IR 05000247/2018003

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Integrated Inspection Report 05000247/2018003 and 05000286/2018003
ML18317A077
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 11/08/2018
From: Daniel Schroeder
Reactor Projects Branch 2
To: Vitale A
Entergy Nuclear Operations
Schroeder D
References
IR 2018003
Download: ML18317A077 (39)


Text

UNITED STATES ember 8, 2018

SUBJECT:

INDIAN POINT NUCLEAR GENERATING - INTEGRATED INSPECTION REPORT 05000247/2018003 AND 05000286/2018003

Dear Mr. Vitale:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating (Indian Point), Units 2 and 3. On October 31, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors documented four findings of very low safety significance (Green) in this report. These findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Indian Point. In addition, if you disagree with a cross-cutting aspect assignment, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at Indian Point. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Daniel L. Schroeder, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Numbers: 50-247 and 50-286 License Numbers: DPR-26 and DPR-64

Enclosure:

Inspection Report 05000247/2018003 and 05000286/2018003

Inspection Report

Docket Numbers: 50-247 and 50-286 License Numbers: DPR-26 and DPR-64 Report Numbers: 05000247/2018003 and 05000286/2018003 Enterprise Identifier: I-2018-003-0076 Licensee: Entergy Nuclear Northeast (Entergy)

Facility: Indian Point Nuclear Generating, Units 2 and 3 Location: 450 Broadway, General Services Building Buchanan, NY 10511-0249 Inspection Dates: July 1, 2018, to September 30, 2018 Inspectors: B. Haagensen, Senior Resident Inspector A. Siwy, Resident Inspector J. Vazquez, Resident Inspector S. Elkhiamy, Reactor Inspector M. Modes, Senior Reactor Inspector J. Nicholson, Senior Health Physicist S. Wilson, Health Physicist K. Wood, Senior Nuclear Engineer, NRR Approved By: Daniel L. Schroeder, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergys performance at Indian Point Nuclear Generating, Units 2 and 3, by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information: NRC-identified and self-revealing findings, violations, and additional items are summarized in the table below.

List of Findings and Violations Inadequate Procedural Guidance for Spent Fuel Movement and Storage Requirements Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green H.3 - Change 71152 Non-Cited Violation (NCV) Management 05000247/2018003-01 Closed The inspectors identified a Green NCV of Title 10 of the Code of Federal Regulations (10 CFR)

Part 50, Appendix B, Criterion V, Procedures, when Entergy did not have appropriate documented instructions or written procedures for spent fuel movement and storage requirements adjacent to potentially degraded Boraflex panels. Specifically, configuration restrictions were not addressed in some cases and, therefore, did not comply with controls to meet the criticality analysis of record (CAOR) in 2016; and the resultant revised guidance did not accurately reflect the modeled supporting analysis.

Containment Fan Coolers 21 and 24 Motor Cooler Elbow Through-Wall Leaks Due to Excessive Service Water Flow Rates and Safety System Functional Failures of Containment Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green None 71152 NCV 05000247/2018003-02 Closed A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified when Entergy did not ensure that measures were established for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the structures, systems, and components.

Specifically, in 1998, when the former license-holder for Unit 2 decided to replace the original-construction large-radius, butt-welded elbow joints in the service water motor cooler return lines from the Unit 2 fan cooler units (FCUs) with a new design (a short-radius, socket-weld fitting), these elbow joints were not properly evaluated for suitability of application. The service water flow velocity through the modified FCU return piping was in excess of the vendor-allowable flow velocity limit, which resulted in the gradual erosion of the motor cooler elbow joints, eventually leading to through-wall leaks on an American Society of Mechanical Engineers (ASME) class III piping system inside containment, leading to breaches of containment integrity and safety system functional failures.

Containment Fan Cooler 24 Through-Wall Service Water Leak Caused by Inadequate Application of Epoxy Coating Resulting in Corrosion and a Safety System Functional Failure of Containment Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green H.13 - 71152 NCV 05000247/2018003-03 Consistent Closed Process A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, was identified when Entergy did not ensure that activities affecting quality were prescribed by documented instructions or procedures, of a type appropriate to the circumstances, and that these activities were accomplished in accordance with these instructions, procedures or drawings. Furthermore, Entergy did not ensure that the instructions or procedures included appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished. Specifically,

Entergy did not ensure that the maintenance procedure for applying the internal Enecon'

epoxy coating to the 24 fan cooler main cooler supply line elbow was adequate to ensure proper epoxy coating adherence, and Entergy did not adequately verify the coating adherence prior to placing the elbow in service. This resulted in a through-wall leak and a safety system functional failure of containment.

Inadequate Procedure for Turbine Startup Caused a Reactor Trip Cornerstone Significance Cross-Cutting Inspection Aspect Results Section Initiating Events Green H.13 - 71153 NCV 05000247/2018003-04 Consistent Closed Process A self-revealing Green NCV of Technical Specification (TS) 5.4.1, Procedures, was identified because Entergy did not provide adequate guidance in 2-SOP-26.4, Turbine Generator Startup, Synchronization, Voltage Control, and Shutdown. Specifically, Entergy did not provide adequate procedural direction to ensure the main turbine control oil stop valve Z was in the correct position. As a result, the steam generator water level exceeded the trip setpoint for the main boiler feed pumps which led the operators to insert a manual reactor trip.

Additional Tracking Items Type Issue number Title Report Status Section LER 05000247/2015001-02 Technical Specification 71153 Closed Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for Containment LER 05000247/2015004-00 Safety System Functional 71153 Closed Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe LER 05000247/2016010-00 Safety System Functional 71153 Closed and Failure Due to an Inoperable 05000247/2016010-01 Containment Caused by a Through-Wall Defect in a Service Water Supply Pipe Elbow to the 24 Fan Cooler Unit LER 05000247/2018001-00 Penetration Indications 71153 Closed Discovered During Reactor Pressure Vessel Head Inspection LER 05000247/2018002-00 Manual Reactor Trip Due to 71153 Closed Trip of Both Main Boiler Feedwater Pumps LER 05000286/2016001-00 Safety System Functional 71153 Closed and Failure Due to an Inoperable 05000286/2016001-01 Containment Caused by a Flaw on the 31 Fan Cooler Unit Service Water Return Coil Line Affecting Containment Integrity LER 05000286/2017003-00 Condensate Storage Tank 71153 Closed Declared Inoperable Per Technical Specification

TABLE OF CONTENTS

PLANT STATUS

...........................................................................................................................

INSPECTION SCOPES

................................................................................................................

REACTOR SAFETY

..................................................................................................................

RADIATION SAFETY

..............................................................................................................

OTHER ACTIVITIES - BASELINE

..........................................................................................

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

INSPECTION RESULTS

............................................................................................................

EXIT MEETINGS AND DEBRIEFS

............................................................................................ 29 THIRD PARTY REVIEWS .......................................................................................................... 29

DOCUMENTS REVIEWED

......................................................................................................... 30

PLANT STATUS

Unit 2 operated at or near rated thermal power for the entire inspection period.

Unit 3 began the inspection period at rated thermal power. On July 30, 2018, Unit 3 reduced

power to 50 percent after the 33 condensate pump failed. Unit 3 was returned to 100 percent

on August 3, 2018, after completing repairs to the 33 condensate pump. On September 7,

2018, Unit 3 was shutdown to Mode 4 to repair a leak on the boron injection tank. Unit 3 was

returned to rated thermal power on September 17, 2018. On September 18, 2018, Unit 3 was

tripped from 100 percent when a steam leak on a reheater steam line to a feedwater heater

occurred. The line was repaired and the unit was returned to rated thermal power on

September 24, 2018, and remained at or near rated thermal power for the remainder of the

inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met,

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess Entergys performance and

compliance with Commission rules and regulations, license conditions, site procedures, and

standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdowns (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

Unit 2

(1) 21 safety injection pump on July 20, 2018

(2) 22 safety injection pump on July 20, 2018

Unit 3

(3) 32 safety injection pump on July 19, 2018

(4) Main and reheat steam system on September 24, 2018

71111.05A/Q - Fire Protection Annual/Quarterly

Quarterly Inspection (9 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

Unit 2

(1) Intake structure pre-fire plan (PFP-264) on August 13, 2018

Unit 3

(2) Control building exhaust fan/diesel generator air filter enclosure (PFP-354A) on July 3,

2018

(3) Electrical cable tunnels (PFP-355, PFP-356, PFP-357, and PFP-358) on July 3, 2018

(4) Safety injection pump room and main corridor (PFP-305) on July 19, 2018

(5) Component cooling pump room (PFP-306A) on July 19, 2018

(6) Containment spray pump room (PFP-306B) on July 19, 2018

(7) Mini containment and pipe tunnels, primary auxiliary building/fan house (PFP-305A), on

August 6, 2018

(8) 480V switchgear room (PFP-351) on August 28, 2018

(9) Auxiliary feedwater building (PFP-365, PFP-366, PFP-367, and PFP-367A) on

September 26, 2018

71111.07T - Heat Sink Performance

Heat Sink (Triennial) (4 Samples)

The inspectors evaluated exchanger/sink performance on the following components from

July 16 to 18, 2018:

(1) 21 Component cooling heat exchanger, Section 02.02b

(2) 31 Component cooling heat exchanger, Section 02.02b

(3) 32 Component cooling heat exchanger, Section 02.02b

(4) Unit 3 Intake, Section 02.02d, specifically Sections 02.02d5 and 02.02d7 were

completed

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (2 Samples)

Unit 2

(1) The inspectors observed and evaluated operator requalification activity during simulator

training sessions on August 23, 2018, and September 5, 2018.

Unit 3

(2) The inspectors observed and evaluated operator requalification activity during an

emergency planning drill on August 1, 2018.

Operator Performance (3 Samples)

Unit 3

(1) The inspectors observed and evaluated operator performance activity during a reactor

rapid downpower on July 30, 2018, and subsequent power ascension on August 3,

2018, following a condensate pump trip.

(2) The inspectors observed and evaluated operator performance activity during a reactor

startup from a forced outage on September 16, 2018.

