern of these bolts exceeded the acceptance criteria in the plants analysis that was prepared in advance of the baffle bolt examinations; therefore, PSEG reported this discovery to the NRC as an unanalyzed condition in Event Notification 51902 on May 3, 2016. PSEG staff completed corrective actions to replace 189 of 192 potentially degraded baffle bolts. PSEG did not remove and replace three bolts that were

potentially degraded due to difficulties encountered during the removal/replacement process. As previously documented in Section 1R18, one bolt had an indication during ultrasonic testing but was not visibly damaged. The second bolt was inaccessible for ultrasonic testing, which would have required replacement. The third bolt had successfully passed an ultrasonic test but had a visual indication on one of the lock bar welds which may have indicated a crack in the weld.

The inspectors determined that PSEG staff performed an acceptable bolt pattern analysis that evaluated the replacement bolt pattern for Unit 1. The inspectors found the results of the analysis accounted for a conservative failure rate of bolts and provided appropriate margin for one cycle of operation. The inspectors verified that PSEGs methodology for its acceptable bolt pattern analyses, including its determination of margin, was consistent with the NRC-approved methodology in topical report WCAP-15029-NP-A (ML15222A882). The inspectors determined that PSEG staff tracked corrective actions to re-examine the Unit 1 baffle bolts during the next planned refueling outage. The inspectors noted the new baffle bolts were made of a material (316 SS) with improved resistance to IASCC and included an improved design to reduce the stresses at the head to shank transition, both of which are enhancements compared to the original bolts.

As part of an extent of condition assessment, PSEG entered NOTF 20727590 in its corrective action program to evaluate the potential for degraded baffle bolts on Unit 2.

PSEG operators performed an IOD and concluded that the baffle assembly was operable. PSEG staff performed a subsequent technical evaluation that concluded Unit 2 would experience less baffle bolt degradation than Unit 1 based on several plant factors. The inspectors reviewed PSEGs technical evaluations, including the inputs for the operability determination, and noted that PSEG staff concluded there was not a degraded condition at Unit 2.

As a corrective action, PSEG staff performed operability evaluation (OpEval) 2016-015 and demonstrated that the Unit 2 baffle assembly remained operable. The inspectors concluded that this supplemental evaluation provided adequate technical justification for the continued operation of Unit 2 until the next refueling outage in spring 2017, at which time PSEG plans to examine the baffle bolts. PSEG also implemented compensatory measures to monitor the reactor coolant system for any signs of fuel leakage, which could be an indicator of baffle bolt failures and to generate additional contingency actions in response to indications of increased unidentified leakage or receipt of a metal impact monitoring system alarm.

The inspectors reviewed Westinghouse Nuclear Safety Advisory Letter NSAL-16-1, which discussed the results of recent baffle bolt inspections and provided Westinghouses recommendations on this issue. The letter described the plants as most susceptible (i.e. Tier 1a) to this degradation as Westinghouse 4-loop reactors limited to those with a down-flow configuration and using Type 347 stainless steel. A non-proprietary presentation on the contents of NSAL-16-1 can be found at ML16202A063.

The inspectors noted the recommendation was to complete UT volumetric examination of the baffle bolts at the next scheduled refueling outage, and that PSEG had already planned this action for Unit 2. The inspectors determined PSEGs overall response to the issue was commensurate with the safety significance, was timely, and included appropriate compensatory actions. The inspectors concluded that the actions completed and planned were reasonable to address the ongoing aging management of baffle bolts.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 4 samples)

.1 Plant Events (2 samples)

a. Inspection Scope For the plant events listed below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and compared the event details with criteria contained in IMC 0309, Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive inspection activities. As applicable, the inspectors verified that PSEG made appropriate emergency classification assessments and properly reported the event in accordance with 10 CFR 50.72 and 50.73. The inspectors reviewed PSEGs follow-up actions related to the events to assure that PSEG implemented appropriate corrective actions commensurate with their safety significance.

  • Unit 1, Baffle to former bolts found broken or degraded on May 3 (EN 51902)

b. Findings No findings were identified.

.2 (Closed) LER 05000311/2016-001-000: Auxiliary Feedwater Loop Response Time Exceeded Technical Specifications a. Inspection Scope While evaluating surveillance instrumentation loop time response test data associated with the 21 AFW pump that was collected during the Unit 2 plant shutdown for the fall 2015 refueling outage, PSEG determined that a channel of the pumps ESFAS automatic actuation logic was inoperable. In November 2015, PSEG personnel identified the slow loop response time during surveillance testing. The cause of the slow loop response was due to the isolation valve to the 21 AFW pump discharge pressure transmitter (2PA3450) being closed. The pressure transmitter provided input into the pump run-out protection and flow control circuit. The closed isolation valve caused the pressure transmitter to take longer to sense pump discharge pressure which resulted in slow opening of the pump steam generator flow control valves (valves 23AF21 and 24AF21). PSEGs investigation determined that the condition existed since April 20, 2015, following the completion of maintenance on the pressure transmitter. An engineering review concluded that, although the AFW loop response time test results did not satisfy TS requirements, the accident analysis assumptions remained valid and the condition did not result in an unanalyzed condition. This issue is discussed in more detail in Section 4OA2.1 of this report. No other issues were identified during the review of the LER. This LER is closed.

b. Findings The enforcement aspects of this violation are discussed in Section 4OA7.

.3 (Closed) LER 05000311/2016-002-00: Automatic Reactor Trip Due to Main Turbine Trip a. Inspection Scope On February 4, Salem Unit 2 automatically tripped from approximately 74 percent power.

Power had been reduced at the beginning of dayshift to support a 500 kV transmission line outage. The reactor trip was due to a Main Turbine trip caused by a Main Generator Protection signal initiated by a main generator AVR volts/hertz over excitation protection relay. All emergency core cooling systems and emergency safeguards feature systems functioned as expected. PSEG submitted this LER in accordance with 10 CFR 50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," specifically automatic actuation of the Reactor Protection System and the Auxiliary Feedwater System for this event. The inspectors reviewed the LER, the associated cause evaluation, and interviewed PSEG staff. This LER is closed.

b. Findings Introduction. A Green, self-revealing FIN was identified against MA-AA-716-010, Maintenance Planning Process, Revision 18, when PSEG WOs did not specify the appropriate procedure to perform satisfactory modification testing of the main generator AVR protective relay (model STV1). Consequently, the relay actuated below its design setpoint on February 4, 2016, resulting in an automatic trip of the Unit 2 main turbine and reactor.

Description. On February 4, 2016, Unit 2 experienced an automatic main turbine and reactor trip from approximately 74 percent power, initiated by a trip of the main generator AVR STV 1 relay. The STV1 is designed to protect the main generator, main power transformers, and auxiliary transformer from over-excitation due to over-voltage operation, and consists of an adjustable pickup dial setting between 1.8 and 2.5 voltz/hertz (V/Hz), ranging from 108 - 150 V at 60 Hz. PSEG design calculation ES-7.007, Salem Unit 2 Generator and Transformer Protective Relay Setpoint Determination, Revision 5, established a design setpoint for the STV1 relay of 138 V at 60 Hz, corresponding to a V/Hz dial setting of 2.3, with an associated time delay of 45 seconds. Just prior to the Unit 2 trip on February 4, the main generator was operating at approximately 26.1 kV following a manual MVAR adjustment, which corresponded to 2.175 V/Hz sensed at the STV1. After the Unit 2 trip, PSEG troubleshooting determined the as-found pick-up value of the STV1 was 2.17 V/Hz. The post-trip sequence-of-event data showed the STV1 time delay unit picked up 45 seconds after exceeding 2.17 V/Hz, which tripped the AVR and resulted in a loss of field to the main generator, thereby causing a turbine trip and coincident reactor trip.

