IR 05000373/1988011

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Insp Repts 50-373/88-11 & 50-374/88-10 on 880325-0509. Violations Noted.Major Areas Inspected:Operational Safety, Surveillance,Maint,Training,Ler,Emergency planning-emergency Detection & Classification & Mgt Meeting
ML20155A374
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 05/25/1988
From: Ring M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20155A362 List:
References
50-373-88-11, 50-374-88-10, NUDOCS 8806100041
Download: ML20155A374 (8)


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U. S.' NUCLEAR REGULATORY COMMISSION

REGION III

Report No /88011(DRP);50-374/88010(DRP)

Docket No ; 50-374 Licenses No. NPF-11; NPF-18 Licensee: Commonwealth Edison Company Post Office Box 767 Chicago, IL- 60690 ,

Facility Name: LaSalle County Station, Units 1 and 2

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Inspection At: LaSalle Site, Marseilles, IL Inspection Conducted: March 25 through May 9, 1988 Inspectors: R. Kopriva J s.' ,

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Approved y:f . Ring, '5 25.BS

r,eactor Projects Section IB Jate Inspection Summary

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Inspection on March 25 through May 9, 1988 (Reports No. 50-373/88011(DRP); l 50-374/88010(DRP))

Areas Inspected: Routine, unannounced inspection conducted by resident inspectors of licensee actions on previous inspection findings; operational safety; surveillance; maintenance; training; Licensee Event Reports; emergency <

planning-emergency detection and classification; and management meetin I Results: Of the eight areas inspected, one violation was identified in l Paragraph 4. The licensee is currently 40% complete with their Unit 1

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refueling outage. Work on the drywell cooling modification, snubbe reduction  !

and reactor recirculation cump are going well and appear to be on or near i

schedule. During the previous inspection report period, there were several problems (i.e. missed surveillances, health physics violation, procedural violations) which appear to have been isolated occurrences, as these problems have not reoccurred during this report period. Due to the large amount of work taking place during the outage, the licensee should remain diligent in -

their efforts of controlling the work activities, i

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8806100041 880525 PDR ADOCK 05000373 ,

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, 1 DETAILS

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1. Persons Contacted  ;

G. J. Diederich, Manager, LaSalle_ Station .

  • Huntington, Services Superintendent ,
  • J. C. Renwick, Production Superintendent

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D. Berkman, Assistant Superintendent, Work Planning ]

J. Schmeltz, Assistant Superintendent, Operations .

P. Manning, Assistant Superintendent, Technical Services T. Hammerich, Assistant Technical Staff Supervisor i W. Sheldon, Assistant Superintendent, Maintenance .

J. Atchley, Operating Engineer i

  • D A. Brown, Quality Assurance Supervisor  ;
  • Settles, Assistant Technical Staff Supervisor
  • G. Santic, Master Instrument Mechanic
  • Denotes personnel attending the exit interview on May 13, 198 Additional licensee technical and administrative personnel were contacted  !

by the inspectors during the course of the inspectio . Licensee Action cn Previous Inspection Findings (92701)

(Closed) Unresolved Item (374/88004-01): Personnel error during instrument surveillance causing the reactor recirculation pump motors to trip and subsequent reactor scram. The unresolved item is closed and a Notice of Violation 374/88010-01 on this event is being issue (Closed)UnresolvedItem(373/88004-01;374/88004-02): Inadequate I procedures covering reactor core power oscillations. The inspector  :

reviewed the licensee's procedures and had several discussions with the s licensee's staff pertaining to the contents of these procedures. The .

procedures had been written incorporating knowledge the licensee had  ;

gained from preoperational testing and vendor analysis. The licensee e revised their procedures to mitigate future events of this natur l No violations or deviations were identified in this are .

