IR 05000282/2010008

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IR 05000282-10-008, 05000306-10-008, on 06/15/2009 - 03/26/2010, Prairie Island Nuclear Generating Plant, Units 1 and 2; Ultimate Heat Sink
ML101031371
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 04/12/2010
From: Ann Marie Stone
NRC/RGN-III/DRS/EB2
To: Schimmel M
Northern States Power Co
References
IR-10-008
Download: ML101031371 (16)


Text

pril 12, 2010

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 ULTIMATE HEAT SINK INSPECTION REPORT 05000282/2010008; 05000306/2010008

Dear Mr. Schimmel:

On March 26, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an Ultimate Heat Sink inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report documents the inspection findings, which were discussed on March 26, 2010, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, one NRC-identified finding of very low safety-significance was identified. This finding involved a violation of NRC requirements. However, because of the very low safety-significance, and because the issue was entered into your corrective action program, the NRC is treating the issue as an Non-Cited Violation (NCV) in accordance with Section VI.A.1 of the NRC Enforcement Policy. If you contest the subject or severity of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Prairie Island Nuclear Generating Plant. In addition, if you disagree with the characterization of the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Prairie Island Nuclear Generating Plant. The information that you provide will be considered in accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Ann Marie Stone, Chief Engineering Branch 2 Division of Reactor Safety Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60

Enclosure:

Inspection Report 05000282/2010008; 05000306/2010008 w/Attachment: Supplemental Information

REGION III==

Docket Nos: 50-282; 50-306 License Nos: DPR-42; DPR-60 Report No: 05000282/2010008; 05000306/2010008 Licensee: Northern States Power Company, Minnesota Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2 Location: Welch, MN Dates: June 15, 2009, through March 26, 2010 Inspectors: G. ODwyer, Reactor Inspector A. Dunlop, Senior Reactor Inspector Approved by: A.M. Stone, Chief Engineering Branch 2 Division of Reactor Safety Enclosure

SUMMARY OF FINDINGS

IR 05000282/2010008, 05000306/2010008; 06/15/2009 - 03/26/2010; Prairie Island Nuclear

Generating Plant, Units 1 and 2; Ultimate Heat Sink.

This report covers an announced baseline inspection by regional inspectors. One Green finding associated with a Non-Cited Violation (NCV) was identified by the inspectors. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings, for which the SDP does not apply, may be Green or assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

A finding of very low safety-significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to determine the minimum cooling water system flow required after a design basis earthquake (DBE) to safely shutdown both reactors and to correctly translate these results into procedures. Specifically, the licensee failed to determine the cooling water flow rate necessary to shutdown both reactors after a DBE and ensure that this flow rate remained within the capacity of the emergency intake line. As a result, design bases were not correctly translated into procedures. The licensee confirmed through a preliminary calculation that the system remained operable.

The finding was determined to be more than minor because the failure to determine the cooling water flow necessary to shutdown both reactors after a DBE could have provided incorrect guidance in the procedure and to the operators. This finding is of very low safety-significance (Green) because the design deficiency was confirmed not to result in loss of operability or functionality. This finding has a cross-cutting aspect in the area of problem identification and resolution because the licensee did not take appropriate corrective actions to address safety issues in a timely manner, commensurate with its safety-significance and complexity. P.1(d) (Section 1R07.1.b.(1))

Licensee-Identified Violations

No violations of significance were identified.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R07 Heat Sink Performance

.1 Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed completed surveillances, vendor manual information, associated calculations, performance test results, and cooler inspection results associated with the Unit 2 emergency diesel generator D2 lube oil cooler (034-021).

This heat exchanger was chosen based on its risk significance in the licensees probabilistic safety analysis, its important safety-related mitigating system support functions, and its relatively low margin.

The inspectors verified that testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs were adequate to ensure proper heat transfer. This was accomplished by verifying the test method used was consistent with accepted industry practices or equivalent, the test conditions were consistent with the selected methodology and the test acceptance criteria were consistent with the design basis values. The inspectors also verified that the test results appropriately considered differences between testing conditions and design conditions and that the frequency of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values.