In response to the Unit 2 reactor trip, PSEG performed RCE 70183932, Unit 2 Automatic Reactor Trip on Generator Protection, to determine why the STV1 relay actuated below the design setpoint. PSEG identified two root causes: 1) setpoint drift due to a damaged rheostat; and 2) the damaged rheostat was not identified due to an inadequately planned work order that specified a less than adequate post-modification test method. PSEG DCP 80109718, Salem Unit 2 AVR Replacement, supplement 10, documented that a modification test was required for the STV1 relay in accordance with Relay Department test procedures, which subsequently required the use of an engineering-approved Relay Test Order (RTO). However, Maintenance Planning prepared WO 60122561-0014 to perform STV1 modification testing without specifying the applicable test procedures. MA-AA-716-010, step 4.5.7, states If approved

procedure(s) are available which cover all or part of the work scope, then specify in the work package to perform work in accordance with the procedure(s). Additionally, step 3.1.1 states, in part, Maintenance Planners are responsible to interface with: System Engineers for providing supplemental technical direction on a case by case basis as needed; and Maintenance Shops to obtain information needed to produce an adequately detailed work package.

Additionally, the RCE determined that WO 60122561-0014 directed the PSEG LTS department to perform modification testing of the STV1 relay. However, LTS utilized different testing procedures than the Relay department procedures specified in the DCP.

The LTS modification testing performed on October 5, 2015, did not functionally test the STV1 relay at its design setpoint of 138 volts at 60 Hz, which corresponded to a dial setting of 2.3 as discussed above. The RCE determined the manufacturer-specified acceptance testing required verifying the V/Hz pick-up was within one percent of all V/Hz adjustable dial settings, whereas the LTS procedure required the V/Hz pickup at a four percent tolerance on the 2.0 dial setting, or four percent of 120 volts at 60 Hz. The STV1 relay pickup value from the LTS testing on October 5, 2015, fell outside of the one percent tolerance specified by the manufacturer, and LTS did not have a technical basis to support an allowable tolerance of four percent. The RCE determined that returning the relay to the manufacturer-specified setting of one percent would have required adjusting the damaged rheostat to a position where the relay would not have functioned, and therefore would have resulted in a failed acceptance test that would have prevented the relay from being installed in the plant. The inspectors verified that the STV1 RTO specified a one percent tolerance at the design setpoint of 138 volts at 60 Hz.

Analysis. The inspectors determined that a performance deficiency existed because PSEG WOs did not specify the appropriate procedure to perform satisfactory modification testing of the main generator AVR protection relay STV1. This issue was more than minor since it was associated with the procedure quality attribute of the Initiating Events cornerstone and adversely impacted its objective to limit the likelihood of events that upset plant stability (main generator and turbine trip) and challenge critical safety functions. Specifically, due to a work order that was not planned properly, PSEG did not test the STV1 relay at the applicable design setpoint and manufacture-specified tolerance. Consequently, the relay actuated below its design setpoint on February 4, 2016, resulting in an automatic trip of the Unit 2 main turbine and reactor. Using IMC 0609, Attachment 4 and Appendix A, Exhibit 1, the inspectors determined that this finding was of very low safety significance, or Green, since mitigating equipment relied up to transition the plant to stable shutdown remained available.

The finding had a cross-cutting aspect in the area of Human Performance, Work Management, in that the organization implements a work process that includes the need for coordination with different groups or job activities. Specifically, the PSEG process for planning the STV1 relay modification test WO included the need for maintenance planners to coordinate with engineering to provide design setpoint and tolerance specifications, as well as electrical maintenance departments to verify appropriate test procedures were specified in the WO. The inspectors determined that PSEG did not adequately implement the work process in accordance with MA-AA-716-010. [H.5]

Enforcement. MA-AA-716-010, Maintenance Planning Process, Revision 18, step 4.5.7, states If approved procedure(s) are available which cover all or part of the work scope, then specify in the WO to perform work in accordance with the procedure(s). Contrary to the above, PSEG did not specify in the WO to perform work in accordance with approved Relay department test procedures, and the associated RTO, for modification

testing of the STV1 relay on October 5, 2015. Specifically, due to a work order that was not planned properly, PSEG did not test the STV1 relay at the applicable design setpoint and manufacturer-specified tolerance. Consequently, the relay actuated below its design setpoint on February 4, 2016, resulting in an automatic trip of the Unit 2 main turbine and reactor. PSEG entered the issue in CAP as notification 20717849 and performed RCE 70183932. Planned corrective actions included replacing the failed STV1 relay with a properly tested STV1 relay, verifying other STV relays were appropriately tested as an extent of condition, and revising LTS department relay test procedures to ensure all applicable acceptance criteria are incorporated. This finding does not involve enforcement action because no violation of a regulatory requirement was identified. Because this finding does not involve a violation and is of very low safety significance, it is identified as a Finding. (FIN 05000311/2016002-03, Inadequate Work Order Planning Results in Main Generator AVR STV Relay Trip)

4OA5 Other Activities

.1 (Closed) URI 05000272; 311/2015008-01: Inadequate Maintenance Rule System Performance Criteria (PC) Selection a. Inspection Scope In IR 05000272; 311/2015-008, inspectors identified a URI associated with inadequate Maintenance Rule Performance Criteria selection.

During this review the inspectors noted approximately 25 high safety significant systems (HSS) with reliability PC greater than two maintenance preventable functional failures (MPFFs). According to ER-AA-310-1003, Attachment 3, flowchart Process for Selecting Reliability Performance Criteria, HSS SSCs, with reliability PC greater than or equal to two MPFFs require SSC past performance documentation. When the inspectors requested that PSEG provide past performance documentation for the HSS SSCs with reliability PC greater than two MPFFs, PSEG provided documentation of HSS SSC PC approval from 1997, when the MRule Program was first implemented by PSEG. The inspectors determined this documentation did not support the assigned PC, because it did not consider the last 18 years of SSC past performance.

The inspectors also reviewed ER-AA-310-1007, Maintenance Rule - Periodic (a)(3)

Assessment. Step 5.11.1.4 states to determine that the number of MPFFs allowed per evaluation period is consistent with the assumptions in the probabilistic risk assessment (PRA). Contrary to ER-AA-310-1007, step 5.11.4, the last two periodic (a)(3)

assessments performed by PSEG: April 1, 2011, through September 9, 2012; and October 1, 2012 through June 30, 2014; did not verify that the number of MPFFs allowed per evaluation period were consistent with the assumptions in the PRA. Additionally, ER-AA-310-1003, step 4.3.2, states, in part, that unless justified and approved by the Maintenance Rule Expert Panel, the number of MPFFs selected, as a Reliability PC, may not be higher than the PRA-supplied number of functional failures.