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3. Operational Safety Verification (71707) i

The inspector observed control room operations, reviewed applicable logs, and conducted discussions with control room operators during (

i the inspection period. The inspector verified the operability of  !

selected emergency systems, reviewed tagout records, and verified . ,

proper return to service of affected components. Tours of Unit 1 l

and 2 reactor buildings and turbine buildings were conducted to  ;

i observe plant equipment conditions, including potential fire i hazards, fluid leaks, and excessive vibrations, and to verify that  :

maintenance requests had been initiated for equipment in need of <

maintenance. The inspector, by observation and direct interview, .

verified that the physical security plan was being implemented in  :

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accordance with the station security plan ircluding the following: 1

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[the apprcpriate number of security personnel were on site; access

'; control barriers were operational; protected areas were well

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maintaincd, and vital area barriers were well maintained. The iminctor verified the licensee's radiological protection program

.; was implemented in accordance with the facility policies and

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programs and in compliance with regulatory requirement o . During the month of April 1988, the inspector walked down the

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accessible portions of the following systems to verify operability:

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2A Diesel Generator Standby Gas Treatment Systems

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Unit 2 High Pressure Core Spray System Unit 2 Reactor Core Isolation Cooling System Monthly Surveillance Observation (61726)

The inspector observed Technical Specification required surveillance testing and verified for actual activities observed that testing was performed in accordance with adequate procedures, that test instrumenta-tion was calibrated, that Limiting Conditions for Operation were met, that removal and restoration of the affected components were accomplished, that test results conformed with Technical Specification and procedure requirements and were reviewed by personnel other than the individual  ;

directing the test, and that any deficiencies identified during the testing were properly reviewed and resolved by appropriate management personne The inspector witnessed portions of the following test activities:

LIS-RP-03 Main Steam Isolation Valve Closure Scram Response Time Test LIS-MS-407 Unit 2 Reactor Vessel Low-Low-Low Water (Level I) Main Steam Isolation Valve Isolation Functional Test LIS-LP-105 Unit 1 Low Pressure Core Spray Flow Indication Calibration LOS-DG-SR4 28 Diesel Generator Action Statement Operability Test LES-RH-100 Unit 1 Residual Heat Removal System Relay Logic Test Division I

, On March 9, 1988, at 5:32 p.m. while performing surveillance LIS-NB-404, "Unit 2 Reactor Vessel Low Low Water Level RCIC Initiation, Low-Low-Low Water Level LPCS/RHR Initiation, and ADS Permissive Functional Test," an instrument mechanic inadvertently valved in the variable and reference legs of differential pressure .

switch 2821-N0378B with the e *

unresolved item 374/88004-01)qualizing . A secondvalve open observing technician (refer to the test informed the first technician of the error. The variable and reference leg isolation valves were imediately closed, however, this had caused a perturbation in the instrument rack causing the

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reactor recirculation pumps to trip, reactor core power oscillations, and subsequent reactor scra Technical' Specification 6.2.A requires that detailed written ,

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procedures including applicable checkoff lists shall be prepared, approved, and adhered to; including those procedures recommended in Appendix "A" of Regulatory Guide 1.33, Revision 2, February 1987, and surveillance and testing requirements. Regulatory Guide 1.33 includes procedures for control of measuring and test equipment and for surveillance' tests, procedures and calibration Contrary to the above, on March 9, 1988, while performing surveillance LIS-NB-404, "Unit 2 Reactor Vessel Low Low Water Level RCIC Initiation, Low-Low-Low Water Level LPCS/RHR Initiation, and ADS Permissive Functional Test", the procedure was not adhered to when an instrument technician inadvertently valved in the variable and reference legs of the differential pressure switch being tested with the equalizing valve open. The technician failed to adhere to the procedure in that he manipulated the wrong valves. This is considered a violation (374/88010-01).

There were several items which could have prevented this erro There were no precautions or special notes in the procedure to alert the technician that improper valve manipulation (s) could cause problems. The second technician possibly could have recognized and prevented the first technician from manipulating the wrong valves prior to valving in the reference and variable legs of the switc Valve identification may have aided the technician in selecting the proper valves, but at present there is no specific identification of these valves for the differential pressure switches. The licensee is reviewing this problem, but they have not found an acceptable resolution for labeling the valves, b. On April 12, 1988, at approximately 2:15 a.m. CDT, the licensee was performing surveillance LIS-HP-205, "Unit 2 High Pressure Core Spray (HPCS) Minimum Flow Bypass Calibration." At 2:55 a.m., during the testing, static-o-ring (SOR) switch 2E22-N006 was found to actuate outside of its calibration limits. The switch actuated at 18 inches of water column and the rejection limit for this switch is less than 20 inches of water column. The licensee then placed the HPCS minimum flow bypass valve in the closed position and declared the !