The inspectors also reviewed the methods and results of heat exchanger performance inspections. The inspectors verified that the methods used to inspect and clean heat exchangers were consistent with as-found conditions identified and expected degradation trends and industry standards, the licensees inspection and cleaning activities had established acceptance criteria consistent with industry standards, and the as-found results were recorded, evaluated, and appropriately dispositioned such that the as-left condition was acceptable.

In addition, the inspectors verified the condition and operation of the Unit 2 emergency diesel generator D2 lube oil cooler (034-021) was consistent with design assumptions in heat transfer calculations and as described in the final safety analysis report. This included verification that the number of plugged tubes was within pre-established limits based on capacity and heat transfer assumptions. The inspectors verified that the licensee evaluated the potential for water hammer and established adequate controls and operational limits to prevent heat exchanger degradation due to excessive flow induced vibration during operation. In addition, eddy current test reports and visual inspection records were reviewed to determine the structural integrity of the heat exchanger.

The inspectors verified the performance of the ultimate heat sink (UHS) by tests or other equivalent methods to ensure availability and accessibility to the inplant cooling water systems, which at Prairie Island Nuclear Generating Plant is designated the cooling water (CL) system. The focus was on attributes listed in IP 71111-07, Section 02.02.d.1, 2, and 4.

The inspectors verified that the licensees inspection of the intake canal was thorough and of significant depth to identify degradation of the shoreline protection or loss of structural integrity. The inspectors performed walkdowns of accessible portions of the intake canal. This included verification that vegetation present along the slopes was trimmed, maintained and was not adversely impacting the embankment. In addition, the inspectors verified the licensee ensured sufficient reservoir capacity by trending and removing debris or sediment buildup in the UHS.

The inspectors reviewed the results of the licensees inspection of the safety-related and non-safety-related intake bays. The inspectors verified that identified settlement or movement indicating loss of structural integrity and/or capacity was appropriately evaluated and dispositioned by the licensee. In addition, the inspectors verified that the licensee ensured sufficient reservoir capacity by trending and removing debris or sediment buildup in the UHS. The inspectors performed a walkdown of accessible portions of the plant screenhouse and the intake screenhouse.

The inspectors reviewed the licensees operation of the service water system and the UHS. This included verification that instrumentation, which is relied upon for decision making, was available and functional. In addition, the inspectors verified that macrofouling was adequately monitored, trended, and controlled by the licensee to prevent clogging. The inspectors verified that the licensees biocide treatments for biotic control were adequately conducted and that the results were monitored, trended, and evaluated. The inspectors also reviewed design changes to the service water system and the UHS. The inspectors reviewed the licensees system configuration and flow assumptions during design basis earthquake conditions.

In addition, the inspectors reviewed corrective action program documents related to the heat exchangers/coolers and heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. The documents that were reviewed are included in the to this report.

These inspection activities associated with the Unit 2 emergency diesel generator D2 lube oil cooler and the UHS attributes constituted two heat sink inspection samples as defined in IP 71111.07-05.

b. Findings

(1) Failure to Determine the Minimum Cooling Water (CL) System Flow Required after a Design Basis Earthquake (DBE)
Introduction:

A finding of very low safety-significance and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to determine the minimum CL system flow required after a DBE to safely shutdown both reactors and to correctly translate these results into procedures.

