ML093000301

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IR 05000445-09-004 & 05000446-09-004 on 06/21/09 - 09/19/09 for Comanche Peak
ML093000301
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 10/27/2009
From: Webb Patricia Walker
NRC/RGN-IV/DRP/RPB-A
To: Flores R
Luminant Generation Co
References
IR-09-004
Download: ML093000301 (50)


See also: IR 05000445/2009004

Text

UNITED STATES

NUC LE AR RE G UL AT O RY C O M M I S S I O N

R E GI ON I V

612 EAST LAMAR BLVD , SU I TE 400

AR LI N GTON , TEXAS 76011-4125

October 27, 2009

Rafael Flores, Senior Vice President

and Chief Nuclear Officer

Luminant Generation Company, LLC

Comanche Peak Steam Electric Station

P.O. Box 1002

Glen Rose, TX 76043

Subject: COMANCHE PEAK STEAM ELECTRIC STATION - NRC INTEGRATED

INSPECTION REPORT 05000445/2009004 AND 05000446/2009004

Dear Mr. Flores:

On September 19, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Comanche Peak Steam Electric Station. The enclosed integrated inspection

report documents the inspection findings, which were discussed on October 1, 2009, with you

and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents six NRC-identified findings of very low safety significance (Green).

These findings were determined to involve violations of NRC requirements. However, because

of the very low safety significance and because they are entered into your corrective action

program, the NRC is treating these findings as noncited violations, consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you contest the noncited violations or the

significance of the noncited violations, you should provide a response within 30 days of the date

of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the

Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd,

Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the

Comanche Peak Steam Electric Station facility. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region IV, and the NRC Resident Inspector at the Comanche Peak Steam

Electric Station. The information you provide will be considered in accordance with Inspection

Manual Chapter 0305.

Luminant Generation Company, LLC -2-

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Wayne C. Walker, Chief

Project Branch A

Division of Reactor Projects

Docket: 50-445: 50-446

License: NPF-87; NPF-89

Enclosure:

NRC Inspection Report 05000445/2009004 and 005000446/2009004

w/Attachment 1: Supplemental Information

w/Attachment 2: Results of the Staffs Review of Manual Actions in the Licensing Basis

cc w/Enclosure:

Mike Blevins, Chief Operating Officer

Luminant Generation Company LLC

Comanche Peak Steam Electric Station

P.O. Box 1002

Glen Rose, TX 76043

Mr. Fred W. Madden, Director

Regulatory Affairs

Luminant Generation Company LLC

P.O. Box 1002

Glen Rose, TX 76043

Timothy P. Matthews, Esq.

Morgan Lewis

1111 Pennsylvania Avenue, NW

Washington, DC 20004

County Judge

P.O. Box 851

Glen Rose, TX 76043

Luminant Generation Company, LLC -3-

Mr. Richard A. Ratliff, Chief

Bureau of Radiation Control

Texas Department of Health

P.O. Box 149347, Mail Code 2835

Austin, TX 78714-9347

Environmental and Natural

Resources Policy Director

Office of the Governor

P.O. Box 12428

Austin, TX 78711-3189

Mr. Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

Austin, TX 78711-3326

Ms. Susan M. Jablonski

Office of Permitting, Remediation

and Registration

Texas Commission on

Environmental Quality

MC-122

P.O. Box 13087

Austin, TX 78711-3087

Anthony Jones

Chief Boiler Inspector

Texas Department of Licensing

and Regulation

Boiler Division

E.O. Thompson State Office Building

P.O. Box 12157

Austin, TX 78711

Chief, Technological Hazards

Branch

FEMA Region VI

800 North Loop 288

Federal Regional Center

Denton, TX 76209

Luminant Generation Company, LLC -4-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (John.Kramer@nrc.gov)

Resident Inspector (Brian.Tindell@nrc.gov)

Senior Project Engineer (Bob.Hagar@nrc.gov)

Branch Chief, DRP/A (Wayne.Walker@nrc.gov)

CP Site Secretary (Sue.Sanner@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

DRS STA (Dale.Powers@nrc.gov)

OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)

ROPreports

File located:R:\_REACTORS\_CPSES\CP 2009004 RP-JGK.doc ML#093000301

SUNSI Rev Compl. ;Yes No ADAMS ;Yes No Reviewer Initials

Publicly Avail ;Yes No Sensitive Yes ; No Sens. Type Initials

SRI:DRP/A RI/DRP/A C:DRS/OB C:DRS/PSB1 C:DRS/PSB2

JKramer BTindell RLantz MShannon GWerner

/RA/ /RA/ /RA/ /RA/ /RA/

10/26/09 10/26/09 10/19/09 10/20/09 10/20/09

C:DRS/EB1 C:DRS/EB2 C:DRP/A C:DRP/A

RLKellar NOKeefe WWalker RHagar

/RA/ /RA/ /RA/ /RA/

10/19/09 10/19/09 10/27/09 10/27/09

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-445, 50-446

License: NPF-87, NPF-89

Report: 05000445/2009004 and 05000446/2009004

Licensee: Luminant Generation Company LLC

Facility: Comanche Peak Steam Electric Station, Units 1 and 2

Location: FM-56, Glen Rose, Texas

Dates: June 21 through September 19, 2009

Inspectors: J. Kramer, Senior Resident Inspector

B. Tindell, Resident Inspector

P. Elkmann, Senior Emergency Preparedness Inspector

R. Hagar, Senior Project Engineer

J. Mateychick, Senior Reactor Inspector

Approved By: Wayne Walker, Chief, Project Branch A

Division of Reactor Projects

-1- Enclosure

SUMMARY OF FINDINGS

IR 05000445/2009004, 05000446/2009004; 06/21/2009 - 09/19/2009; Comanche Peak Steam

Electric Station, Units 1 and 2, Fire Protection, Flood Protection Measures, Plant Modifications,

Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by region based inspectors. Six Green noncited violations were identified.

The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the

significance determination process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a Green noncited violation of License

Condition 2.G for the failure of the licensee to seal a penetration in the Unit 2

train B safety chiller electrical cabinet. As a result, the equipment was vulnerable

to water damage from a fire sprinkler activation during a postulated fire on the

redundant train. The licensee entered the finding into their corrective action

program as Smart Form SMF-2009-001069-00.

The finding was more than minor because it was associated with the protection

against external events attribute of the Mitigating Systems cornerstone and

adversely affected the cornerstone objective, in that, it decreased the reliability of

the redundant safety chiller train in case of fire on the Unit 2 train A safety chiller.

Using NRC Manual Chapter 0609, the inspectors determined that a Phase 3

analysis was required. Based on the senior reactor analyst's significance

determination process Phase 3 analysis, this finding was determined to have

very low safety significance. The finding did not have a crosscutting aspect

because it was not representative of current licensee performance

(Section 1R05).

  • Green. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, for the failure of the licensee to follow the design basis

and seal electrical penetration conduits in the containment spray pump rooms.

As a result, the water from a pipe break in the valve isolation tank rooms would

flow into the conduits in the containment spray pump room and could cause a

train of residual heat removal, safety injection, and containment spray equipment

to become inoperable. The licensee entered the finding into their corrective

action program as Smart Form SMF-2009-000926-00.

The finding was more than minor because it was associated with the design

control attribute of the Mitigating Systems cornerstone and adversely affected the

cornerstone objective to ensure the capability of systems that respond to events.

Using NRC Manual Chapter 0609, the inspectors determined that a Phase 3

analysis was required. Based on the senior reactor analyst's significance

-2- Enclosure

determination process Phase 3 analysis, this finding was determined to have

very low safety significance. The finding did not have a crosscutting aspect

because it was not representative of current licensee performance

(Section 1R06).

  • Green. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a for failure to comply with the work control procedure which

requires that all transient equipment be tracked. Specifically, the licensee placed

a floating dock in the service water intake structure for maintenance activities and

did not track the dock in Maximo, the licensees computer program for tracking

work. As a result, the dock remained in place significantly longer than allowed

without doing an engineering evaluation for the effects, potentially reducing the

reliability of the service water pumps in case of a fire or flood. The licensee

entered the finding into their corrective action program as Smart Form

SMF-2009-001548-00.

The finding was more than minor because it was associated with the protection

against external factors attribute of the Mitigating Systems cornerstone, and

adversely affected the objective, in that, the reliability of the service water system

was reduced in the cases of a fire or the probable maximum flood. The

inspectors determined that because the fire scenario did not reflect the dominant

risk of the finding, the flooding scenario would be used for the significance

determination process. Using NRC Manual Chapter 0609, Attachment 4, Phase

1 - Initial Screening and Characterization of Findings, the finding was

determined to be of very low safety significance because the performance

deficiency did not cause the loss of any safety function. This finding has a

human performance crosscutting aspect associated with resources, in that the

licensee failed to provide adequate training for personnel H.2b] (Section 1R18).

  • Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.d for the failure to maintain adequate written procedures

covering fire protection program implementation. Specifically,

Procedure ABN-803A, Response to a Fire in the Control Room or Cable

Spreading Room, Revision 8, which is used to perform an alternative shutdown

from outside of the control room, failed to assure that the train A charging pump,

relied on for achieving postfire safe shutdown, would not be damaged because of

a loss of suction. During an alternative shutdown, operators must use the train A

charging pump for the reactivity control and reactor coolant makeup functions by

providing borated water from the refueling water storage tank. The licensee

entered the finding into their corrective action program as Smart Form

SMF-2009-004453-00.

Failure to ensure that Procedure ABN-803 contained sufficient instructions to

ensure that the credited train A centrifugal charging pump would be available

following a postulated control room abandonment was a performance deficiency.

This finding was more than minor because it was associated with the protection

against external factors attribute of the Mitigating Systems cornerstone, and

affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to external events (such as fire) to prevent

undesirable consequences. Based on the senior reactor analyst's significance

-3- Enclosure

determination process Phase 3 analysis, this finding was determined to have

very low safety significance. The finding did not have a crosscutting aspect

because it was not representative of current licensee performance

(Section 4OA5.4).

  • Green. The inspectors identified a noncited violation of Unit 1 License

Condition 2.G and Unit 2 License Condition 2.G. Specifically, the licensee failed

to ensure that one train of the equipment required to achieve and maintain safe

hot shutdown conditions remained free from fire damage as specified in the

approved fire protection program. The inspectors identified that the licensee

relied upon local manual actions to mitigate the effects of potential fire damage

rather than provide the physical separation or protection required in the approved

fire protection program. The licensee entered the finding into their corrective

action program as Smart Form SMF-2009-004454-00.

Failure to ensure that one train of the systems required for hot shutdown is free

from fire damage was a performance deficiency. This finding was more than

minor because it was associated with the protection against external factors

attribute of the Mitigating Systems cornerstone, and affected the cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to external events (such as fire) to prevent undesirable consequences.