HPCS system inoperabl The 50R switch has been replace Upon initial investigation, it appears that there was no diaphragm ;

failure in the switch. This appears to be the first failure of the SOR switch in this application, c. On April 22, 1988, at approximately 1:20 p.m. (CDT), the licensee was replacing a K1A relay in the Unit 1 Reactor Protection System (RPS) which had failed its response time testing. The technician l installed the K1A relay improperly which tripped the 'A' bus of j the Unit 1 RPS due to the shorting in the 'A' Average Power Range '

Monitor (APRM). This caused the 'A' RPS Motor / Generator (M/.G) set output breaker and power monitoring assemblies to trip, and the fuse associated with the K1A relay blew causing actuation of the reactor building ventilation isolation dampers, which closed. This action automatically started the Unit 1 and 2 Standby Gas Treatment (SBGT)

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trains. The unit operators installed jumpers on the Main Steam Line (MSL) tunnel temperature and differential temperature switches for Unit 2 to preclude their actuatio The licensee investigated the isolation actuation and then reopened the reactor building ventilation isolation dampers, restarted the Unit 1 and 2 ventila-tion fans and returned the SBGT trains back to nonnal standby status. At 1:50 p.m. the jumpers were removed from the Unit 2 MSL tuvel temperature and differential temperature switche . Monthly Maintenance Observation (62703)

During the inspection period, the inspector observed portions of the following maintenance activities:

Unit 1 - Jet pump disassembly, inspection and reassembl Unit 1 - Control rod drive removal, rebuild and reinstallatio Unit 1 'A' turbine driven reactor feed pump maintenanc Unit 2 - Motor driven reactor feed pump maintenanc Unit 1 - High pressure core spray motor disassembly, In September 1987, after the startup of Unit 1, it was noted that the No. 3 jet pump looted in the reactor, was not achieving its expected flow, Upon further review of the problem, the licensee concluded that the jet pump appeared to be partially blocked reducing its total flow capacity. During the present Unit I refueling outage, jet pump No. 3 was disassembled and inspecte During the inspection, the inside of the jet pump exhibited several areas that appeared to be scratched or worn by a foreign object which had passed through +he jet pump. Upon further inspection, the male disc insert to the 'A' Reactor Recirculation (RR) pump discharge valve was found lodged in the nozzle area of the jet pum The disc insert had been identified as a missing piece during the disassembly of the 'A' RR pump discharge valve which took place in the sumer outage of 1987. A search to find the missing disc insert, at that time, proved unsuccessful. A loose parts analysis had been performed by the reactor vendor which analyzed operating the unit with the disc insert in the reactor or associated recirculation syste The disc insert was in one piece and had been lodged firmly in the jet pump. There were no indications in the jet pump that the disc insert had been moving around, potentially causing excessive wear or deterioration of the jet pump. Upon removal of the disc insert from the jet pump and completion of the inspection, the jet pump was reassemble On May 3, 1988, at approximately 5:40 p.m. CDT with Unit 1 in a refueling outage and Unit 2 at 97% power, the secondary containment ventilation system automatically isolated and the Standby Gas i

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Trehtment (SBGT) System auto started on both units in response i to a dual unit Group 4 isolation signal. The licensee was making preparations to move the 1A reactor recirculation pump impeller to *

the refueling floor while the 1A reactor recirculation pump was being rebuilt. As part of the preparations, the licensee was jumpering out the refueling floor process radiation monitors to prevent a Group 4 isolation signal from being generated while the recirc impeller was being moved. The jumper slipped off one of the screw terminals to which it was attached and grounded out to the metal enclosure causing a fuse to blow. When this occurred, the Group 4 isolation signal that the licensee was attempting to prevent was generated. By 6:38 p.m. CDT, the licensee had restored both secondary containment ventilation systems and one train of SBG The second train of SBGT was allowed to run for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> for surveillance purpose No violations or deviations were identified in this are . Training (41400)

The inspector, through discussions with personnel and a review of 1 training records, evaluated the licensee's training program for l

operations and maintenance personnel to determine whether the general '

i knowledge of the individuals was rufficient for their assigned task , In the areas examined by the inspector, no items of concern were <

identifie I

No violations or deviations were identified in this are . Licensee Event Reports (92700) l

Through direct observations, discussions with licensee personnel, and review of records, the following Licensee Event Reports (LERs) were reviewed to determine that reportability requirements were fulfilled, immediate corrective action was accomplished, and corrective action to prevent recurrence had been accomplished in accordance with Technical Specifications, The following reports of nonroutine events were reviewed by the inspectors. Based on this review it was determined that the events

were of minor safety significance, did not represent program

deficiencies, were properly reported, and were properly compensated for. These reports are closed:

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373/88001-00 - Failure of reactor core isolation cooling high l

reactor water level switch due to setpoint drift caused by stripped !

