ML20154H011

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Augmented Insp Repts 50-373/88-08 & 50-374/88-08 on 880316-24.No Violations or Deviations Noted.Major Areas Inspected:Root Cause Determination,Safety Significance & Performance of Operators & Equipment Re 880309 Reactor Trip
ML20154H011
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 05/11/1988
From: Azab B, Ron Kopriva, Phillips L, Ring M, Shemanski P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20154H008 List:
References
REF-GTECI-B-19, REF-GTECI-TH, TASK-B-19, TASK-OR 50-373-88-08, 50-373-88-8, 50-374-88-08, 50-374-88-8, GL-86-02, GL-86-2, NUDOCS 8805250195
Download: ML20154H011 (30)


See also: IR 05000373/1988008

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

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Report No. 50-373/88008; 50-374/88008

Docket No. 50-373; 50-374

License No. NPF-11; NPF-18

Licensee:

Commonwealth' Edison Company

P. O. Box 767

Chicago, IL 60690

Facility Name:

LaSalle County Station, Units 1 and 2

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Inspection At:

LaSalle Site, Marseilles, IL

Inspection Conducted: March 16 through 24, 1988

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Inspectors:

NRC Augmented Inspection Team

Team Leader:

M. A. Ring

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Date

Team Members:

R.A.KoprivD

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L. E. Pn11l'i

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P. Shemansk

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Date

B. A. AzaD7h b 6

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Approved By:

W. L. Forney, Ch'ief W

/e/r .

Reactor Projects Branch 1

Date

Inspection Summary

Inspection on March 16 through 24, 1988 (Report No. 50-373/88008(DRP);

50-374/88008(DRP))

Areas Inspected:

Special Augmented Inspection Team (AIT) inspection conducted

in response to the dual recirculation pump trip and subsequent core power

8805250195 880516

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ADOCK 05000373

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oscillations resulting in a reactor trip on March 9, 1988, at LaSalle, Unit 2.

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The review included root cause determination, safety significance, performance

of operators and equipment, adequacy of procedures, effects on the reactor,

reporting actions and potential generic implications.

Results: No violations or deviations were identified; however, the licensee.

has committed to procedure and Technical Specification changes as well as

further study in the areas of inherent shutdown mechanisms, instrumentation

'c'apability and uncertainties in the decay ratio calculations.

The licensee's

interim report, as required by the CAL, is included as attachment 5 to this

report.

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Augmented Inspection Team Report

Page*No.

I.

Introduction

1

A.

Synopsis of Event

1

B.

AIT Formation

1

C.

AIT Charter

2

D.

Persons Contacted

2

II. Description - Dual Recirculation Pump Trip Event

of March 9, 1988

3

A.

Narrative Description

3

B.

Sequence of Events

5

III. Investigative Efforts

7

A.

Synopsis of AIT Activities

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B.

Core Nuclear and Thermal Hydraulic Performance

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1.

Core Performance

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2.

Chemistry Results

10

3.

Equipment Performance

11

a.

Recirculation Pumps & Flow Control Valves

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b.

Feedwater Heaters

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c.

Power to Flow Scram

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d.

Reactor Protection System

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e.

ATWS System

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C.

Operator Performance

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D.

Procedure Adequacy and Training

16

1.

Technical Specifications

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2.

GE SIL 380

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3.

Abnormal Procedures and Training

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Page No.

4.

Simulator Training

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E.

Reporting

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Reporting Sequence

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2.

Reporting Evaluation

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IV. AIT Concerns and Recommendations

21

A.

Concerns

21

1.

Decay Ratio

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2.

Technical Specifications

21

3.

Instrumentation

22

4.

Oscillation Characteristics

23

5.

Additional Concerns

24

B.

Recommendations

24

V.

AIT Conclusions

24

VI. Exit

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Attachments

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Attachment'No.

Descriotion

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Confirmatory Action Letter (CAL-RIII-88-03)-

2

Augmented Inspection Team (AIT) Charter

3

Figures

Figure 1

BWR Power to Flow Map

Figure 2

Decay Ratio

Figure 3

Startrec Traces - Beginning of Event

Figure 4

Startree Traces - Oscillations

4.

Technical Specifications

5

Commonwealth Edison Company (Ceco)

Response to CAL item 5, dated

April 15, 1988

6

LER 88-003-00

7.

GE SIL 380

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I.

INTRODUCTION

A.

Synopsis of Event

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On Wednesday, March 9, 1988, around 5:30 p.m. CST, the LaSalle Unit

2 reactor was operating at steady state conditions at approximately

84% power.

Instrument Maintenance Department personnel were in the

process of performing an instrument surveillance when a valving

error produced a pressure pulse which actuated the instrumentation

which causes a trip of both recirculation (RR) pumps in order to

decrease power in the event of an Anticipated Transient Without

Scram (ATWS). Both RR pumps tripped causing a flow and power

decrease.

Control rods remained in the high power (99% Flow Control

Line (FCL)) position. As a result of the rapid power decrease caused

by the trip of the RR pumps, the feedwater heater level control

system was unable to control level in the feedwater heaters and

began isolating extraction steam from the heaters.

This resulted in

cooler feedwater being supplied to the reactor. Approximately five

minutes after the RR pump trip, operators observed the Average Power

Range Monitor (APRM) indication in the control room to be oscillating

between 25% and 50% power every 2 to 3 seconds. Approximately

seven minutes after the RR pump trip, as operators were attempting

to restore forced flow and making preparations to scram, the reactor

automatically scrammed on high neutron flux as seen by the APRMs.

At 6:32 p.m. CST, the licensee notified the NRC of the RR pump trip,

the loss of feedwater heating, and the resultant scram.

B.

AIT Fomation

At the time of the event on March 9, 1988, the Resident Inspector

assigned to LaSalle was offsite attending the Resident Seminar and

the Senior Resident Inspector position for LaSalle was vacant due

to a recent promotion. The initial licensee report on the event

did not discuss the flux oscillations but indicated that the event

was still being investigated. Upon further investigation and

appreciation of the magnitude of the oscillations a Region III

morning report update of the event was issued on March 15, 1988.

On March 16, 1988, an Augmented Inspection Team (AIT) was formed

which included three Region III individuals; M. A. Ring, Chief,

Reactor Projects Section 18 and Team Leader, R. A. Kopriva, LaSalle

Resident Inspector, and B. A. Azab, Reactor Safety Inspector, and

two NRR individuals; L. E. Phillips, Senior Nuclear Engineer, and

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P. Shemanski, LaSalle Project Manager. All of the AIT members had

arrived onsite by the morning of March 17, 1988. Concurrent with

the AIT activities, Region III issued a Confirmatory Action Letter

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(CAL-RIII-88-03) which was received by the licensee on March 17,

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1988, and is included as Attachment 1 to this report.

The CAL

confirmed certain actions to be taken by the licensee in support of

the AIT and established conditions to be met prior to the restart of

LaSalle, Unit 2.

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C.

AIT Charter

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On March 17, 1988, a draft charter for the AIT was formulated and

transmitted to the AIT onsite (Attachment 2 to this report).

The

general areas to be investigated were:

Sequence of events

Core performance during the event

Operator performance

Procedure adequacy

Reactor effects

Reporting

D.