(3) The inspectors observed and evaluated operator performance activity during a plant trip

on September 18, 2018, and a plant startup on September 23, 2018, following a

feedwater reheater steamline break.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (4 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated

with the following equipment and/or safety significant functions:

Unit 2

(1) Main turbine lube oil system on August 29, 2018

Unit 3

(2) Reheater drain system on September 20, 2018

Units 2 and 3

(3) Core exit thermocouple monitoring system on August 30, 2018

(4) 13.8kV system on August 30, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent

work activities:

Unit 2

(1) Yellow Fire Risk for loss of LI-3101 on July 25, 2018

(2) Planned Yellow risk during gas turbine transformer maintenance on August 14, 2018

Unit 3

(3) Planned Yellow risk during emergently concurrent nuclear power range channel N-41

testing and 31 residual heat removal pump oil sampling on August 13, 2018

(4) Planned Yellow risk for 480V safety bus under-voltage and degraded-voltage testing on

August 16, 2018

71111.15 - Operability Determinations and Functionality Assessments (9 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

Unit 2

(1) CR-IP2-2018-04258, Multiple core exit thermocouples failed low on July 16, 2018

(2) CR-IP2-2018-04269, Inadequate service water flow to the 23 FCU and restoration of

flow balance on July 18, 2018

(3) CR-IP2-2018-05048, 21 emergency diesel generator (EDG) operability following repairs

to a lube oil leak on September 6, 2018

(4) CR-IP2-2018-05069, Black start diesel functionality with degraded battery on

September 7, 2018

(5) CR-IP2-2014-04414, Spent fuel pool operability on September 27, 2018

Unit 3

(6) CR-IP3-2018-01894, Safety inspection system operability with boric acid deposits

identified in electrical cable tunnel on July 6, 2018

(7) CR-IP3-2018-02638, Review operability call for entry into TS 3.0.3 in response to a

safety injection system leak in the boron injection tank on September 7, 2018

(8) CR-IP3-2018-02508 and CR-IP3-2018-02660, Operability decisions for motor circuit

analysis (Baker') testing results for 31 residual heat removal and 36 service water

pump motors on August 27, 2018, and September 9, 2018

(9) CR-IP3-2018-02773, 480V safety bus operability with high-energy-line-break conditions

in the turbine building on September 19, 2018

71111.18 - Plant Modifications (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change Package 79305 - Boron Injection Tank Thermowell Removal

(permanent modification) at Unit 3 on September 12, 2018

71111.19 - Post Maintenance Testing (8 Samples)

The inspectors evaluated post maintenance testing for the following maintenance/repair

activities:

Unit 2

(1) 21 containment recirculation fan 480V breaker cubicle replacement on July 23, 2018

(2) 22 service water pump following motor replacement on September 5, 2018

Unit 3

(3) 39 service water pump 480V breaker cubicle replacement on July 26, 2018

(4) 32 EDG return to service following maintenance period on August 3, 2018

(5) 32 and 33 condensate pumps following motor and seal replacements on August 3, 2018

(6) Residual heat remover heat exchanger outlet valves following circuit breaker

maintenance on August 23, 2018

(7) Hydrostatic test post maintenance testing for boron injection tank weld repairs on

September 15, 2018

(8) 31 and 32 exciter air coolers following tube sleeve installation on September 16, 2018

71111.20 - Refueling and Other Outage Activities (2 Samples)

(1) The inspectors evaluated the Unit 3 forced outage (3FO18B) activities for boron injection

tank repairs from September 7 to 17, 2018.

(2) The inspectors evaluated the Unit 3 forced outage (3FO18C) activities to repair the

reheat steam line in containment from September 18 to 23, 2018.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (4 Samples)

(1) 3-PT-M079C, 33 EDG surveillance test and thermography at Unit 3 on August 2, 2018

(2) 3-PT-M079B, 32 EDG monthly surveillance test at Unit 3 on August 3, 2018

(3) 2-PT-M021A, 21 EDG annual thermal performance test and biannual post diagnostic

test at Unit 2 on August 9, 2018

(4) 3-PT-2Y001A, 31 EDG overspeed trip test at Unit 3 on August 29, 2018

Inservice (2 Samples)

(1) 2-PT-Q013-DS021 and 2-PT-Q013-DS022, 22 containment spray pump discharge valve

tests at Unit 2 on July 26, 2018

(2) 2-PT-Q024A, 21 EDG fuel oil transfer pump test at Unit 2 on August 9, 2018

Reactor Coolant System Leak Detection (1 sample)

(1) 0-SOP-LEAKRATE-001, Elevated unidentified leakage rate during charging pump

maintenance at Unit 3 on September 19, 2018

Containment Isolation Valve (1 Sample)

(1) 2-PT-Q035B and 2-PT-Q013-DS038, 22 containment spray pump and header stop valve

tests at Unit 2 on July 26, 2018

71114.06 - Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated the conduct of a routine Entergy emergency planning drill at the

Unit 3 Emergency Operations Facility on August 1, 2018.

Drill/Training Evolution (1 Sample)

The inspectors evaluated the conduct of a routine Entergy emergency planning NRC

evaluated exercise at Unit 2 on September 25, 2018.

RADIATION SAFETY

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (1 Sample)

The inspectors evaluated airborne controls and monitoring. The inspectors observed

temporary ventilation system setups and portable airborne radioactivity monitoring systems

and verified Entergys established alarm setpoints for evaluating levels of airborne for both

beta and alpha emitting radionuclides.

Use of Respiratory Protection Devices (1 Sample)

The inspectors evaluated the respiratory protection program. The inspectors reviewed

Entergys as low as reasonably achievable reviews and the storage, selection, and use of

respiratory protection devices and verified that air used in supplied air devices meets or

exceeds Grade D quality. The inspectors also reviewed the qualifications of several

individuals to ensure they were qualified to use respiratory protections devices.

Self-Contained Breathing Apparatus for Emergency Use (1 Sample)

The inspectors evaluated the self-contained breathing apparatus program. The inspectors

verified that personnel who are required to use self-contained breathing apparatus were

trained and qualified and that the control rooms were stocked with an adequate variety of

respirator face pieces.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified Entergys performance indicators submittals listed below for the

period from July 1, 2017, through June 30, 2018 (10 Samples).

Unit 2

(1) Emergency AC Power Systems (MS06)

(2) High Pressure Injection Systems (MS07)

(3) Heat Removal Systems (MS08)

(4) Residual Heat Removal Systems (MS09)

(5) Cooling Water Support Systems (MS10)

Unit 3

(6) Emergency AC Power Systems (MS06)

(7) High Pressure Injection Systems (MS07)

(8) Heat Removal Systems (MS08)

(9) Residual Heat Removal Systems (MS09)

(10) Cooling Water Support Systems (MS10)

71152 - Problem Identification and Resolution

Annual Follow-Up of Selected Issues (2 Samples)

The inspectors reviewed Entergys implementation of its corrective action program (CAP)

related to the following issues:

(1) CR-IP2-2014-04414, Accelerated neutron-absorber (Boraflex) degradation in the spent

fuel pit (SFP) at Unit 2

(2) CR-IP2-2015-03550, CR-IP2-2015-05755, CR-IP2-2016-06934, and

CR-IP3-2016-03607, Containment FCU leaks corrective actions at Units 2 and 3

71153 - Follow-Up of Events and Notices of Enforcement Discretion

Events (2 Samples)

The inspectors evaluated response to the following events:

(1) Unit 3 shutdown to Mode 4 after an entry into TS 3.0.3 due to a leak in the boron

injection tank on September 7, 2018

(2) Unit 3 shutdown following the failure of the 26C Feedwater Heater MSR drain line on

September 18, 2018

Licensee Event Reports (LERs) (7 Samples)

The inspectors evaluated the following LERs:

(1) LER 05000247/2015001-02, Technical Specification Prohibited Condition Due to an

Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That

Results in Exceeding the Allowed Leakage Rate for Containment (Agencywide

Documents Access and Management System (ADAMS) Accession No. ML17248A466)

The inspectors reviewed the updated (Revision 2) LER submittal which provided an

updated causal assessment for a leak on the 24 FCU motor cooler inlet line elbow. The

previous LER submittals (Revisions 0 and 1) were reviewed and closed in the Indian

Point Integrated Inspection Report 05000247/2016004 and 05000286/2016004 (ADAMS

Accession No. ML17037C541), and an associated performance deficiency was

addressed therein with Green NCV 05000247/2016004-02. The circumstances

surrounding this LER are documented in the Inspection Results section, NCV 05000247/2018003-02, and Observations, Annual Follow-Up of Selected Issues.

(2) LER 05000247/2015004-00, Safety System Functional Failure Due to an Inoperable

Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor

Cooling Return Pipe (ADAMS Accession No. ML16057A178)

The circumstances surrounding this LER are documented in the Inspection Results

section, NCV 05000247/2018003-02, and Observations, Annual Follow-Up of Selected

Issues.

(3) LER 05000247/2016010-00 and 05000247/2016010-01, Safety System Functional

Failure Due to an Inoperable Containment Caused by a Through-Wall Defect in a

Service Water Supply Pipe Elbow to the 24 Fan Cooler Unit (ADAMS Accession Nos.

ML17003A008 and ML17069A170)

The circumstances surrounding this LER are documented in the Inspection Results

section, NCV 05000247/2018003-03, and Observations, Annual Follow-Up of Selected

Issues.

(4) LER 05000247/2018001-00, Penetration Indications Discovered During Reactor

Pressure Vessel Head Inspection (ADAMS Accession No. ML18149A126)

The circumstances surrounding this LER were previously documented in Inspection

Report 05000247/2018-002, NCV 05000286/2018-002-01. The inspectors concluded

that no additional performance deficiencies or violations of NRC requirements were

identified.

(5) LER 05000247/2018002-00, Manual Reactor Trip Due to Trip of Both Main Boiler

Feedwater Pumps (ADAMS Accession No. ML18173A127)

The circumstances surrounding this LER are documented in the Inspection Results

section, NCV 05000247/2018003-04.