Based on the senior reactor analyst's significance determination process Phase 3

analysis, this finding was determined to have very low safety significance. The

finding did not have a crosscutting aspect because it was not representative of

current licensee performance (Section 4OA5.5).

  • Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.d for the failure to maintain adequate written procedures

covering fire protection program implementation. Specifically, during operator

walkthroughs, the inspectors identified that Procedure ABN-803A, Response to

a Fire in the Control Room or Cable Spreading Room, Revision 8, used to

perform an alternative shutdown from outside of the control room, had two

examples of critical actions that could not be completed in the time required by

the postfire safe shutdown analysis. The steps to respond to a potential spurious

opening of the train A power-operated relief valve and a potential loss of station

service water cooling to the emergency diesel generator were not completed

within the maximum allowable times specified in the procedure. As a

compensatory measure, the licensee issued night orders to alert operators of

these procedural concerns. The licensee entered the finding into their corrective

action program as Smart Form SMF-2009-004455-00.

Failure to provide adequate procedural guidance to implement the requirements

of the approved fire protection program was a performance deficiency. This

finding was more than minor because it was associated with the protection

against external factors attribute of the Mitigating Systems cornerstone, and

affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to external events (such as fire) to prevent

undesirable consequences. Based on the senior reactor analyst's significance

determination process Phase 3 analysis, this finding was determined to have

very low safety significance. The finding did not have a crosscutting aspect

-4- Enclosure

because it was not representative of current licensee performance

(Section 4OA5.6).

B. Licensee-Identified Violations

None

-5- Enclosure

REPORT DETAILS

Summary of Plant Status

Comanche Peak Steam Electric Station Unit 1 operated at approximately 100 percent power for

the entire reporting period.

Comanche Peak Steam Electric Station Unit 2 operated at approximately 100 percent power for

the entire reporting period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Final Safety Analysis Report for

features intended to mitigate the potential for flooding from external factors. As part of

this evaluation, the inspectors checked that the roofs did not contain obstructions or

obvious loose items that could clog drains in the event of heavy precipitation.

Additionally, the inspectors performed a walkdown of the protected area to identify any

modification to the site that would inhibit site drainage during a probable maximum

precipitation event or allow water ingress past a barrier. The inspectors also reviewed

the abnormal operating procedure for mitigating the design basis flood to ensure it could

be implemented as written.

These activities constitute completion of one external flooding sample as defined in

Inspection Procedure 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

Partial Equipment Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • July 13, 2009, Unit 2, uninterruptible power supply heating, ventilation, and

cooling systems

-6- Enclosure

  • July 16, 2009, Unit 2, diesel generator 2-01 while the turbine driven auxiliary

feeedwater pump was unavailable for maintenance

  • July 29, 2009, Unit 1, diesel generator 1-01 while diesel generator 1-02 was

unavailable for maintenance

  • August 19, 2009, Unit 1, safety injection train B while train A was unavailable for

maintenance

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Final Safety Analysis Report, technical specification requirements,

outstanding work orders, Smart Forms, and the impact of ongoing work activities on

redundant trains of equipment in order to identify conditions that could have rendered

the systems incapable of performing their intended functions. The inspectors also

walked down accessible portions of the systems to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the corrective action program with the appropriate significance

characterization.

These activities constituted completion of four partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns in the following risk-significant plant

areas:

room

  • September 10, 2009, fire area EN, Unit 1 cable spreading room
  • September 10, 2009, fire area EM, Unit 2 cable spreading room
  • September 10, 2009, fire zone AA154, Unit 2, safety chillers

-7- Enclosure

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a plant

transient, or their impact on the plants ability to respond to a security event. Using the

documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use, that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits, and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constituted completion of four quarterly fire-protection inspection

samples as defined in Inspection Procedure 71111.05-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of License Condition

2.G for the failure of the licensee to seal a penetration in the Unit 2 train B safety chiller

electrical cabinet. As a result, the equipment was vulnerable to water damage from a

fire sprinkler activation during a postulated fire on the redundant train.

Description. On February 26, 2009, while performing a walkdown of the Unit 2 safety

chillers, the inspectors discovered an unsealed penetration on the top of a cabinet that

contained electrical equipment for the Unit 2 train B safety chiller. The redundant train A

safety chiller is separated from train B by a partial height wall and a water curtain. The

water curtain consists of a group of fast acting fire sprinklers above the wall. With a

train A safety chiller fire and a water curtain actuation, the water curtain spray would

reach the electrical cabinet for the train B chiller. The cabinet was designed so the spray

would not enter the cabinet and wet electrical equipment.

The inspectors observed sprinkler locations, the location of the unsealed penetration,

and the electrical equipment inside of the cabinet. The inspectors concluded that if a fire

occurred on the train A safety chiller, it was reasonable that water would enter the

cabinet and short control power to the train B safety chiller, which would then render

both safety chillers inoperable.

The inspectors determined, through a review of the licensees basic cause evaluation,

that the unsealed penetration in the cabinet was likely created during construction

because no work history that could have caused the hole could be found. The

inspectors walked down a sample of other electrical enclosures and no other unsealed

cabinet penetrations were found. The inspectors concluded that this performance

deficiency was not representative of current licensee performance.

-8- Enclosure

Analysis. The licensees failure to seal a penetration in equipment was a performance

deficiency, which resulted in redundant equipment that was vulnerable to water damage.

The finding was more than minor because it was associated with the protection against

external events attribute of the Mitigating Systems cornerstone and adversely affected

the cornerstone objective, in that, it decreased the reliability of the Unit 2 train B safety

chiller train in case of fire in the Unit 2 train A safety chiller. The inspectors determined

that NRC Manual Chapter 0609, Appendix F, Fire Protection Significance Determination

Process, was not applicable for assessing the significance of this finding and that a

Phase 3 analysis was required.

A senior reactor analyst performed a bounding Phase 3 significance determination to

evaluate the fire protection finding. First, the analyst identified an approximate

frequency for a chiller fire from the NRC Manual Chapter 0609, Appendix F,

Attachment 4, Fire Ignition Source Mapping Information: Fire Frequency, Counting

Instructions, Applicable Fire Severity Characteristics, and Applicable Manual Fire

Suppression Curves. The analyst selected the most conservative fire initiation

frequency for a chiller component that was listed in the table. The frequency was

6.5 x 10-4/year and was for large electric motors (greater than 100 horsepower). There

were no other significant fire initiation contributors in the room. The analyst used the

Comanche Peak SPAR model, Revision 3.50, dated May 27, 2009, to calculate the

conditional core damage probability for a bounding event that included a fire, plant trip

and failure of both chillers. The analyst used a cutset truncation of 1.0 x 10-13 and

assumed a duration of 1 year. The conditional core damage probability was 5.8 x 10-5.

The approximate bounding delta core damage frequency (CDF), assuming a zero

baseline and giving no credit for fire mitigation or consideration that the alternate chiller

might not fail from sprinkler spray, was a product of the conditional core damage

probability and the fire initiating frequency:

CDF = 6.5 x 10-4 * 5.8 x 10-5 = 3.8 x 10-8

Since the calculated CDF was less than 1 x 10-6, the finding was of very low safety

significance (Green). Since the CDF was less than 1 x 10-7, the analyst determined

that there was not a significant contributor to the large early release frequency.

The inspector determined that no crosscutting component is associated with this finding

because it is not representative of current licensee performance.

Enforcement. The Unit 2 Facility Operating License Condition 2.G. states, Luminant

Generation Company LLC shall implement and maintain in effect all provisions of the

approved fire protection program as described in the Final Safety Analysis Report

through Amendment 87. Comanche Peak Final Safety Analysis Report Section 13.3B,

CPSES Fire Protection Program, Amendment 101, states, CPSES is committed to

meeting the requirements of the Fire Protection Report. Comanche Peak Fire

Protection Report, Revision 25, Deviation 1b (2) states Equipment is provided with

spray shields and penetrations into the equipment are sealed to protect against water

damage due to sprinkler actuation. Contrary to the above, on February 26, 2009, a

Unit 2 train B safety chiller electrical equipment cabinet penetration was not sealed to

protect against water damage due to sprinkler actuation. Since the violation was of very

low safety significance and was documented in the licensees corrective action program

as Smart Form SMF-2009-000714-00, it is being treated as a noncited violation,

-9- Enclosure

consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000446/2009004-01, Failure to Seal Electrical Enclosure.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed selected risk important plant design features to protect the plant

and its safety related equipment from internal flooding events. The inspectors reviewed

flood analysis, design documents, engineering calculations, and the Final Safety

Analysis Report. Specific documents reviewed during this inspection are listed in the

attachment. To verify proper wall penetration seals were in place, on March 15, 2009,

the inspectors walked down the Unit 2 containment spray pump rooms.

These activities constitute completion of one flood protection measures inspection

sample as defined by IP 71111.06-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, for the failure of the licensee to follow the design basis and seal

electrical penetration conduits in the Unit 2 containment spray pump rooms. As a result,

the water from a pipe break in the valve isolation tank rooms would flow into the conduits

in the containment spray pump room and could cause a train of residual heat removal,

safety injection, and containment spray equipment to become inoperable.

Description. On March 15, 2009, the inspectors performed a walkdown of the Unit 2

containment spray pump rooms and did not observe sealant in the electrical

penetrations between the containment spray pump rooms (Rooms 51 and 54) and the

valve isolation tank rooms (Rooms 63 and 65). The inspectors informed the licensee

about the observation and the possible breach of a fire barrier. The licensee inspected

the penetrations and determined that the penetrations were not sealed. The licensee

reviewed the fire protection requirements for the penetrations and determined that the

penetrations went through a wall that was a non-rated fire barrier and there was not a

need to seal the penetrations for fire protection. However, the licensee determined that

the wall penetrations were credited in the building flooding analysis. The licensee

performed a walkdown of the Unit 1 penetrations and found them to be correctly sealed.

The inspectors determined that Design Basis Document DBD-ME-002, Penetration

Seals, Revision 8, establishes the design basis for penetration seals and that

Section 5.1.2 documents that pressure rated barriers are determined by reviewing

Calculation 2-FP-0001, Barrier Functional List. Calculation 2-FP-0001, Attachment 1

provided a listing of the functional barrier requirements of the Unit 2 penetrations and

documented that the penetrations will have a pressure rating of 150 inches of water.

The inspectors determined that the penetrations did not meet the pressure rating

requirement.

The inspectors discussed the missing penetration seals with the licensee and

determined the seals were most likely not sealed during the initial construction

timeframe. The inspectors concluded that this finding was not representative of current

licensee performance.