Persons Contacted

Commonwealth Edison Company

  • G. J. Diederich, Station Manager
  • N. Kalivianakis, General Manager, BWR Operations
  • D, Galle, Vice President, BWR Operations
  • H. E. Bliss, Manager of Nuclear Licensing
  • W. R. Huntington, Services Superintendent
  • T. Rausch, Nuclear Fuel Services
  • W. F. Naughton, Nuclear Fuel Services Manager
  • M. Turbak, Assistant Licensing Manager
  • J. Bitel, Manager Nuclear Safety
  • R. J. Raguse, Production Training Supervisor
  • T. Shaffer, Training Supervisor
  • R. O. Armitage, lead License Instructor
  • K. W. Peterman, Nuclear Fue? 5+cvices
  • L. H. Lauterbach, Onsite Nuclear Safety Supervisor
  • H. McLain, Onsite Nuclear Safety
  • W. S. Marcus, Engineering-Site Supervisor
  • J. C. Renwick, Productica Superintendent
  • J.

A. Miller, Technical Staff

  • M. H. Richter, Assistant Technical Staff Supervisor
  • D. A. Brown, Quality Assurance Superintendent
  • P. F. Manning, Assistant Superintendent - Technical Services
  • T. A. Hammerich, Technical 5taff Supervisor
  • A. C. Settles, Regulatory Assurance

B. S. Westphal, Operating Engineer

R. W. Stobert, Director of Quality Assurance Operations

J. A. Silady, Nuclear Licensing

M. Wagner, Dresden Nuclear Group

M. G. Santic, Master Instrument Engineer

L. W. Raney, Nuclear Safety Braidwood

R. Weidner, Production Training

J. Dedin, Production Training

R. Graham, Nuclear Station Operator

E. McVey, Technical Staff

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General Electric Company (GE)

H. Pfefferlen, licensing

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G. A. Watford, Engineering

  • Denotes those attending the exit meeting on Marcil 24, 1988.

In addition, several other members of the LaSalle staff were contacted by

the AIT.

II.

DESCRIPTION - DUAL RECIRCULATION PUMP TRIP EVENT OF MARCH 9,1988

A.

Narrative Description

On Wednesday, March 9, 1988, around 5:32 p.m. CST, the LaSalle Unit 2

reactor was operating at steady state conditions at approxir.iately

84% power with 76% rated core flow using both recirculation (RR)

pumps and with the control rods withdrawn to the 99% flow control

line.

Feedwater temperature was 402 F.

LaSalle Unit I was

operating at power in steady state conditions and was unaffected by

the subsequent events on Unit 2.

Instrument Maintenance Technicians

(IMs) were in the process of performing a surveillance test on Wide

Range level instrument 2B21-N0378B to check the Reactor Core

Isolation Cooling (RCIC) initiation function at -50 inches reactor

level.

The IMs were stationed at the instrument rack and in the

control room and had received permission from the appropriate

operations personnel to perform the surveillance.

The IM at the

instrument rack had correctly isolated and equalized the instrument

(2821-NO378B) in accordance with the functional test procedure,

LIS-NB-404.

The next action was to open the test / vent valves,

however, instead the IM technician opened the isolation valves to the

variable and reference legs to the instrument.

Since the equalizing

valve was still open, a pressure equalization occurred between the

variable and reference legs for this instrument and all the other

instruments which share the same reference leg. At the time of the

valving error feedwater level control was selected to channel B

which takes input from an instrument which utilizes the same

reference leg as 2821-NO37B8.

The equalization produced by the

valving error resulted in a high "indicated" level to feedwater

level control, causing the operating feedwater pumps (A turbine

driven reactor feedwater pump - TDRFP, and the motor driven reactor

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feedwater pump - MDRFP) to begin reducing flow.

The IMs realized a

valving error had been made and attempted to correct the error by

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shutting the reference and variable leg isolation valves.

This

action caused a pressure pulse on the reference leg of all the

instruments which share the same reference leg at that instrument

rack.

Increasing pressure on the reference leg caused the level

instruments to indicate low reactor vessel level. The key instru-

ments which were affected by this pulse were the ATWS RR pump trip

switches 2B21-N036C and 2B21-N0360, which are designed to trip the A

and B RR pumps to off.

Both RR pumps did, in fact, trip off.

Instrument 2B21-N024B which provides a reactor protection system

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(RPS) channel B1 low level 1/2 scram was also affected and resulted

in.a 1/2 scram signal and the associated alarm.

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The trip of the RR pumps resulted in a large and rapid power

reduction (approximately 45%) as a result of the large flow

reduction (to natural circulation conditions).

The control rods

remained in their pre-RR pump trip position on the 99% control line

(see Attachment No. 3-BWR Power to Flow Map). This region of the

BWR Power to Flow Map was known to be susceptible to instabilities

in some BWRs. As a result of the large drop in power, a large drop

in steam flow occurred causing large changes in extraction steam

flow and extraction steam pressure.

Extraction steam supplies the

heating to the feedwater heaters. The changes in extraction steam

caused severe perturbations in the feedwater heater level control

system due to water flashing to steam from lower shell pressures,

reductions in shell side input from reduced steam flow, and changes

in condensing rate. The feedwater heater level control was unable

to react fast enough to control the large load reduction and tripped

the extraction steam input to the heaters in order to prevent

induction of water into the main turbine.

The st. curing of steam

heating to the feedwater heaters resulted in cooler feedwater being

supplied to the reactor (approximately 45'F decrease in 4 minutes)

which is the equivalent of a positive reactivity addition. This

resulted in an increased power to flow ratio which further reduced

the margin to instability.

At this point in the event, the operators in the control room were

primarily concerned with attempting to restore feedwater heaters.

The operators had correctly determined that an ATWS event had not

occurred but that an instrument problem had resulted in the loss of

both RR pumps.

The loss of feedwater heating was r.ot unexpected for

the large power drop caused by the RR pump trip.

The operators also

realized that the reactor was operating in a region of the power to

flow map where instability was possible. Between 4 and 5 minutes into

the event, the Average Power Range Monitor (APRM) indications were

observed by the operators to be oscillating between 25% power and

50% power every 2 to 3 seconds and the Local Power Range Monitor

(LPRM) down scale alarms began to annunicate and clear.

(Later

examination of the STARTREC, Startup Transient Recorder, (a high

speed, multi-channel recording system installed for startup testing

which starts recording when selected parameters exceed predetermined

limits) showed the oscillations to be much larger than the operators

were able to see).

The APRM indications confirmed the onset of

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instabilities and the operators attempted to restart a RR pump in

order to increase flow to leave the instability region. Attempt 3 to

start a RR pump were unsuccessful and the shift commenced preparations

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to manually scram the reactor. About 7 minutes into the event and

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before the shift was able to perform a manual scram, the reactor

automatically scrammed on high neutron flux as seen by the APRMs.

The scram shutdown the reactor as designed and recovery from the

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scram proceeded normally.

Some m r r equipment problems occurred

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during recovery and subsequent - shutdown, however, these were

judged by the AIT to have no ef.a t on the event and will not be

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discussed further in this report.

Tne licensee informed the NRC

at 6:32 p.m. CST of the RR pump loss, feedwater heating loss and

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resultant scram.

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B.

Sequence of Events

Times and sequences of events in the previous narrative description

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were derived by the AIT from a combination of interviews and hard

data.

The following sequence of events represents a compilation

of information by the AIT taken from the alarm printer, the Startrec

recording system and interviews with licensee personnel. Times are

given in 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> clock time (17:32 equals 5:32 p.m.) and are all

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Central Standard Time.

SEQUENCE OF EVENTS FOR MARCH 9, 1988

LASALLE UNIT 2 INSTABILITY EVENT

Initial Conditions

84% Reactor Power (930 MWe)

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Steady State Conditions

99% Flow Control Line

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76% Rated Core Flow (82 x 10 lb/hr)

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Feedwater Temperature = 402 F

LIS-NB-404 in process (Surveillance that tests RCIC initiation

at -50" reactor water level .)