(6) LER 05000286/2016001-00 and 05000286/2016001-01, Safety System Functional

Failure Due to an Inoperable Containment Caused by a Flaw on the 31 Fan Cooler Unit

Service Water Return Coil Line Affecting Containment Integrity (ADAMS Accession Nos.

ML17003A007 and ML17047A463)

The inspectors determined that it was not reasonable to foresee or correct the cause

discussed in the LER; therefore, no performance deficiency was identified. The

inspectors also concluded that no violation of NRC requirements occurred.

(7) LER 05000286/2017003-00, Condensate Storage Tank Declared Inoperable Per

Technical Specification (ADAMS Accession No. ML17248A467)

The inspectors determined that it was not reasonable to foresee or correct the cause

discussed in the LER; therefore, no performance deficiency was identified. The

inspectors also concluded that no violation of NRC requirements occurred.

Personnel Performance (1 Sample)

The inspectors evaluated response during the following non-routine evolutions or transients.

(1) Unit 3 underwent an unplanned power reduction to 45 percent on July 30, 2018,

following the loss of the 32 condensate pump. Initially, following the loss of the pump,

reactor power was reduced to 83 percent. However, because axial flux deviation was

found to be outside of the acceptable operation limits following the downpower,

operators took action to reduce power below 50 percent, in accordance with TS 3.2.3,

Condition C.

OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL

60845 - Operation of Inter-Unit Fuel Transfer Canister and Cask System

The inspectors evaluated the inter-unit wet fuel transfer canister and cask system on

September 10 to 13, 2018. Specifically, the inspectors reviewed or observed the following

activities:

Fuel selection and fuel loading of the shielded transfer canister (STC)

Heavy load movement of the loaded STC

Closure bolting of the STC

Helium leak test of the STC lid

STC pressure rise test

Radiological field surveys

Transfer and transport evolutions

INSPECTION RESULTS

Inadequate Procedural Guidance for Spent Fuel Movement and Storage Requirements

Cornerstone Significance Cross-Cutting Aspect Report

Section

Barrier Green H.3 - Change Management 71152

Integrity NCV 05000247/2018003-01

Closed

Introduction: The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion V, Procedures, when Entergy did not have appropriate documented instructions or

written procedures for spent fuel movement and storage requirements adjacent to potentially

degraded Boraflex panels. Specifically, configuration restrictions were not addressed in some

cases and, therefore, did not comply with controls to meet the CAOR in 2016; and the

resultant revised guidance did not accurately reflect the modeled supporting analysis.

Description: The Unit 2 SFP is composed of high-density racks with Boraflex neutron

absorber panels between cells. In 2002, Unit 2 TS 3.7.13, Spent Fuel Pit Storage, was

amended to allow for soluble boron credit in the criticality analysis, due to the degradation of

the Boraflex absorbers. This amendment also divided the SFP into regions and placed

restrictions on fuel assemblies that could be placed in each region based on cooling time,

burnup, initial enrichment, and number of integral fuel burnable absorbers. Entergy continued

to perform periodic testing of the Boraflex panels through 2013 to confirm the assumptions in

the CAO

R. In February 2014, Entergy determined that additional panels in Region 2-2

exceeded the degradation assumptions of the CAOR and that more panels would exceed the

assumptions based on absorbed dose and residency in the SFP. This issue was

documented in CR-IP2-2014-04414 (see Section 4OA2 in Indian Point Integrated Inspection

Report 05000247/2014003 and 05000286/2014003 (ADAMS Accession No. ML14223A045).

Entergy placed administrative controls into effect to ensure the criticality (k-effective) limits of

CFR 50.68(b)(4) would still be met until the condition was corrected.

The administrative controls included placing additional control over boron concentration and

development of configuration restrictions in procedure 0-NF-203, Internal Transfer of Fuel

Assemblies and Inserts, Revision 18, near any panels that were screened as potentially

degraded. The procedure allows the following approaches for meeting the CAOR in

Region 2-2:

Use the TS 3.7.13 loading requirements for Region 2-1 (more restrictive than

Region 2-2) on both sides of a degraded Boraflex panel

Maintain an empty cell on one side of a degraded panel

Maintain a rod cluster control assembly in a fuel assembly on one side of a degraded

panel

In 2016, the inspectors reviewed the SFP loading configuration to determine if it met the

administrative controls. The inspectors noted that three degraded panels in Region 2-2 along

the periphery did not meet one of the three approaches. An alternate approach was taken,

taking credit for a 1.25 inch water gap between adjoining modules between cells. Entergy

subsequently wrote CR-IP2-2016-01505 and completed a reanalysis to confirm the

configuration is bounded by the CAO

R. Based on the results of the vendor reanalysis,

Entergy updated the SFP operability evaluation and revised 0-NF-203, Revision 21, with

additional restrictive guidance.

Inspectors reviewed the revised guidance contained in procedure 0-NF-203, Revision 21.

This guidance contained two sets of rules for storing fuel in Region 2-2 of Entergys SFP.

The first set of rules governed storage within an SFP rack or across the interface between

two racks, without credit for the water gap between the racks. The second set of rules

governed storage across a rack interface with credit for the water gap between the racks.

This second set of rules is referred to as the interface rules.

The interface rules were established to meet analysis conditions, such as the boundary

conditions for adjacent assemblies. However, the inspectors identified that burnup

requirements and required placement of empty cells or assemblies with a control rod were not

sufficiently explicit to meet the analysis assumptions. Specifically, the model assumed a

specific 2 x 2 array; but the procedure allowed variations in the array. Certain variations, if

used in the SFP, would result in an unanalyzed level of activity and could potentially

challenge SFP requirements. Additionally, the wording in the procedure did not capture the

requirement that each fuel assembly has to have at least the amount of burnup required for a

given assembly in Region 2-2. The wording would have allowed one or more fuel assemblies

to have less burnup than that required for assemblies in Region 2-2, provided the aggregate

of the four fuel assemblies along the interface exceeded the Region 2-2 requirement by

GWD/M

T. This scenario, if used, also has the potential to increase reactivity and

challenge SFP requirements. The inspectors noted that Entergy had not used these

procedure steps to date at the time of NRC review.

Corrective Actions: Entergy generated CR-IP2-2016-01505 and performed a vendor

calculation of the impacted cells, updated the SFP operability evaluation, and revised

procedure 0-NF-203 to include additional restrictive guidance. Additionally, Entergy

generated CR-IP2-2018-03316 to revise guidance in 0-NF-203 to more accurately reflect the

vendor-modeled supporting analysis.

Corrective Action References: CR-IP2-2016-01505 and CR-IP2-2018-03316

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to have appropriate

documented instructions or written procedures for spent fuel movement and storage

requirements for configuration restrictions to meet the CAOR was a performance deficiency.

This performance deficiency was reasonably within Entergys ability to foresee and correct

and should have been prevented.

Screening: The inspectors determined the performance deficiency was more than minor

because it is associated with the design control attribute of the Barrier Integrity cornerstone

and adversely impacted the cornerstone objective to provide reasonable assurance that

physical design barriers (fuel cladding) protect the public from radionuclide releases caused

by accidents or events. Specifically, by not demonstrating compliance with the CAOR,

Entergy did not provide reasonable assurance that the SFP conditions would remain in

compliance with k-effective subcriticality requirements and that the fuel cladding barrier would

be maintained. This is similar to IMC 0612, Appendix E, Example 3.j, wherein an engineering

calculation error results in a condition where there is now a reasonable doubt on the

operability of a system or component, or wherein significant programmatic deficiencies are

identified with an issue that could lead to worse errors if uncorrected.

Significance: The inspectors assessed the significance of this finding using IMC 0609,

4, Phase 1, Initial Screening and Characterization of Findings, worksheet, which

directs the user to IMC 0609, Appendix A, The Significance Determination Process for

Findings At-Power. From IMC 0609, Appendix A, Exhibit 3, Barrier Integrity Screening

Questions, question D4, Does the finding affect the SFP neutron absorber, fuel bundle

misplacement (i.e., fuel loading pattern error) or soluble boron concentration (pressurized-

water reactor only)?, the inspectors determined that the final significance must be

determined using IMC 0609, Appendix M, Significance Determination Process Using

Qualitative Criteria. In accordance with Appendix M, a qualitative bounding evaluation was

performed, which determined that the finding was of very low safety significance (Green)

because a prior similar violations significance bounded this findings significance. The prior

similar violation occurred at the Peach Bottom Atomic Power Station, which was documented

in an integrated inspection report as NCV 05000277 and 05000278/2012002-03 (ADAMS

Accession No. ML12129A016), Untimely Corrective Actions Resulted in Spent Fuel Pool

Boraflex Degradation Exceeding Design Limits (EA-11-224). Peach Bottoms case involved

multiple inoperable cells which contained spent fuel assemblies; whereas, in the present

case, the extent of condition was much more limited. Because this violation was determined

to be of very low safety significance and entered into the CAP as CR-IP2-2016-01505 and

CR-IP2-2018-03316, it is being treated as an NCV, consistent with Section 2.3.2 of the NRC

Enforcement Policy.

Cross-Cutting Aspect: The finding had a cross-cutting aspect in the area of Human

Performance, Change Management, because Entergy did not utilize a systematic process for

evaluating and implementing changes, such that nuclear safety remained the overriding

priority. Specifically, when making changes to 0-NF-203, the station did not ensure that all

requirements were met.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion V, states that activities affecting quality shall

be prescribed by documented instructions, procedures, or drawings, of a type appropriate to

the circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Instructions, procedures, or drawings shall include appropriate

quantitative or qualitative acceptance criteria for determining that important activities have

been satisfactorily accomplished. Entergy procedure 0-NF-203 provides the instructions to

meet the requirements in the CAOR and compensates for having unconservative technical

specifications.