The inspectors determined that the failure to meet ER-AA-310-1007, step 5.11.4, and ER-AA-310-1003, step 4.3.2, was a performance deficiency. However, at the time of inspection, as documented in the IR referenced above, the inspectors did not have the information needed to determine whether the performance deficiency was more than minor. The inspectors reviewed PSEGs actions in response to the URI, to determine whether the performance or condition of HSS SSCs was effectively controlled through the performance of appropriate preventive maintenance under 10 CFR 50.65(a)(2), and

also to determine if those HSS SSCs being monitored under 10 CFR 50.65(a)(1) were assigned appropriate goals and monitoring when considered against the appropriate reliability PC threshold.

b. Findings No findings were identified.

PSEG captured the performance deficiency associated with the URI in the CAP under notifications 20694641, 20699573, and 20716722. In response, the PSEG Engineer performed detailed reviews of all the HSS reliability performance criteria against the basic event failure assumptions in the most recent PRA model. For any systems that were identified to have reliability performance criteria deviations from the PRA basic event failure data, performance criteria changes were proposed to more closely align with the PRA. Any proposed changes to system performance criteria were scheduled for review by the Maintenance Rule Expert Panel, including a review of system performance during the last 36 months. The inspectors observed a sampling of the Expert Panel meetings, and reviewed meeting minutes for several others. Upon completion of the PSEG system reviews and expert panel meetings, a total of 12 HSS had reliability performance criteria reductions to more closely align with PRA failure data.

Five of the 12 systems were already being monitored under 10 CFR Part 50.65(a)(1)

prior to the reduction in performance criteria. None of the 12 systems were moved to (a)(1) as a result of the performance criteria reductions. The inspectors sampled the performance criteria adjustments to determine if HSS classified under (a)(2) were being appropriately monitored, and to verify that (a)(1) systems had appropriate goals assigned. No performance deficiencies were identified. The inspectors determined that PSEGs scope of actions restored compliance with ER-AA-310-1007, step 5.11.4, and ER-AA-310-1003, step 4.3.2.

This URI is closed.

.2 License Renewal Commitments Inspection - Phase I Observation of License Renewal Activities (71003 - 1 sample)

a. Inspection Scope License renewal inspections verify the license conditions added as part of the renewed operating license, regulatory commitments, and selected aging management programs, and are implemented in accordance with 10 CFR Part 54, Requirements for the Renewal of Operating Licenses for Nuclear Power Plants. This inspection was completed during 1R24 to observe the implementation of select aging management program activities that are only available for observation during a refueling outage. This inspection is described as Phase 1 in NRC Inspection Manual Procedure 71003, Post-Approval Site Inspection for License Renewal and is intended to be completed during the last refueling outage prior to a nuclear power facility entering the period of extended operation.

As part of this review the inspectors observed the implementation of aging management programs and activities described in the license conditions, and regulatory commitments, as well as any testing or visual inspections of systems, structures, and components which are only accessible at reduced power levels or during a refueling outage.

The inspectors observed the ultrasonic thickness inspection of 1S-FWR-P-21-L1, which is a 6-inch diameter elbow in the Feedwater Recirculation system. The component is part of the No. 12 SG Feed pumps 24-inch discharge header. The inspectors observed the test grid being applied and the recording of measurements in accordance with test procedure OU-AA-335-004 under the flow accelerated program guidance ER-AA-430-1001 as directed by WO 30285966.

The inspectors also observed the preparation for the replacement of a Moisture Separator Reheat Drain system 4-inch diameter piping section. The line is the drain from the No. 11 West Moisture Separator Reheat Main Steam Coil going to the No. 11 West Main Steam Coil Drain Tank. This was the planned replacement of 27 feet of piping with corrosion resistant P22/Chrome Moly material. The work was being performed on the 140 Turbine deck, under WO 60123316.

The inspectors observed the No. 12C Miscellaneous Drains drain manifold replacement spool piece. This 12-inch diameter manifold receives three drain lines from the No. 15A, B, & C Bleed Steam lines and is being replaced with corrosion resistant P22 (Chrome Moly) material. The replacement was in progress and performed under WO 60123347.

After reviewing WO 60120251, the inspectors observed the removal and evaluation of random samples of inaccessible Salem Unit 1 containment liner covered by insulation.

The inspectors observed the containment interior liner insulation being removed, unremediated containment liner sections, and containment liner sections that were cleaned, brushed, and prepared for panel installation. The inspectors reviewed ultrasonic thickness data to verify whether the program was in conformance with American Society of Mechanical Engineers, Boiler and Pressure Vessel Code,Section XI.

b. Findings and Observations No findings were identified.

4OA6 Meetings, Including Exit On July 28, 2016, the inspectors presented the inspection results to Mr. Robert DeNight, Salem Operations Director, and other members of the PSEG staff. On August 11, 2016, an additional exit meeting was conducted and the inspectors presented inspection results specific to the baffle bolt issues in this report to Mr. Eric Carr, Acting Station Vice President. Additionally, the inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by PSEG and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation (NCV).

  • TS LCO 3.3.2.1 requires the ESFAS instrumentation channels and interlocks shown in Table 3.3-3 shall be operable. Table 3.3-3, Function 8, requires two channels of AFW automatic actuation logic to be operable in Modes 1, 2, and 3. With the number of operable channels one less than the required number of channels, TS LCO 3.3.2.1 requires the inoperable channel to be restored to operable status within

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> or, be in at least Hot Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in at least Hot Shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Contrary to TS LCO 3.3.2.1, one less than the required number of channels of AFW automatic actuation logic were operable from April 20, 2015, until Unit 2 entered Mode 4 for a scheduled refueling outage on October 23, 2015. This was due to the 21 AFW pump loop time response being greater than the allowed TS value because the isolation valve for the pressure override defeat pressure transmitter was in the closed position. PSEG entered this issue into the CAP as NOTFs 20709417, 20716352, 20710947, and 20711796.

This performance deficiency was more than minor because it was associated with the human performance attribute of the Mitigating System cornerstone, and adversely affected the cornerstone objective of ensuring the reliability and capability of systems that respond to initiating events to prevent undesirable consequences.

The inspectors evaluated this finding using IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2. The inspectors determined that the finding was of very low safety significance (Green) because the finding did not represent an actual loss of function of at least a single train for greater than its TS allowed outage time.