- 10 - Enclosure

Analysis. The licensees failure to seal the electrical penetrations is a performance

deficiency and, as a result, water from a pipe break in the valve isolation tank rooms

would flow into the conduits in the containment spray pump room and could cause a

train of residual heat removal, safety injection, and containment spray equipment to

become inoperable. The finding was more than minor because the performance

deficiency was associated with the design control attribute of the mitigating systems

cornerstone and adversely affected the cornerstone objective to ensure the capability of

systems that respond to events. Using NRC Inspection Chapter 0609, the inspectors

determined that a Phase 3 analysis was required.

A senior reactor analyst performed a Phase 3 significance determination to evaluate the

flooding concern. First, the analyst identified the approximate frequency for a break of

the affected system piping. Using Comanche Peak Internal Flooding Analysis - Flood

Zone Scenario Frequency Screening, Table 4.1.1-3, dated October 17, 2005, the

analyst determined the estimated break frequency as 1.8 x 10-5/year for each affected

room. The analyst used the Comanche Peak SPAR model, Revision 3.50, dated May

27, 2009, to calculate the conditional core damage probability (CCDP) for a bounding

event that included a failure of the piping, a plant trip and the failure of one train of

residual heat removal coincident with a failure of one train of safety injection. All other

initiating events were set to false. The analyst used a cutset truncation of 1.0 x 10-13 and

assumed an exposure interval of 1 year. The CCDP for that event was 6.4 x 10-7. For a

flood in one room, the approximate delta core damage frequency (CDF) was a product

of the flood frequency and the calculated CCDP: CDF/room = 1.8 x 10-5 * 6.4 x 10-7 =

1.2 x 10-11. Assuming a based CDF of 0.0, the total CDF was calculated as:

CDF/room * 2 rooms = 1.2 x 10-11 * 2 = 2.4 x 10-11

Since the calculated CDF was less than 1 x 10-6, the finding was of very low safety

significance (Green). Since the CDF was less than 1 x 10-7, the analyst determined

that there was not a significant contributor to the large early release frequency.

The inspector determined that no crosscutting component isassociated with this finding

because it is not representative of current licensee performance.

Enforcement. The inspectors determined that 10 CFR Part 50, Appendix B, Criterion III,

requires, in part, that measures shall be established to assure that the design basis for

safety related functions of structures, systems, and components are correctly translated

into specifications, drawings, procedures and instructions. Design Basis Document

DBD-ME-002, Penetration Seals, Revision 8, Section 5.1.2 documents, in part, that

pressure rated barriers are determined by reviewing Calculation 2-FP-0001, Barrier

Functional List. Calculation 2-FP-0001, Attachment 1 provides a listing of the functional

barrier requirements of the Unit 2 penetrations and on page 3 documented that the

containment spray pump room to electrical chase 780 penetration will have a pressure

rating of 150 inches of water. Contrary to the above, the licensee failed to seal the

penetration and provide the appropriate design pressure rating. As a result, a pipe

break and flood in the valve isolation tank room could cause a train of residual heat

removal, safety injection, and containment spray equipment to become inoperable.

Since the violation was of very low safety significance and was documented in the

licensees corrective action program as Smart Form SMF-2009-000926-00, it is being

- 11 - Enclosure

treated as a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NRC 05000446/2009004-02, Failure to Seal Electrical Penetrations.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Quarterly Licensed Operator Requalification Program Inspection

a. Inspection Scope

On August 31, 2009, the inspectors observed a crew of licensed operators in the plants

simulator to verify that operator performance was adequate, evaluators were identifying

and documenting crew performance problems, and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to implement appropriate emergency plan actions and notifications

The inspectors compared the crews performance in these areas to pre-established

operator action expectations and successful critical task completion requirements.

These activities constituted completion of one quarterly licensed operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated the following risk significant systems, components, and

degraded performance issues:

  • Unit 1 flow path for emergency boration
  • Unit 1 diesel generator 1-02

The inspectors reviewed events where ineffective equipment maintenance has resulted

in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures

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  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring

The inspectors verified appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance through

preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the

establishment of appropriate and adequate goals and corrective actions for systems

classified as not having adequate performance, as described in 10 CFR 50.65(a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified that

maintenance effectiveness issues were entered into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constituted completion of two quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and

safety-related equipment listed below to verify that the appropriate risk assessments

were performed prior to removing equipment for work:

  • July 30, 2009, Unit 1, diesel generator 1-02 maintenance and severe

thunderstorm warning

heat removal pump 1-01 concurrent outages

available during testing

driven auxiliary feedwater pump 2-01 inoperability during pump discharge check

valve reverse flow testing

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

- 13 - Enclosure

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These activities constituted completion of four maintenance risk assessments and

emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • SMF-2009-003309-00, Unit 2, safety injection 2-01 voiding
  • SMF-2009-003767-00, Unit 1, diesel generator 1-02 with water identified in the

cylinder head water during engine roll

  • SMF-2009-003927-00, hot flux channel factor relaxed axial offset control
  • SMF-2009-003970-00, Unit 2, offsite power operability during lagging MVAR

testing

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and Final Safety

Analysis Report to the licensees evaluations, to determine whether the components or

systems were operable. Where compensatory measures were required to maintain

operability, the inspectors determined whether the measures in place would function as

intended and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors reviewed a sampling of corrective action documents to verify that the licensee

was identifying and correcting any deficiencies associated with operability evaluations.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constituted completion of four operability evaluation inspection samples

as defined in Inspection Procedure 71111.15-05.

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b. Findings

No findings of significance were identified.

1R18 Plant Modifications (71111.18)

a. Inspection Scope

To verify that the safety functions of important safety systems were not degraded, the

inspectors reviewed the temporary modification that involved placing a floating dock in

the service water intake structure.

The inspectors reviewed the temporary modification and the associated safety

evaluation screening against the system design bases documentation, including the

Final Safety Analysis Report and the technical specifications, and verified that the

modification did not adversely affect the system operability/availability. The inspectors

also verified that the installation and restoration were consistent with the modification

documents and that configuration control was adequate. Additionally, the inspectors

verified that the temporary modification was identified on control room drawings,

appropriate tags were placed on the affected equipment, and licensee personnel

evaluated the combined effects on mitigating systems and the integrity of radiological

barriers.

These activities constitute completion of one sample for temporary plant modifications as

defined in Inspection Procedure 71111.18-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a for failure to comply with the work control procedure which requires

that all transient equipment be tracked. Specifically, the licensee placed a floating dock

in the service water intake structure (SWIS) for maintenance activities and did not track

the dock in Maximo, the licensees computer program for tracking work. As a result, the

licensee left the dock remained in place significantly longer than allowed without

completing an engineering evaluation for the effects, thereby potentially reducing the

reliability of the service water pumps in case of a fire or flood.

Description. The inspectors reviewed the licensees process to control the installation of

a floating dock inside the service water intake structure. The licensee uses Maximo, an

electronic work control process, to ensure that transient equipment is tracked and only

allowed to remain in place for less than 90 days or evaluated as a permanent change.

However, the inspectors noted that the licensee failed to track the floating dock in the

service water intake structure and left the equipment in place for 244 days, before

removing it on April 27, 2008.

The licensee had installed the dock on August 27, 2007, for use as a diving platform to

support pump bay cleaning as preventative maintenance every three years. The

evaluation related to the temporary floating dock, FDA-1999-001657-01-01, states, The

SWIS is a highly sensitive fire area. Because of this sensitivity, and the fact that the

floating deck consists of a very large quantity of combustible plastic, the use of the

floating dock is restricted under the Fire Protection Program. The dock is to be installed

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temporarily for use only during times of need, as discussed above. The Comanche

Peak Fire Protection Report, Revision 25, in Deviation 1a for having all redundant

service water equipment in one fire area, states in part, that, A fire caused by transient

combustibles is mitigated because the area is designated No Storage area. The area

is below the pumps is sensitive because it can affect all four trains of service water.

However, because of the distance to the targets, and because the dock was floating in

water, the inspectors concluded that a fire of the floating dock would have a very low

probability of failing redundant service water equipment.

The inspectors questioned the licensee about potential for the floating dock to damage

equipment in the service water intake structure during a probable maximum flood. The

licensee evaluated the concern and determined that the dock would impact non-safety

equipment and potentially crush it during the flood. The foreign material caused by this

event had a potential for entering all four service water pumps which would affect the

reliability of the pumps in both units. The inspectors concluded that although non-safety

related equipment could be damaged during the flood, there was a very small likelihood

that the foreign material would cause all of the pumps to fail simultaneously.

The licensee conducted a cause evaluation for the performance deficiency and

concluded that the cause was due to planning personnel transferring to a new role

without adequate training. The inspectors reviewed the evaluation and concluded that

the failure to provide adequate training was the most significant contributor to the

performance deficiency.

Analysis. The licensees failure to track the floating dock in the service water intake

structure was a performance deficiency and resulted in transient equipment remaining in

the plant for an extended period of time. As a result, the service water systems

reliability could have been reduced, in that the dock increased the exposure of system

components to flood and fire damage. The finding was more than minor because it was

associated with the protection against external factors attribute of the Mitigating Systems

cornerstone, and adversely affected the objective, in that the reliability of the service

water system could have been reduced in the cases of a fire or the probable maximum

flood. The inspectors determined that because the fire scenario did not reflect the

dominant risk of the finding, the flooding scenario would be used for the significance

determination process. Using NRC Manual Chapter 0609, Attachment 4, Phase 1 -

Initial Screening and Characterization of Findings, the finding was determined to be of

very low safety significance because the performance deficiency did not cause the loss

of any safety function. This finding has a human performance crosscutting aspect

associated with resources because the licensee failed to provide adequate training for

personnel H.2b].

Enforcement. Technical Specification 5.4.1.a requires, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A. Regulatory Guide 1.33, Appendix A, Item 9.e., requires, in part, procedures for the control of maintenance,

repair, replacement, and modification work. Procedure STA-606, Control of

Maintenance and Work Activities, Revision 29, Step 6.1.6 requires, in part, that transient

equipment shall be tracked in Maximo to ensure the requirements of Procedure STA-602

Temporary Modifications and Transient Equipment Placements are satisfied. Contrary

to the above from August 27, 2007 to April 27, 2008, the licensee failed to track the

- 16 - Enclosure

floating dock in Maximo to ensure the transient equipment placement requirements were

satisfied. Since the violation was of very low safety significance and was documented in

the licensees corrective action program as Smart Form SMF-2009-001548-00, it is

being treated as a noncited violation, consistent with Section VI.A.1 of the NRC

Enforcement Policy: NCV 05000445/2009004-03; 05000446/2009004-03, Failure to

Control Transient Equipment.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • July 21, 2009, control room air conditioning unit X-04 testing following oil heater

replacement

  • July 30, 2009, diesel generator 1-02 testing following diesel generator cylinder

head replacement

discharge to steam generator 1-02 flow control valve, diagnostic testing following

valve refurbishment

  • August 19, 2009, safety injection train A testing following maintenance on valve

1-8922A, safety injection pump 1-01 discharge check valve

  • September 1, 2009, safety injection pump 2-02 testing following 6.9 kV breaker

replacement

  • September 2, 2009, diesel generator 2-02 testing following a maintenance

activity to measure crank shaft deflection

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated the activities to ensure the

testing was adequate for the maintenance performed, the acceptance criteria were clear,

and the test ensured equipment operational readiness.