Contrary to this requirement, Entergy had not included appropriate criteria in procedures for

spent fuel assembly movement and storage in the Unit 2 SFP within Procedure 0-NF-203,

Internal Transfer of Fuel Assemblies and Inserts, Revision 21. Specifically, configuration

restrictions were not addressed in some cases, and therefore did not comply with controls to

meet the CAOR in 2016; and the resultant revised guidance did not accurately reflect the

modeled supporting analysis. Entergy generated CR-IP2-2016-01505 and performed a

vendor calculation of the impacted cells, updated the SFP operability evaluation, and revised

procedure 0-NF-203 with additional restrictive guidance. Additionally, Entergy generated

CR-IP2-2018-03316 to revise guidance in 0-NF-203 to more accurately reflect the

vendor-modeled supporting analysis.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Containment Fan Coolers 21 and 24 Motor Cooler Elbow Through-Wall Leaks Due to

Excessive Service Water Flow Rates and Safety System Functional Failures of

Containment

Cornerstone Significance Cross-Cutting Report

Aspect Section

Barrier Integrity Green None 71152

NCV 05000247/2018003-02

Closed

Introduction: A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion III,

Design Control, was identified when Entergy did not ensure that measures were established

for the selection and review for suitability of application of materials, parts, equipment, and

processes that are essential to the safety-related functions of the structures, systems, and

components. Specifically, in 1998, when the former license-holder for Unit 2 decided to

replace the original-construction large-radius, butt-welded elbow joints in the service water

motor cooler return lines from the Unit 2 FCUs with a new design (a short radius, socket-weld

fitting), these elbow joints were not properly evaluated for suitability of application. The

service water flow velocity through the modified FCU return piping was in excess of the

vendor-allowable flow velocity limit, which resulted in the gradual erosion of the motor cooler

elbow joints, eventually leading to through-wall leaks on an ASME class III piping system

inside containment, leading to breaches of containment integrity and safety system functional

failures.

Description: Between August 11, 2015, and November 21, 2016, Unit 2 experienced two

through-wall leaks on the service water motor cooler return lines to the 21 and 24

containment FCUs while operating at 100 percent reactor power. These leaks were identified

when the operators noted increased unidentified leakage into containment and confirmed that

the leakage was from service water coming from the following return lines:

FCU motor cooler return line: A 2-gpm leak was identified on the 24 FCU return

line elbow on August 11, 2015. Entergy maintained this line in service until an

engineered clamp was installed to stop the leak. Upon inspection, the leak in the

elbow was determined to have been caused by flow-accelerated corrosion because

the velocity of the service water stream was higher than the allowable flow velocity in

the elbow joint, as specified by the vendor (LER 0205000247/2015001-02, Technical

Specification Prohibited Condition Due to an Inoperable Containment Caused by a

Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed

Leakage Rate for Containment, on July 24, 2018 (ADAMS Accession No.

ML17248A466)).

FCU motor cooler return line: A 1-gpm leak was identified on the 21 FCU return

line elbow on December 20, 2015. Entergy isolated service water flow to the 21 FCU

and the leaking elbow was replaced. Upon inspection, the leak in the elbow was

determined to have been caused by erosion/corrosion because the velocity of the

service water stream was higher than the allowable flow velocity in the elbow joint, as

specified by the vendor (LER 05000247/2015004-00, Safety System Functional

Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan

Cooler Unit Service Water Motor Cooling Return Pipe, on February 18, 2016 (ADAMS

Accession No. ML16057A178)).

In 1998, the former license-holder for Unit 2 elected to replace the large radius, butt-welded

elbow joints in the Unit 2 FCU motor cooler return lines with short radius, socket-welded

elbows, because of operating experience with through-wall leaks (CR-IP2-1998-06507).

Subsequently, Entergy experienced through-wall leaks on the copper-nickel FCU piping, due

to corrosion when in service, in 2001, 2006, and 2008. In 2009, Entergy began a project to

replace all copper-nickel piping to the FCUs with AL6XN stainless steel piping to prevent

further leaks due to corrosion. In 2013, Entergy cancelled this project after noting that no

additional leaks had occurred since 2008.

In 2015, during the causal investigation into the above leaks, Entergy identified that the

service water flow rates through the motor cooler return lines from the Unit 2 FCUs had

exceeded the vendor-specified flow rate for the piping elbows by a significant amount. The

measured flow rate through the FCU motor cooler elbow joints were measured at 55 to

gpm. The vendor-allowable flow rate through these elbows was limited to

6-feet-per-second flow velocity, which correlated to a service water flow rate of 17 gpm, to

prevent erosion of the copper-nickel elbow wall.

In 1998, when the licensee replaced the Unit 2 FCU service water return line large radius

elbows with socket-welded, short-radius elbows, they did not assess the vendor-specified

limits on flow rates. The licensee considered this replacement as a like-for-like replacement,

because the elbows were listed in the piping specification tables, even though the

replacement elbows had a very different form factor. The elbow radius was much shorter,

and the imposition of a socket weld on the inside of the elbow bend created a small intrusion

into the flow stream; both of these differences from the original-design piping configuration

created additional turbulence. Excessive turbulence in the flow stream creates cross-flows

and eddy currents that can erode copper-nickel piping if the flow velocity is excessive.

Corrective Actions: All Unit 2 FCU motor cooler service water supply elbows were inspected

and replaced during the refueling outage. The service water flow rates were reduced from

55-to-60 gpm to 25-to-30 gpm, which reduced the turbulence and erosion rates in the elbow

joints. These corrective actions appear to have been effective, as there have been no

additional leaks in the FCU service water lines since 2016.

Corrective Action References: CR-IP2-1998-06057, CR-IP2-2015-03550,

CR-IP2-2015-05755, CR-IP2-2016-07188, and CR-IP2-2016-07271

Performance Assessment:

Performance Deficiency: Entergy did not ensure that measures were established to

adequately control service water flow rates through the FCU motor cooler supply elbow joints

and maintain these flow rates below vendor-specified limits on flow velocity. The excessive

flow rates caused excessive turbulence in the elbow joints, which led to erosion of the

copper-nickel elbows. Excessive flow eventually created through-wall leaks in an ASME

class III piping system, which caused a breach in containment integrity and a safety system

functional failure.

Screening: The inspectors determined that this self-revealing finding was within Entergys

ability to foresee and prevent. Entergy had identified that the FCU elbow joints were

experiencing leaks in 2001, 2006, and 2008 but did not recognize the excessive service water

flow condition. These previous leaks, although not directly caused by flow erosion, provided

an opportunity to have identified the problem at an earlier date, before the flow erosion

compromised the integrity of the FCU motor cooler piping elbows. Using IMC 0612,

Appendix B (Issue Screening), the inspectors determined the performance deficiency was

more than minor because it was associated with the design control attribute of the Barrier

Integrity cornerstone, and it adversely affected the cornerstone objective of providing

reasonable assurance that physical design barriers (fuel cladding, reactor coolant system,

and containment) protect the public from radionuclide releases caused by accidents or

events. Specifically, the FCU service water lines are the barrier between containment and

the environment. A hole in the FCU service water lines during accident conditions when

containment is pressurized could potentially result in the release of radioactive material into

the Hudson River. These leaks represented a safety system functional failure of the

containment barrier.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix A, Exhibit 3, and IMC 0609, Appendix

H. Using Appendix A, the issue was referred

to Appendix H because each FCU through-wall leak represented an open pathway in the

physical integrity of reactor containment. Using Appendix H, the inspectors determined that

the finding screened to Green. The finding was determined to be a Part B finding (affecting

the large early release frequency but not affecting core damage frequency (CDF) because for

each example, the minor reduction in service water flow due to the small leak rate did not

compromise the capability of the FCUs to remove heat from containment. Using Table 4.1

and Figure 4.1 of IMC 0609, Appendix H, the finding screened to Green because CDF was

not affected; the FCUs capability to remove heat from containment was not degraded. In

addition, any release through the service water lines would be thoroughly scrubbed for

particulates and Iodine.

Cross-Cutting Aspect: The inspectors did not assign a cross-cutting aspect for this issue

because it was not indicative of current Entergy performance. The initial performance

deficiency occurred in 1998, when the previous license-holder for Unit 2 did not complete an

adequate design change review of replacement FCU joints. Entergy eventually took

appropriate corrective action when they identified that the service water flow rates were in

excess of the vendor-specified limits for the replacement FCU elbows.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criteria III, Design Control, requires, in part, that

measures shall be established for the selection and review for suitability of application of

materials, parts, equipment, and processes that are essential to the safety-related functions

of the structures, systems, and components.

Contrary to the above, in 1998, the previous license-holder for Unit 2 decided to replace the

original construction large-radius, butt-welded elbow joints in the service water return lines

from the Unit 2 FCUs with a new design - a short radius, socket-weld fitting. These elbow

joints were not properly evaluated for suitability of application. From 1999 for a period of

years, the service water flow rates through the modified FCU return piping were in excess

of the vendor-specified flow velocity. This condition ultimately caused erosion of the elbow

joints, which eventually caused through-wall leaks on an ASME class III piping system inside

containment, leading to breaches of containment integrity and safety system functional

failures.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Containment Fan Cooler 24 Through-Wall Service Water Leak Caused by Inadequate

Application of Epoxy Coating Resulting in Corrosion and a Safety System Functional

Failure of Containment

Cornerstone Significance Cross-Cutting Report

Aspect Section

Barrier Integrity Green H.13 - 71152

NCV 05000247/2018003-03 Consistent

Closed Process

Introduction: A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, was identified when Entergy did not ensure that

activities affecting quality were prescribed by documented instructions or procedures, of a

type appropriate to the circumstances, and that these activities were accomplished in

accordance with these instructions, procedures or drawings. Furthermore, Entergy did not

ensure that the instructions or procedures included appropriate quantitative or qualitative

acceptance criteria for determining that important activities have been satisfactorily

accomplished. Specifically, Entergy did not ensure that the maintenance procedure for

applying the internal Enecon' epoxy coating to the 24 fan cooler main cooler supply line

elbow was adequate to ensure proper epoxy coating adherence, and Entergy did not

adequately verify the coating adherence prior to placing the elbow in service. This resulted in

a through-wall leak and a safety system functional failure of containment.

