ML20217D067

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Insp Repts 50-373/97-23 & 50-374/97-23 on 971222-980306. Violations Noted.Major Areas Inspected:Engineering
ML20217D067
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 03/23/1998
From: Jeffrey Jacobson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20217D010 List:
References
50-373-97-23, 50-374-97-23, NUDOCS 9803270293
Download: ML20217D067 (11)


See also: IR 05000373/1997023

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U.S. NUCLEAR REGULATORY COMMISSION

REGIONlli

Docket Nos:

50-373;50-374

License Nos:

NPF-11; NPF-18

Report Nos:

50-373/97023(DRS); 50-374/97023(DRS)

Licensee:

Commonwealth Edison Company

Facility:

LaSalle County Station, Units 1 and 2

Location:

2601 N. 21st Road

Marseilles,IL 61341

Dates:

December 22,1997, through March 6,1998

Inspector:

Eric Duncan, Reactor Engineer

Approved by:

John M. Jacobson, Chief

Lead Engineers Branch

Division of Recctor Safety

9803270293 980323

PDR

ADOCK 05000373

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PDR

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- EXECUTIVE SUMMARY

LaSalle County Station, Units 1 and 2

NRC inspection Report 50-373/97023(DRS); 50-374/97023',DRS)

Engineering

The inspector reviewed the licensee's response to information Notice 87-10 related to

the potent;al for waterhammer in the residual heat removal (RHR) system if a Loss-Of-

Coolant-Accident (LOCA) concurrent with a Loss-Of-Offsite-Power (LOOP) were to

occur while the system was aligned for suppression pool cooling. (Section E8.1)

Allowable tolerances in the construction of the drywell may cause a delay in leakage

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entering the floor drain sump for detection. However, technical specification leakage

requirements would be still be met assuming the worst case drywell floor holdup volume.

(Section E8.2)

The shell side of the Unit 1 and Unit 2 RHR pump seal coolers did not meet design

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pressure requirements and were not procured as required by 10 CFR 50, Appendix B,

Criterion IV," Procurement Document Control." _ (Section E8.3)

A design modification to add screens to the Unit 2 floor and equipment drain sumps to

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prevent foreign material intrusion into the sump piping and containment isolation valves

was not controlled as required by 10 CFR 50, Appendix B, Criterion ill, " Design Control."

(Section E8.4)-

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Report Details

Exercise of Enforcement Discretion

A violation described in Section E8.3 of this report is based upon licensee activities which were

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identified after, but occurred prior to the licensee announcing, in December 1996, an extended

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shutdown of the LaSalle County Station. This violation satisfies the appropriate criteria in

Section Vll.B.2," Violations identified During Extended Shutdowns or Work Stoppages," of the

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" General Statement of Policy and Procedures for NRC Enforcement Actions,"(Enforcement

Policy), NUREG-1600, and a Notice of Violation is not being issued for this violation because

the criteria specified in Section Vll.B.2 were met, which allows enforcement discretion to be

applied. Specifically, the violation was licensee-identified as a result of a comprehensive

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program for problem identification and correction that was developed in response to the

shutdown, the violation would not be categorized at a severity level higher than Severity Level

ll, and the violation was not willful. In addition, actions specified in Confirmatory Action Le#er

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Rlll-96-0088 effectively prevent the licensee from starting up LaSalle County Station witl at

implicit NRC approval.

Ill. Engineering

E8

Miscellaneous Engineering issues

E8.1

(Ocen) Insoection Follow uo item 50-373/97013-01: 50-374/97013-01: Review of

Information Notice 87-10.

As discussed in inspection report 50-373/97013; 50-374/97013, the inspector reviewed

the licensee's response to Information Notice 87-10 related to the potential for

waterhammer in the RHR system if a Loss-Of-Coolant-Accident (LOCA) concurrent with

a Loss-Of-Offsite-Power (LOOP) were to occur while the system was aligned for

suppression pool cooling.