ATTACHMENT: SUPPLEMENTARY INFORMATION

A-1 SUPPLEMENTARY INFORMATION KEY POINTS OF CONTACT Licensee Personnel J. Perry, Site Vice President E. Carr, Acting Site Vice President J. Barkhamer, PSEG Engineer J. Bergeron, Superintendent of Instrumentation and Controls T. Cachaza, Senior Regulatory Compliance Engineer R. Cary, Environmental Coordinator L. Clark, Instrument Supervisor B. Daly, Nuclear Environmental Affairs, Sustainability D. Denelsbeck, RP Support Supervisor B. Down, PSEG Engineer P. Essner, System Engineer P. Fabian, Salem Steam Generator Engineer T. Giles, Salem ASME Section XI Program Owner F. Grenier, RP Supervisor, Dosimetry M. Hassler, Salem Radiation Protection Manager B. Kerkorian, Salem Steam Generator Supervisor D. Kolasinski, Senior Engineer A. Kraus, Manager, Nuclear Environmental Affairs T. MacEwen, Principal Compliance Engineer J. Mallon, Compliance Director S. Markos, Manager, Design Engineering J. Marooney, MPR Engineering Consultant P. Martitz, Technical Support Superintendent J. Melchionna, Engineering Services R. Moore, System Engineering Branch Manager D. Mora, Salem NDE Program Coordinator G. Morrison, Mechanical Engineer T. Mulholland, Shift Operations Manager A. Ochoa, Senior Compliance Engineer B. Ohmert, System Engineer T. Oliveri, Salem Unit 1 and Unit 2, NDE Manager J. ORourke, Regulatory Affairs J. Owad, Design Engineering M. Phillips, Regulatory Assurance M. Pyle, Chemistry Manager N. Ruvis, Westinghouse B. Sebastian, Manager Fire Protection/Industrial Safety J. Stairs, Manager Plant Engineering C. Wend, Radiation Protection Manager D. Yilgic, Lead Engineer Quality Control Chemistry Attachment

A-2 LIST OF ITEMS OPENED, CLOSED AND DISCUSSED Open 05000272/2016002-01 URI Baffle-Former Bolts with Identified Anomalies (Section 1R08)

Open and Closed 05000311/2016002-03 FIN Inadequate Work Order Planning Results in Main Generator AVR STV Relay Trip (Section 4OA3.3)

Closed 05000272;311/2015-008-01 URI Inadequate Maintenance Rule System Performance Criteria Selection (Section 4OA5)

05000311/2016-001-00 LER Auxiliary Feedwater Loop Response Time Exceeded Technical Specifications (Section 4OA3.1)

05000311/2016-002-00 LER Automatic Reactor Trip Due to Main Turbine Trip (Section 4OA3.3)

A-3 LIST OF DOCUMENTS REVIEWED

  • Indicates NRC-identified Section 1R01: Adverse Weather Protection Procedures SC.OP-SO.500-0001, Trip-A-Unit Scheme Operation, Revision 10 OP-AA-108-107-1001, Electric System Emergency Operations and Electric Systems Operator Interface, Revision 4 Notifications 20731655* 20731657* 20731658* 20731659* 20731662 20731729*

20731735*

Section 1R04: Equipment Alignment Procedures SC.MD-ST.125-0003, Quarterly Inspection and Preventive Maintenance of Units 1, 2, & 3 125 Volt Station Batteries, Revision 30 S1.OP-ST.CAN-0007, Refueling Operations - Containment Closure, Revision 25 S2.OP-SO.SW-0005, Service Water System Operation, Revision 42 S2.OP-SO.ABV-0001, Auxiliary Building Ventilation System Operation, Revision 25 S2.OP-SO.SJ-00001, Preparation of the Safety Injection System for Operation, Revision 19 OP-SA-102-106, Salem Operations Master List of Timed Actions, Revision 0 OP-AA-108-103, Locked Equipment Program, Revision 4 Notifications 20702800 20707221 20724871 20729878* 20732182 20732551 20732785* 20732994* 20733091 Drawings 205337, Sheet 1, No. 2 Unit Auxiliary Building - Ventilation, Revision 43 205242, Sheet 1, No. 2 Unit Service Water Nuclear Area, Revision 81 205242, Sheet 2, No. 2 Unit Service Water Nuclear Area, Revision 76 Maintenance Orders/Work Orders 50180453 50182431 60125981 60129782 Section 1R05: Fire Protection Procedures FP-SA-2542, Pre-Fire Plan Unit 2 Spent Fuel/Component Cooling Heat Exchanger and Pump Area, Revision 0 FP-SA-2552, Pre-Fire Plan Unit 2 Boric Acid Evaporator Unit & Chemistry Area, Revision 0 FP-SA-2651, Pre-Fire Plan Unit 2 Service Water Intake Structure, Revision 0 FP-SA-2555, Pre-Fire Plan Unit 2 Diesel Generator Area, Revision 0 FP-SA-2556, Pre-Fire Plan Unit 2 Inner Piping Penetration Area & Chiller, Revision 0

A-4 Notifications 20723743 20730150* 20732820* 20732836*

Section 1R07: Heat Sink Performance Notifications 20726947 20727041 20727041 Maintenance Orders/Work Orders 30255437 Section 1R08: In-service Inspection NDE Procedures Liquid Penetrant Examination Procedure, OU-AA-335-002, Revision 3 Nondestructive Examination Procedure, Manual Ultrasonic Examination of Vessel Nozzle Inner Radius Regions, Procedure Number 54-ISI-132-011, 1/27/2011 Nondestructive Examination Procedure, Ultrasonic Examination of Austenitic Piping Welds, Procedure Number 54-ISI-836-014, 8/21/2013 Areva NP Inc., Nondestructive Examination Procedure, Multi-Frequency Eddy Current Examination of Tubing, Procedure Number 54-ISI-400-021, 6/12/2013 Notifications 20682192 20694861 20697140 20697577 20697669 20699820 20699859 20699910 20704139 20707057 20707057 20707125 20712181 20712774 20713572 20713573 20713849 20713849 20714082 20716581 20720745 20722494 20724667 20725857 20726340 20726743 Maintenance Orders/Work Orders 60114705 60123261 60126260 Evaluations 70178672 70178814 70178821 70179375 70183001 70185980 Self Assessments Check-In Self-Assessment, Salem INPO PWR Materials Review, 7/30/2015 NDE Records Salem Unit 1, Liquid Penetrant Report No. PT-16-002, 11-RHRHEX Vessel Support, 4/15/16 (Summary No.205170)

Salem Unit 1, Liquid Penetrant Report No. PT-16-001, Pipe Lugs 8-RH-2116-10PL-1 thru 4, 4/15/16 (Summary No. 263631)

Salem Unit 1, Liquid Penetrant Report No. PT-16-004, Pipe to Penetration IA, Component 12 SJ-2152-36PS-4, 4/19/16 (Summary No. 263904)

A-5 Salem Unit 1, Liquid Penetrant Report No. PT-16-003, Inlet Nozzle-to-Pump (11 Charging Pump), Component 6-CV-2111-14R1, 4/15/16 (Summary No. 220757)

Salem Unit 1, Liquid Penetrant Report No. PT-16-005, PIPE TO VALVE (11CS48)

component ID: 8-CS-2114-60, 4/15/16 (Summary No. 356640)

Design Change Package 80092579, Salem Unit 1 - Steam Generator Bowl Drain Repair, SG 11, 12, 13, and 14 (removal of Alloy 600 and associated 82/182 weld material from each SG Channel Head (SGCH)

bowl drain plugs PSEG NUCLEAR VTD NUMBER: 900013(019), Title Stress Analysis of Tube-Tubesheet Weld AREVA RSG, 11/23/15; Calculation Summary Sheet, 7/25/2015.