The inspectors evaluated the activities against technical specifications, the Final Safety

Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC

generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with postmaintenance tests to

determine whether the licensee was identifying problems and entering them into the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constituted completion of six postmaintenance testing inspection

samples as defined in Inspection Procedure 71111.19-05.

- 17 - Enclosure

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Final Safety Analysis Report, procedure requirements,

technical specifications, and corrective action documents to ensure that the surveillance

activities listed below demonstrated that the systems, structures, and/or components

tested were capable of performing their intended safety functions:

Pump or Valve Inservice Test

generators check valve testing in accordance with OPT-530B, AFW Check Valve

Reverse Flow Test, Revision 2

Routine Surveillance Testing

  • August 12, 2009, diesel generator 1-01 monthly test in accordance with

Procedure OPT-214A, Diesel Generator Operability Test, Revision 19

  • September 9, 2009, Unit 2, Channel 0548, steam generator narrow range level

channel operational test in accordance with procedure INC-7332B, Analog

Channel Operational Test and Channel Calibration Steam Generator Narrow

Range Level, Loop 4, Protection Set III, Channel 0548, Revision 1

Reactor Coolant System Leakage Detection Surveillance Testing

  • August 3 through 14, 2009, unit 1 reactor coolant leakage calculations performed

in accordance with Procedure OPT-303, Reactor Coolant System Water

Inventory, Revision 13

Containment Isolation Valve Test

  • September 16, 2009, local leak rate test for penetration 2-MIII-0022 performed

on March 31, 2008, in accordance with OPT-825B, Appendix J LLRT for

Penetration 2-MIII-0022, Revision 1

The inspectors either witnessed or reviewed test data to verify that the significant

surveillance test attributes were adequate to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data

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  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Reference setting data

Specific documents reviewed during this inspection are listed in the attachment.

These activities constituted completion of five surveillance testing inspection samples

(one in-service test sample, two routine surveillance testing samples, one reactor

coolant system leakage test, and one containment isolation valve test) as defined in

Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

On August 12, 2009, the inspectors evaluated the conduct of a licensee emergency drill

to identify any weaknesses and deficiencies in classification, notification, and protective

action recommendation development activities. The inspectors observed emergency

response operations in the simulator and technical support center to determine whether

the event classification, notifications, and protective action recommendations were

performed in accordance with procedures. The inspectors also compared any inspector-

observed weakness with those identified by the licensee staff in order to evaluate the

critique and to verify whether the licensee staff was properly identifying weaknesses and

entering them into the corrective action program. As part of the inspection, the

inspectors reviewed the drill package and other documents listed in the attachment.

These activities constituted completion one emergency preparedness drill sample as

defined in Inspection Procedure 71114.06-05.

b. Findings

No findings of significance were identified.

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the second

quarter 2009 performance indicators for any obvious inconsistencies prior to its public

release in accordance with NRC Inspection Manual Chapter 0608, Performance

Indicator Program.

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This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - Emergency ac Power System (MS06)

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Emergency ac Power System performance indicator for Units 1 and 2 for the

period from the third quarter 2008 through the second quarter 2009. To determine the

accuracy of the performance indicator data reported during those periods, the inspectors

used definitions and guidance contained in Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 5. The inspectors

reviewed the licensees operator narrative logs, mitigating systems performance index

derivation reports, issue reports, event reports and NRC integrated inspection reports for

the period of the third quarter 2008 through the second quarter 2009 to validate the

accuracy of the submittals. The inspectors reviewed the mitigating systems performance

index component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable Nuclear Energy Institute guidance. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two mitigating systems performance index

emergency ac power system samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.3 Mitigating Systems Performance Index - High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - High Pressure Injection Systems performance indicator for Units 1 and 2 for the

period from the third quarter 2008 through the second quarter 2009. To determine the

accuracy of the performance indicator data reported during those periods, the inspectors

used definitions and guidance contained in Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 5. The inspectors

reviewed the licensees operator narrative logs, issue reports, mitigating systems

performance index derivation reports, event reports and NRC integrated inspection

reports for the period of the third quarter 2008 through the second quarter 2009 to

validate the accuracy of the submittals. The inspectors reviewed the mitigating systems

performance index component risk coefficient to determine if it had changed by more

- 20 - Enclosure

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable Nuclear Energy Institute guidance. The inspectors also

reviewed the licensees issue report database to determine if any problems had been

identified with the performance indicator data collected or transmitted for this indicator

and none were identified. Specific documents reviewed are described in the attachment

to this report.

These activities constitute completion of two mitigating systems performance index high

pressure injection system samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.4 Mitigating Systems Performance Index - Heat Removal System (MS08)

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Heat Removal System performance indicator for Units 1 and 2 for the period

from the third quarter 2008 through the second quarter 2009. To determine the accuracy

of the performance indicator data reported during those periods, the inspectors used

definitions and guidance contained in Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 5. The inspectors

reviewed the licensees operator narrative logs, issue reports, event reports, mitigating

systems performance index derivation reports, and NRC integrated inspection reports for

the period of the third quarter 2008 through the second quarter 2009 to validate the

accuracy of the submittals. The inspectors reviewed the Mitigating Systems

Performance Index component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable Nuclear Energy Institute guidance. The inspectors also

reviewed the licensees issue report database to determine if any problems had been

identified with the performance indicator data collected or transmitted for this indicator

and none were identified. Specific documents reviewed are described in the attachment

to this report.

These activities constitute completion of two mitigating systems performance index heat

removal system samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

- 21 - Enclosure

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included: the complete and

accurate identification of the problem; the timely correction, commensurate with the

safety significance; the evaluation and disposition of performance issues, generic

implications, common causes, contributing factors, root causes, extent of condition

reviews, and previous occurrences reviews; and the classification, prioritization, focus,

and timeliness of corrective actions. Minor issues entered into the licensees corrective

action program because of the inspectors observations are included in the attached list

of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities, so these reviews and did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

- 22 - Enclosure

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the 6-month period of the

second and third quarter 2009, although some examples expanded beyond those dates

where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and maintenance rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one semi-annual trend inspection sample as

defined in Inspection Procedure 71152-05.

b. Findings

No findings of significance were identified.

.4 Selected Issue Follow-up Inspection

a. Inspection Scope

The inspectors completed a review of the licensees actions with regard to reactivity

management. The inspectors attended a reactivity management team meeting. The

inspectors discussed reactivity management with the program owner and reviewed

corrective action documents associated with reactivity management. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in IP 71152-05.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors performed observations of security force

personnel and activities to ensure that the activities were consistent with the licensees

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

- 23 - Enclosure

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

.2 Temporary Instruction 2515/175, Emergency Response Organization, Drill/Exercise

Performance Indicator, Program Review

a. Inspection Scope

The inspectors performed Temporary Instruction 2515/175, ensured the completeness of

Attachment 1, and forwarded the data to NRC Headquarters.

b. Findings

No findings of significance were identified.

.3 Institute of Nuclear Power Operations Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the Institute of Nuclear Power Operations

plant assessment for the Comanche Peak Steam Electric Station conducted in

June 2008. The inspectors reviewed the report to ensure that issues identified were

consistent with the NRC perspectives of licensee performance and to verify if any

significant issues were identified that required further NRC follow-up.

b. Findings

No findings of significance were identified.

.4 (Closed) Unresolved Item 05000445/2008006-01; 05000446/2008006-01, Inadequate

Postfire Safe Shutdown Procedure

Introduction. The inspectors identified a noncited violation of Technical

Specification 5.4.1.d for the failure to maintain adequate written procedures covering fire

protection program implementation. Specifically, Procedure ABN-803A, Response to a

Fire in the Control Room or Cable Spreading Room, Revision 8, which is used to

perform an alternate shutdown from outside of the control room, failed to assure that the

charging pump relied on for achieving postfire safe shutdown would not be damaged

because of a loss of suction. During an alternate shutdown, operators use the charging

pump for the reactivity control and reactor coolant makeup functions by providing

borated water from the refueling water storage tank.

Description. During normal plant operations, the chemical and volume control system

provides a continuous feed (charging and seal injection) and bleed (letdown and seal

- 24 - Enclosure

leak-off) for the reactor coolant system. Normally one centrifugal charging pump is in

operation.

In the event of fire in the control room or cable spreading room, operators accomplish

inventory makeup using the train A centrifugal charging pump with the refueling water

storage tank as a source of borated water makeup. Procedure ABN-803A included

steps to establish a suction path from the refueling water storage tank to the charging

pumps. However, the inspectors determined that, if the charging pump credited for safe

shutdown was running at the time of the fire, a spurious closure of one of the two

series-connected volume control tank outlet valves prior to opening one of the refueling

water storage tank outlet valves would result in a loss of suction and damage to the

credited charging pump.

Valves 1-LCV-0112D and 1-LCV-0112E, refueling water storage tank to charging pump

suction, are motor-operated valves connected in parallel to the suction of the charging

pumps. Each valve is controlled from a switch on Panel CB-06 in the control room.

Prior to evacuating the control room and establishing control at the remote shutdown

panel, Procedure ABN-803A, Section 2.3, Step 4(g) directed operators to open

Valves 1-LCV-0112D and 1-LCV-0112E. However, these actions are not credited

because they were not approved by the NRC, since the time available to perform actions

prior to evacuating the control room may be very limited. From a review of related wiring

diagrams, the inspectors determined that the occurrence of a single short to ground for

each valve could preclude the success of this step. In addition, Procedure ABN-803A

includes a back-up action outside the control room to ensure Valve 1-LCV-112E is open;

however, the inspectors determined operators did not complete this step for at least

20 minutes during a walk-through of the procedure. The licensee has entered this issue

into their corrective action program as Smart Form SMF-2009-004453-00.

Analysis. The inspectors determined that, in the event of a postulated fire in the control

room or cable spreading room, the train A centrifugal charging pump may fail from lack

of an open suction path. If the train A pump was running at the time of the fire, a

spurious closure of either volume control tank outlet valves, prior to operators opening

one of the refueling water storage tank outlet valves, would result in a loss of suction and

damage to the pump. The inspectors determined that the failure to ensure that

Procedure ABN-803 contained sufficient instructions to ensure that the train A centrifugal

charging pump would be available following a postulated control room abandonment

was a performance deficiency. This deficiency was more than minor because it was

associated with the protection against external factors attribute of the Mitigating Systems

cornerstone, and affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to external events (such as fire) to prevent

undesirable consequences.