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As part of that effort, the inspector reviewed the RHR waterhammer analysis prepared

by Sargent & Lundy (S&L) which concluded that although a waterhammer would occur,

the RHR system would maintain its pressure boundary integrity, structural stability, and

functional capability during the waterhammer event. The inspector questioned the

methodology which the licensee employed in the calculation including the basis for the

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assumptions made and the basis for the analysis acceptance criteria. Inspection follow

up item 50-373/97013-01; 50-374/97013-01 was opened pending further NRC review.

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During this inspection, the inspector obtained the Office of Nuclear Reactor Regulation's

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(NRR) respon.se to Task Interface Agreement (TIA) 96-0389, " Quad Cities, Unit 1 and 2,

Regarding NEDC-32523 Applicability to RHR Water Hammer Potential," dated October

12,1997. In that response, NRR stated the following:

In accordance with General Design Criteria 35," Emergency Core Cooling,"

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licensees are required to address unavailability of either onsite or offsite power

(whichever is more limiting) concurrent with a LOCA and the consequences of

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the event. If the loss of offsite power is more limiting, the licensee is required to

consider the LOOP concurrent with a LOCA.

Since the probability of a waterhammer event increases as the amount of time

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the system is operated in the suppression pool cooling (SPC) mode increases,

and the likelihood of damage to the system increases with the frequency of

waterhammer events, operating in the SPC mode more often that assumed in

the Updated Final Safety Analysis Report (UFSAR) may be an unreviewed

safety question.

If licensee's determine that the frequency of use of the SPC mode of RHR is

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greater than that assumed in the UFSAR, then LOCA occurrence during SPC

mode should be postulated and the corresponding draindown and waterhammer

should be addressed.

Therefore, based on the discussion in TIA 96-0389, a waterhammer analysis was not

required if operation in the SPC mode of RHR was less than that assumed in the

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UFSAR. The inspector discussed this information with licensee personnel.

Subsequently, the inspector determined that although no specific amount of time spent

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in shutdown cooling was addressed or prescribed in the UFSAR, historically the time

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spent in this configuration was low which indicated that a valid waterhammer analysis

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may not be required. At the end of the inspection, the licensee was in the process of

establishing a maximum SPC operation limit, above which an acceptable waterhammer

analysis would be required.

This item will remain open pending NRC review of this established operation limit.

E8.2 (Closed) Licensee Event Reoort (LER) 50-373/97021-00: Undrainable Low Areas in the

Drywell Floor Resulting in a Degradation of the Leak Detection System (LDS) Due to

increased Delays in Detection of Unidentified Leakage.

As discussed in inspection report 50-373/97013; 50-374/97013, and LER

50-373/97021-00, the licensee determined that the ability of the drywell floor to

accumulate water was inconsistent with the UFSAR description. Specifically, the

licensee's response to UFSAR question 212.17 stated that there were no undrainable

low points in the primary or secondary containment which would result in a delay in the

detection of leakage. Contrary to this description, there were undrainable areas which

would result in the delay of the detection of leakage.

During the licensee's investigation of this problem, an additional problem related to the

reliability of instrumentation associated with portions of the LDS was identified.

Regulatory Guide 1.45 required that the sensitivity and response time for the LDS

should be adequate to identify a leakage rate of 1 gallon per minute (gpm) in less than 1

hour. To meet this requirement, a capacitance probe was used to measure

instantaneous sump level which is electronically converted to a flow rate. However,

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operating experience had demonstrated that the capacitance probe frequently drifted

and was unreliable. As a result, the recurrent failure of the electronic level indication

resulted in the LDS not meeting design basis requirements.

As part of the licensee's immediate corrective actions, the LDS was declared inoperable.

In addition, the licensee planned the following long-term actions:

Resolution of the discrepancy between the as-built configuration of the plant and

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the description contained in response to UFSAR question 212.17.

Improving the reliability of the sump level monitoring instrumentation.

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Confirming that there were no other hold up volumes in the containment which

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could result in unacceptable delays in the detection of unidentified leakage.

