IR 05000416/1981021

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IE Insp Rept 50-416/81-21 on 810609-12.No Noncompliance Noted.Major Areas Inspected:Preoperational Testing,Licensee Identified Items & Violation Corrective Actions
ML20010A542
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 07/14/1981
From: Burnett P, Hunt M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20010A538 List:
References
50-416-81-21, NUDOCS 8108110530
Download: ML20010A542 (6)


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Roport No. 50-416/81-21 Licensee: Mississippi Power and Light Company Jackson, MS 39205 Facility Name: Grand Gulf Unit 2 Docket No. 50-416 Licensc No. CPPR P.B Inspection at Grand Gulf Nuclear facility near Port Gibson, MS M. D. Hunt '~

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7-//-M PM6rnVEt, A6tirig Section Chief Date Engineering Inspection Branch Division of Engineering and Technical Inspection SUMMARY Inspection on Jure 9-12, 1981 Areas Inspected This routine, unannounced inspection involvad 26 inspector-hours onsite in the areas of preoperational testing; licensee identified items and violation corrective actions.

Results Of the three areas inspected, no violatio,1s or deviations were identified.

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DETAILS 1.

Persor.s Contacted Licensee Employees

  • S. F. Tanner, QA Coordinator
  • J. M. Kelly, QA Specialist
  • J. C. Bell, QA Representative
  • J. W. Yelverton, QA Supervisor
  • B. C. Lee, QA Representative
  • B. D. Stewart, Construction Manager
  • C. C. Hutchinson, Start-up Manager G. B. Rogers, Site Manager Other Organizations
  • M. R. Lindsey, QA Supervisor, Bechtel Power Corporation (BCP)

i NRC Resident Inspector

  • A. G. Wagner
  • Attended exit interview 2.

Exit Interview 1'

The inspection scope and findings were summarized on June 12, 1981 i

with those persons indicated in Paragraph 1 above.

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3.

Licensee Action on Previous Inspection Findings (Closed) INF 50-416/80-08-01, Failure to follow pipe support in-

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stallation and inspection procedures.

The licensce's final report I

dated June 17, 1980 informed Region II that two nonconforming reports and two condition reports had been issued regarding this noncompliance. The inspector verified that these reports are now completed and closed.

4.

Unresolved Items Unresolved items were not identified during this inspection.

5.

Pre-Operational Tests - Procedure Review a.

The following test procedures was reviewed for conformance with R.G.1.68, FSAR Chapter 14, Grand Gulf Startup Manual chapters 5000 and 7000, and MPL Topical-1 Quality Assurance Manual.

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Procedure No.1CIPT01, Rev.1, Control Rod Drive Hydraulic System.

It was noted that in several instances the instruction /pra-cedure required the removal of a jumper that had been installed in several steps previously.

The removal instructions contain only the words " Remove the jumper installed in step...".

The inspector commented that the procedure would insure more accuracy if the Jumpet points of installation were identified in the removal statement. The licensee representatives advised the inspector that as a rule the points of jumpers installation were identified in removal instructions and the case in point was an oversight.

The procedure had been reviewed and approved by management, stated the pertinent prequisites, specified initial test conditions, provided for signoffs of each step and review by the appropriate personnel.

b.

The following irocedure while classified as a startup procedure involved certair, testing during pre-op testing:

Procedure 1-E41-ST01, Rev. 1, Reactor Vessel Flow - Induced Vibration Testing Prior to Fuel Load.

This is a prototype BWR/6 reactor vessel internals for a 251 inch inside diameter vessel. Therefore a comprehensive assess-ment program has been developed to include in-depth analysis

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of extensive field measurements and full inspection as required by R.G 1.20.

Part of this test was performed during the open vessel injection portion of the high pressure core spray system pre-operation test 1-E22-PT-01.

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The procedure was compared to the requirements of FSAR Sections 3.9.2.4 and 14.2.12.1.37 and RG 1.20.

The review revealed no items of concern.

Within tha areas examined, no violation were identified.

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Plant Tour

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The inspector conducted a walk-through examination of the control, auxiliary and reactor buildings.

It was noted that in several areas conduit was being attached to cable tray supports. The licensee advised the inspector that the conduit and additional cable weights had been included as part of the seismic support

analysis.

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i Testing for turnover to pre-op was in progress in several areas.

Access control to certain rooms has been instituted.

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Within the are s examined, no violations were identified.

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Jumper Control The inspector noted that the pre-op prccedures required the use of jumpers.

The procedures require the removal and signoff for these jumpers, but there is no inventory taken of the jumpers used and jumpers removed.

The inspector inquired of the licensee about the establishment of a method for jumper control.