Event Summary

March 9, 1988

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Time

Event

17:32 (approximately)

Instrument Maintenance Technician valved

in the variable and reference legs of a

differential pressure switch with the

equalizing valve open; initiating a

pressure equalization between the two legs

and a high "indicated" reactor level.

17:32i33

High Reactor Water Level Alarm initiated.

STARTREC (Startup Transient Recorder)

initiated on increase in narrow range

level and ran for programmed 1 minute

duration.

Instrument Maintenance Technician corrected

valving error by isolating reference leg

from variable leg which resulted in a low

"indicated" level spike cauting other

instrumentaticn to actuate.

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17:32:49

2A/2B ATWS alarm initiated a trip of both

Reactor Recirculation (RR) pumps and power

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and flow began coasting down to natural

circulation levels.

Division 2 Reactor

low Level Alarm initiated.

2A ATWS cleared.

17:32:50

Half scram-on +12.5" reactor water level

initiated,

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2B AiVS cleared.

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Division 2 Reactor lo Level Alarm cleared.

Reactor Water Level 3 Alarm (+12.5") initiated.

17:32:51

Reactor Water Level 3 Alarm cleared.

Reactor Water Level Hi Channel B trip.

17:32:52

Reactor Water Level Hi Channel B was

manually reset.

Half Primary Containment Isolation System

(PCIS) level trip was manually reset.

Nuclear Station Operator (NS0) saw that

B narrow range reactor water level

indicator was approximstely 30" and rising

while A and C were steady at approximately

40".

17:33:10

First feedwater heater high level alarm

annunciated.

17:33:20

First feedwater heater isolates.

Feedwater

heaters continue to isolate for duration

of event.

Unit 2 NSO reviewed feedwater heater

situation and planned to reopen extraction

steam valves after valves fully closed to

regain feedwater heating.

Shift foreman discharged to local heater

controllers to aid in reestablishing feed-

water heating.

17:36(approximately)

Shift engineer entered control room.

Operators observed APRMS oscillating

between 25% and 50% power with an

approximate 2-3 second period.

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Operators attempted to restart the RR

pumps per abnormal operating procedure,

LOA-RR-07.

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B RR flow control valve locked up.

Equipment Operator discharged to reset the

lockouts on flow control valves.

17:37:21

First LPRM downscale alarm annunciated. The

LPRM downscale alarms continued to flash

and clear, on a 2 second period.

17:37:51

First LPRM Hi Alarm annunciated.

17:38:20

The A flow control valve was reset.

STARTREC initiated on increase in narrow

range level and ran for 1 minute.

NSO ramped the A flow control valve to

minimum position.

17:39(approximately)

NS0 attempted restart of 2A RR pump twice,

but was unsuccessful.

Shift Engineer directed a manual scram to

be initiated.

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17:39:19

STARTREC terminated its second 1 minute run.

17:39:23

Channel A neutron APRM trip.

17:39:25

Channel B neutron APRM trip.

Reactor scrammed on 118% neutron flux.

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NOTE:

Designates that ne Hathaway Recorder time was available for the

event.

However, the event is listed in the approximate sequence

in which it occurred.

III. INVESTIGATIVE EFFORTS

A.

ynopsis of AIT Activities

The AIT members had all arrived onsite on March 17,1988.

~1 were

thoroughly briefed on the event by the licensee and Gen'-r) Ilectric

personnel in a meeting at the site at 1:00 p.m. hours c: Aoch 17.

The team was provided with pertinent instrument records d the

event (including Sequence of Events data), and with documentation

comprising the safety evaluation by the licensee. The latter

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included correspondence between the licenses and the reactor vendor

(GE),

In response to a team request, the 1.censee also provided a

written description of the operator response and assessment'of the

event as it occurred.

The inspection team had various meetings with the LaSalle plant

management and staff and with GE supporting staff during the

assessment of the event.

Subsequent to telephone conferences with

Headquarters and Region III offices, the plant was allowed to

restart at approximately 10:45 p.m. on March 17.

Operation was to

be under operating procedures which had been modified by a standing

order to require manual scram after trip of the recirculation pumps

in Operating Modes 1 or 2.

The AIT investigation continued with interviews of control room

operating personnel and a walkdown of the control room response to

the event.

The AIT documented several issues and concerns which

were presented to the licensee at a preliminary exit meeting on

March 18. The AIT concluded onsite activities with an exit meeting

on March 24, 1988.

B.

Core Nuclear and Thermal Hydraulic Performance

1.

Core Performance

In general, the AIT confirmed the adequacy of the assessment

of core performance performed by the licensee and the reactor

vendor.

Several concerns and questions, however, were

developed by the AIT and these are discussed in the Concerns

and Recommendations portion of this report (paragraph IV).

The following paragraphs provide a discussion of core

performance during the event.

Following the trip of the RR pumps, Core Thermal Power (CTP)

decreased and stabilized within about 30 seconds at about 40%.

The APRMs showed stable indications (the APRMS read neutron

flux as distinguished from CTP, however, both were stable at

this point). As feedwater temperature decreased, CTP increased

slightly to 43%. At approximately 4.8 minutes after the RR

trip, the APRMs began oscillating and the LPRM down scale

alarms were received. At 5.8 minutes after the RR pump trip,

the STARTREC system initiated its second recording for the

designed 1 minute period and stopped about 8 seconds before

the full scram.

STARTREC information is not available to the operators in the

control room at the time of recording, so from the APRM

recorders in the control room, the operators believed the

oscillations were approximately 25% power (neutron flux) in

magnitude (between 25% and E0% power) every 2 te 3 seconds.

Analysis of the STARTREC traces showed APRM peak to peak

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oscillations ranging from 20% to about 95% power.

Extrapola-

tion of the traces to the time of the scram leads the AIT

to believe the oscillations were at least 100% peak to peak

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when the scram occurred.

The oscillation frequency was

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approximately 0.45 hz.

The approximately 2 second period of

the oscillation is driven by core flow hydraulic conditions,

primarily the time it takes a void perturbation to travel the

length of the fuel . The APRMs measure neutron flux and during

reactivity changes the neutron flux leads the fuel cladding

heat flux by the thermal time constant of the fuel

pellet / pellet-clad-gap arrangement.

This time constant is

pproximately 6-7 seconds and acts to filter neutron flux

spikes. Consequently, the heat flux oscillations for this

event are estimated to be less than 10% of the neutron flux

oscillations cycling around an average CTP of about 45% during

the final minute of STARTREC recording.

Based on LPRM alarm

signals at 87% APRM power and LPRM readings after pump trip,

the AIT estimates that the peaking factor increased from 2.11

price to the event to a value of 2.65 at the time of the APRM

alann. This corresponds to a peak neutron flux level of 312i

(relative to rated core average) at the 118% APRM scram level.

However, because of the smaller changes in heat flux, the 13.4

Kw/ft fuel design limit was not exceeded and no core damage was

indicated by chemistry results.

One of the more important considerations in this type of event

is whether the LPRM swings are in phase with the APRMs or not.

The reason for this concern'is that the core protection actions

are actuated by the APRM signals, so, if some LPRMs were

oscillating out of phase with the core average, the effect

would be to lower the APRM signals that these LPRMs feed.