During this inspection period, the licensee reviewed documents associated with the as-

built configuration of the plant and identified that the floor of the Unit 1 and Unit 2

drywells were poured to conform to American Concrete Standard (ACl) 301-72,

" Specifications for Structural Concrete for Buildings," as required by S&L Standard

Specification for Concrete Work (Form 1715-Q) and were certified by quality control

inspectors on the " pour checkout cards." Table 4.3.1 of ACI 301-72 allowed up to a 3/4-

inch variation from the level or from the grades specified in the contract documents.

Therefore, although the UFSAR stated that there were no undrainable low points in the

primary or secondary containment which would result in a delay in the detection of

leakage, in fact, there was a potential that holdup volumes in the drywell floor may exist,

which would delay the detection of RCS leaksge.

The licensee reviewed this information and subsequently determined that assuming a

worst case with the floor drain 3/4 inch above all the rest of the floor and that 15 percent

of the floor was taken up with equipment mounting, then the calculated holdup volume

was about 1800 gallons.

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Technical Specification (TS) 3/4.4.3.2, " Reactor Coolant System Operational Leakage,"

required that RCS leakage shall be limited to a 2 gpm increase in unidentified leakage

over any 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. The inspector verified that given a 2 gpm leakage rate, and

assuming a worst case holdup volume, that the leakage would be conducted to the floor

drain sump well within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and therefore the ability for detection to meet the

requirements of TS 3/4.4.3.2 would still be present.

The inspector concluded that allowable tolerances in the construction of the drywell may

cause a delay in leakage entering the floor drain sump for detection, although the

licensee indicated in the UFSAR that there were no undrainable low points in the

primary or secondary containment which would result in a delay in the detection of

leakage. However, the inspector also concluded that technical specification leakage

requirements would be still be met assuming the worst case drywell floor holdup volume.

However, it also appeared that the as-built construction of the drywell may be outside

the plant's licensing basis since undrainable low points may exist in the drywell although

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the UFSAR stated that there were no undrainable low points in the primary containment.

Resolution of the discrepancy between the as-built configuration of the plant and the

description in the UFSAR as well as improvements to sump level monitoring

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instrumentation is an unresolved item (URI 50-315/97023-01(DRS);

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50-316/97023-01(DRS)) pending NRC review of the licensee's corrective actions.

E8.3 (Closed) LER 50-373/98018-00: RHR Pump Seal Coolers Do Not Meet Design

Pressure Requirements Because Requirements Were Not included in Original Purchase

Specification to Pump Manufacturer.

As discussed in the subject LER, the licensee identified that the shell side of the Unit 1

and Unit 2 RHR pump sea! coolers did not meet design pressure requirements.

Specifically, the licensee determined that the shell side of the coolers had a design

' pressure of 75 pounds per square inch gauge (psig) although the design pressure of the

RHR Service Water (RHRSW) system that supplied the cooling water had a design

pressure of 150 psig.

The licensee performed a root cause investigation and determined that the coolers were

purchased during initial plant construction without regard to pressure requirements and

that, as a result, the coolers were procured with a shell side design pressure of 75 psig

(which was about normal system operating pressure) vice the 150 psig design pressure

requirements.

To determine the significance of this event, the licensee obtained the hydrostatic testing

results for the cooler casings and determined that although the coolers were rated at 75

psig, they were able to withstand significantly higher pressures. Specifically, in addition

to successfully hydrostatically testing each cooler's casing to twice the design pressure,

the manufacturer had also performed a hydrostatic test to destruction of an identical

cooler casing. The destruction test pressure where the casing was first noted to be

leaking was found to be 450 psig. The licensee concluded that the seal coolers would

not fall catastrophically when exposed to a pressure of 150 psig and would remain intact

and operational.

As part of the licensee's corrective actions, the affected seal coolers were replaced with

coolers rated at a design pressure of 150 psig. In addition, the licensee verified that

similar procurement problems did not exist for other coolers.

The inspector reviewed this event and verified that modifications were installed to

replace the cast iron RHR seal coolers with cast steel seal coolers which met system

design pressure requirements. In addition, the inspector reviewed the hydrostatic test

results for the coolers removed as well as the replacement coolers and had no

additional concems.