The inspectors evaluated the deficiency using NRC Inspection Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process. However, the

deficiency required a Phase 3 evaluation because Manual Chapter 0308, Attachment 3,

Appendix F, Technical Basis for Fire Protection Significance Determination Process for

at Power Operations, states that Manual Chapter 0609, Appendix F, does not include

explicit treatment of fires in the control room.

- 25 - Enclosure

The senior reactor analyst used the fire ignition frequency for the control room (FIFCR)

and the cable spreading room (FIFCSR) listed in the Comanche Peak Steam Electric

Station Individual Plant Examination of External Events for Severe Accident

Vulnerabilities, as the best available information. The analyst multiplied the fire initiation

frequencies by an appropriate severity factor (SF) and a nonsuppression probability. For

the control room, the nonsuppression probability was developed to indicate the chance

that operators failed to extinguish the fire within 20 minutes, assuming 2-minute

detection, leading to abandonment of the control room (NPCRE). For the cable spreading

room, the nonsuppression probability included the probability that the automatic halon

system failed (NPCS-A) and the probability that the fire brigade failed to manually

suppress the fire prior to damage that required abandonment of the control room

(NPCS-M). The resulting control room and cable spreading room evacuation frequencies

(EVAC) were calculated as follows:

Postulated Control Room Fire

EVAC = (FIFCR * SF * NPCRE)

= (1.9 x 10-2/year * 0.1 * 1.3 x 10-2)

= 2.5 x 10-5/year

Postulated Cable Spreading Room Fire

EVAC = (FIFCSR * SF * NPCS-A * NPCS-M)

= (3.2 x 10-3/year * 0.1 * 5.0 x 10-2 * 2.4 x 10-1)

= 3.8 x 10-6/year

The control room has 116 panels for Unit 1 and common equipment, each unit cable

spreading room has 99 electrical panels. The circuitry for the volume control tank valves

are located in 6 different panels in the control room, one which contains cabling for both

valves, and 2 termination cabinets in the cable spreading room. Additionally, at least

one smart short would have to occur in the cabinet to fail the valve closed. The analyst

estimated the probability of this short to be 0.6 using accepted industry values. Finally,

as stated above, the performance deficiency will only impact risk if the train A pump is

operating at the time of the postulated fire. This represents a 0.5 probability that one of

two centrifugal charging pumps is running (PPUMP).

The resulting probability that a control room fire would affect the panels and/or cabinets

of interest (PCR-Affected) is the fraction 5/116 multiplied by the probability of having a single

smart short in the cabinet plus the fraction 1/116 multiplied by the probability of having

one of two smart shorts in the cabinet (3.3 x 10-2). Likewise, the probability that a cable

spreading room fire would affect the panels and/or cabinets of interest (PCSR-Affected) is the

fraction 2/99 multiplied by the probability of having a smart short in the cabinet

or 1.2 x 10-2. The intersections of postulated fires in either fire area that affect either of

the subject valves, while the train A pump is running, and leading to control room

abandonment (intersection) were calculated as follows:

- 26 - Enclosure

Postulated Control Room Fire

intersection = PCR-Affected * PPUMP * EVAC

= 3.3 x 10-2 * 0.5 * 2.5 x 10-5/year

= 4.1 x 10-7/year

Postulated Cable Spreading Room Fire

intersection = PAffected * PPUMP * EVAC

= 1.2 x 10-2 * 0.5 * 3.8 x 10-6/year

= 2.3 x 10-8/year

The analyst determined the delta conditional core damage probability (CCDP) by

subtracting the base case conditional core damage probability for a control room

abandonment (0.1) from the bounding fire damage conditional core damage probability

(1.0) for a value of 0.9. The bounding delta conditional core damage frequencies

(CDF) for a 1-year exposure (EXP), representing the current assessment period, were

calculated by multiplying the frequencies of occurrence by the delta conditional core

damage probability as follows:

Postulated Control Room Fire

CDF = intersection * CCDP * EXP

= 4.1 x 10-7/year * 0.9 * 1 year

= 3.7 x 10-7

Postulated Cable Spreading Room Fire

CDF = intersection * CCDP * EXP

= 2.3 x 10-8/year * 0.9 * 1 year

= 2.1 x 10-8

Because postulated fire ignition frequencies for the control room and the cable spreading

room are independent from each other, the total CDF can be determined by simple

addition of the two probabilities above (3.9 x 10-7).

In accordance with Manual Chapter 0609, Appendix A, Attachment 1, step 2.2.6,

Screen for the Potential Risk Contribution Due to Large Early Release Frequency

(LERF), the finding was screened for its potential risk contribution to the large, early

release frequency because the total CDF was greater than 1 x 10-7. The analyst

evaluated the affect of the finding on the large, early release frequency in accordance

with Inspection Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process. Given that Comanche Peak has a large, dry containment and

that control room abandonment sequences do not include steam generator tube ruptures

or intersystem loss of coolant accidents, the analyst determined that this finding was not

significant with respect to the large-early release frequency. Therefore, the analyst

determined this finding was of very low risk significance (Green).

Enforcement. Technical Specification 5.4.1.d states that written procedures shall be

established, implemented, and maintained covering fire protection program

implementation. Procedure ABN-803A, Revision 8, implements this requirement for fires

- 27 - Enclosure

requiring the control room to be evacuated. Contrary to the above, the licensee failed to

provide adequate procedures for implementing the fire protection program. Specifically,

the procedural guidance for implementing the postfire safe shutdown strategy would fail

to prevent damage to the credited centrifugal charging pump if it was in operation at the

time of a fire requiring an evacuation of the control room.

Since the violation was of very low safety significance and was documented in the

licensees corrective action program as Smart Form SMF-2009-004453-00, it is being

treated as a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NCV 05000445/2009004-04; 00500446/2009004-04, Inadequate Postfire Safe

Shutdown Procedure.

.5 (Closed) Unresolved Item 05000445/2008006-02; 05000446/2008006-02, Unapproved

Local Manual Actions For Hot Shutdown

Introduction. The inspectors identified a Green noncited violation of Unit 1 License

Condition 2.G and Unit 2 License Condition 2.G. Specifically, the licensee failed to

ensure that one train of the equipment required to achieve and maintain safe hot

shutdown conditions remained free from fire damage as specified in the approved fire

protection program. The licensee relied upon local manual actions to mitigate the effects

of potential fire damage rather than provide the physical separation or protection

required in the approved fire protection program.

Description. The inspectors reviewed a sample of three fire areas in Unit 1, which do not

require evacuation of the control room during the shutdown. The inspectors reviewed

the approved fire protection program as defined in License Condition 2.G and

determined that one train of equipment required to achieve and maintain hot shutdown is

required to be free from fire damage. The inspectors noted that the approved fire

protection program allows local manual actions to respond to spurious operations of

other equipment that could impact the safe shutdown but do not directly perform the

required safe shutdown functions.

The inspectors conducted walkdowns with operations personnel of

Procedure ABN-804A, Response To a Fire In The Safeguards Building,

Revision 5, and Procedure ABN-806A, Response To a Fire In The Electrical and

Control Buildings, Revision 5. The inspectors found that the fire protection program, as

implemented, relied on the use of local manual actions to align and control equipment

required to achieve and maintain hot shutdown resulting from potential fire damage

instead of assuring that one train was free from fire damage. This approach expanded

the use of local operator manual actions outside of the control room beyond the

response to spurious operations allowed in the approved fire protection program.

The inspectors concluded that the licensees fire protection program, as implemented,

provided less physical separation and protection from the affects of fire than the

approved program required, and was inherently less reliable than ensuring that one train

of the required systems remained free from fire damage.

An example of this concern was the licensees treatment of air-operated valves in the

charging and auxiliary feedwater systems, which were required to perform the reactor

coolant inventory control and decay heat removal functions, respectively. The licensee

did not designate the instrument air system as a required support system and ensure it

- 28 - Enclosure

would remain free of fire damage, so air may not be available to operate these

air-operated valves. Consistent with this approach, the licensee did not protect the

circuits required to operate these air-operated valves from fire damage. These

air-operated valves are normally controlled from the control room to reach and maintain

hot shutdown. For postfire safe shutdown, the licensee did not assure the ability to

control these valves from the control room by protecting valve control circuits or the air

supply. Instead, the licensee relies on local manual actions outside of the control room

to de-energize the air-operated valves to their failed positions, and in the case of the

turbine-driven auxiliary feedwater pump, to then control the turbine manually. The

licensee also assigns an equipment operator to control flow to the steam generators by

throttling other manual valves as directed by the control room operators via radio to

compensate for the loss of control of the air-operated valves.

The licensee disagreed with the inspectors interpretation of the fire protection program

requirements and believed the current program complies with their license condition.

The licensee submitted the basis for their position in Luminant letter CP-200800962,

TXX-08105, dated July 24, 2008. This issue was discussed with the license and the

Office of Nuclear Reactor Regulation, and the staff has concluded that the NRC did not

approve manual actions in lieu of protection for equipment required for safe shutdown

(refer to Attachment 2 of this report).

Comanche Peak Unit 1 License Condition 2.G states:

Luminant Generation Company LLC shall implement and maintain in effect all

provisions of the approved fire protection program as described in the Final

Safety Analysis Report through Amendment 78 and as approved in the SER

(NUREG-0797) and its supplements through SSER 24.

In Supplemental Safety Evaluation Report 12, the NRC staff documented the review of

the AFire Protection of the Safe Shutdown Capability@ against the guidelines of Standard

Review Plan Section 9.5.1, Position C.5.b. The NRC staff concluded:

AThe applicant's analysis indicates that at least one of the redundant trains

needed for safe shutdown would be free of fire damage by providing separation,

fire barriers, and/or alternative shutdown capability;@

and

AAssociated circuits whose fire-induced spurious operation could affect shutdown

were identified to determine those components whose maloperation could affect

safe shutdown. These spurious operations are terminated by operator actions.

The applicant identified these operator actions and allowed the operator sufficient

time to perform these actions. On the basis of its evaluation, the staff concludes

that these operator actions will terminate spurious operations that could affect

plant shutdown.@ (Emphasis added)

The manual actions discussed related to spurious actuations resulting from damage to

associated circuits. The NRC staff did not discuss or approve any deviations from the

requirements for physical separation or protection specified in the standard review plan

to allow the use of local operator manual actions to operate components necessary to

- 29 - Enclosure

achieve or maintain hot shutdown. The licensee has entered this issue into their

corrective action program as Smart Form SMF-2009-004454-00.

Analysis. Failure to ensure that one train of the systems required for hot shutdown was

free from fire damage was a performance deficiency. The inspectors determined that

this finding was more than minor because it is associated with the protection against

external factors attribute of the Mitigating Systems cornerstone, and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to external events (such as fire) to prevent undesirable consequences.