Description:

During this inspection, the inspectors noted that the licensee had submitted License Amendment Request (LAR) letter dated May 3, 2004, to change the methodology for demonstrating functionality of the CL system following a DBE. The revised methodology was to verify that the CL system flow to required components after a DBE would be adequate to safely shutdown both reactors and remain within the 11,600 gpm capacity limitation of the emergency intake line (EIL). In Section 2, the licensee stated the post-seismic event flow values, times, and UFSAR would be revised as necessary based on actual calculation results following approval of this new methodology. On May 10, 2005, the NRC issued a Safety Evaluation Report (SER) for Amendment Nos. 169 and 159. In Section 3.3.1 of the SER, the staff stated:

During a seismic event, it is expected that the intake canal will pump down, at which point CL system flow is limited to the capacity of the emergency intake line. The CL system flow rate during a seismic event (to be determined by the revised analysis) will determine when this limitation in flow capacity will occur (i.e., how long it takes for the intake canal to pump down) and when operators will be required to reduce CL system flow to within the capacity of the emergency intake line.

The inspectors noted that the calculation of record at the time the LAR was submitted was ENG-ME-310, Evaluation of CL System Response following a Seismic Event with Reduced System Flow Rate, Revision 0, which was issued on March 17, 1997, prior to the LAR submittal. During this inspection the inspectors requested a copy of the new analysis or calculation performed in support of the SER and was informed that the analysis was not completed.

On September 13, 2006, the licensee initiated Action Request (AR) 01050047 to address an apparent discrepancy with Abnormal Operating Procedure AB-3, Earthquakes; calculation ENG-ME-310, Revision 0; and the plants safe-shutdown list.

As a result of lowering levels in the intake bay due to an earthquake (loss of the downstream dam), procedure AB-3 directed operators to reduce CL flow to within the capability of the EIL. The loss of the dam would result in lowering river and intake bay levels such that the EIL, which takes its suction from a low section in the river, would be the only source of water for the plants ultimate heat sink (UHS). In AR 01050047, the licensee identified that AB-3 directed operators to reduce CL flow to a value within the capability of the EIL; however, this value was not supported by a calculation that determined the minimum required flow rate to safely shutdown both reactors. In addition, the licensee noted in the AR that the procedure directed operators to secure equipment that was credited for operation in the safe-shutdown list. The procedure also directed operators to secure all four containment fan coil units (FCUs), which was not consistent with the calculation that maintained two FCUs in operation. The licensees initial review determined these issues did not affect the operability of the CL system.

The preliminary analysis concluded that the required flow rate to support the shutdown of both units was within the 11,600 gallons per minute (gpm) capacity of the EIL. This analysis was never finalized, nor was procedure AB-3 updated to match the results of the analysis.

On February 7, 2007, the licensee initiated AR 01076107 as a result of a self-assessment prior to the NRCs component design basis inspection. This AR documented several concerns related to CL system calculation, including determining the impact on CL flow when a CL strainer was in backwash and the assumed river level at the start of an analyzed accident. The licensee performed a sensitivity analysis with the strainers in a backwash condition and determined that the flow rate required to support safety-related plant equipment remained below the EIL capacity limit.

On December 17, 2009, the inspectors identified that procedure AB-3 did not isolate the containment chiller system by closing valves MV-32144 and MV-32159. As a result, procedure AB-3 would not be able to reduce CL flow below the EIL capacity limit of 11,600 gpm and that other operator actions would be needed to reduce the CL flow to within the limitations of EIL. The licensee initiated AR 01211137, which concluded that other procedures that the operators would be performing during this time frame would close these valves or isolate their respective lines. These included procedures C35 AOP5, Cooling Water Leakage Outside of Containment, and C35 AOP2, Loss of Pumping Capacity or Supply Header Without SI, which would be entered based on flooding scenario from non-seismic CL piping or low CL system pressure. Although implementation of these additional procedures would have at some point during the event reduced CL flow to within the capacity of the EIL, it was not recognized that AB-3 would not have been able to be performed as written until these other actions were taken. The inspectors reviewed these scenarios and associated procedures and concluded that the procedures should have provided sufficient guidance to support AB-3 in reducing CL flow rate below the capacity of the EIL. On January 6, 2010, based on the inspectors questions, the licensee found that the analysis only considered the case where one CL pump was operating after a DBE and failed to consider the more likely case of two CL pumps operating after a DBE. The licensee initiated AR 01212778 to document this omission. The licensee determined by an additional preliminary analysis that these issues did not affect the operability of the CL system.