Consequently, the effectiveness of the APRMs as a protective

system would be less and local areas of the core would be

undergoing oscillations of much greater magnitude than

indicated by the APRMs. Analysis of the alarm printout of the

LPRM downscale and LPRM hi alarms, the "clean" sinusoidal wave

shape, and the in phase APRM traces from STARTREC by the

licensee and the reactor vendor (GE) determined that the LPRMs

and APRMs were in phase with each other.

The AIT verified this

analysis and concurred with the licensee's interpretation.

This type of oscillation is less severe with lower power peaks

to trip than would occur with regional oscillations which have

becn observed in foreign reactors. Generic analyses performed

during the resolution of Generic Issue B-19 bound the LaSalle

Unit 2 instability and demonstrated that the fuel thermal or

mechanical limits were not exceeded during the event.

General Electric's evaluation of the LaSalle event concluded

that the frequency and magnitude of oscillations which Unit 2

experienced were consistent with the characteristics cbserved

during stability testing and operation at other BWRs. GE

further concluded that the event was bounded by the generic

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analysis and that no fuel thermal or mechanical limits were

exceeded during the event. While the AIT did not agre.e or

disagree with the GE conclusions at the time of exit, there

were several questions and concerns relating to unexpected

aspects of the event which required further study. These

included the following:

(1)

failure to predict the susceptibility of the Unit 2 core

to thermal hydraulic oscillations based on the calculated

decay ratio.

(2) magnitude of the oscillations compared to previous events

with similar behavior,

(3) potential for out of phase regional oscillations of much

larger magnitude and the lack of a defined boundary based

on inherent shutdown mechanisms,

(4)' questions about the adequacy of instrumentation for

detection, suppression, and evaluation of limit cycle

neutron flux oscillations, and

(5) questions about the adequacy of technical specifications

and procedures for detection and suppression of neutron

flux oscillations.

These issues are discussed in more detail in paragraph IV,

"Concerns and Recommendations".

2.

Chemistry Results

Following the scram on March 9,1988, the LaSalle Station

Chemistry Department took post shutdown samples of the reactor

coolant water in order to determine if there were any

indications of fuel damage. Analysis of the iodine result

fromthissampleindicatednoabnormalities(between2x10~3

5

and 1x1f microcuries per gram for iodine 131 through 135

ThereactorwaterdoseequivalentI-131waslessthan2x10}4

microcuries per gram as compared to a Technical Specification

limit of 0.2 microcuries per gram.

This data, as well as the

past two months sample data for both Units 1 and 2, was made

available to the AIT for verification by the licensee. At a

result of the CAL, the licensee developed an increased

frequency sampling program of reactor water and off gas which

was implemented following restart of Unit 2.

The results of

this sampling are documented in Attachment 5 and show no

indications of fuel damage or abnormalities from readings prior

to the event.

10

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3.

Equipment Performance

The following paragraphs summarize the AIT's conclusicas

regarding the performance of specific systems or pieces of

equipment during the event. By the CAL, the licensee was also

requested to address equipment performance and that assessment

is included in Attachment 5.

(a) Recirculation Pumps and Flow Control Valves

A trip of both RR pumps is a designed feature of the

LaSalle plant in order to cause a power reduction in the

event of an ATWS, as indicated by a loss of reactor level

without an associated scram.

The pressure pulse on the

reference leg of the ATWS switches appeared to be

sufficient to provide this indication and consequently

the trip of both pumps occurred as would be expected.

During the RR pump trip recovery, the operators attempted

to restart the RR pumps and were unsuccessful. At the

time of the exit, the RR pump start failure was believed

to be due to the failure to satisfy one of the pump start

interlocks.

Exactly which interlock was not satisfied was

not conclusively determined, however, likely candidates

include the recirculation flow control valve not fully

in minimum position and the hi speed start permissive

(depends on feedwater flow). The operators have no

indication available in the control room to determine

which DD

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follow

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NSO wat

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vas not reset Decause there was an

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abnormal signal alarm which would have required additional

operator actions.

FCV lockout was not fully investigated

4

by the AIT.

i

11

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,

.

f

l

b.

Feedwater Heaters

Shortly after the RR pump trip, the feedwater heater level

control system began isolating extraction steam from the

heaters in order to protect the turbine from water

induction. The resultant cooler feedwater which was

supplied to the reactor caused the reactor to become even

more susceptible to instability. The AIT reviewed the

feedwater and feedwater heater performance and concluded

that the feedwater heater actions were as expected and had

been seen before for similar large rapid drops in load.

A more complete description is provided in Attachment 5.

This observation, however, negated an initial licensee

statement that two abnormal conditions, operation at high

power in natural circulation and reduced feedwater heating,

were necessary to put the reactor into the unstable

region, in that, feedwater heating would be expected to

be lost every time both RR pumps were lost from high

power. The AIT believed the licensee efforts in investi-

gating the performance of the feedwater system were

appropriate,

c.

Power to Flow Scram (APRM flow-biased trip)

Since the reactor ends up at lower power following a RR

pump trip, and the reactor eventually scrammed on high

power in terms of APRM flux, concern was expressed over

the operation of the power to flow or APRM flow-biased

trip.

The APRM flow-biased trip is designed to protect against

spurious scrams due to transient events that cause spikes

in neutron flux. APRM neutron flux correlates to thermal

power level during steady state conditions. However,

during power increase events the APRMs will over-predict

themal power because the neutron flux leads the reactor

heat flux due to the thermal time constant of the fuel and

cladding.

It should be noted that no credit is taken for

the flow-biased scram in the transient analysis; only the

120% high flux scram is credited.

The APRM flow-biased trip circuitry receives the APRM

neutron flux signal and filters it through an R-C circuit

with a 6 second time constant. This R-C circuit which

is known as the "themal power monitor" essentially

integrates the APRM neutron flux signal over the past 6

seconds and develops an APRM reading which simulates

thermal power by :ccounting for the lag in response of the

fuel cladding heat flux to neutron flux variations.

The

output of the thermal power monitor is then compared to

the flow-biased scram setpoint which is calculated by the

equation:

S=0.66 WD + 51%. W is the driving flow which

D

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t

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_ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ -

_

.,

.

.

that at 6.9 minutes following the RR pump trip, RPS APRM

channels A and B actuated to produce the full scram.

APRMs A, C, and E all indicated neutron monitoring trip

and are grouped as channel A in the logic scheme'. 'No

trip indications appeared for t.he D and F APRMs which is

believed to be due to the fact that the B APRM signal

completed the logic and actuated the scram.

The

licensee's review included a functional check of the APRM

trip setpoints following the event, a comparison utilizing

gain adjustment factors, and an evaluation of whether the

flux oscillations could have been missed by the scram

logic. The AIT concurred in the licensee's conclusion

that the Reactor Protection System performed as designed.

The licensee's investigation of RPS performance was

appropriate.

e.

Anticioated Transient Without Scram (ATWS)

The oni; ATWS mitigation equipment actuated by the event

was the dual RR pump trip actuated by the pressure pu'se

,

to the ATWS RR pump trip switches' reference leg.

T'.ie s e

functioned as designed to trip off the RR pumps on

indicated low reactor level. The operators spent the

first 20-30 seconds after the RR pump trip and associated

alarm confirming that no condition existed which required

a scram without a scram occurring, hence no ATWS. The

available recordings also confirmed no other ATWS

actuations, which is consistent with the personnel

interviews and the initial valving error, in~that, no

other ATWS actuations would be expected.

l

C.

Operator Performance

On March 17, 1988, as part of the AIT charter, members of the

l

inspection team interviewed the on shift operators and supervisors

l

who had been assigned to Unit 2 during the March 9, 1988, reactor

power oscillation event.