Description: On November 21, 2016, a 15-gpm leak was identified on the 24 FCU main

cooler service water supply line elbow inside containment, an ASME,Section XI, code

class III boundary. The leaking component was a 3-inch carbon steel pipe elbow that had

been previously coated with Enecon' epoxy on the interior surfaces to prevent corrosion.

The leak represented a direct release pathway from containment and was determined to be a

safety system functional failure by Entergy. The cause of the leak was attributed to the failure

of the Enecon' epoxy coating to adequately adhere to the interior walls of the elbow

(LER 05000247/2016010-00 and 05000247/2016010-01, Safety System Functional Failure

Due to an Inoperable Containment Caused by a Through-Wall Defect in a Service Water

Supply Pipe Elbow to the 24 Fan Cooler Unit).

The FCU main cooler supply lines are made of 3-inch diameter, cement-lined carbon steel

piping. The elbow was also made of carbon steel, but was internally coated with Enecon'

epoxy (not cement-lined) to prevent corrosion. Entergys causal assessment attributed the

cause of the through-wall leak to the compromise of the integrity of the Enecon' coating.

The Enecon' coating had a small defect which allowed brackish service water to contact the

carbon steel and corrode the metal. Entergy attributed the failure to an inadequate

maintenance procedure, 0-SYS-409-GEN, Belzona and Enecon' Metal Repair

Applications, which did not mandate detailed instructions or require post-coating quality

control inspections. The FCU main cooler supply line was classified as ASME,Section XI,

class III piping boundary.

The through-wall leak was detected by a rise in the waste holdup tank and containment sump

levels. The leak was immediately isolated, and the 24 FCU was removed from service. The

service water piping is part of the containment boundary, and the leak represented a safety

system functional failure of containment. The leak was isolated within the outage time

allowed per TS 3.6.1, and a non-emergency notification was made to the NRC for a safety

system functional failure under 10 CFR 50.72(b)(3)(v) by Event Notification number 5238.

Corrective Actions: Maintenance procedure 0-SYS-409-GEN was revised, and all FCU main

cooler supply line elbows were inspected during the last refueling outage. No other

indications or coating failures were identified. The 24 FCU supply line elbow was

weld-repaired and recoated with Enecon' epoxy. The Generic Letter 89-13, Service Water

System Problems Affecting Safety-Related Equipment, program was also revised to include

a requirement to conduct and document a 100-percent internal lining visual inspection of all

3-inch FCU piping elbow spool pieces, when removed during future FCU cooling coil

maintenance activities. These corrective actions appear to have been effective, as there

have been no additional leaks in the FCU service water lines since 2016.

Corrective Action References: CR-IP2-2016-06934 and CR-IP2-2016-07271

Performance Assessment:

Performance Deficiency: Entergy failed to ensure that the procedure, 0-SYS-409-GEN, that

controlled the application and quality control testing of Enecon' epoxy coating, was

adequate to ensure epoxy adherence to the safety-related pipe wall, as required, prior to

placing the 24 FCU main cooler supply elbow in service.

Screening: The inspectors determined that this self-revealing finding was within Entergys

ability to foresee and prevent. Using IMC 0612, Appendix B (Issue Screening), the inspectors

determined the performance deficiency was more than minor because it was associated with

the design control attribute of the Barrier Integrity cornerstone and adversely affected the

cornerstone objective of providing reasonable assurance that physical design barriers (fuel

cladding, reactor coolant system, and containment) protect the public from radionuclide

releases caused by accidents or events. Specifically, the FCU service water line is the barrier

between containment and the environment. A hole in the service water line during accident

conditions when containment is pressurized could potentially result in the release of

radioactive material into the Hudson River. The leak represented a safety system functional

failure of the containment barrier.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix A, Exhibit 3, and IMC 0609, Appendix

H. Using Appendix A, the issue was referred

to Appendix H because the FCU through-wall leak represented an open pathway in the

physical integrity of reactor containment. Using Appendix H, the inspectors determined that

the finding screened to Green. The finding was determined to be a Part B finding (affecting

the large early release frequency but not affecting CDF) because for each example, the minor

reduction in service water flow due to the small leak rate did not compromise the capability of

the FCUs to remove heat from containment. Using Table 4.1 and Figure 4.1 of IMC 0609,

Appendix H, the finding screened to Green because CDF was not affected; the FCUs

capability to remove heat from containment was not degraded. In addition, any release

through the service water lines would be thoroughly scrubbed to reduce any radioactive

particulates and iodine prior to release to the atmosphere.

Cross-Cutting Aspect: Human Performance, Consistent Process: Individuals use a

consistent, systematic approach to make decisions. Risk insights are incorporated as

appropriate. Specifically, Entergy did not ensure that the maintenance procedure

appropriately considered the risk impact of a failure of the epoxy coating. They did not

recognize that this process could affect the integrity of a safety-related component and was

required to be controlled under the quality assurance program.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings,

requires, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, or drawings. Instructions,

procedures, or drawings shall include appropriate quantitative or qualitative acceptance

criteria for determining that important activities have been satisfactorily accomplished.

Contrary to the above, Entergy did not provide an adequate procedure for the application of

the Enecon' epoxy coating and did not require an adequate quality control hold point

inspection prior to placing the component in service.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Inadequate Procedure for Turbine Startup Caused a Reactor Trip

Cornerstone Significance Cross-Cutting Report

Aspect Section

Initiating Events Green H.13 - 71153

NCV 05000247/2018003-04 Consistent

Closed Process

Introduction: A self-revealing Green NCV of TS 5.4.1, Procedures, was identified because

Entergy did not provide adequate guidance in 2-SOP-26.4, Turbine Generator Startup,

Synchronization, Voltage Control, and Shutdown. Specifically, Entergy did not provide

adequate procedural direction to ensure the main turbine control oil stop valve Z was in the

correct position. As a result, the steam generator water level exceeded the trip setpoint for

the main boiler feed pumps which led the operators to insert a manual reactor trip.

Description: On April 19, 2018, operators on Unit 2 were performing a startup of the main

generator turbine to perform overspeed testing. Load limit 2 was selected to raise turbine

speed, and load limit 1 was to be raised and maintained at a higher level to ensure that load

limit 2 was in control. However, unknown to operators, control oil valve Z had been

inadvertently closed, which removed load limit 2 from service, thereby placing load limit 1 in

control. When load limit 1 was raised, the resulting increase in load limit 1 oil pressure

caused the turbine stop and control valves to open rapidly. This led to an increase in steam

flow from 0 to 1.0 million lbm per hour in 17 seconds with a corresponding increase in steam

generator water levels from 38 percent to 73 percent. The steam generator water level

increase caused a main feedwater isolation, a trip of the main boiler feed pumps, and a

turbine trip. A reactor trip signal was inserted by operators in accordance with procedure

2-AOP-FW-1, Loss of Feedwater, with reactor power at 8 percent and no main boiler feed

pumps running.

Entergy performed a root cause evaluation and determined the direct cause of the event to be

the misposition of the main turbine generator control oil valve Z. A contributing cause was an

inadequate process used to determine which equipment lineup check off lists are performed

at the end of an outage. The turbine had undergone extensive maintenance during the

refueling outage and there were numerous maintenance workers who worked on jobs in the

near vicinity of the turbine front standard where the valve was located. Although there was no

specific evidence of when the valve position was changed, a detailed search of work orders

determined that the valve should not have been repositioned as the result of outage work.

The decision to perform check off lists at the end of the outage that are not required is left to

the judgement of operations management who did not adequately consider the risk of a valve

being mispositioned in light of the extensive amount of work in the vicinity of the Z valve.

Corrective Actions: Entergy repositioned the main turbine generator control oil Z valve and

revised procedure 2-SOP-26.4 to provide guidance to operators to check the position of the

valve when starting the turbine generator. Entergy also revised IP-SMM-OU-104, Shutdown

Risk Assessment, to require a turbine control oil valve line up verification prior to startup

following a refueling outage.

Corrective Action Reference: CR-IP2-2018-02806

Performance Assessment:

Performance Deficiency: The inspectors determined that not providing adequate guidance in

procedure 2-SOP-26.4 was a performance deficiency that was within Entergys ability to

foresee and prevent and should have been corrected. Specifically, Entergy did not provide

adequate procedural direction to ensure the turbine control oil valve was in the correct

position before starting the turbine generator, which subsequently led to the operators

manually inserting a reactor trip.

Screening: In accordance with IMC 0612, Appendix B (Issue Screening), this finding is more

than minor because it is associated with the procedure quality attribute of the Initiating Events

cornerstone and adversely affected the cornerstone objective of limiting the likelihood of

events that upset plant stability and challenge critical safety functions during shutdown as well

as power operations. Specifically, the failure to provide adequate procedural direction to

ensure the main turbine generator control oil valve was in the correct position before starting

the main turbine generator led to operators placing the system in a configuration that

increased the likelihood of events that upset plant stability of the main turbine generator to

respond to load limit instrumentation.

Significance: The inspectors assessed the significance of this finding using IMC 0609.04,

Initial Characterization of Findings, and IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power. This finding was determined to be of very low

safety significance (Green) because the finding did not cause a reactor trip and the loss of

mitigation equipment relied upon to transition the plant from the onset of the trip to a stable

shutdown condition.

Cross-Cutting Aspect: This finding had a cross-cutting aspect in the area of Human

Performance, Consistent Process, because Entergy did not use a consistent, systematic

approach to make decisions. Specifically, Entergy did not use an an adequate process to

determine which equipment lineup check off lists are performed at the end of an outage. Had

a consistent and adequate process for valve checks been established, rather than relying on

judgement-based decision making, that process could have ensured that valves with a high

trip risk would have been checked to ensure that they had not been inadvertently manipulated

during outage activities.

Enforcement:

Violation: Unit 2 TS 5.4.1 requires that written procedures shall be established, implemented,

and maintained as recommended by Appendix A of Regulatory Guide 1.33, Revision 2.