The inspectors initiated an evaluation of this finding using the significance determination

process in Manual Chapter 0609, Appendix F, Fire Protection Significance

Determination Process, because it affected fire protection defense-in-depth strategies

involving postfire safe shutdown systems. Additional information was required from the

licensee concerning the scope of components identified as requiring manual actions, the

fire areas where the manual actions were required and the routing of the cables of

interest within those fire areas for Unit 1. Thirty-three components required to achieve

and maintain hot shutdown were identified for further evaluation. Plant walkdowns were

performed in 12 fire areas to identify fire scenarios that could potentially damage the

cables of interest for these 33 valves credited for establishing and maintaining hot

shutdown.

Using the methodology in Manual Chapter 0609, Appendix F, the plant walkdown results

identified seven fire scenarios in three fire areas with the potential to damage cables for

eleven valves required to establish and maintain hot shutdown. Since the issue involved

multiple fire areas, a modified Phase 2 analysis was developed to access the risk due to

the seven fire scenarios. The analysis was reviewed by a senior reactor analyst, who

confirmed the issue resulted in a total delta core damage frequency of 3.7 x 10-7 and that

the issue had very low safety significance.

Enforcement. The Unit 1 License Condition 2.G states, Luminant Generation Company

LLC shall implement and maintain in effect all provisions of the approved fire protection

program as described in the Final Safety Analysis Report through Amendment 78 and as

approved in the SER (NUREG-0797) and its supplements through SSER 24. In

Supplemental Safety Evaluation Report 12, the NRC staff concluded from review of the

AFire Protection of the Safe Shutdown Capability@ against the guidelines of Standard

Review Plan Section 9.5.1, Position C.5.b, AThe applicant's analysis indicates that at

least one of the redundant trains needed for safe shutdown would be free of fire damage

by providing separation, fire barriers, and/or alternative shutdown capability.

Contrary to the above, the licensee failed to properly implement the approved fire

protection program. Specifically, the licensee did not assure that one train of equipment

required to achieve and maintain safe hot shutdown conditions remained free from fire

damage. The fire protection program, as implemented, relied on the use of local

operator manual actions to operate components required to achieve and maintain safe

hot shutdown conditions resulting from potential fire damage thus providing less physical

separation and protection from the affects of fire than required by the approved fire

protection program.

- 30 - Enclosure

Since the violation was of very low safety significance and was documented in the

licensees corrective action program as Smart Form SMF-2009-004454-00, it is being

treated as a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NCV 05000445/2009004-05; 00500446/2009004-05, Failure to Assure that One

Train of Equipment is Free From Fire Damage.

.6 (Closed) Unresolved Item 05000445/2008006-03; 05000446/2008006-03, Inadequate

Alternative Shutdown Procedure

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.d for the failure to maintain adequate written procedures covering fire

protection program implementation. Specifically, Procedure ABN-803A, Response to a

Fire in the Control Room or Cable Spreading Room, that is used to perform an alternate

shutdown, had two examples of critical actions that could not be completed in the time

required by the postfire safe shutdown analysis. The licensee documented this

deficiency in Smart Form SMF-2009-004455.

Description. Technical Specification 5.4.1.d states that written procedures shall be

established, implemented, and maintained covering fire protection program

implementation. Alternate shutdown at the Comanche Peak Steam Electric Station

requires operators to safely shutdown the plant in accordance with Procedure ABN-803A

for Unit 1 for fire in the control room or cable spreading room requiring evacuation of the

control room.

The inspectors performed a walkthrough of Procedure ABN-803A for a simulated fire in

either the control room or cable spreading room that required operators to shutdown the

plant using manual actions and controls at the remote shutdown panel.

Procedure ABN-803A, Attachment 13 specified the maximum allowable times to

complete certain actions. The inspectors noted during the timed walkthrough by

operators that the following actions could not be performed within the required times.

Example 1 - Spurious Opening of the Train A Power-Operated Relief Valve

A fire in either the control room or cable spreading room could result in a

power-operated relief valve spuriously opening. To close the trains A and B

power-operated relief valves, a relief reactor operator would, in accordance with

Procedure ABN-803A, Attachment 2, transfer control of the power-operated relief valves

from the control room to the remote shutdown panel. When this is accomplished, the fire

induced hot short would be isolated and the power-operated relief valve would return to

its closed position. According to Attachment 13 of Procedure ABN-803A, operators must

complete this action within 5 minutes to avoid empting the pressurizer.

Procedure ABN-803A, Attachment 2, step D instructed the relief reactor operator to

transfer control of 46 switches at the transfer panel from the control room to the remote

shutdown panel. The inspectors timed the completion of all 46 transfer switches to be 7

minutes and 24 seconds. The inspectors estimated that the transfer of the train A

power-operated relief valve would occur at approximately 6 minutes. Attachment 2,

step C, stated that the transfer of the 46 switches cannot be started until communication

has been established with the reactor operator at the remote shutdown panel.

- 31 - Enclosure

The inspectors determined from the walkthrough that the reactor operator performing

Attachment 1 would not reach the remote shutdown panel until 4 minutes and

26 seconds after the reactor was tripped. Thus, the relief reactor operator could not

procedurally start the transfer switch process until 4 minutes and 26 seconds, which

delayed these actions. The inspectors estimated that the train A power-operated relief

valve would not be closed until 10 minutes and 26 seconds after the reactor trip, which

exceeded the 5 minute requirement in Procedure ABN-803A.

Example 2 - Loss of Station Service Water Cooling to the Emergency Diesel Generators

A fire in either the control room or cable spreading room could result in a loss-of-offsite

power with the subsequent automatic start of both emergency diesel generators. In

addition, the fire could also cause damage to the circuits of the station service water

system resulting in the loss of cooling to the emergency diesel generators.

Procedure ABN-803A, Attachment 1, step F, instructs the reactor operator to initiate

station service water at the remote shutdown panel if it is not operating. The inspectors

timed the completion of this step at 12 minutes and 7 seconds. Attachment 13 states

that station service water must be initiated within 7 minutes.

In Procedure ABN-803A, Attachment 2, step F, the relief reactor operator transfers the

train A emergency diesel generator controls to LOCAL. If the emergency diesel

generator had undergone an emergency start from standby, the automatic high

temperature trip would be bypassed. The relief reactor operator should recognize at this

step that station service water cooling was not available and shut down the running

emergency diesel generator at 9 minutes and 45 seconds.

The licensee provided the inspectors Evaluation 2003-000404-01-00, which analyzed

the effects of the loss of station service water cooling on emergency diesel water jacket

water temperature. The analysis determined that during the summer, if the emergency

diesel generator emergency starts from standby with a load of 6.3 MW, the time to

failure of the emergency diesel generator would be 4 minutes and 4 seconds. The time

to failure without cooling water under the expected load during postfire safe shutdown

has not been specifically analyzed.

Fire damage resulting in the automatic starting of the credited emergency diesel

generator without starting the required station service water cooling could result in the

loss of the electrical power supply credited for postfire safe shutdown since the

procedure removes offsite power.

Analysis. The inspectors and a senior reactor analyst evaluated each example of the

violation as described below.

Example 1 - Spurious Opening of the Train A Power-Operated Relief Valve

In the event of a postulated fire in the control room or cable spreading room, a

pressurizer power-operated relief valve may spuriously open from fire damage.

Inspectors determined that, by following Attachment 2 of Procedure ABN-803A,

operators would not be able to close the open valve in a timely manner. This could

result in the emptying of the pressurizer before level control could be established

following a postulated control room abandonment. Failure to provide adequate

- 32 - Enclosure

procedural guidance to implement the requirements of the approved fire protection

program was a performance deficiency. The inspectors determined that this deficiency

was more than minor because it is associated with the protection against external factors

attribute of the Mitigating Systems cornerstone and could affect the availability, reliability,

and capability of systems that respond to external events (such as fire) to prevent

undesirable consequences.

The inspectors evaluated the deficiency using NRC Inspection Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process. However, the

deficiency required a Phase 3 evaluation because Manual Chapter 0308, Attachment 3,

Appendix F, Technical Basis for Fire Protection Significance Determination Process for

at Power Operations, states that Manual Chapter 0609, Appendix F, does not include

explicit treatment of fires in the control room.

As documented in Section 4OA5.4 of this inspection report, the analyst determined that

the control room abandonment frequencies were 2.5 x 10-5/year for postulated control

room fires and 3.8 x 10-6/year for postulated cable spreading room fires.

The controls and cabling for the power-operated relief valve are located in three different

panels in the control room, one which contains cabling for both valves, and two

termination cabinets in the cable spreading room. Additionally, at least one smart short

would have to occur in the cabinet to fail a single valve open. The analyst estimated the

conditional probability of this short to be 0.6 using accepted industry values.

The resulting probability that a control room fire would affect the panels and/or cabinets

of interest (PCR-Affected) is the fraction 2/116 multiplied by the probability of having a single

smart short in the cabinet plus the fraction 1/116 multiplied by the probability of having

one of two smart shorts in the cabinet (1.8 x 10-2). Likewise, the probability that a cable

spreading room fire would affect the panels and/or cabinets of interest (PCSR-Affected) is the

fraction 2/99 multiplied by the probability of having a smart short in the cabinet

or 1.2 x 10-2. The intersections of postulated fires in either fire area that affect either of

the subject valves leading to control room abandonment (intersection) were calculated as

follows:

Postulated Control Room Fire

intersection = PCR-Affected * EVAC

= 1.8 x 10-2 * 2.5 x 10-5/year

= 4.3 x 10-7/year

Postulated Cable Spreading Room Fire

intersection = PCSR-Affected * EVAC

= 1.2 x 10-2 * 3.8 x 10-6/year

= 4.7 x 10-8/year

As documented in Section 4OA5.4 of this inspection report, the analyst determined that

the bounding delta conditional core damage probability for control room abandonment

scenarios was 0.9. Therefore, the bounding CDFs for an exposure period of 1 year

were calculated as follows:

- 33 - Enclosure

Postulated Control Room Fire

CDF = intersection * CCDP * EXP

= 4.3 x 10-7/year * 0.9 * 1 year

= 3.9 x 10-7

Postulated Cable Spreading Room Fire

CDF = intersection * CCDP * EXP

= 4.7 x 10-8/year * 0.9 * 1 year

= 4.2 x 10-8

Because postulated fire ignition frequencies for the control room and the cable spreading

room are independent from each other, the total CDF can be determined by simple

addition of the two probabilities above (4.3 x 10-7). As documented in Section 4OA5.4,

the analyst determined that this finding was not significant with respect to the large-early

release frequency. Therefore, the analyst determined that this finding was of very low

risk significance (Green).

Example 2 - Loss of Station Service Water Cooling to the Emergency Diesel Generators

In the event of a postulated fire in the control room or cable spreading room, an

automatic start of the train A emergency diesel generator could occur coincident with a

fire-induced failure to provide cooling to the diesel via the station service water system.