. setpoint locking mechanism screw, l 373/88002-00 - Type 'B' and Type 'C' total leakage exceeded 0.6 La during leak rate testing.

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374/88001-00 - 28 Diesel Generator cooling water pump failure to auto start.

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, 374/88002-00 - Group 10 isolation due to test switch failure found during surveillance testin /88004-00 - Missed Technical Specification surveillance due to personnel error, The following reports of nonroutine events involved violations of regulatory requirements. These reports are considend close Eve.t closure is being tracked by the associated violatio Appropriate cross references are provide /88003-00 - Reactor scram on high average power range monitor flux level due to the personnel valving erro No violations or deviations were identified in this are . Emergency Planning - Emergency Detection and Classification (82201) On April 13, .988, at approximately 9:25 a.m. CDT, the licensee informed the resident inspector that a subcontractor technician had been taken off site by ambulance for what appeared to have been a

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heart attack. Charles U. Miller, a General Electric Co. technician,

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was in the licensee's protected area in the service building on his way to the mask (respirator) fit area. Mr. Miller had just finished walking up a set of stairs when he became dizzy and then unconsciou He was revived and appeared coherent for a moment and then stopped breathing. Other workers in the area started administering cardio pulmonary resuscitation (CPR) with no response. They continued to

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administer CP Mr. Miller was then transported off site by ambulance to Saint Mary's Hospital in Streator, Illinois where Mr. Miller was pronounced dead. Mr. Miller was 57 years old and a diabetic. He was still in the process of completing the licensee's training for radiation protection and had not been in any radioactive or contaminated areas of the plant when the event occurred.

Preliminary diagnosis by the coroner was that Mr. Miller had suffered a massive heart attack, On April 23, 1988, at 9:50 p.m. (CDT), a contractor fell while working on the main steam turbine. At 10:12 p.m. the licensee declared an unusual event (GSEP) due to the fact that they would

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be transporting a potentially contaminated person to the hospita The licensee elected to leave the contractor's anti contamination clothing on due to potential back injuries. The contractor was working in the turbine building on the platform for the main steam

turbine rotor. He fell approximately 10 feet. During the fall, the contractor struck his left shoulder and small of his back on an

'I' bea The Emergency Notification SJstem (ENS) notification was

made at 10:15 p.m.. The ambulance left the site at 10:20 p. l The contractor received attention at t'.. Mary's in Streator, l

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Illinois and at 11:15 p.m. was found not to be contaminated. The licensee then terminated the unusual event, On May 8, 1988, at approximately 6:25 p.m. COT, an off duty security guard called the LaSalle County Nuclear Station stating that he had seen a tornado and that it appeared to be heading in the general -

direction of the site. The station contacted the load dispatcher-to

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relay the message and the station was informed that there had been i several electrical problems in the area due to high blowing wind The licensee also experienced some problems with comunications over local phone lines. The station declared an Unusual Event per their GSEP procedures at 6:30 p.m.. By 7:10 p.m., the high winds had decreased and the station terminated the Unusual Event. No site damage was sustained. The ENS notification was made at 7:15 p. No violations or deviations were identified in this are . Management Meeting (30703)

On April 15, 1988, select NRC Region III staff and the resident '

inspectors met with the licensee's staff for a routine plant tour, plant outage update, and an overview of the sites operational performance for the past month. The plant tour included the Emergency Core Cooling System (ECCS) pumps, valves and heat exchanger The NRC personnel then observed shift turnover in the control room and attended the licensee's morning briefing meeting. The licensee included with their presentation

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of plant performance and their update on the outage, a brief discussion j of their preventive maintenance program and how they implement i . Exit Interview (30703) l The inspectors met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection period and summarized the scope and findings of the inspection activities. The licensee acknowledged these findings. The inspectors also discussed the likely informational content of the inspection report with regard to documents or processes reviewed by the inspector during the inspectio The licensee did not identify any such documents or processes as proprietar )

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