Appendix A requires operating procedures for turbine startup. Specifically, procedure

2-SOP-26.4 did not provide adequate procedural direction to ensure the turbine control oil

valve was in the correct position before starting the turbine generator, which subsequently led

to the operators manually inserting a reactor trip.

Contrary to the above, Entergy did not adequately maintain operating procedure 2-SOP-26.4,

Turbine Generator Startup, Synchronization, Voltage Control, and Shutdown, by not

including specific steps or precaution detail to ensure the turbine control oil valve was in the

correct position before starting the turbine generator.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy. The disposition of this finding and associated violation closes LER 05000247/2018002-00.

Observations 71152

Annual Follow-Up of

Selected Issues

Accelerated Neutron-Absorber (Boraflex) Degradation in the Unit 2 SFP Documented in

CR-IP2-2014-04414

The inspectors reviewed CR-IP2-2014-04414, which documented Entergys actions in

response to BADGER testing (periodic testing of the Boraflex panels) that revealed panels in

the Unit 2 SFP did not meet the requirements of the CAOR in Region 2-2, where Boraflex is

credited. The description of the event, corrective actions, and enforcement aspects of this

event are documented in the Inspection Results section, NCV 05000247/2018003-01.

The inspectors assessed Entergys problem identification threshold, operability determination,

problem analysis, extent-of-condition reviews, compensatory measures and/or administrative

controls, and prioritization timeliness of corrective actions to determine whether Entergy was

appropriately identifying, characterizing, and correcting problems associated with this issue

and whether the planned or completed corrective actions were appropriate. The inspectors

compared the actions taken to the requirements of Entergy's CAP and 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action.

Entergy classified the issue (in addition to another five SFP Boraflex reviewed condition

reports) as Category-C, which are broke/fix and require no formal evaluation. This is the

lowest level of review specified by CAP procedure EN-LI-102, Corrective Action Process.

The CAP procedural guidance for Category-C reactivity management events in place at the

time classified a Category-C item as an adverse condition classified as non-significant or a

non-adverse condition and as a condition that has or would have minimal effect on the safe

or reliable operation of the plant or personnel. The guidance further stated that a

Category-C condition does not meet the definition of significant and that repeat occurrence

of the problem is viewed as acceptable.

The issue was minor because, although the condition reports were screened incorrectly and

no evaluation was completed, Entergy performed all of the actions required by higher level

classifications. Entergy performed vendor calculations and operability evaluations and

completed all planned corrective actions. The inspectors noted that a trend of this type of

misclassification has been identified in the semi-annual trends, as documented in quarterly

resident reports. Entergy documented this issue in CR-IP2-2018-03306.

The inspectors reviewed extent of condition as part of this inspection. CR-IP2-2012-05966

described the results of categorization of fuel in the Unit 2 SFP. The Unit 2 TSs were

non-conservative for Region 2-2 with respect to fuel assemblies greater than certain U235

enrichments, although fuel stored in the region still met 10 CFR 50.68 requirements and

operability was maintained. The station planned a corrective action to perform an

extent-of-condition review on Unit 3; however, no analysis or evaluation has been performed.

This issue was initially documented in 2012. The inspectors identified that the corrective

action was incorrectly closed to a lower-tier process and was therefore not tracked under the

same requirements. EN-LI-102, Corrective Action Process, Revision 20, step 5.9[4]B states

that the only process that a corrective action or (condition report) can be closed to is a work

order with a priority of 1. Contrary to this requirement, Entergy personnel closed out the

corrective action to an SFP management tracker, which is a lower-tier process. The issue

was minor since the Unit 3 SFP does not use Boraflex as a neutron absorber and is not

subject to the same degradation. Entergy documented this issue as CR-IP2-2018-03262.

Observations 71152

Annual Follow-Up of

Selected Issues

Containment FCU Elbow Leaks: Units 2 and 3 experienced four service water leaks in FCU

piping elbows in 2015 and 2016. The purpose of this inspection was to review the causal

evaluations for potential common causes and corrective actions implemented as a result of

these leaks.

Purpose: The FCUs are used to cool the containment air during power operations and during

an event. The Unit 2 FCUs are supplied with service water as a cooling medium through

3-inch diameter cement-lined carbon steel piping to the main coolers (heat exchangers) and

2-inch copper-nickel lines to the motor coolers. Unit 3 has Type 904L stainless steel supply

and return lines. These supply and return lines are classified as ASME,Section XI, code

class III piping boundaries into containment. A leak from one of these FCU service water

lines may constitute a breach of containment if the leak rate exceeds TS 3.6.1 allowable leak

rate (La) because the operating pressure in the service water lines is lower than the design

pressure during a design basis accident inside containment.

LER Sequence: Entergy experienced a series of four leaks in the piping elbow joints that

route the service water to the FCUs:

1. 24 FCU motor cooler return line on August 11, 2015 (LER 05000247/2015001-02)

2. 21 FCU motor cooler return line on December 20, 2015 (LER 05000247/2015004-00)

3. 31 FCU main cooler return line on November 3, 2016 (LER 05000286/2016001-00 and

05000286/2016001-01)

4. 24 FCU main cooler supply line on November 21, 2016 (LER 05000247/2016010-00

and 05000247/2016010-01)

Design Control: In 1998, Unit 2 experienced several through-wall leaks on the FCU motor

cooler return lines. The former licensee replaced the large-radius 2-inch FCU butt-welded

copper-nickel motor cooler return line elbows with socket welded elbows

(CR-IP2-1998-06057). At the time, this modification was determined to be a like-for-like

replacement, and the licensee did not use an engineering change package to ensure that the

new design was functionally equivalent to the old design. However, the new design elbow

had a much tighter bend radius and was installed using a socket-welded fitting rather than a

butt-welded fitting. These differences in form factor created greater turbulence in the service

water flow stream inside the new elbow joints. The elbows appeared to be eroded

through-wall at the socket intrados (where the socket fitting weld is located). In 2016, while

completing the causal assessment for leaks in the 21 and 24 FCUs, Entergy researched the

specifications of the replacement elbows and discovered that the vendor-specified flow

velocity was limited to 6 feet per second. This is equivalent to a service water flow rate of

gpm. The actual flow rate through the motor return line elbows was 55 to 60 gpm. As a

result of over 15 years of excessive flow conditions, the copper-nickel elbows had been

severely eroded by the turbulent flow stream leading to through-wall leaks. Entergy reduced

the flow rate through these lines to 25 to 30 gpm and subsequently replaced all FCU motor

cooler elbow fittings with new elbows during the 2016 outage. It was not possible to reduce

the flow rate to under 17 gpm because this would not have provided sufficient cooling flow to

the containment FCU motors to remove heat during accident conditions. However, it is

expected that the new FCU elbows will adequately resist erosion and remain in service until

20, when Unit 2 is scheduled to shut down.

FCU Motor Cooler Return Line Leak: When the first elbow leak (2 gpm) occurred in

August 2015 on the 24 FCU motor cooler return line, Entergy assessed that the leak rate from

containment to the environment would not be sufficiently high to exceed the TS 3.6.1

allowable leakage value, La, based on engineering judgment. The inspectors questioned this

determination and issued a Green NCV (05000247/2015003-02 in Indian Point Integrated

Inspection Report 05000247/2015003 and 05000286/2015003 (ADAMS Accession No.

ML15316A083)) for failing to properly assess operability for the containment. In 2016,

Entergy analyzed the limiting leak rate to the environment during design basis accident

conditions and determined that any service water in-leakage rate greater than approximately

0.024 gpm into containment during normal operating conditions, where service water pressure

is greater (at ~20 psig) than containment pressure (at ~0 psig), would exceed the TS

allowable out-leakage rate, La, of 0.1 percent of containment air weight per day

(77,677 cc/day). The leakage from containment into the environment under accident

conditions (when containment is pressurized (at ~54 psig) higher than service water pressure

(at ~15 psig) operating at its design basis maximum load conditions) rendered containment

inoperable and constituted a safety system functional failure.

FCU Motor Cooler Return Line Leak: Subsequently, when the second elbow leak (1 gpm)

occurred on the 21 FCU motor cooler return line on December 20, 2015, Entergy took action

to immediately isolate the leak and replaced the leaking elbow within the allowable outage

time for TSs.

Violation: As a result of the leaks in 2015 on the 21 and 24 FCU motor return lines, the

inspectors issued a Green NCV against 10 CFR Part 50, Appendix B, Criteria III, Design

Control (NCV 05000247/2018003-02).

FCU Main Cooler Supply Line Leak: The Unit 2 FCU main cooler supply lines are 3-inch

lines made of cement-lined carbon steel piping. The elbows in the supply line were coated

with a layer of Enecon' advanced polymer coating (not cement-lined) to prevent brackish

water from the Hudson River from corroding the carbon steel. The flow balance is established

to these lines by throttling the discharge valves to ensure proper flow rates. When a 10-gpm

leak occurred on the 24 FCU main cooler supply line in November 2016, Entergy took

appropriate actions to immediately isolate the line, submit an 8-hour prompt report under

CFR 50.72, and installed a clamp to stop the leakage until the elbow could be replaced

during the next outage. When the leaking elbow was removed and inspected, there was a

small defect in the Enecon' coating that allowed Hudson River water to contact the carbon

steel and corrode a small hole through the elbow. In the apparent casual analysis, Entergy

reached the conclusion that a small defect in the Enecon' coating was caused by the failure

to properly apply the Enecon' coating. Corrective actions included a change to the

procedure 0-SYS-409-GEN, Belzona and Enecon' Metal Repair Applications, to ensure

that the Enecon' coating is properly applied and inspected to ensure that there are no

defects in the coating application prior to installation and updating the qualification

requirements for coating and lining inspections.

Violation: The inspectors issued a Green NCV against 10 CFR Part 50, Appendix B, Criteria

V, Procedures (NCV 05000247/2018003-03).

