IR 05000272/2022001
| ML22124A025 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 05/04/2022 |
| From: | Brice Bickett Division of Operating Reactors |
| To: | Carr E Public Service Enterprise Group |
| Bickett B | |
| References | |
| IR 2022001 | |
| Download: ML22124A025 (10) | |
Text
May 4, 2022
SUBJECT:
SALEM NUCLEAR GENERATING STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000272/2022001 AND 05000311/2022001
Dear Mr. Carr:
On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Salem Nuclear Generating Station, Units 1 and 2. On April 7, 2022, the NRC inspectors discussed the results of this inspection with Mr. Dave Sharbaugh, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Brice A. Bickett, Chief Projects Branch 3 Division of Operating Reactor Safety
Docket Nos. 05000272 and 05000311 License Nos. DPR-70 and DPR-75
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000272 and 05000311
License Numbers:
Report Numbers:
05000272/2022001 and 05000311/2022001
Enterprise Identifier: I-2022-001-0051
Licensee:
Facility:
Salem Nuclear Generating Station, Units 1 and 2
Location:
Hancocks Bridge, NJ
Inspection Dates:
January 1, 2022 to March 31, 2022
Inspectors:
J. Dolecki, Senior Resident Inspector
P. Finney, Senior Project Engineer
M. Hardgrove, Resident Inspector
G. Walbert, Reactor Engineer
Approved By:
Brice A. Bickett, Chief
Projects Branch 3
Division of Operating Reactor Safety
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Salem Nuclear Generating Station,
Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Salem Unit 1 and Unit 2 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2, service water bays 2 and 4 with 25 service water pump out of service for planned maintenance, on January 19, 2022
- (2) Unit 1, 11 chilled water system during 12 chiller replacement, on February 8, 2022
- (3) Unit 1, 1A emergency diesel generator, on February 28, 2022
- (4) Unit 2, 23 turbine driven auxiliary feedwater (AFW) pump room and 22 AFW pump during 21 AFW pump in-service testing, on March 2, 2022
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Unit 1, diesel generator area in pre-fire plan FP-SA-1555, on January 4, 2022
- (2) Unit 1, turbine building elevation 120', pre-fire plan FP-SA-1161, on January 6, 2022
- (3) Unit 2, turbine building elevation 120', pre-fire plan FP-SA-2161, on January 6, 2022
- (4) Unit 1, auxiliary building 84', fire areas 1FA-AB-84B and 1FA-AB-84C, on February 2, 2022
- (5) Unit 1, 64' and 84' switchgear rooms, on February 2, 2022
- (6) Unit 2, auxiliary building 84' and 10 ton CO2 tank room, fire areas 2FA-AB-84B and 2FA-DG-84F, on February 2, 2022
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Units 1 and 2, 13.8 kV cable vaults in switchyard, on March 23, 2022
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed Units 1 and 2 operations personnel during pre-refueling outage and surveillance activities, on March 14 and 16, 2022
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed a Unit 2 simulator evaluation that included charging system leak, degraded turbine lube oil pressure, failure of 500 kV breaker, reactor trip, and small break loss of coolant without recirculation capability, on January 18, 2022
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Unit 2, emergent work on pressurizer power-operated relief valve block valve, 2PR7, following failure to reopen during surveillance testing, on January 25, 2022
- (2) Unit 2, elevated risk during scheduled activities on 21 safety injection and 23 charging systems, on February 1, 2022
- (3) Units 1 and 2, elevated risk during scheduled activity on 500 kV Bus Section 2, on February 9, 2022
- (4) Unit 2, emergent work on pressurizer power-operated relief valve lines following elevated tailpipe temperature during planned 500 kV Bus Section 1 outage, during week of February 14, 2022
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (8 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Unit 1, 22 component cooling water heat exchanger inlet valve (22SW122) flow oscillations following valve modification during refueling outage 2R25, on January 3, 2022 (Notification (NOTF) 20888338)
- (2) Unit 1, 1B emergency diesel generator due to degraded stroke time testing of service water isolation valve, 12SW39, on January 11, 2022 (NOTF 20894475)