At the end of the inspection period, the licensee had not yet approved the revision to calculation ENG-ME-310, nor revised procedure AB-3 to address the above deficiencies.

Specifically, the licensee had not determined the minimum CL system flow rate required to safely shutdown both reactors after a DBE and therefore, could not verify this flow would be within the capacity of the EIL. In addition, the licensee needed to ensure that the results of the analysis did not conflict with the plants licensing basis used by the NRC in its conclusions documented in the SERs associated with the CL system.

Specifically, the NRC noted statements that the volume in the intake canal provided about a 4.8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> supply of water or that the intake canal contained two to three times the minimum water volume for operator action needed to be reviewed. The licensee determined by preliminary analyses that these issues did not affect the operability of the CL system.

Analysis:

The inspectors determined that the failure to ensure that the minimum CL flow being supplied by the EIL was sufficient to safely shutdown both reactors after a DBE and incorporate these results into plant procedures was a performance deficiency.

The performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability and capability of safety-related equipment to respond to initiating events to prevent undesirable consequences. Specifically, the failure to determine the CL flow necessary to shutdown both reactors after a DBE could have provided incorrect guidance in the procedure. As a result, the operators may have reduced flow below the minimum required flow rates that could have caused the respective temperatures for the affected equipment to exceed their design or licensing limits.

The inspectors evaluated the finding using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, SDP Phase 1 screening. The finding screened as very low safety-significance (Green) because the finding was a design deficiency confirmed not to result in loss of operability or functionality. Specifically, the licensee verified by preliminary analysis that the required CL flow necessary to shutdown both reactors after a DBE was within the capability of the EIL. As such, the required flow rates available to the affected equipment would be within their design and licensing limits. The inspectors performed an independent review of this analysis and had no further concerns.

This finding has a cross-cutting aspect in the area of problem identification and resolution, because the licensee did not take appropriate corrective actions to address safety issues in a timely manner, commensurate with their safety-significance and complexity. Specifically, the licensee initial evaluations were not adequate to fully address all of the concerns without further reviews by plant personnel and NRC inspectors. In addition, although the issue was first identified in 2006, the corrective actions to address this concern are untimely as the licensee still has not approved the required calculation, nor has the procedure been revised to reflect the calculations conclusions. P.1(d)

Enforcement:

Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to the above, as of February 26, 2010, the licensee failed to correctly translate applicable design basis into procedures. Specifically, calculation ENG-ME-310 was not revised to determine the CL flow rate necessary to shutdown both reactors after a DBE and that this flow rate remained within the capacity of the EIL. As a result, design bases were not correctly translated into procedure AB-3. Because this violation was of very low safety-significance and it was entered into the licensees corrective action program (ARs 01050047, 01076107, 01211137, and 01212778), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000282/2010006-01; 05000306/2010006-01).

OTHER ACTIVITIES

4OA6 Management Meetings

.1 Exit Meeting Summary

On March 26, 2010, the inspectors presented the inspection results to Mr. Kevin Ryan and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Ryan, Plant Manager
J. Anderson, Regulatory Affairs Manager
S. Skoyen, Engineering Programs Manager
R. Murray, Plant Engineering Supervisor
S. Myers, Engineering Support Manager
J. Loeffler, Mechanical Design Engineer
C. Sansome, Mechanical Design Engineer (former GL 89-13 Program Owner)
J. Connors, Mechanical Design Engineering Supervisor, Fleet Design
K. Den Herder, GL 89-13 Program Owner
M. Davis, Regulatory Affairs Analyst
K. Mews, Licensing Engineer, Regulatory Affairs

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000282/2010008-01; NCV Failure to Determine the Minimum Cooling Water System
05000306/2010008-01 Flow Required After a Design Basis Earthquake

Discussed

None Attachment

LIST OF DOCUMENTS REVIEWED