FCU Main Cooler Supply Line Leak: The Unit 3 FCU main cooler supply lines are 3-inch

lines made of Type 904L stainless steel pipe, which is not generally susceptible to corrosion

by chlorides in brackish water. When a 0.16-gpm leak occurred on the 31 FCU main cooler

supply line on November 3, 2016, Entergy took appropriate actions to immediately isolate the

line, submit an 8-hour prompt report under 10 CFR 50.72, and install a clamp to stop the

leakage until the elbow could be replaced during the next outage.

Operators noted that the containment sump water contained a higher-than-normal level of

chlorides. Operator inspections of the FCU service water lines identified a 0.16-gpm

through-wall leak on the 31 FCU main cooler return line on November 3, 2016. The FCU

return lines on Unit 3 are 3 inches in diameter and are made of Type 904L stainless steel

pipe, which is not generally susceptible to corrosion by chlorides in brackish water. However,

the leak was in the heat-affected region of the elbow weld transition joint, and Entergys

causal analysis determined that the joint was likely not properly welded with the correct weld

material. As a result, microbiologically-influenced corrosion corroded a pinhole through the

heat-affected weld area. This failure was not associated with high-service water flow rates or

lack of epoxy coating adherence. There have been very few through-wall leaks on the Unit 3

FCU service water lines since original construction, and there is little internal operating

experience with this mode of failure. The Type 904L stainless steel construction has

generally made these lines impervious to corrosion. Entergy immediately isolated this leak

and promptly reported it within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> under 10 CFR 50.72. LER 05000286/2016001-01

(Revision 2) dated January 6, 2017, acknowledged that the condition was a safety system

functional failure of containment.

There was no performance deficiency identified associated with the 31 FCU main cooler

supply line leak. Entergy identified this through-wall leak as the result of deliberate

observations of plant conditions during operator rounds and inspections. The leak rate was

significantly smaller than the other FCU leaks. There was no violation identified. Entergy

received code relief from the NRC to complete repairs.

Prompt Reporting Considerations: These four FCU leaks each constituted safety system

functional failures for containment. Initially, Entergy used engineering judgment to determine

that the small leak rates did not result in a failure of containment. However, in response to an

NRC-issued prior violation, Green NCV 05000247/2015003-02 in Indian Point Integrated

Inspection Report 05000247/2015003 and 05000286/2015003 (ADAMS Accession No.

ML15316A083), Entergy conducted an engineering analysis of the effects of the service water

leak rate on containment operability. The results of this analysis showed that any service

water leakage that exceeded approximately 0.024 gpm would result in out-leakage from

containment during design basis accident conditions in excess of TSs for containment

operability and would result in a safety system functional failure. After discussing these

results with the Entergy fleet, the decision was made to consider these piping failures as

safety system functional failures of containment. These results were confirmed by an

independent vendor analysis in August of 2018.

The 24 FCU motor cooler return line leak occurred on August 11, 2015, and was later

reported as a safety system functional failure under LER 05000247/2015001-01 on

September 15, 2016, over one year after the event occurred. Entergy reported the leak on

the 21 FCU in LER 05000247/2015004-00 on February 18, 2016, 60 days after the event

occurred, as a safety system functional failure. Although Entergy did not initially report either

safety system functional failures within the 8-hour non-emergency prompt reporting

requirement under 10 CFR 50.72(b)(3)(v)(C), they did ultimately report the underlying

conditions under 10 CFR 50.73(a)(2)(v)(C) in their LER submittal after recognizing that the

event or condition could have prevented the fulfillment of the safety function of structures or

systems that are needed to control the release of radioactive material. Entergys failure to

promptly report the leaks under 10 CFR 50.72(b)(3)(v)(C) was considered to be a minor

violation, in accordance with NRC enforcement guidance, because the conditions were

eventually reported, and the NRC would not have taken any additional regulatory action had

they been promptly reported within the 8-hour period. Entergy subsequently promptly

reported the leaks on both the 24 FCU main cooler supply line (LER 05000247/2016010-00)

and the 31 FCU main air cooler supply line (LER 05000286/2016001-00) as safety system

functional failures.

There have been no additional service water through-wall leaks in the FCUs at either unit

since 2016. As a result, the actions taken by Entergy appear to have been effective in

correcting the underlying conditions.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public

disclosure.

On October 31, 2018, the inspectors presented the quarterly resident inspector inspection

results to Mr. Anthony Vitale, Site Vice President and other members of the Entergy staff.

THIRD PARTY REVIEWS

The inspectors reviewed Institute of Nuclear Power Operations reports that were issued during

the inspection period.

DOCUMENTS REVIEWED

Common Documents Used

Indian Point Units 2 and 3, Control Room Narrative Logs

Indian Point Units 2 and 3, Individual Plant Examination

Indian Point Units 2 and 3, Individual Plant Examination of External Events

Indian Point Units 2 and 3, Plan of the Day

Indian Point Units 2 and 3, Technical Requirements Manual

Indian Point Units 2 and 3, Technical Specifications and Bases

Indian Point Units 2 and 3, Updated Final Safety Analysis Report

71111.04

Procedures

2-COL-10.1.1, Safety Injection System, Revision 36

3-COL-MS-1, Main and Reheat Steam System, Revision 28

3-COL-SI-001, Safety Injection System, Revision 44

Condition Reports (CR-IP3-)

2018-02889

71111.05A/Q

Procedures

EN-DC-161, Control of Combustibles, Revision 18

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2017-03012 2018-03103 2018-04749*

Condition Reports (CR-IP3-) (*initiated in response to inspection)

2018-01894* 2018-01930* 2018-02527* 2018-02538* 2018-02889*

Maintenance Orders/Work Orders

WO 00477858

Miscellaneous

PFP-305, Safety Injection Pumps/Main Corridor - Primary Auxiliary Building, Revision 0

PFP-305A, Mini Containment and Pipe Tunnels - PAB/Fan House, Revision 0

PFP-306A, Containment Cooling Pumps, Primary Auxiliary Building, Revision 0

PFP-306B, Containment Spray Pumps, Primary Auxiliary Building, Revision 15

PFP-351, 480V Switchgear Room, Control Building, Revision 15

PFP-354A, Control Building Exhaust Fan Room and EDG Air Intake Enclosure, Revision 0

PFP-355, Lower Electrical Tunnel, Revision 5

PFP-356, Lower Electrical Penetration Area, Revision 0

PFP-357, Upper Electrical Tunnel, Revision 5

PFP-358, Upper Electrical Penetration Area, Revision 15

PFP-365, Auxiliary Feedwater Pump Room, Auxiliary Feedwater Building, Revision 15

PFP-366, Chemical Additive Room, Auxiliary Feedwater Building, Revision 13

PFP-367, Atmospheric Steam Dumps, Auxiliary Feedwater Building, Revision 5

PFP-367A, Auxiliary Feedwater Building, 64-Foot and 77-Foot Elevations, Revision 4

Transient Combustible Evaluations (*initiated in response to inspection)

18-054*

71111.07

Condition Reports (CR-IP2-)

2017-02865 2018-00892 2018-01346 2018-01979 2018-01981 2018-02068

Condition Reports (CR-IP3-)

2016-03337 2016-03346 2016-03350 2016-03360

Miscellaneous

Indian Point 89-13 Program Summary, February to March 2018

71111.11

Procedures

2-AOP-FW1, Loss of Main Feedwater, Revision 15

2-E-0, Reactor Trip or Safety Injection, Revision 8

2-E-1, Loss of Reactor or Secondary Coolant, Revision 4

2-ES-1.3, Transfer to Cold Leg Recirculation, Revision 9

2-ES-1.4, Transfer to Hot Leg Recirculation, Revision 3

2-FR-P.1, Response to Imminent Pressurized Thermal Shock, Revision 5

3-POP-1.2, Reactor Startup, Revision 58

3-POP-1.3, Plant Startup from Zero to 45 Percent Power, Revision 69

3-POP-2.1, Operation at Greater than 45 Percent Power, Revision 67

3-SOP-CVCS-003, Reactor Coolant System Boron Concentration Control, Revision 43

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2018-04543 2018-04544 2018-04545 2018-04546 2018-04547 2018-04548

71111.12

Procedures

EN-DC-315, Flow Accelerated Corrosion Program, Revision 13

Drawings

21-F-20233, Flow Diagram - Moisture Separator and Reheater Drains and Vents, Sheet 1,

Revision 26

21-F-20233, Flow Diagram - Moisture Separator and Reheater Drains and Vents, Sheet 2,

Revision 15

Miscellaneous

IP3-RPT-HD-01922, Maintenance Rule Basis Document for System F40-0083 - Heater Drains,

Moisture Separator Drains, and Vents System, Revision 0

IP3-RPT-Mult-01921, Maintenance Rule Basis Document for Plant Level Performance,

Revision 1

71111.13

Procedures

EN-OP-119, Protected Equipment Postings, Revision 9

EN-WM-104, On Line Risk Assessment, Revision 18

IP-SMM-OP-104, Offsite Power Continuous Monitoring and Notification, Revision 13

Condition Reports (CR-IP2-)

2018-03714 2018-03779 2018-02021

Condition Reports (CR-IP3-) (*initiated in response to inspection)

2018-02339 2018-02388*

Miscellaneous

Unit 2 Equipment Out of Service on Line Risk Assessment for August 14, 2018

Unit 2 Protected Equipment Posting Log Sheet for August 14, 2018

Unit 3 Equipment Out of Service on Line Risk Assessment for August 13, 2018

Unit 3 Equipment Out of Service on Line Risk Assessment for August 16, 2018

Unit 3 Unit Log for August 13, 2018

71111.15

Procedures

2-PT-V67A, Essential Service Water Header Flow Balance, Revision 5

EN-HU-104, Technical Task Rigor and Risk, Attachment 9.6, Risk Rank Determination Form,

dated September 7, 2018

EN-MA-145, Maintenance Standard for Torque Applications, Revision 9

ENN-MS-S-009-IP3, Attachment 2, Unit 3 Mission Time System List, Revision 2

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2018-04258 2018-04269 2018-05048 2018-05069 2018-05504*

Condition Reports (CR-IP3-) (*initiated in response to inspection)