During discussions it was pointed out

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that numbered jumpers assigned to wertain tests could provide a method for identifying any jumper that might be overlooked during the removal effort.

The licensee agreed to look further into this situation.

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8.

Licensee Identified items (LII) 10 CFP 50.55(e)

(Closed) LII 50-416/80-02-02: Polypropylene pulling rope cut through

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cable jacket and insulation and exposed the conductors. MP&L reported this item to Region II March 13, 1980.

The inspector reviewed the results of tests conducted as reported May 19, 1981.

The corrective actions ap; ear adequate.

(Closed) LII 50-416/80-12-18:

Consip Inc. reported Part 21 per-taining to pump damage where sample inlet and outlet are closed off while the pump is running.

This itern was reported April 30, 1980.

The final report submitted May 30, 1980 called for a bypass or l

recircumation line with a pressure operated check valve to be

' nstalled between the pump discharge and the pump suction lines.

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Records indicate the work is complete and tested.

(Closed) LII 50-416/81-21-01:

Consip Inc. Motor Shaft Failure.

This item was reported to Region II February 11, 1981.

The final report dated May 26, 1981 stated the manufacturer had redesigned the motor shafts to make then stronger.

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(Ciosed) LII 50-416/79-04-01: Work performed without a QA program.

That a GE subcontractor had performed and was performing electrical activities without a QA program was reported tc Region II February 12, 1979.

The final report dated May 29, 1981 advised that a QA program was instituted February 16, 1979 and all work done prior to this date was reinspected and evaluated.

The inspector reviewed various records that support this information.

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l (Closed) LII 50-416/79-04-03:

"As shipped" panels do not match "as shipped drawings".

This item was reported to Region II February 23,

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1979.

The final report dated May 29, 1981 advised that this item l

resulted due to changes requested by the AE and mada by the vendor, l

but due to time lag in drawing revisions the mismatch occurred.

l The site QC organization nerformed a comparison inspection between

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the panels and drawings and identified the discrepancies. The drawings were then revised to reflect the "as shipped" conditions.

A QA audit (80-93) was reviewed by the inspector. This audit was a i

sampling check of cabinets and verified that the cabinets checked did conform to the drawings.

(Closed)LII 50-416/79-04-02:

Inadequate crimping of connecting pins. This item was reported February 23, 1979.

The final report dated February 20, 1981 contained a st.mmary of test results for

pull tests of samples of the crimped connections.

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indicate the connector crimp is acceptable.

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(Closed) LII 50-416/79-20-04:

Powell valve company computer code l

challenged.

This item was reported September 4, 1979. The final report dated August 1, 1980 indicated that corrective actions were in progress. This work has now bnen completed for Unit 1.

(Closed)LII 50-416/80-20-19: Bechtel supplier drawing revision notice program inadequate controls.

This item was reported to Region II August 6, 1980. The final report dated April 10, 1981 indicates that the problem was investigated and corrective actions taken.

(Closed) LII 50-416/80-19-03: Anchor bolt ultimate strength. This item was reported August 14, 1980. The final report was submitted i

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May 5,1981 and included a Part 21 evaluation.

The manufacturer has now revised the load capacities of the 1" diameter bolt anchor, and the licensee's AE has incorporated these specifications in their design.

(Closed) LII 50-416/B0-20-03: Station Service water pumps picked up debris from SSW Basin. This item was reported June 13, 1980.

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final report submitted March 6,1981 advises that pump suction services have now been installed.

(Closed) LII 50-416/80-20-11:

Diesel generator - fractured valve l

body on water jacket. This item was reported June 26, 1980.

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final report dated April 3,1981 advised that the vslves had been replaced and the installation instructions have been revised to preclude recurrence.

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(Closed) LII 50-416/80-20-20: RPV servicing lines - possible shearing by reflective insulations. This item was reported August 8, 1980.

The final report dated May 1,1981 advises that design changes have been made to include pipe sleeve extensions and reflectors i

to protect the insulation panels from maximum pressure watered by the LOCA.

(Closed) LII 50-416/80-12-05:

Loss of offsite power effects.

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item was reported to Region II March 17, 1980.

The licensee's final report dated April 21, 1981 concluded that the item was not reportable under 10 CFR 50.55(e), but did conclude that the power supply configuration was operationally undesirable.

Evaluations

are underway to address this situation. The licensee will provide

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descriptions of all actions taken in this regard.

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(0 pen-Closed) LII 50-416/81-21-02: Starter / Breaker plug-in drawers

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not seismically qualified. This item was reported to Region II February 27, 1981.

The final report was dated June 1, 1981. This deficiency concerns Klockner-Moeller supplied starter / breakers (24 q

inch) plug-in drawer that were not seismically qualified. The

unqualified equipment will be replaced with qualified drawers of varying sizes.

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