The inspectors determined that, by following Procedure ABN-803A, Attachment 1,

operators would not be able to initiate station service water cooling in a timely manner.

This could result in the failure of the electrical power supply credited following a

postulated control room abandonment, namely the train A emergency diesel generator.

Failure to provide adequate procedural guidance to implement the requirements of the

approved fire protection program was a performance deficiency. The inspectors

determined that this deficiency was more than minor because it is associated with the

protection against external factors attribute of the Mitigating Systems cornerstone and

could affect the availability, reliability, and capability of systems that respond to external

events (such as fire) to prevent undesirable consequences.

The inspectors evaluated the deficiency using NRC Inspection Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process. However, the

deficiency required a Phase 3 evaluation because Manual Chapter 0308, Attachment 3,

Appendix F, Technical Basis for Fire Protection Significance Determination Process for

at Power Operations, states that Manual Chapter 0609, Appendix F, does not include

explicit treatment of fires in the control room.

As documented in Section 4OA5.4 of this inspection report, the analyst determined that

the control room abandonment frequencies were 2.5 x 10-5/year for postulated control

room fires and 3.8 x 10-6/year for postulated cable spreading room fires.

The controls and cabling for the power-operated relief are located in three different

panels in the control room, one which contains cabling for both valves, and two

termination cabinets in the cable spreading room. Additionally, at least one smart short

would have to occur in the cabinet to fail a single valve open. The analyst estimated the

conditional probability of this short to be 0.6 using accepted industry values.

- 34 - Enclosure

The resulting probability that a control room fire would affect the panels and/or cabinets

of interest (PCR-Affected) is the fraction 2/116 multiplied by the probability of having a single

smart short in the cabinet plus the fraction 1/116 multiplied by the probability of having

one of two smart shorts in the cabinet (1.8 x 10-2). Likewise, the probability that a cable

spreading room fire would affect the panels and/or cabinets of interest (PCSR-Affected) is the

fraction 2/99 multiplied by the probability of having a smart short in the cabinet

or 1.2 x 10-2. The intersections of postulated fires in either fire area that affect either of

the subject valves leading to control room abandonment (intersection) were calculated as

follows:

Postulated Control Room Fire

intersection = PCR-Affected * EVAC

= 1.8 x 10-2 * 2.5 x 10-5/year

= 4.3 x 10-7/year

Postulated Cable Spreading Room Fire

intersection = PCSR-Affected * EVAC

= 1.2 x 10-2 * 3.8 x 10-6/year

= 4.7 x 10-8/year

As documented in Section 4OA5.4 of this inspection report, the analyst determined that

the bounding delta conditional core damage probability for control room abandonment

scenarios was 0.9. Therefore, the bounding CDFs for an exposure period of 1 year

were calculated as follows:

Postulated Control Room Fire

CDF = intersection * CCDP * EXP

= 4.3 x 10-7/year * 0.9 * 1 year

= 3.9 x 10-7

Postulated Cable Spreading Room Fire

CDF = intersection * CCDP * EXP

= 4.7 x 10-8/year * 0.9 * 1 year

= 4.2 x 10-8

Because postulated fire ignition frequencies for the control room and the cable spreading

room are independent from each other, the total CDF can be determined by simple

addition of the two probabilities above (4.3 x 10-7). As documented in Section 4OA5.4,

the analyst determined that this finding was not significant with respect to the large-early

release frequency. Therefore, the analyst determined that this finding was of very low

risk significance (Green).

As a compensatory measure, the licensee issued night orders to alert operators of these

procedural concerns and has entered these issues into their corrective action program

as Smart Form SMF-2009-004455-00.

- 35 - Enclosure

Enforcement. Technical Specification 5.4.1.d states that written procedures shall be

established, implemented, and maintained covering fire protection program

implementation. Procedure ABN-803A, Revision 8 implemented the requirements for

fires when the control room must be evacuated. The maximum times for operators to

align the systems used for hot shutdown and to respond to spurious actuations because

of fire damage were listed in Engineering Report ENR-2005-000316-01-00,

Thermal/Hydraulic Analysis of the Fire Safe Shutdown Scenario, Revision 0.

Contrary to the above, the licensee failed to provide adequate procedural guidance for

implementing their fire protection program. Specifically, for postfire safe shutdown

operations the license provided inadequate procedural guidance for the timely

(1) closure of a spuriously open power-operated relief valve and (2) securing the

emergency diesel generator without service water cooling available to prevent potential

damage. This finding could impact the ability to control reactor coolant system inventory

and pressure and assure an electrical power supply to support the safe shutdown

operations.

Since the violation was of very low safety significance and was documented in the

licensees corrective action program as Smart Form SMF-2009-004455-00, it is being

treated as a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NCV 05000445/2009004-06; 00500446/2009004-06, Inadequate Alternative

Shutdown Procedure.

4OA6 Meetings

Exit Meeting Summary

On August 18, 2009, the inspector presented the results of the fire protection triennial

inspection unresolved items closeout to Mr. M. Lucas, Site Vice President, and other

members of the licensee staff. The licensee acknowledged the information presented.

On October 1, 2009, the inspectors presented the resident inspection results to

Mr. R. Flores, Senior Vice President and Chief Nuclear Officer, and other members of

the licensee staff. The licensee acknowledged the issues presented. The inspectors

acknowledged review of proprietary material during the inspection. No proprietary

information has been included in the report.

- 36 - Enclosure

ATTACHMENT 1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Flores, Senior Vice President and Chief Nuclear Officer

M. Lucas, Site Vice President

S. Bradley, Manager, Radiation Protection

D. Fuller, Manager, Emergency Preparedness

T. Hope, Manager, Nuclear Licensing

D. Kross, Plant Manager

F. Madden, Director, Oversight and Regulatory Affairs

B. Mays, Director, Site Engineering

B. Patrick, Director, Maintenance

M. Pearson, Director, Performance Improvement

S. Sewell, Director, Operations

K. Tate, Manager, Security

D. Wilder, Manager, Plant Support

NRC Personnel

J. Kramer, Senior Resident Inspector

B. Tindell, Resident Inspector

LIST OF ITEMS OPENED AND CLOSED

Opened and Closed

05000446/2009004-01 NCV Failure to Seal Electrical Enclosure (Section 1R05)05000446/2009004-02 NCV Failure to Seal Electrical Penetrations (Section 1R06)05000445/2009004-03

NCV Failure to Control Transient Equipment (Section 1R18)05000446/2009004-03

05000445/2009004-04 Inadequate Postfire Safe Shutdown Procedure

NCV 05000446/2009004-04 (Section 4OA5.4)05000445/2009004-05 Failure to Assure That One Train of Equipment Is Free

NCV 05000446/2009004-05 From Fire Damage (Section 4OA5.5)05000445/2009004-06 NCV Inadequate Alternative Shutdown Procedure

A1-1 Attachment 1

Opened and Closed

05000446/2009004-06 (Section 4OA5.6)

Closed

05000445/2008006-01

URI Inadequate Postfire Safe Shutdown Procedure

05000446/2008006-01

05000445/2008006-02

URI Unapproved Local Manual Actions For Hot Shutdown

05000446/2008006-02

05000445/2008006-04

URI Inadequate Alternative Shutdown Procedure

05000446/2008006-04

LIST OF DOCUMENTS REVIEWED

Section 1RO5: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

ABN-901 Fire Protection System Alarms or Malfunctions 8

FPI-510 Electrical and Control Building Chiller Pump Rooms 3

ABN-805B Response to Fire in the Auxiliary Building or the Fuel 4

Building

ABN-806B Response to Fire in the Electrical and Control Building 3

SMART FORMS

SMF-2009-001001-00 SMF-2009-000720-00 SMF-2009-000714-00

Section 1R12: Maintenance Effectiveness

SMART FORMS

SMF-2009-004780-00

A1-2 Attachment 1

OTHER DOCUMENTS

Maintenance Rule Review Panel meetings 04-0226, 06-0321, & 09-0909

EVAL-2005-003441-06

Section 1R15: Operability Evaluations

PROCEDURES

NUMBER TITLE REVISION

MSM-C0-3831 Emergency Diesel Engine Cylinder Head Maintenance 3

WORK ORDERS

3756843 3770269

SMART FORMS

SMF-2009-003342-00 SMF-2009-003309-00 SMF-2009-004117-00

Section 1R18: Plant Modifications

PROCEDURES

NUMBER TITLE REVISION

STA-602 Temporary Modifications and Transient Equipment 16

STA-606 Control of Maintenance and Work Activities 29

10 CFR 50.59 Resource Manual 3

SMART FORMS

SMF-1999-001657-00 SMF-2009-001548-00 SMF-2008-003987-00 SMF-2009-001773-00

WORK ORDERS

2-07-173391-00

A1-3 Attachment 1

Section 1R19: Postmaintenance Testing

PROCEDURES

NUMBER TITLE REVISION

MSM-P0-3343 Emergency Diesel Engine Crankshaft Deflection and 2

Thrust Measurements

MSE-G0-6300 Breaker Enhancement Removal, Enhancement and 0

Installation

SOP-630A 6900 V Switchgear 14

IONC-210 Instrumentation Tubing and Supports Installation and 4

Rework

INC-2031 Valve Calibration Using Viper Control Valve Diagnostic 0

System

INC-2012 Valve Calibration Fisher Controls Type 657 Air-to-Close 4

Valve Actuators

MSM-C0-6604 Fisher Diaphragm Actuator Maintenance (Type 657, Sizes 4

30 - 60)