PSEG Nuclear Work Order 70172201; Areva Reanalysis of Salem Steam Generator tube-to-tubesheet joint as a friction joint and to provide a revised SG stress analysis to PSEG for record purposes WO #60123261, including weld history sheet; Replace SISJ - !SJ248 & 2SJ249 PSEG NUCLEAR LLC VTD NUMBER: AREVA 902739 (001); Salem Unit 1 SG Condition Monitoring for 1R22 AND Final Operational Assessment for Cycles 23 & 24; 8/8/13 Drawings: 02-9124528D, Salem Unit 1 Steam Generator Channel Head Drain Modification, Revision 001 Drawings: 1512E32, Salem REPLACEMENT Steam Generator General Layout; Salem Unit 1 Steam Generator Channel Head Drain Modification, Revision 1 Drawing 02-9124526B, Revision 001, Steam Generator Channel Head Drain Plug Document No.: 51-9207624-000, Salem Unit 1 SG Condition Monitoring for 1R22 and Final Operational Assessment for Cycles 23 & 24 Other Documents NRC Regulatory Issues Summary 2016-02, Design Basis Issues Related To Tube-To-Tubesheet Joints in Pressurized-Water Reactor Steam Generators, March 23, 2016 PSEG NUCLEAR LLC VTD Number: 9000(019); AREVA Stress Analysis of Tube-Tubesheet Weld-AREVA, Vendor Number 32-9235210-001 Section 1R11: Licensed Operator Requalification Program Other Documents SG-1624, Risk Management, SGFP Trip, SGTR, dated 05/21/16 Section 1R12: Maintenance Effectiveness Procedures ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14 Notifications 20689987 20729117* 20730512* 20730513* 20731038* 20732228*

Drawings 265029, Circ Water Swgr Bldg. 125VDC DC Distribution System, Revision 5

A-6 Section 1R13: Maintenance Risk Assessments and Emergent Work Control Procedures OP-AA-108-116, Protected Equipment Program, Revision 12 Notifications 20723781 20724495 20725030* 20725036 20726192 20727564 20727565 20728242 20731749 20733122 Maintenance Orders/Work Orders 60128649 Other Documents ACE 20723873, 11 CFCU Low Speed Breaker Back-Flashed Section 1R15: Operability Determinations and Functionality Assessments Calculations, Analysis, Engineering Evaluations, and Specifications MPR Associates Letter "Salem Service Water Discharge Header - Disposition of Degraded Joints", (0108-0471-0007, Rev 1), 6/3/2016 MPR Associates Letter, Salem PCCP Bell-and-Spigot Joint Degradation-Supplemental Information to (MPR-2650 Revision 0), 10/26/05 MPR Associates Letter, Salem Service Water Discharge Header - Disposition of Degraded Joints (0108-0471-0007, Rev 0), 4/29/2016 MPR Calculation 0108-0333-JEM-01, Structural Evaluation of Service Water Piping Thinned Joints, Revision 0 PSEG VTD 326511-001, "Structural Evaluation of Service Water Piping Thinned Joints" PSEG VTD 326511-002, "Service Water PSEG VTD 326511-003, "Service Water WEKO Seal Structural Repair Relief Request RAI Response Technical Input" PSEG VTD 326511-004, "Request for Use of Mechanical Repair System in Degraded Service Water Pipe Joints - Input for Response to NRG Request for Additional Information dated October 29, 2013" S-C-SW-MEE-1975, Salem Units 1 & 2 Concrete Service Water Pipe Joints - Acceptance Criteria, Revision 0 Drawings, Wiring Diagrams, and Piping and Instrumentation Diagrams 205243, Sheet 1, Auxiliary Building Control Air, Revision 49 0108-0471-0007, Salem Service Water Discharge Header - Disposition of Degraded Joints, 4/29/2016 Evaluations 70097092 70097514 70103845 70131286 70144770 Notifications 20724198 20726264 20727538 20727590 20726001 20726320 20727126 20727354 20727430 20727678 20729040 20730485* 20727242 20727261

A-7 Procedures CC-AA-309-101, Engineering Technical Evaluation, Revision 10 OP-AA-108-115, Operability Determinations & Functionality Assessments, Revision 4 LS-AA-120, Issue Identification and Screening Process, Revision 13 LS-AA-125, Corrective Action Program, Revision 21 NO-AA-10, Quality Assurance Topical Report (QATR), Revision 84 S1.OP-PT.CA-0001, Emergency Control Air Compressor Functional Test, Revision 18 S1.OP-LR.CA-0005, Leak Rate Test 1CA920, Revision 1 SC.OP-LB.DF-0001, Diesel Fuel Oil Testing Program, Revision 3 Maintenance Orders/Work Orders 30265178 50140453 50154389 50154555 50158970 50172136 60115402 Miscellaneous Inspection Manual Chapter 0326, Operability Determinations & Functionality Assessments for Conditions Adverse to Quality or Safety, dated December 3, 2015 Event Notification 51902, Anomalies Identified during Visual Inspection of Reactor Vessel Internals, dated May 3, 2016 70187161, Extent of Condition Review for Salem Unit 2 Susceptibility to Baffle Bolt Failure, Revision 0 70187161, Extent of Condition Review for Salem Unit 2 Susceptibility to Baffle Bolt Failure, Revision 1 OpEval 2016-015, Potentially Degraded Baffle-Former Bolts in Salem Unit 2, Revision 0 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 S2016-156, 50.50 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 S2016-156, 50.50 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 80117136 SUP01, Map of Degraded Bolt Locations, Revision 0 Westinghouse LTR-RIDA-16-125, Rev. 2, Salem Unit 1 Baffle Bolting One Cycle Replacement Pattern Summary Letter, dated May 31, 2016 WCAP-18058-P, Determination of Acceptable Baffle-Former Bolting for Salem Units 1 and 2, Revision 0 ML13093A382, Request for Relief from ASME Code Defect Removal for Service Water Buried Piping, 4/3/2013 ML13227A338, PSEG Response to Request for Additional Information- Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 8/15/13 ML14016A123, PSEG Response to Request for Additional Information (RAI 31 and RAI 32) -

Relief Request SC-14R-1 33, Alternative Repair for Service Water System Piping, 1/8/14 ML14058A228, PSEG Response to Request for Additional Information (RA133 - RAI36)-Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 2/27/14 ML14085A482, PSEG Response to Request for Additional Information (RAJ 37) - Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 3/26/14 ML14097A029, Salem Nuclear Generating Station, Units 1 And 2- Safety Evaluation of Relief Request No. SC-14R-133 for the Alternative Repair for Service Water System Piping (TAC NOS. MF1375 AND MF1376), 4/8/2014

A-8 Modifications 80110461 Other Documents ML13093A382, Request for Relief from ASME Code Defect Removal for Service Water Buried Piping, 4/3/2013 ML13227A338, PSEG Response to Request for Additional Information- Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 8/15/13 ML14016A123, PSEG Response to Request for Additional Information (RAI 31 and RAI 32) -