The licensee's view of operator actions

is included in Attachment 5.

,

l

l

Personnel in the control room at the time of the event included the

IM personnel performing the surveillance on a headset with the

i

technician at the instrument rack, an NSO at each unit, the Center

Desk NSO (who operates Unit 1 and Unit 2 common systems) and the

l

Shift Centrol Room Engineer (SCRE).

The first indication of a

i

problem was a hi level alarm (due to the initial equalization

valving error).

Th:s brought the Center Desk Operator (CD0) over

to the feedwater control station to assist the Unit 2 NSO. As more

alarms came in (low reactor level and 1/2 scram due to the second

valving error and resultant pressure pulse) the Unit 2 NSO stationed

himself at the RR panel. Based on available indication and the fact

that an instrument surveillance was in progress, the operators

suspected an instrument problem. The Unit 2 NSO determined that he

14

,

4

.

is zero when both reactor recirculation pumps are tripped.

Therefore, the scram setpoint (S) during the instability

event was 51%.

.

Although peak APRM readings reached 118%, the peak output

of the thermal power monitor during the instability event

was approximately 42% to 45% because of the effect of the

R-C circuit on the APRM signal. Therefore, the flow-

biased scram never reached its setpoint of 51% and the

reactor tripped on high neutron flux at 118%.

d.

Reactor Protection System (RPS)

From a review of the alarm printer data, the STARTREC

information and interviews with operating personnel, the

AIT verified that the only RPS actuation setpoints

exceeded were those associated with the initial valving

errors and related pressure pulsing of the reference leg

which started the event and the APRM hi flux scram which

ended the event.

The RPS instrumentation which shares the refarence leg

with 2B21-N037BB consists of Level 3 (+12.5 inches

setpoint), Level 2 (-50 inches setpoint), or Level 1

(-129 inches setpoint) differential pressure indicators

and straight pressure indicators.

The pressure pulse

caused by the valving error is believed to have caused the

instruments to see about -40 inches reactor level (or a

pulse equal to about 80 inches of water column).

This

pulse would equal about 2.9 psig which would be too small

to affect any of the pressure instruments significantly.

This corresponds to the alarm printout which indicates no

pressure instrument actuations.

The 40 inches level would

also be expected to be too small to have affected the

Level 1 (-129) or Level 2 (-50) instruments, but would

have been expected to actuate the Level 3 instruments.

No Level 1 actuations were indicated by the alarm printer.

However, the ATWS RR pump trip switches 2B21-N036C and

2B21-N036D which did trip the RR pumps are Level 2

switches.

This indicates the pulse was either larger than

able to be seen by the level transmitter feeding STARTREC

or the switch trip setpoints were conservatively high.

Consequently, other Level 2 actuations may or may not

have occurred depending on setpoint and the strength of

the pulse as seen by the instruments. All of the Level 3

switches actuated as would be expected, including the RPS

channel B1 low level alarm and 1/2 scram and the Automatic

Depressurization System confirmatory alarm. Both of these

are confirmed by the alarm printout.

With regard to the APRM hi flux scram, the licensee's On

Site Review (OSR) had concluded (from the alarm printout)

13

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4

..

had lost RR flow and that ATWS alarms were indicated.

At that

point, efforts were concentrated on ensuring that a valid ATWS event

was not occurring.

,

The Station Control Room Engineer (SCRE) responded to the initial

alarms and, remaining cognizant of his position as the SCRE,

positioned himself such that he could clearly observe operator

actions and reactor parameters.

He then contacted the Shift Engineer

(SE).

l

By this point, the NS0s had determined a valid ATWS did not exist

I

and had directed the IM personnel to stop their surveillance.

Multiple feedwater heater alarms were occurring and many of the

heaters were isolating extraction steam due to the rapid power

reduction. A shift foreman had been sent to the local heater

control panels to help restore feedwater heating. At about the time

of the Shift Engineer's arrival in the control room, preparations

were being made to attempt to restart the RR pumps and power

oscillations of 25'. magnitude ranging from 25'4 to 50*. began to be

seen on the APRM recorders.

The SE, upon arriving in the control

room, quickly assessed the status of the unit, reviewed the

operators' actions, and assumed responsibility for efforts to

recover from the reactor power oscillations. At this point,

operators were uncertain of the specific actions they should be

taking once the power oscillations were observed. The procedures

and training appear to have been inadequate. The operators all

recognized that they were in the region of core instability, but

were uncertain of what actions should be taken.

The procedures

basically instruct the operator to leave the region of instability

without directing "how".

Thoughts included; (1) driving in control

rods in sequence, (2) using the "CRAM" array of control rods, (3)

starting a RR pump, and (4) scram the plant. Operators felt that

driving in control rods in sequence would have been too slow in that

the first rods to go in would be rods of little reactivity worth.

Use of the "CRAM" array of control rods was addressed only in the

licensee's procedures pertaining to a loss of feedwater heating

consequently operators were uncertain if they should use the "CRAM"

array in this condition of 2 RR pump trip and loss of feedwater

heating.

The operators did not want to scram the plant if they

did not have to.

Therefore, they decided to try and leave the

instability region by restarting a RR pump (either a flow increase

or a lowering of the rod line would get the reactor out of the

unstable region) which they may have accomplished if the RR pump

start sequence could have been satisfied.

It is also likely that

if a RR pump had been successfully started, the reactor may have

scrammed anyway on the resultant power increase.

As the operators

were unsuccessful in starting a RR pump and were preparing for a

manual scram, the reactor scrammed automatically.

The AIT evaluated the response of the individuals versus the

information they had available, and has the following observations.

15

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With the exception of the personnel error by the instrument

mechanic (IM) that started the transient, the AIT has concluded

that the personnel on-shift at the time of the event took

prompt corrective action in accordance with the procedures

and training available to them.

The AIT believes that the

operators could have taken better corrective action by driving

in control rods, but that this direction was not provided by

procedures or training.

The procedures available to the operators at the time of the

event appear to be inadequate in that they don't specifically

address the necessary action to be taken in order to exit the

region of instability. General Electric Company's Service

Information Letter (SIL) No. 380, issued February 1984,

addressed the issue of core stability and the actions to be

taken if there were a RR pump (s) trip and the core entered the

region of instability. The GE SIL had not been incorporated

into the licensee's procedures or training.

This issue is

further discussed in paragraph III.D.

D.

Procedure Adequacy and Training

1.

Technical Specifications (see Attachment 4)

The LaSalle Unit 2 Technical Specification (TS) 3.4.1.1.b

contained the requirements for loss of both RR pumps or "no

reactor coolant system recirculation loops in operation".

The TS states "immediately initiate measures to place the unit

in at least HOT SHUTDOWN within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />." The

defined actions, however, were not prescriptive for the seven

minutes in which the operators had to act for this event.

The

TS for loss of a single RR pump 3.4.1.1.a. in step 3.4.1.1.a.2a) 2)

discusses increasing core flow.

While the reactor was not in

this condition (both RR loops were not operating versus one),

the operators were aware of this TS, the associated surveillance

requirements and the fact that increasing flow would get the

reactor out of the unstable region of the power to flow map.

These considerations in their own minds served to back up the

operators decision to restart RR pumps.

The NRR representa-

tives on the AIT were familiar with the development of the

LaSalle TS and indicated that part of the reason that LaSalle

did not have more specific TS was that the Unit 2 decay

factor was submitted as 0.60.