10 CFR 50, Appendix B, Criterion IV," Procurement Document Control," required that

measures shall be established to assure that the applicable regulatory requirements,

design bases, and other requirements which are necessary to assure adequate quality

are suitably included or referenced in documents for procurement. The failure to include

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in procurement documents for the Unit 1 and Unit 2 RHR seal coolers specifications

regarding shell side design pressure was an example where the requirements oi10

CFR 50, Appendix B, Criterion IV, were not met and was a violation. However,

because this violation was based upon activities prior to the events leading to the

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current extended plant shutdown and satisfy the criteria in Section Vll.B.2," Violations

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Identified During Extended Shutdowns or Work Stoppages," of the " General Statement

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of Policy and Procedures for NRC Enforcement Actions"(Enforcement Policy), NUREG-

1600, a Notice of Violation is not being issued (50-373/97023-02; 50-374/97023-02).

Specifically, the violation was licensee-identified as a result of a comprehensive program

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for problem identification and correction that was developed in response to the

shutdown, the violation would not be categorized at a severity level higher than Severity

Level ll, and the violation was not willful. In addition, actions specified in Confirmatory

Action Letter Rlll-96-0088 effectively prevent the licensee from starting up LaSalle

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County Station without implicit NRC approval.

E8.4 (Closed) LER 50-374/95006-00: 50-374/95006-01: Primary Containment Maximum

Allowable Leakage Exceeded Due to Local Leak Rate Test (LLRT) Failure.

As discussed in the subject LER, the licensee identified on March 20,1995, that the Unit

2 maximum allowable primary containment leakage rate was exceeded during th3

performance of a Local Leak Rate Test (LLRT). Specifically, the 2RE024 and 2RE025

Drywell Equipment Drain (RE) Sump containment isolation valves had been leak rate

tested and the leak rate was determined to be excessive (test volume could not be

pressurized). The cause of the leakage was determined to be seat leakage through

both valves. Upon inspection, the seat was found damaged due to foreign material.

As part of the licensee's corrective actions, both valves were repaired and successfully

leak rate tested. In addition, a plant modification was performed which installed

permanent screens in the floor drain and equipment drain sumps to prevent foreign

materialintrusion into the RE piping and isolation valves.

The licensee concluded that since the drywell RE sump would normally be filled with

water which would tend to seal any air leakage, the safety significance of the event was

minimal. In addition, the licensee concluded that in the event that air leakage eventually

occurred through the containment isolation valves, the downstream piping was normally

filled with water and provided additional isolation with normally closed automatic valves

that are designed to open with pump flow.

The inspector reviewed this event including design change packages (DCPs) 9500086

(Unit 1) and 9500087 (Unit 2) which controlled the installation of the foreign material

exclusion (FME) screens in the floor drain and equipment drain sumps. The inspector

reviewed the modification package for Unit 1. No deficiencies were identified. However,

the inspector noted the following weaknesses regarding the licensee's implementation of

the modification on Unit 2:

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Unit 2 Drawings Were Not Upoated as Appropriate

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The inspector identified that although Piping and Instrumentation Drawings

(P&lDs) associated with the floor and equipment drain system had been updated

to reflect the addition of the screens on Unit 1, similar drawings for Unit 2 had not

been updated to reflect the change.

The Unit 2 Design Change Package Was inappropriately Canceled

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Although the Unit 1 DCP (9500086) was statused as complete, the Unit 2 DCP

(9500087) was statused as canceled. Upon further review, the inspector

identified that although the work was documented in the Electronic Work Control

System (EWCS) as accomplished and had been accomplished according to the

cognizant system engineer, the DCP was canceled on March 20,1997, because

the DCP could not be located following completion of the work. As a result,

documentation associated with the work was not available for review.

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The inspector discussed this information with licensee personnel. As a result, Problem

Identification Form (PlF) L1997-07512 was initiated to document the issue. At the end

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of the inspection, the licensee planned to re-construct a new DCP to identify any

required post-modification inspections, revise drawings as appropriate, and perform a

walkdown of the system.