Relief Request SC-14R-1 33, Alternative Repair for Service Water System Piping, 1/8/14 ML14058A228, PSEG Response to Request for Additional Information (RA133 - RAI36)-Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 2/27/14 ML14085A482, PSEG Response to Request for Additional Information (RAJ 37) - Relief Request SC-14R-133, Alternative Repair for Service Water System Piping, 3/26/14 ML14097A029, Salem Nuclear Generating Station, Units 1 And 2- Safety Evaluation of Relief Request No. SC-14R-133 for the Alternative Repair for Service Water System Piping (TAC NOS. MF1375 AND MF1376), 4/8/2014 Section 1R18: Plant Modifications Condition Reports 20733528 20733526 20726264 20735142 Other Documents 80117136, Design Change Package for Salem Unit 1 Baffle-to-Former Bolt Replacement, Revision 0 80117378, Item Equivalency Evaluation for Replacement Baffle Bolts, dated 6/2/2016 EVAL-16-19, Salem Unit 1 Baffle-Former Bolt Replacement 1R24, Revision 0 LTR-RIAM-16-39, Transmittal of Westinghouse Specification 70041 EB to PSEG, dated 5/4/2016 S2016-156, 50.59 Screening Form for DCP 80117136, Revision 0 WCAP-18144-P, Generic Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for 4-Loop Downflow Plants, Revision 0 Procedures 54-ISI-364-00, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessels, Vessel Internals, and Components in Pressurized Water Reactors, dated August 22, 2000 54-ISI-372-005, Remote Underwater In-Vessel Visual Inspection of Baffle to Former Bolts and Baffle Edge Bolts, dated September 23, 2011 54-UT-108-001, Ultrasonic Inspection of Internal Hex Head Baffle Bolts, dated April 24, 2011 GBRA 104650, Work Instruction Bolt Removal, Revision D GBRA 173122, Repair and Inspection Sequence Plan for Baffle-former Bolt Replacement at NPP Salem, Revision 00

A-9 Miscellaneous 180-9257342-000, NDE Services Final Report, Salem Unit 1, 1R24 Baffle to Former Plate Bolt Inspection Report, dated June 2, 2016 51-9256526-000, Technical Justification for Internal Hex Head E Baffle to Former Bolts Volumetric Examination at Westinghouse 4-Loop Reactors, dated April 25, 2016 IVVI-101, 01RF Examination Summary Record, VT-3 of Upper Core and Support Plate, dated 5/9/2001 Inservice Inspection Results, Bolt ID 5-55-C, dated May 3, 2016 Inservice Inspection Results, Bolt ID 6-75-C, dated April 30, 2016 NDE Personnel Qualification and Certification, VT-1, 2, & 3, Employee 16657, dated March 7, 2016 NDE Personnel Qualification and Certification, VT-1, 2, & 3, Employee 114882, dated March 4.

2015 MRP-228, Materials Reliability Program: Inspection Standard for PWR Internals- 2012 Update, Revision 1 54-UT-108-001, Ultrasonic Inspection of Internal Hex Head Baffle Bolts, Revision 1 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 S2016-156, 50.59 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 S2016-156, 50.59 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 80117136 SUP01, Map of Degraded Bolt Locations, Revision 0 Westinghouse LTR-RIDA-16-125, Rev. 2, Salem Unit 1 Baffle Bolting One Cycle Replacement Pattern Summary Letter, dated May 31, 2016 Westinghouse LTR-RIDA-16-125, Rev. 3, Salem Unit 1 Baffle Bolting One Cycle Replacement Pattern Summary Letter, dated July 11, 2016 WCAP-18058-P, Determination of Acceptable Baffle-Former Bolting for Salem Units 1 and 2, Revision 0 WCAP-18144-P, Generic Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for 4-Loop Downflow Plants, Revision 0 VEN-16-041, Remote Visual Examination: Baffle-former Bolts (Core Side), dated July 27, 2016 Section 1R19: Post-Maintenance Testing Procedures SC.MD-PM.CBV-0002, CFCU Motor Heat Exchanger Internal Inspection, Revision 20 SC.MD-PM.SW-0012, Enecon Tubesheet Cladding System, Revision 13 SC.IC-TI.ZZ-0104, Configuration Control for NUS Model MTH801 Summators, Revision 32 S2.IC-CC.RCP-0058, 2FT-542 #24 Steam Generator Flow Protection Channel I, Revision 42 Notifications 20273570 20670175 20672463 20723478 20723652 20723765 20724185 20724217 20725095 20725111 20726481 20727534 Maintenance Orders/Work Orders 30205173 60120462 60128697 60129161

A-10 Evaluations 70171681 Section 1R20: Refueling and Other Outage Activities Procedures LS-AA-119-1003, Calculating Work Hours, Revision 7 MA-AA-716-008-1010, Reactor Services Project FME Plan, Revision 2 S1.OP-IO.ZZ-0006, Hot Standby to Cold Shutdown, Revision 37 S1.OP-TM.ZZ-0001, Reactor Coolant System Pressure - Temperature Curves, Revision 4 SC.OP-DL.ZZ-0001, Reactor Coolant System Heatup/Cooldown Log, Revision 9 SC.OP-DL.ZZ-00012, Pressurizer Heatup/Cooldown Log, Revision 5 Notifications 20723957 20725589* 20725843 20725856 20725917 20726061*

20726121 20726355 20727113 20727298 20727697 20729566 Other Documents 1R24 Shutdown Safety Evaluation and Approval, dated 03/25/16 Section 1R22: Surveillance Testing Procedures S2.OP-ST.RHR-0001, Inservice Testing - 21 Residual Heat Removal Pump, Revision 29 S2.RA-ST.RHR-0001, Inservice Testing 21 Residual Heat Removal Pump Acceptance Criteria, Revision 12 S1.OP-ST.SSP-0001, Manual Safety Injection - SSPS, Revision 32 Notifications 20725279* 20725282* 20725581 20725603 20725936 20726147 20726148 20726342 20728892* 20728962* 20728963*

Maintenance Orders/Work Orders 50182657 Other Documents Unit 1 Operator logs for April 17 and 18, 2016 Section 1EP6: Drill Evaluation Procedures NC.EP-EP.ZZ-0405, Emergency Termination - Redaction - Recovery, Revision S2.OP-AB.Fuel-0001, Fuel Handling Incident, Revision 5 S2.OP-AB.CW-0001, Circulating Water System Malfunction, Revision 36 S2.OP-AB.CVC-0001, Loss of Charging, Revision 9 Notifications 20733529 20733001

A-11 Other Documents S16-01, Salem All Facilities Training Drill, 06/16/16 Section 2RS1: Access Control to Radiologically Significant Areas Procedures RP-AA-301, Radiological Air Sampling Program, Revision 6 RP-AA-460, Control for High and Very High Radiation Areas, Revision 17 RP-AA-463, High Radiation Area Key Control, Revision 4 RP-AA-401-1001, Special Instruction for Highly Radioactive In-core Components, Revision 0 RP-SA-103, Radiological Control of Reactor Cavity and Spent Fuel Pool Operations, Revision 1 RP-AA-210, Dosimetry Issue, Usage, and Control, Revision 13 RP-AA-401, Operational ALARA Planning and Control, Revision 13 Other Documents Audits Locked High Radiation Key Inventory Logs Radiation Protection Job Guides (7 through 14)

Radiological Survey data (various)

Radiation Protection Plant Radionuclide Evaluation Corrective Action Documents (various Notifications)