With this much margin to a Limit

Cycle Oscillation decay factor of 1.0, it was believed that

the probability of oscillations at LaSalle would be very low.

Since oscillations have now been observed and the decay factor

calculation is in question (see Concerns paragraph IV), the

AIT believes that the TS were inadequate.

2.

GE SIL 380 Revision 1 (Attachment 7)

In 1984, GE issued SIL 380 Revision 1 containing recommendations

regarding BWR Core Thermal Hydraulic Stability. This document

16

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.,

.

.

discusses RR pump trip and recommends, "Immediately reduce power

by inserting control rods to or below the 80*4 rod line using

the plant's prescribed control rod shutdown insertion. sequence."

Further, the SIL recommends that the operation of restarting

recirculation pumps should be performed from below the 80* rod

4

line.

These recommendations were not incorporated into

LaSalle's TS or abnormal operating. procedures.

Like with

TS, part of the motivation to not incorporate these recommend-

ations into procedures was based on the margin to instability

provided by the calculated decay factor as well as a skeptical

attitude regarding the susceptibility of the LaSalle reactors

to instability.

3.

Abnormal Procedures and Training

The LaSalle abnormal operating procedures (LOAs) and the

associated surveillance procedures (LOS) and general procedures

(LGP) provided only general guidance regarding what to do in

the event of loss of single or two loop recirculation flow.

While guidance and training had been provided to all the

licensed operators on how to recognize the onset of

instability, there was little guidance provided on what to do

next, other than performance of the TS required surveillance

and to leave the region of likely instability.

The loss of

recirc flow procedures were directed at restarting RR pumps.

The AIT concluded that the operators reacted as their training

and procedures led them, in that, they recognized very well the

onset of instability, however, interviews indicated they were

confused and uncertain as to how to exit the region.

The AIT

believes that both the abnormal procedures and the training

were inadequate in this regard.

4.

Simulator Training

The licensee attempted to simulate LaSalle's instability event

on the simulator, but was unsuccessful.

The event could

possibly be simulated with the instructor interacting with the

computer, however to produce an accurate, detailed simulation

a new program must be written.

Currently, the Production

Training Software Group has the data from the actual event and

is reviewing possible changes.

The licensee stated that they

expect a permanent program will probably be available by

July 1988 and they will keep the resident informed on the

status of the changes.

E.

Reporting

As the nature and magnitude of the core power oscillations on

,

i

LaSalle Unit 2 became widely disseminated and understood such that

the AIT was formed on March 16, 1988, several questions were raised

'

regarding the adequacy of the licensee's reporting of this event.

These questions were in large part motivated by the fact that

17

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.

the majority of the NRC staff did not learn of the core power

oscillations aspect of the event until issuance of the Region III

morning report update on March 15, 1988, even though the event had

occurred on the evening of March 9, 1988.

The AIT examined the

reporting aspects of this event through interviews, individual

recollections and available tape of phone conversations.

The

following summarizes the team's observations.

1.

Reporting Sequence

(a)

Following the trip of the RR pumps and the subsequent

scram at about 5:39 p.m. on March 9, 1988, the licensee's

initial investigation classified the event as reportable

to the NRC within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> under the provisions of 10 CFR 50.72 due to actuation of the Reactor Protection System

(RPS).

The licensee actually notified the NRC within 1

hcur at about 6:32 p.m. on March 9,1988.

The initial

phone call communicated information on the RR pump loss

due to personnel error, loss of feedwater heating and

reactor trip on high APRM flux.

No mention was made of

the core power oscillations, however, the licensee's caller

stated, "we are still investigating all our alarm typers

and everything else." Com.ments were made to the AIT that

the licensee's caller sounded almost jovial over the

phone.

After listening to the tape of the 50.72 call,

this observation was explained to the AIT's satisfaction

in that the NRC Headquarter's Duty Officer (HDO) and the

licensee's caller recognized each other's voices from

previous association and exchanged pleasantries.

This

'

situation did not appear to detract from proper communica-

tion of information.

(b) The HD0 contacted the Regional Duty Officer (RDO) at 7:21

p.m. CST, who, in turn, notified the Cognizant Section

Chief (also AIT leader) and Branch Chief.

(c) At approximately 7:00 p.m. CST on March 9, 1988, the

licensee and the Resident Inspector (RI) succeeded in

establishing contact and the RI was briefed regarding the

event.

The RI was offsite attending the Region III

Resident Seminar (March 8-10).

The licensee informed the

RI that the APRMs had oscillated between 25-50% during

,

the event and that the reactor had scrammed on APRM high

flux at 118% setpoint.

At this point, the RI did not

appreciate a significant concern with the APRM oscillation

in that oscillations are a potentially expected phenomena

given the parameters of high reactor core power and low

reactor core flow.

1

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(d) On March 10, 1988, at approximately 10:00 a.m., Region III

issued a morning report describing the event.

No mention

of oscillations was made in this report.

The high power

scram was attributed to a power surge caused by the cold

feedwater.

(e) At approximately 12:30 p.m. on March 10, 1988, the Region

III Section Chief contacted the LaSalle Station Manager

for the purpose of ensuring the information in a Preliminary

Notification (PN) was correct.

During this conversation,

the Station Manager pointed out that while the PN was

'-

substantially correct, the unit had experienced some

neutron flux oscillations during the event which were

being evaluated. The Region III Section Chief did not

include any information on the oscillations in the PN

based on the evaluation still being in progress.

(f) On Ma.ch 11, 1988, the RI returned to the site and

participated in several discussions with the licensee

involving the event including a meeting where the STARTREC

traces showing the oscillations (20%-95%) were made

available. The RI was informed that the licensee had

involved GE in the evaluation and that GE had indicated

the oscillations were within analysis bounds and provided

for by the APRM high flux scram. Also, on March 11, 1988,

the Station Manager contacted the Region III Section Chief

and provided additional information including an

explanation of the reactor's position on the power to

flow map, the effect of the loss of feedwater heating, and

the onset of flux oscillations.

During this call, the

Section Chief does not recall that the magnitude of the

oscillations was discussed, but, rather the Station Manager

indicated the oscillations were being evaluated and the

reactor vendor was involved.

The Station Manager indicated

that GE felt the oscillations were within analysis bounds,

that the core performed as expected for the conditions and

he offered to make a presentation on the event to Region

III if desired.

The Section Chief indicated this may be

a good idea but wanted to wait until the RI and possibly

Region III core physics inspectors had a chance to look

at the data.

Following his review of the available

information, the RI contacted the Section Chief on

March 11, 1988, and comunicated the oscillation infoma-

tion which indicated the event was more severe than

initially believed. At this point, the Region III Branch

Chief and Division Director were informed that flux

oscillations had occurred but were within analysis and a

more complete description would be available on Monday,

,

March 14 following the RI's further investigation.

The

NRR Projects Office was similarly informed.

19

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(g) On March 14, 1988, the RI was given a copy of CECO's

Potentially Significant Event (PSE) report and an advance

copy of a Rapid SIL generated by GE addressing the event.

Due to following up on additional information on the event

and the length and complexity of the morning report, the

RI was unable to get the report documented and transmitted

by the 10:00 a.m. deadline on March 14, 1988.

Since

Region III was waiting for further information from the

site, no additional actions were taken by the Region on

March 14, 1988.

'

(h) On March 15, 1988, the Region III morning report update

describing the event, including the oscillations, was

disseminated, resulting in the formation of the AIT on

March 16, 1988.

2.