2012-03262 2018-01894 2018-02508 2018-02638 2018-02660

Maintenance Orders/Work Orders

WO 00501433 WO 05817384

Drawings

21-F-27353, Flow Diagram Safety Injection System Sheet 1, Revision 44

21-F-27503, Flow Diagram Safety Injection System Sheet 2, Revision 58

IP3-299-0007, Boron Injection Tank, Revision 1

Miscellaneous

Critical Decision Paper for MCA Testing

SWP 36 and RHR 31 Motor Test Summaries

Training Lesson Plan on ECCS

71111.18

Procedures

3-PT-R127, BIT Leakage Test, Revision 10 (with TPC)

Engineering Evaluations

EC-79305, Removal of BIT Thermowell Nozzles TW-917 and TW-918, Revision 0

71111.19

Procedures

2-PMP-004-SWS, Johnston (18EC - S Stage) Service Water Pump and Motor Replacement,

Revision 13

2-PT-Q026B, 22 Service Water Pump, Revision 22

3-BKR-016-CUB, Westinghouse 480V Switchgear Cubicle Inspection and Cleaning, Revision 14

3-MCC-001-ELC, Westinghouse 480 Volt MCC Maintenance Inspection, Revision 48

3-SOP-C-002, Condensate System Operation, Revision 55

3-SOP-EL-004, Electrical Equipment Operations, Revision 42

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2018-05003 2018-05039

Condition Reports (CR-IP3-) (*initiated in response to inspection)

2018-02126 2018-02157 2018-02158 2018-02474 2018-02481

Maintenance Orders/Work Orders

WO 00508289 WO 51445346 WO 52710250 WO 52711072

WO 52712979 WO 52774512 WO 52813355

Miscellaneous

Operational Decision-Making Issue, 32 Condensate Pump Leakage, Revision 1

71111.22

Procedures

0-EDG-407-ELC, Emergency and Appendix R Diesel Generator Engine Analysis/Inspection,

Revision 8

2-PT-M021A, Emergency Diesel Generator 21 Load Test, Revision 33

2-PT-Q013-DS021, Valve 866C Inservice Test Data Sheet, Revision 20

2-PT-Q013-DS022, Valve 866D Inservice Test Data Sheet, Revision 20

2-PT-Q013-DS038, Valve 869B Inservice Test Data Sheet, Revision 38

2-PT-Q024A, 21 Emergency Diesel Generator Fuel Oil Transfer Pump, Revision 13

2-PT-Q035B, 22 Containment Spray Pump Test, Revision 19

3-PT-2Y001A, 31 Diesel Generator Overspeed Trip Test, Revision 6

3-PT-M079A, 21 EDG Functional Test, Revision 54

3-PT-M079A, 31 EDG Functional Test, Revision 54

3-PT-M079C, 33 EDG Functional Test, Revision 59

Condition Reports (CR-IP2-)

2018-04621 2018-04623 2018-04625 2018-04630

Condition Reports (CR-IP3-)

2017-03659 2018-00354 2018-02193 2018-02531*

Maintenance Orders/Work Orders

WO 00398191-Y WO 52683136 WO 52712053 WO 52821039-01

WO 52821039-01 WO 52828697 WO 52830515 WO 52830521

WO 53828692

Miscellaneous

Fairbanks Morse Guidance Regarding Operation of Alco 251 Engines Under Low Load

Conditions, dated March 7, 2000

71114.06

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2018-04521 2018-04544 2018-04546 2018-04547 2018-04548 2018-04571

Miscellaneous

IPEC ERO Team D Site Drill After Action Drill Report/Improvement Plan, dated August 1, 2018

71124.03

Procedures

EN-RP-501, Respiratory Protection Program, Revision 5

EN-RP-502, Inspection and Maintenance of Respiratory Protection Equipment, Revision 10

EN-RP-502-02, Flow Testing MSA Breathing Apparatus, Revision 0

EN-RP-503, Selection, Issue, and Use of Respiratory Protection Equipment, Revision 7

EN-RP-504, Breathing Air, Revision 4

Condition Reports (CR-IP2-)

2016-05509 2017-00845 2017-00912 2017-01230 2017-03100 2017-04486

2018-02499

Condition Reports (CR-IP3-)

2018-01561

Miscellaneous

IP-RPT-16-0047, 2016 Groundwater Project Units 2 and 3 Floor Drains Flow Verification and

Current Condition, Revision 2

IP3LO-2016-00121, RP Program Annual Review for 2016, per 10 CFR 20.1101(c), dated

June 8, 2017

Passive Monitor Sensitivity Tests, June 2016

71151

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2018-04646 2018-04977

71152

Procedures

0-NF-203, Internal Transfer of Fuel Assemblies and Inserts, Revisions 17 to 21

0-SYS-409-GEN, Belzona and Enecon' Metal Repair Applications, Revision 6

EN-DC-149R10-160804, Racklife Projections to January 2017 for Badger Testing

EN-LI-102, Corrective Action Process, Revisions 17, 20, 23, and 27

IP-RPT-15-00023, Best Estimate K for Indian Point Unit 2 Spent Fuel Pool, Revision 0

IP-SMM-AD-102, IPEC Implementing Procedure Preparation, Review and Approval, Revision15

NET-28091-000-01, Calculations to Support Loading Rules for Assemblies at Interfaces in the

Indian Point U2 Spent Fuel Pool, Revision 0

PI-AA-125, Corrective Action Program Procedure, Revision 8

PI-AA-125-1003, Corrective Action Program Evaluation Manual, Revision 4

Condition Reports (CR-HQN)

2011-00267

Condition Reports (CR-IP2-) (*initiated in response to inspection)

1998-06507 2012-01141 2012-05966 2013-03676 2014-00776 2014-04414

2016-01505 2016-04959 2018-03262* 2018-03306* 2018-03316* 2018-03889*

Miscellaneous

Indian Point Unit 2 Technical Specifications

Indian Point Unit 2 UFSAR

Letter from John

P. Boska to Michael A. Balduzzi, Indian Point Nuclear Generating Unit

Nos. 2 and 3 - Conforming License Amendments to Incorporate the Mitigation

Strategies Required by Section B.5.b of Commission Order EA-02-026, dated July 11,

2007

Letter from

M. Harris (NETCO) to G. Delfini (IPEC), Extent of Condition of IP2 Boraflex

Degradation and Guidance for Future Moves, dated February 25, 2014

Letter from

M. Harris (NETCO) to G. Delfini (IPEC), Racklife Projections through July 2016 and

Comparison to COAR Assumed Uniform Distribution and Panel Proximity for Region 2-2,

dated May 20, 2016

NRC Information Notice 2011-03: Non-Conservative Critical Safety Analyses for Fuel Storage,

dated February 16, 2011

Spent Fuel Pool Maps for Degraded Panels, July 2018

71153

Condition Reports (CR-IP2-) (*initiated in response to inspection)

2015-03550 2015-05755 2016-06934 2016-07188 2016-0727 2018-02806

Condition Reports (CR-IP3-) (*initiated in response to inspection)

2016-03607 2017-03513 2017-03515 2017-03555 2018-02265 2018-02266

2018-02267

Maintenance Orders/Work Orders

WO 00498158 WO 52568740 WO 52708009 WO 52709908

Calculations

IP-CALC-04-01420, FCX-0538, Calculation of Effective Degradation Years for the IP2 Reactor

Vessel Head by 2R18

Engineering Evaluations

IP2-SW-DBD, Service Water System, Revision 2

LPI Report F15565-R-001, Evaluation of Wall Thinning of Fan Cooler Unit Elbow - Indian Point

Energy Center - Unit 2, Revision 2, dated July 22, 2016

LPI Report LF170507, Evaluation of Service Water Type 904L Pipe Weld Pinhole Leak,

FCUY Return in Containment, Revision 1

Lucius Pitkin, Inc., Analysis on Relief Valve CD-123, Contract Document Number 10520627,

Serial Number D00987-0006

Miscellaneous

IPP-R23-OH01-03-01, Ultrasonic Report Data Sheet

IPP-R23-PEN3ET-SCAN2-12940, Eddy Current Report Data Sheet

LER 05000247/2015001-02, Technical Specification Prohibited Condition Due to an Inoperable

Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in

Exceeding the Allowed Leakage Rate for Containment

LER 05000247/2015004-00, Safety System Functional Failure Due to an Inoperable

Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor

Cooling Return Pipe

LER 05000247/2016010-00 and 05000247/2016010-01, Safety System Functional Failure Due

to an Inoperable Containment Caused by a Through-Wall Defect in a Service Water

Supply Pipe Elbow to the 24 Fan Cooler Unit

LER 05000247/2018001-00, Penetration Indications Discovered During Reactor Pressure

Vessel Head Inspection

LER 05000247/2018002-00, Manual Reactor Trip Due to Trip of Both Main Boiler Feedwater

Pumps

LER 05000286/2016001-00 and 05000286/2016001-01, Safety System Functional Failure Due

to an Inoperable Containment Caused by a Flaw on the 31 Fan Cooler Unit Service

Water Return Coil Line Affecting Containment Integrity

LER 05000286/2017003-00, Condensate Storage Tank Declared Inoperable Per Technical

Specification

60845

Procedures

0-FTR-402-GEN, STC Movement Between Unit 2 and Unit 3, Revision 6

0-RP-RWP-430, Radiological Controls for Inter-Unit Wet Fuel Transfer, Revision 2

2-FTR-001-GEN, Unit 2 STC Unloading Operations, Revision 15

3-FTR-003-GEN, Air Pad Operation for Unit 3, Revision 3

3-FTR-006-GEN, Unit 3 STC Loading and Sealing Operations, Revision 21

3-NF-322, Fuel Selection for Wet Fuel Transfer in the Shielded Transfer Canister, Revision 3

Miscellaneous

Engineering Report No. IP-RPT-1 1-00032, Entergy Nuclear Engineering Report Title:

Licensing Report on the Inter-Unit Transfer of Spent Nuclear Fuel at the Indian Point

Energy Center (Non-Proprietary), Revision 5, dated December 17, 2017