MSG-1060 Electrical Terminations (Wire Sizes 26 awg thru 10 awg) 1

MSE-G0-1212 Low Voltage Insulating Material Installation 4

OPT-204A SI System 13

WORK ORDERS

367376 397278 3766683 3665095

SMART FORMS

SMF-2009-004117-00

A1-4 Attachment 1

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION

TDM-804A Equipment Data Tank Height VS Volume 2

OPT-303 Reactor Coolant System Water Inventory 13

INC-7332B Analog Channel Operational Test and Channel Calibration 1

Steam Generator Narrow Range Level

WORK ORDERS

3749480 3749478 3749476 3749474

SMART FORMS

SMF-2009-003905-00 SMF-2009-004038-00 SMF-2009-004058-00 SMF-2009-004630-00

Section 1EP6: Drill Evaluation

SMART FORMS

SMF-2009-004095-00 SMF-2009-004096-00 SMF-2009-004099-00 SMF-2009-004100-00

SMF-2009-004102-00 SMF-2009-004103-00

Section 4OA1: Performance Indicator Verification

SMART FORMS

SMF-2008-003132-00

Section 4OA2: Identification and Resolution of Problems

PROCEDURES

NUMBER TITLE REVISION

OPT-308 Estimated Critical Condition Calculation 8

A1-5 Attachment 1

Section 4OA5: Other Activities

DRAWINGS

NUMBER TITLE REVISION

M1-0202 Flow Diagram Main Steam Reheat and Steam Dump CP-33

M1-0202, Sheet 03 Flow Diagram Main Steam Reheat and Steam Dump CP-2

M1-0206 Flow Diagram Auxiliary Feedwater System CP-20

M1-0206, Sheet 01 Flow Diagram Auxiliary Feedwater Trains CP-14

M1-0253 Flow Diagram Chemical and Volume Control System CP-21

M1-0253, Sheet A Flow Diagram Chemical and Volume Control System CP-10

M1-0255 Flow Diagram Chemical and Volume Control System CP-27

Volume Control Tank Loop

M1-0255, Sheet 01 Flow Diagram Chemical and Volume Control System CP-23

Charging and Positive Pump Trains

M1-0229, Sheet A Flow Diagram Component Cooling Water System CP-21

M1-0229, Sheet B Flow Diagram Component Cooling Water System CP-25

2323-EI-0601-11 Safeguard Building Cable Tray Segments Elevation 4

790-6

2323-EI-0603-11 Safeguard Building Cable Tray Segments Elevation 4

852-6

2323-EI-0713-12 Auxiliary and Electrical Control Buildings Cable Tray 6

Segments Elevation 790-6 & 792-0

2323-EI-0716-12 Electrical Equipment Area Cable Tray Segments 4

Elevation 810-6

2323-EI-0717-12 Auxiliary and Electrical Control Buildings Cable Tray 4

Segments Elevation 832-0

2323-EI-0603-11 Safeguard Building Cable Tray Segments Elevation 4

852-6

PROCEDURES

NUMBER TITLE REVISION

ABN-803A Response To a Fire In The Control Room or Cable Spreading 8

Room

ABN-804A Response To a Fire In The Safeguards Building 5

A1-6 Attachment 1

NUMBER TITLE REVISION

Response to Fire in the Auxiliary Building or the Fuel Building

ABN-805A 5

ABN-806A Response To a Fire In The Electrical and Control Buildings 5

SOP-304A Auxiliary Feedwater System 16

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

CPSES Fire Protection Report 3, 6, and 27

License Number Luminant Generation Company LLC, Docket Number Amendment

NPF-87 50-445, Comanche Peak Steam Electric Station, Unit 139

Number 1, Facility Operating License

FSAR Section 9.5.1 Fire Protection Program Amendments

78 & 87

50000445/87-22 NRC Inspection Report January 11,

1988

50000445/8839, NRC Inspection Report June 24, 1988

50000446/8833

NUREG-0797 Safety Evaluation Report Related to the Operation July 1981

Comanche Peak Steam Electric Station

NUREG-0797 Safety Evaluation Report Related to the Operation Supplements

Comanche Peak Steam Electric Station 12, 21, 23, 25,

26, and 27

A1-7 Attachment 1

ATTACHMENT 2

RESULTS OF THE STAFF'S REVIEW OF MANUAL ACTIONS IN THE LICENSING BASIS

Background

On July 24, 2008, Luminant Power submitted letter serial CP-200800962, TXX-08105, entitled

Comanche Peak Licensing Basis on Use of Manual Actions for Fire Protection. This was

submitted in response to the NRC's issuance of Unresolved Item 05000445/2008006-02;

05000446/2008006-02, Unapproved Local Manual Actions for Hot Shutdown. This letter

requested that the staff consider information provided in the attachment of the letter in the

resolution of Unresolved Item 05000445/2008006-02; 05000446/2008006-02.

The following discussion addresses how the staff considered the licensee's information and

provides the staff's conclusions.

NRC Staff Review

The NRC agreed to review the issues discussed in the licensee's letter. The lead inspector and

a senior reactor analyst visited the site to discuss the licensee's information and the NRC

understanding of their licensing basis. In addition, conference calls were held with licensee

management on July 14 and 29, 2009. As discussed in Section 4OA5 of this report, the staff

has confirmed that the unresolved item was associated with a violation of NRC requirements.

The basis for this conclusion is expanded upon here.

The licensee's letter documented why they believed that the NRC approved manual actions

within the fire protection program. Inspections had previously attempted to resolve this same

question, but had been unable to resolve the meaning of unclear references that interconnected

multiple documents. However, during the 2008 triennial fire protection inspection, it became

apparent that the proper issue that needed to be resolved related to whether the licensee met

the requirements for protecting and separating components identified by the licensee as

required to achieve and maintain a hot shutdown condition in the event of a fire. These required

components must be protected and separated so that they remain free of fire damage. The

manual actions of concern could only be assessed in the context of whether or not they were

intended to restore redundant trains of required equipment because of inadequate protection

and separation.

The staff's review of the documents that comprise the approved fire protection program are

specified in License Condition 2.G, which states:

Luminant Generation Company LLC shall implement and maintain in effect all the

provisions of the approved fire protection program as described in the Final Safety

Analysis Report through Amendment 78 and as approved in the SER (safety evaluation

report) (NUREG-0797) and its supplements through SSER (supplemental safety

evaluation report) 24, subject to the following provision:

Luminant Generation Company LLC may make changes to the approved fire protection

program without prior approval of the Commission only if those changes would not

adversely affect the ability to achieve and maintain safe shutdown in the event of a fire.

In each of the documents that comprise the fire protection program defined by the license

condition that were submitted by the then-applicant, the applicant described that one of the

three methods that listed in 10 CFR 50, Appendix R, Section III.G.2 would be used to satisfy the

NRC-required separation and protection schemes when more than one train of redundant

A2-1 Attachment 2

equipment was located in the same fire area, unless another method was justified. The staff

concluded that such a justification for an alternate method of compliance would necessarily

require a specific request for the staff to approve a deviation from the existing separation and

protection requirements. The staff's review concluded that there were no deviations requested

to substitute manual actions for recovering the use of required equipment that was susceptible

to fire damage, and therefore no justification was provided to the NRC for approval.

The staff also noted that for each section of the Fire Hazards Analysis dealing with a fire area

where more than one of the redundant trains needed for safe shutdown had cables located in

that area, the licensee stated that: One set of the redundant equipment and components within

the area is protected by one of the means provided in Section II-4.5. This statement reiterated

on an area by area basis that the applicant met the NRC's separation requirements.

The staff reviewed the NRC Safety Evaluation Report, which provided the bases for the NRC's

decisions concerning the acceptability of the fire protection program. Supplement 12 concluded

that: The applicant's analysis indicates that at least one of the redundant trains needed for

safe shutdown would be free of fire damage by providing separation, fire barriers, and/or

alternative shutdown capability. The safety evaluation report does not mention any exceptions

to this conclusion.

The staff reviewed the licensee's contention that the NRC had reviewed the applicant's use of

manual actions. The staff was able to confirm that the NRC had reviewed and approved a

specific set of manual actions. These were clearly documented in the fire protection program

documents. However, these manual actions related to addressing possible spurious operation

caused by fire damage to equipment that was not required to achieve and maintain hot

shutdown. The NRC verified that manual actions involving non-required equipment that could

prevent required equipment from achieving or maintaining hot shutdown could be performed

within sufficient time to ensure the functioning of the required systems. In some cases, this

review involved manual actions that were required to be performed locally in the same area as

the postulated fire. Because these manual actions involved non-required components, manual

actions that could be demonstrated to be reliably performed were determined by the NRC to be

acceptable. Supplement 12 stated:

Associated circuits whose fire-induced spurious operation could affect shutdown were

identified to determine those components whose maloperation could affect safe

shutdown. These spurious operations are terminated by operator actions. The applicant

identified these operator actions and allowed sufficient time to perform these actions.

On the basis of its evaluation, the staff concludes that these operator actions will

terminate spurious operations that could affect plant shutdown.

The licensee verbally reported that the NRC conducted onsite inspections into the details of

manual actions beyond these examples. Both the licensee and the staff were unable to locate

documentation concerning the scope or results of such reviews. In discussions with the

licensee, it was apparent that the licensee's procedures and analyses had not documented the

purpose for each manual action in the fire response procedures. Inspection guidance caused

them to focus on whether the manual actions were reasonable and feasible, not specifically why

the manual actions were needed. Fire response procedures can be expected to have

acceptable operator manual actions, including: actions to implement the approved alternative

shutdown strategy (i.e. control room evacuation); actions to control the plant so as to achieve

and maintain a shutdown to hot standby condition; actions intended for property protection and

good operating practice (e.g. securing equipment that is not being used for safe shutdown); and

actions to address possible spurious operation caused by fire damage to equipment that was

not required to achieve and maintain hot shutdown. However, while actions to restore

A2-2 Attachment 2

equipment required for safe shutdown to hot standby are not acceptable, these actions can be

challenging to differentiate from the acceptable actions.

The licensee was required to identify the list of equipment required for safe shutdown. In

Comanche Peak's case, the Safe Shutdown Equipment List is not typical of other sites;

Comanche Peak's documents listed the required equipment at the system or function level,

rather than at the component level. Lists identifying individual components located in each fire

area and requiring manual actions based on the location of a fire did not differentiate between

components being operated to restore required safe shutdown functions and those being

operated in response to spurious operations. This added a significant challenge to identification

of unacceptable manual actions that were intended to restore equipment that was actually

required to have been protected from fire damage. Following issuance of Unresolved Item

05000445; 446/2008006-02, inspectors requested that the licensee provide the purpose for the

operator manual actions specified in fire response procedures where inspectors could not

confirm the purpose. The licensee's response provided the first clear indication that some of

these manual actions were intended to restore required equipment that the licensee had

previously recognized was not protected from fire damage.

The inspectors also noted that the most challenging statement in the licensing basis

documentation to place in context was a statement in the Fire Protection Report,

Section III-3.1.1, which listed assumptions used in the fire analyses methodology description. It

stated:

Manual operations are allowed to achieve hot standby following a reactor trip and to

maintain hot standby conditions.

The licensee contended that this statement allows the use of manual actions. The staff's review

of the Safety Evaluation Report found that this part of the Fire Protection Report is not

discussed. However, operators are allowed to perform manual actions to operate plant

equipment in the normal manner to achieve and maintain hot standby, whether the need arose

from a fire or some other reason. This statement does not specifically discuss using manual

operations to restore equipment that was required to achieve and maintain hot standby that was

damaged by fire and not available to be operated by the normal means. This statement does

not directly address separation or protection of equipment. Therefore, the staff concluded that

this statement does not have relevance to the requirements to separate and protect required

equipment.

For completeness, the staff also considered whether the licensee may have made a change to

the approved fire protection program under the belief that such changes were permissible under

with the provisions in License Condition 2.G. The licensee clearly stated that the manual

actions in question were not made as part of a change to the fire protection program as

originally submitted for approval.

A2-3 Attachment 2