Reporting Evaluation

In the AIT's view, the licensee correctly classified the event

on the initial call on March 9, 1988, as being 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

reportable based on the requirements of 10 CFR 50.72 for

an RPS actuation. While the initial call did not mention

oscillations, the caller stated that the information was still

being evaluated.

Consequently, the AIT believes the initial

call was satisfactory for as far as it went. However,10 CFR 50.72(c) requires the licensee to make followup notifications

in addition to initial notifications as follows:

(2) Immediately report (i) the results of ensuing

evaluations or assessments of plant conditions,

(ii) the effectiveness of response or protective

measures taken, and (iii) information related

to plant behavior that is not understood.

The licensee made no formal followup reports via the ENS

circuit (red phone) to the HDO.

The AIT believes that such a

followup call would have been appropriate since the occurrence

of oscillations and the nature and magnitude of the

oscillations would significantly add to the information

communicated on the initial call.

The AIT believes the

licensee felt that subsequent calls to the RI and the Region

III Section Chief would accomplish the intent of communicating

followup information. The AIT believes this to be incorrect

for two reasons.

First, the intent of 10 CFR 50.72 is to

l

describe the formal notification process which is to be

conducted over the ENS circuit and notification of other NRC

personnel (including the RI) does not relieve the licensee of

l

the responsibility to notify the NRC via ENS, Second, the

information communicated to the NRC in the subsequent calls was

-

insufficient to allow the NRC to appreciate the nature and

l

magnitude of the oscillations.

The NRC has a need for prompt,

pertinent information on this type event which is at least

'

equivalent to the information which the licensee furnished

'

to GE.

20

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IV. AIT CONCERNS AND RECOMMENDATIONS

A.

Concerns

-

The following paragraphs document concerns developed by the AIT

t

during the review of this event.

Several of these concerns were

discussed with the licensee prior to the exit and the licensee has

provided several responses in Attachment 5 to this report.

These

responses had not been completely evaluated at the time of the

writing of this report.

Other issues may require further study and

subsequent response.

1.

Decay Ratio

Decay ratio in a reactor is a measure of the response of the

neutron flux to a change or perturbation.

A decay ratio of

,

less than 1.0 indicates that the response to a perturbation

will decay to the steady state value (see Attachment 3, Figures

2, 3 and 4). A decay ratio of 1.0 represents the special

condition when the response to a perturbation will be a steady

state oscillation of constant magnitude (limit cycles).

GE predictive methods for determining BWR decay ratio were

approved with 20*4 uncertainty.

Predicted decay ratio for

LaSalle conditions was 0.60 (40*4 uncertainty) yet limit cycles

were observed.

The only obvious deviation from prediction

assumptions was in core water level and associated natural

circulation flow rate.

The 40% difference needs to be

explained. Have calculations been discredited as acceptable

evidence of core stability?

2.

Technical Specifications (TS)

BWR thermal hydraulic stability was the subject of Generic

Issue B-19.

Early BWRs were designed to maintain decay

ratios less than 0.5 (a decay ratio = 1.0 corresponds to an

undamped limit cycle oscillation).

Later core designs tended

,

towards decay ratios of 1.0 due to higher power density cores

'

and changing fuel design characteristics.

In the resolution of Generic Issue B-19, core designs which

were potentially unstable (DR = 1.0) under natural circulation

operating conditions were approved with the provision that

operating procedures and technical specifiestions would assure

that neutron flux oscillations indicative of core instability

would be readily detected and suppressed as required by GDC 12.

Licensees were informed by Generic Letter 86-02 that

such procedures and TS must be implemented for new reload

cores unless it could be demonstrated by approved calculation

methods that the core was stable throughout permissible

operating regions of the power / flow map.

Calculated core decay

ratios of less than 0.80 by General Electric methods were

approved as acceptable evidence of core stability,

j

21

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.

LaSalle Unit 2 did not have fully implemented procedures and

TS in accordance with the B-19 resolution because the

calculated decay ratio for the current operating cycle is

0.60.

LaSalle Unit 2 did have TS and procedures for

stability surveillance under conditions of single loop

operation (SLO). but had declined suggestions by the NRC staff

that these should also apply to two loop operation because

higher decay ratios were certain for future reloads.

The

licensee has been informed that revised TS are required for

Unit 2 now that oscillations have actually been observed.

LaSalle Unit 1 is currently under review for reload. The

licensee has been informed that stability technical specifi-

cations will be required for that reactor even though the

calculated decay ratio is 0.75 (indicative that it is less

stable than Unit 2).

Since several BWRs have higher decay ratios than LaSalle, the

issue of decay ratio in paragraph IV.A and stability TS is

considered generic.

Improved standard technical specifications

relating to stability need to be developed.

Further, the

implementation status of stability TS on all BWRs should be

reviewed with particular attention to the adequacy of require-

ments for response to loss of RR pumps.

The criteria for

applicability of stability TS based on decay ratio calculations

and reactor type should be reexamined.

3.

Instrumentation

The following concerns with the available instrumentation at

LaSalle were developed by the AIT:

The slow pen response time and chart speed of the APRM

strip chart recorders in the control room reduced

indicated amplitude of oscillations.

Time delay relays for the LPRM Hi and APRM Hi alarms

delay recognition.

Running Average of APRM signal in Power / Flow circuit

delays or prevents reactor trip at lower power levels

with reactor oscillations.

If oscillations are regional in nature and LPRM signals

are out of phase, LPRM inputs to APRMs will tend to cancel

each other so that oscillations are not evident on the

APRMs.

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Hi Speed Recording of APRM signals used for event evalua-

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tion was triggered by Low Water Level signal

- not

always a condition of the instability event. This data

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is needed to assess the nature and magnitude of neutron

flux' oscillations and the safety of restart after an

instability event.

-

LaSalle and some other BWRs do not have high speed data

recording instrumentation which can be' committed for

availability during plant operation.

4.

Oscillation Characteristics

Some characteristics of the LaSalle neutron flux oscillations

were atypical of previous events and have led to concerns about

the applicability of previous safety analyses.

The magnitude of

in-phase limit cycle oscillations previously observed on the

APRMs curing special stability tests and operating reactor

events were typically in the range of 5', to 15% (peak-to peak) of

rated power, and as high as 25%.

This compares to peak-to peak

values of about 100% at the time of the 118% neutron flux trip

for LaSalle.

The estimated value of local power at the time of trip was

greater than 310% and LPRM readings indicate that the core power

peak shifted and increa:ed by 25%.

Even though the fuel LHGR

limit of 13.4 kw/ft was not exceeded because of the thermal time

constant of the fuel, the increased power peaking was unexpected

based on Vermont Yankee stability tests, and was not factored

into the generic safety evaluation performed by GE during review

of the thermal hydraulic stability Generic Issue B-19.

The previous GE safety analyses considered several limiting

moderate frequency transients which were initiated while the

neutron flux was oscillating below the 120% scram setpoint, and

included a rod withdrawal error with the flux oscillating up to

the 120*. scram level . Additional analyses were performed to

evaluate the impact of oscillations that approached 300% of

rated neutron flux (e.g., regional oscillations) without scram

prior to rod insertion and termination of the event. All of

these analyses showed that significant fuel thermal margin

existed to safety limits. While there are several aspects of

these analyses which differ from LaSalle (initial power level

and amplitude of the oscillations; no change in bundle peaking

factors due to the event, etc.), the AIT agrees that they are

sufficiently representative and conservative to demonstrate that

no fuel thermal or mechanical limits were exceeded during the

event.

However, reliable detection and suppression provisions

are necessary to assure protection against future events which

could involve regional oscillations to higher power levels.