Section 2RS2: Occupational ALARA Planning and Controls Procedures RP-AA-401, Operational ALARA Planning and Control, Revision 13 CY-AP-120-1030, Estimating RCS Crud Release for Refueling Outage, Revision 1 S1. CH-IO.ZZ-111(Z), Salem Unit 1 Shutdown Chemistry Plan, Revision 8 Other Documents Refueling Outage Radiological Performance Report ALARA Plans (various)

Radiation Protection Job Guides (7 through 14)

ALARA Work In-process Reviews Outage Chemistry Control Plan 1R24 Hard Gamma Projection Corrective Action Documents (various Notifications)

Section 2RS3: In-plant Airborne Radioactivity Control and Mitigation Procedures RP-SA-103, Radiological Control of Reactor Cavity and Spent Fuel Pool Operations, Revision 1 RP-AA-220, Annual Bioassay Review, Revision 9 RP-AA-301, Radiological Air Sampling Program, Revision 6 RP-AA-401, Operational ALARA Planning and Control, Revision 13 NF-AA-430, Failed Fuel Action Plan, Revision 8

A-12 Other Documents Radiological Source Term Data - 10 CFR 61 waste stream report Airborne Radioactivity Sampling Results (various)

Corrective Action Documents (various Notifications)

Section 2RS4: Occupational Dose Assessment Procedures RP-AA-401, Operational ALARA Planning and Control, Revision 13 Other Documents Radiation Protection Job Guides (7 through 14)

General Source Term Data (various)

Corrective Action Documents (various notifications)

Section 2RS5: Radiation Monitoring Instrumentation Procedures RP-AA-301, Radiological Air Sampling Program, Revision 6 RP-AA-504, Routine Operation of the Radiation Protection Gross Counting facility Other Documents Instrument Source Check and Operability data (various)

Corrective Action Documents (various notifications)

Section 2RS7: Radiological Environmental Monitoring Program Procedures RP-AA-228, 10 CFR 50.75(g0 and 10 CFR 50.72.30(d) Documentation, Revision 3 EN-AA-170-500, Meteorological Monitoring System Calibration and Maintenance (Metrological Tower), Revision 1 EN-AA-170-1000, Radiological Environmental Monitoring Program (REMP) and Meteorological Program (MET) Implementation, Revision 1 EN-AA-1001, REMP Vendor Dosimetry and Laboratory QA Program EN-AA-170-4000, Radiological Ground water Protection program Implementation, Revision 0 EN-AA-170-4160, Station RGPP Controlled sample Points, Revision 0 EN-AA-170-4200, Disposal of Water from Excavation projects, Revision 0 EN-AA0170-4300, Investigative Process for Evaluation of Anomalous Tritium Data from On-site Wells, Revision 1 CY-AA-170-400, Radiological Ground water protection program, Revision 4 AD-LTS-10, Laboratory and Testing Service (LTS) Quality Assurance Program, Revision 4 Instruction NASSV-1.2.2NS, Service of Low Volume Sampler, Revision 19 Instruction MLKSA-1.1.2, Collection of Raw Milk samples, Revision 12 Instruction VGTSA-1.1.7, Collection of Vegetable, Vegetation and Fodder Crops, Revision 8 Instruction 1.1.9, Collection of Potable Water Samples, Revision 3 Instruction TLDSV-1.2.1, Installation of Area Monitoring Dosimeters in the Field, Revision 16 Instruction AQUACOLL-1.1.10, Collection of Aquatic samples, Revision 11 Instruction GMSA -1.1.11, Collection of Game samples, Revision 3 Instruction VEGECEN-0.3.2, Salem/Hope Creek Vegetable Garden Census, Revision 6

A-13 Instruction NRESCEN, Salem/Hope Creek Nearest Resident Census, Revision 5 Instruction MLKCEN 0.3.1, Salem/Hope Creek Census of Milk Animals, Revision 6 Instruction H2OSA-1.1.1, Collection of Water Samples, Revision 13 Instruction SOLSA -1.1.3, Collection of Soil Samples, Revision 8 Instruction ESS-1.1.5, Collection of Sediment Samples, Revision 9 Instruction ESFCH -1.1.6, Pickup of Fish and Crab Samples, Revision 7 Other Documents Salem and Hope Creek Offsite Dose Calculation Manuals (ODCM)

UFSAR Section 11.6, Offsite Radiological Monitoring Program Hope Creek Nuclear Station Buried and Underground Piping Asset Management Plan, Revision 0 Salem and Hope Creek 2015 Annual Effluent Releases Reports NEI-07-07, Structure, System, Component (SCC) Review for Turbine Roof Structure (Hope Creek)

Salem and Hope Creek Annual Radiological Environmental Monitoring Reports Salem/Hope Creek Meteorological Program Status Report (2014, 2015)

Salem/Hope Creek Metrological Tower Updated Vegetation Review, June 3, 2016 Comparison of 2015 Atmospheric Dispersion Factors for Salem and Hope Creek, dated March 28, 2016 Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report, NOSA-SLM-16-04, May 11, 2016 2016 Self-Assessment REMP Program Inspection Teledyne Brown Environmental Service Annual Quality Assurance Report GEL 2015 - Annual Quality Assurance Report (REMP)

Residential Survey, dated December 22, 2015 Milk Animal Survey dated December 2015 Vegetable garden Survey dated August 2015 Calibration Data (Dry Gas Meters 61182898, 14522708, 2424590)

Calibration Data (Laminar Flow Element 16300942)

Global Solutions Annual Testing, dated May 26, 2015 Passive Environmental Dosimetry Calibration data Ground Water Monitoring Data and RGPP Data Salem/Hope Creek Part 61 Analysis Review, dated April 27, 2016 Salem Remedial Action Plan Progress Reports Corrective Action Documents (various Notifications)

Ground Water Monitoring Data Corrective Action Documents (various Notifications)

Section 4OA2: Problem Identification and Resolution Condition Reports 20724198 20726264 20727538 20727590 20728329 20732892 20731786 20725142 20736630 Maintenance Orders/Work Orders 70136205 70140618 70154315 70168067 70168874 70180750 70182469 70182519 70183590 70183629