The inspector concluded that the design of the modification to add screens to the Unit 1

and Unit 2 floor and equipment drain sumps was good. In addition, no deficiencies were

identified in the implementation of the modification on Unit 1. However, the inspector

also concluded that the implementation of the modification on Unit 2 was poor since the

DCP was canceled when the DCP paperwork could not be located and design drawings

were not updated to reflect the installation of the modification.

The inspectors determined that the design modification to add screens to the Unit 2 floor

and equipment drain sumps was not controlled as required by 10 CFR 50, Appendix B,

Criterion 111, " Design Control," and was a violation (50-374/97023-03(DRS)).

This LER is closed.

E8.5 [Clqged) LER 50-373/96021-00: Inadequate Review of Modification of Main Control

Room Atmospheric Control System Radiation Monitoring Logic Results in an

Unreviewed Safety Question.

This event was discussed in inspection report 50-373/97003; 50-374/97003. No new

issues were revealed by the LER.

This LER is closed.

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VI. Management Meeting

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Exit Meeting Summary

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The inspector presented the results of these inspections to licensee management at an

exit meeting on March 6,1998. The licensee acknowledged the findings presented.

The inspector asked the licensee if any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Comed

F. Dacimo

Site Vice President

G. Poletto

Site Engineering Manager

E. Connell

Design Engineering Supervisor

R. Palmieri

System Engineering Supervisor

P. Bames

Regulatory Assurance Manager

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J. Damron

System Engineering

G. Kats

System Engineering

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INSPECTION PROCEDURES USED

IP 37550

Engineering

IP 37551

Onsite Engineering

IP 90712

In-Office Review of Written Reports of Nonroutine Events at Power Reactor

Facilities

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IP 92700

Onsite Follow-Up of Written Reports of Nonroutine Events at Power Reactor

Facilities

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ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-373/97023-01; 50-374/97023-01 URI

Floor and Equipment Drain System Sump Level

Monitoring Problems

50-373/97023-02; 50-374/97023-02 NCV RHR Pump Seal Coolers Do Not Meet Design

Pressure Requirements

50-373/97023-03; 50-374/97023-03 VIO

Inadequate Drywell Sump Screen Modification

Closed

50-373/97021-00

LER

Undrainable Low Areas in the Drywell Floor

Resulting in a Degradation of the LDS

50-373/96018-00

LER

RHR Pump Seal Coolers Do Not Meet Design

Pressure Requirements

50-374/95006-00; 50-374/95006-01 LER

Primary Containment Maximum Allowable Leakage

Exceeded Due to LLRT Failure.

50-373/96021-00

LER

Inadequate Review of Modification of MCR

Atmospheric Control System Radiation Monitoring

Logic

Discussed

50-373/97013-01; 50-374/97013-01 IFl

Review of Information Notice 87-10

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LIST OF ACRONYMS USED

ACI

American Concrete Institute

ASME

American Society of Mechanical Engineers

CFR

Code of Federal Regulations

DCP

Design Change Package

DRS

Division of Reactor Safety

EWCS

Electronic Work Control System

FME

Foreign Material Exclusion

gpm

gallons per minute

IFl

Inspection Follow up item

LDS

Leak Detection System

LER

Licensee Event Report

LLRT

Local Leak Rate Test

LOCA

Loss Of Coolant Accident

LOOP

Loss Of Offsite Power

NCV

Non-Cited Violation

NRR

Office of Nuclear Reactor Regulation

PDR

Public Document Room -

P&lD

Piping and Instrumentation Drawing

PIF

Problem Identification Form

psig

pounds per square inch gauge

RCS

Reactor Coolant System

RE

Drywell Equipment Drain System

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

S&L

Sargent & Lundy

SPC

Suppression Pool Cooling

TIA

Task Interface Agreement

TS

Technical Specification

UFSAR

Updated Final Safsty Analysis Report

URI

Unresolved item

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