The licensee was also asked to review the impact of the event on

stability considerations addressed in the 1979 GE Generic ATWS

report, "Assessment of BWR Mitigation of ATWS" (NEDE-24222).

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The report does specifically investigate the sensitivity and

potential impact of limit cycle neutron flux oscillations up to

500% of rated bundle power following recirculation pum'p trip.

It was concluded that oscillations of this magnitude would not

result in sufficient fuel clad temperature variation (130'F) to

affect fuel integrity.

It was further concluded that a loss of

clad integrity due to prolonged exposure to limit cycles was an

acceptable consequence in view of the importance of the

recirculation pump trip (RPT) to minimize the energy deposited

-in the suppression pool (thereby maintaining containment

pressure within limits) during an ATWS event.

In view of the large magnitude of the APRM oscillations in

LaSalle, the AIT believes that the ultimate power level without

scram is unknown, and that the 500% level assumed in the ATWS

investigation may not be bounding.

LPRM oscillation magnitudes

more than seven times those of the APRMs have betn observed in

the case of regional oscillations. The licensee reports that

the BWROG is discussing this issue (inherent power limits) and

the licensee will provide a status report on July 1, 1988.

5.

Additional Concerns

Several additional concerns were presented to the licensee in

the form of questions. These questions and the licensee's

response are contained in Attachment 5 to this report.

B.

Recommendations

The A" recommends that the concerns identified in items IV. A.1

+'

,i IV.A.5 of this report be examined by NRR for generic and

sie specific resolution.

In the interim, the AIT recommends

that revised stability TS as discussed in IV.A.2 be developed for

LaSalle Units 1 and 2 and the licensee be authorizied via letter to

modify interim operating procedures provided they remain consistent

with the new T.S.

The revised technical specifications and

procedures should incorporate the changes summarized in Attachment 5

(Appendix A, Item 3), which include immediate insertion of high worth

rods and observation of APRM/LPRM noise when no pumps are operating

and power is above the 80% Rod Control Line. The reactor is to be

tripped immediately whenever instability is suspected.

It is

expected that the time available (greater than 5 minutes) to

instability following a two pump trip transient is sufficient to

permit manual power reduction, avoiding the need for reactor trip

unless the core is unstable by a large margin. Proposed procedures

permit manual action for up to two minutes (prior to scram) to

reverse operating actions which may result in small margins of

instability when one or both pumps are operating.

V.

AIT CONCLUSIONS

The AIT finds that the core power oscillations observed on LaSalle Unit 2

on March 9, 1988, were initiated by a aersonnel error resulting in the

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trip of both recirculation pumps compounded by the loss of steam heating

to the feedwater.

The licensee's evaluation of the event (including

assistance from the reactor vendor) is still continuing, however, -to date

is believed to have been thorough and proper.

No evidence of any fuel

damage has been noted related to the event.

Performance of equipment

during the event is believed to have been as designed for the conditions

encountered during the event. Operator performance, while it could have

been better, is believed to have been prompt, appropriately controlled and

within the bounds of the procedures and training available to them. Both

4

the procedures and training available to the operators are believed to

have been inadequate in that prudent recommendations of GE SIL 380 were

,

not incorporated and little direction was provided regarding what to do in

the event of instability.

Reporting is believed to have been inadequate

in that no formal followup report was made regarding the results of the

investigation and determination of flux oscillations.

The licensee's

response to NRC initiatives by shutting down, providing the AIT with

prompt and technically sound information and responding to the CAL is

believed to have been excellent.

Several concerns and recommendations on

'

this event remain to be followed as documented in paragraph IV.

On March 17, 1988, the AIT determined that the licensee had complied with

.

the restart provisioas of the CAL, includ ,g a requirement for a manual scram in the event of a loss of both recirculation pumps from an operating

condition, and the Region III Administrator's designee authorized restart

of LaSalle Unit 2 at 10:45 p.m.

The AIT and the licensee have agreed on

,

the essential features of revised technical specifications and operating

procedures to protect against this event during futur6 operation.

VI.

EXIT INTERVIEW

The inspectors met with licensee representatives (denoted in paragraph

I.D.) informally throughout the inspection period and at the conclusion

,

of the onsite inspection activities on March 24, 1988, and summarized

the scope and findings of the inspection activities.

The inspectors also discussed the likely informational content of the

inspection report with regard to documents or processes reviewed by the

inspectors during the inspection. While the inspectors did review some

proprietary material, none of the areas expected to be contained in the

report were identified by the licensee as proprietary.

The licensee

ackn1wledged the findings of the inspection

i

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CONFIRETORY ACTION LETTER

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CAL-RIII-88-03

Docket No. 50-374

Comonwealth Edison Company

ATTN: Mr. Cordell Reed

Senior Vice President

Post Office Box 767

Chicago, IL 60690

Gentlemen:

This letter confirms the telephone conversation between E. G. Greenman of

this office and you on March 17, 1988, related to the dual recirculation pump

trip and related core performance anomalies occurring at LaSalle Unit 2 on

March 9, 1988. With regard to this event, we understand that you will:

1.

Perform an evaluation of reactor performance during this event including

secondary systems, the reactor protection system, and ATWS systems.

2.

Perform an evaluation of operator performance during this event.

3.

Evaluate the adequacy of your Technical Specifications, operating

procedures, abnormal operating procedures, and emergency procedures with

respect to this event and vendor recommendations (GE SIL-380).

4.

Perfonn increased activity level sampling during Unit 2 startup to

verify no abnormalities.

5.

Submit to NRC Region III a formal report of your findings and conclusions

within 30 days of receipt of this letter.

Throughout this investigative effort, we understand that you will take those

actions necessary to ensure that complete documentary evidence of the

conditions being examined is maintained, and furnished to the NRC's Augmented

Inspection Team which was initiated on March 16, 1988.

Q&$WV

y

CONFIRMATORY ACTION LETTER

_

CONFIRMATORY ACTION LETTER

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Comonwealth Edison Company

2

We further understand that startup of Unit 2 will occur after a detennination

has been made by the AIT Team Leader that equipment performance was satisfactory,

including verification of reactor coolant samples, and that interim procedural

changes are satisfactory including a requirement to trip the reactor if no

reactor recirculation loops are in operation, and the reactor is in operational

conditions 1 or 2, and with concurrence of the Regional Administrator or his

designee.

Issuance of this Confinnatory Action Letter does not preclude the

issuance of an order requiring implementation of the above commitments.

None of the actions specified herein should be construed to take precedence

over actions which you feel necessary to ensure plant and personnel safety.

Please advise us immediately if your understanding differs from that set

forth above.

Sincerely,

Orignial Signed by A. Bert Davis

A. Bert Davis

Regional Administrator

cc:

D. Butterfield, Nuclear

Licensing Manager

G. J. Diederich, Plant

Manager

DCD/DCB (RIDS)

Licensing Fee Management Branch

Resident Inspector, RIII

Richard Hubbard

J. W. McCaffrey, Chief, Public

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Utilities Division

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David Rosenblatt, Governor's

!

Office of Consumer Services

J. M. Taylor, DED0

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T. E. Murley, NRR

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E. L. Jordan, AEOD

'

J. Lieberman, OE

M. Johnson, ED0

W. Lanning, NRR

F. Miraglia, NRR

G. Holahan, NRR

D. Crutchfield, NRR

J. Partlow, NRR

J. Strasma, RIII

J. Goldberg, 0GC

0. Muller, NRR

CONFlitMATORY ACTION LETTER

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