A-14 Miscellaneous Westinghouse LTR-RIDA-16-125, Rev. 2, Salem Unit 1 Baffle Bolting One Cycle Replacement Pattern Summary Letter, dated May 31, 2016 Westinghouse LTR-RIDA-16-125, Rev. 3, Salem Unit 1 Baffle Bolting One Cycle Replacement Pattern Summary Letter, dated July 11, 2016 WCAP-18058-P, Determination of Acceptable Baffle-Former Bolting for Salem Units 1 and 2, Revision 0 Non-Proprietary Safety Evaluation of WCAP-17096-NP, Revision 2, Reactor Internals Acceptance Criteria Methodology and Data Requirements (TAC No. ME4200). (ADAMS Accession No. ML16061A243), dated May 3, 2016 Westinghouse Calculation Note, CN-RIDA-15-34, Rev. 4, Units 1 and 2 Acceptable Baffle-Former LOCA and Seismic Analysis, dated May 16, 2016 Westinghouse Calculation Note CN-RIDA-15-64, Rev. 2, Salem Units 1 and 2 Acceptable Baffle-Former Bolting Pattern Fuel Grid Impact Analysis, dated May 16, 2016 Event Notification 51902, Anomalies Identified during Visual Inspection of Reactor Vessel Internals, dated May 3, 2016 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 S2016-156, 50.50 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 0 S2016-156, 50.50 Screen: DCP 80117136, Salem Unit 1 Baffle to Former Bolt Replacement, Revision 1 80117136 SUP01, Map of Degraded Bolt Locations, Revision 0 Westinghouse LTR-RIDA-16-112, Rev. 0, Summary of Salem Unit 1 Baffle-Former Bolt Real-time Analysis Results, dated May 11, 2016 WCAP-18058-P, Determination of Acceptable Baffle-Former Bolting for Salem Units 1 and 2, Revision 0 Westinghouse LTR-RIAM-16-38 Rev. 0, Salem Unit 1 Real-Time Analysis Results for LOCA/Seismic Dynamic Analysis and Fuel Grid Impact Analysis, dated May 3, 2016 Westinghouse LTR-RIAM-16-39 Rev. 0, Transmittal of Westinghouse Specification 70041 EB to Public Service Enterprise Group, dated May 4, 2016 Information Notice 98-11, Cracking of Reactor Vessel Internal Baffle-former Bolts in Foreign Plants, dated March 24, 1998 Eval-16-19, Westinghouse Electric Company 10 CFR 50.59 Applicability Determination, Salem Unit 1 Baffle-former Bole Replacement 1R24, Revision 0 MRP-228, Materials Reliability Program: Inspection Standard for PWR Internals - 2012 Update, Revision 1 Unit 1 and 2 Technical Specifications, Revision 28 ACM 16-011, Baffle Plates Monitoring, dated June 17, 2016 ACM 16-011, Baffle Plates Monitoring, dated July 25, 2016 WCAP-15030-NP-A, Westinghouse Methodology for Evaluating the Acceptability of Baffle-Former-Barrel Bolting Distributions Under Faulted Load Conditions, dated January 1999 NRC Safety Evaluation of Topical Report wCAP-25029, Westinghouse Methodology for Evaluating the Acceptability of Baffle-Former-Barrel Bolting Distributions Under Faulted Load Conditions (TAC No. MA1152), dated November 16, 1998 NRC Letter, Leak Before Break Evaluation of Primary Loop Piping, Salem Nuclear Generating Station, Units 1 and 2 (TAC NOS. M85799 and M85800), dated May 25, 1994 51-92566526, Technical Justification for Internal Hex Head E Baffle to Former Bolts Volumetric Examination at Westinghouse 4-Loop Reactors, dated April 28 2016

A-15 54-ISI-364-00, IVVI Inspection Data Sheet Salem 1R14, dated May 8, 2001 Areva Letter, Completion and Status of Octants 1, 2, 3, 4, 5, 6, 7, and 8 (i.e., 1-8), dated May 5, 2016 OTDM 16-005, Salem Unit 2 Baffle to Former Bolting of Reactor Vessel Internals, dated June 16, 2016 WCAP-18144-P, Generic Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for 4-Loop Downflow Plants, Revision 0 Westinghouse LTR-LIS-11-381, LOCA Assessment of Core Coolable Geometry for Grid Deformation in Peripheral Fuel Assemblies, dated June 27, 2011 Event Notification 51902, Anomalies Identified during Visual Inspection of Reactor Vessel Internals, dated May 3, 2016 70187161, Extent of Condition Review for Salem Unit 2 Susceptibility to Baffle Bolt Failure, Revision 0 70187161, Extent of Condition Review for Salem Unit 2 Susceptibility to Baffle Bolt Failure, Revision 0 Op Eval 2016-015, Potentially Degraded Baffle-Former Bolts in Salem Unit 2, Revision 0 VEN-16-041, Remote Visual Examination Baffle-former Bolts (Core Side), dated July 27, 2016 Procedures ER-AA-2003, System Performance Monitoring and Analysis, Revision 10 54-ISI-364-00, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessels, Vessel Internals, and Components in Pressurized Water Reactors, dated August 22, 2000 54-UT-108-001, Ultrasonic Inspection of Internal Hex Head Baffle Bolts, dated April 28, 2016 Notifications 20704666 20706027 20709417 20710340* 20710947 20711723 20711796 20715617 20716352 20716358 20716401 20716402 20716404 20716754 20721375 20726684 20728492* 20730946 20734279* 20734280* 20734281* 20734284* 20734286* 20734856*

Other Documents S2.OP-ST.SSP-0011(Q), Engineered Safety Features Response Time Testing performed October 18, 2015 NRC Event Notification 51663 Exelon PowerLabs Report PSE-65422, 07/01/13 Exelon PowerLabs Report PSE-82817, 11/13/13 Exelon PowerLabs Report PSE-00915, 03/18/14 Exelon PowerLabs Report PSE-19717, 10/22/15 Exelon PowerLabs Report PSE-88030, Draft Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion Notifications 20733919*

A-16 LIST OF ACRONYMS 10 CFR Title 10 of the Code of Federal Regulations AC alternating current ACE apparent cause evaluation ADAMS Agencywide Documents Access and Management System AFW auxiliary feedwater ALARA as low as is reasonably achievable ASME American Society of Mechanical Engineers AVR automatic voltage regulator CAP Corrective Action Program CCE common cause evaluation CFCU containment fan cooling unit CFR Code of Federal Regulations CS containment spray DC direct current DCP design change package EC eddy current ECAC emergency compressed air compressor ECCS Emergency Core Cooling System ECT eddy current testing EDG emergency diesel generator EFPY effective full power years EPD electronic personal dosimeter EPRI Electric Power Research Institute ESFAS engineered safety feature actuation system FIN finding FOSAR foreign object search and retrieval GPI Groundwater Protection Initiative HRA high radiation area HSS high safety significant systems HX heat exchanger IMC Inspection Manual Chapter IOD immediate operability determination IR inspection report ISI In-service inspection IASCC Irradiation Assisted Stress Corrosion Cracking kV kilovolt LCO limiting conditions for operation LER licensee event report LHRA locked high radiation area LLRT local leak rate test LTS Laboratory and Testing Services MPFF maintenance preventable functional failure(s)

MR maintenance rule MRC Management Review Committee NCV non-cited violation NDE nondestructive examination NEI Nuclear Energy Institute

A-17 NOS Nuclear Oversight NOTF notification(s)

NRC Nuclear Regulatory Commission NVLAP National Voluntary Laboratory Accreditation Program ODCM Offsite Dose Calculation Manual PC performance criteria PI performance indicator(s)

PM preventive maintenance PRA probabilistic risk assessment PSEG Public Service Enterprise Group Nuclear LLC QHPI Quick Human Performance Investigation RCE root cause evaluation RCS reactor coolant system REMP Radiological Environmental Monitoring Program RFO refueling outage RG regulatory guide RHR residual heat removal RP radiation protection RTO relay test order RWP radiation work permit(s)

SBO station blackout SDP significance determination process SF spent fuel SG steam generator SI safety injection SOC Station Oversight Committee SSC structure, system, and component SW service water TS technical specification(s)

UFSAR Updated Final Safety Analysis Report URI unresolved item UT ultrasonically testing V/Hz volt/hertz VHRA very high radiation areas WGE work group evaluation WOs work order(s)