- (3) Unit 2, reactor coolant head vents due to part 21 regarding nonconformance of main disc lift misalignment, on January 19, 2022 (NOTF 20844061)
- (4) Unit 2, performance of surveillance for core reactivity balance following 60 effective full power days due to missed surveillance and declaring Technical Specification 4.0.3, on January 19, 2022 (NOTF 20895239)
- (5) Unit 2, pressurizer power-operated relief valve 2PR2 elevated tailpipe temperatures following seat leakage, on February 15, 2022 (NOTF 20897290)
- (6) Unit 2, 22 service water strainer due to high internal clearances, on February 24, 2022 (Operability Engineering Justification (OEJ) 70221624)
- (7) Unit 1, 12 chiller anchorage discrepancy due to stainless steel bolting, on February 28, 2022 (OEJ 70221911)
- (8) Unit 1, 1C emergency diesel generator due to jacket water leakage during testing, on March 28, 2022 (Work Order (WO) 702105821)
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:
- (1) Unit 2, 23 containment fan coil unit pillow block bearing repacking, on January 19-20, 2022 (WO 40047349)
- (2) Unit 2, adjustment to motor control center cabinet connections to repair degraded stroke time of pressurizer motor-operated block valve, 2PR7, on January 26, 2022 (WO 60152902)
- (3) Unit 1, 1B emergency diesel generator service water inlet valve to cooler, 12SW39, repair to degraded stroke time, on March 7, 2022 (WO 60152748)
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:
Surveillance Tests (other) (IP Section 03.01) (2 Samples)
- (1) Unit 1, S1.OP-ST.DG-0002, "1B Diesel Generator Surveillance Test," on January 10, 2022 (WO 50232812, 50231404, 50231410, and 50229673)
- (2) Unit 1, S1.OP-ST.DG-0001(Q), "1A Diesel Generator Surveillance Test," on February 28, 2022 (WO 50232617 and 50230390)
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
- (1) Unit 2, S2.OP-ST.RC-0008, Reactor Coolant System Water Inventory Balance, on March 14, 2022 (NOTF 20898459)
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated the emergency action level notification corresponding to the simulator-scenario conducted at Unit 2, on January 18,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===
- (1) Unit 1, January 1, 2021 - December 31, 2021
- (2) Unit 2, January 1, 2021 - December 31, 2021
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)
- (1) Unit 1, January 1, 2021 - December 31, 2021
- (2) Unit 2, January 1, 2021 - December 31, 2021
BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)
- (1) Unit 1, January 1, 2021 - December 31, 2021
- (2) Unit 2, January 1, 2021 - December 31,
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 7, 2022, the inspectors presented the integrated inspection results to Mr. Dave Sharbaugh, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
Resulting from
Inspection
- 20894017
NRC - pre-fire plan discrepancy
01/06/2022
Work Orders
30355027-0060
1-year preventive maintenance
03/23/2022
71111.11Q Corrective Action
Documents
Resulting from
Inspection
- 20895544
Revision request for TQ-AA-201, Exam Security and
Administration
01/25/2022
Corrective Action
Documents
20897290
PZR Relief Valve Temp Rise
2/14/2022
Corrective Action
Documents
Resulting from
Inspection
- 20897662
Engineering
Evaluations
222064
Elevated Tailpipe Temperature 2PR2
2/14/2022
Corrective Action
Documents
Resulting from
Inspection
- 20898239
Procedure OP-SA-108-115-1001, Operability Assessment and
Equipment Control Program, contains deficiency pertaining to
'operable but degraded'
2/26/2022
Engineering
Evaluations
211325
Assessing safety hazard for 10CFR Part 21 Report, NID#
20007, "Notification of a Defect, Unauthorized Modification of
a Valve Component and Main Disc Lift Misadjustment" for
Target Rock 1 and 2 solenoid operated valve assemblies."
10/25/2021
Work Orders
60150500
Corrective action to replace reactor head vents 2RC40,
2RC41, 2RC42, and 2RC43
Corrective Action
Documents
20898459
Nine consecutive RCS unidentified leakage rates above
quarterly average
03/05/2022
Corrective Action
Documents
Resulting from
20898079
Jacket leak at L4 cylinder
2/28/2022
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Inspection
Procedures
S2.OP-ST.RC-
0008 (Q)
Reactor Coolant System Water Inventory Balance
Revision 46
S2.OP-SO.RC-
0004(Q)
Identifying and Measuring Leakage
Revision 16