IR 05000254/2004011

From kanterella
Jump to navigation Jump to search
IR 05000254-04-011 & 05000265-04-011,10/18/2004 - 10/29/2004; Quad Cities Nuclear Power Station, Units 1 & 2; Problem Identification and Resolution Inspection
ML043340388
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 11/26/2004
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-04-011
Download: ML043340388 (27)


Text

ber 26, 2004

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION REPORT 05000254/2004011; 05000265/2004011

Dear Mr. Crane:

On October 29, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed a team inspection at the Quad Cities Nuclear Power Station. The enclosed report documents the inspection results which were discussed on October 29, 2004, with you and members of your staff.

This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, compliance with the Commissions rules and regulations and with the conditions of your operating license. Within these areas, the inspection involved selected examination of procedures and representative records, observations of activities, and interviews with personnel. No findings were identified.

On the basis of the sample selected for review, the team concluded that in general, problems were being properly identified, evaluated, and corrected. While no findings were identified during the inspection, the team had several observations regarding the effectiveness of corrective action program implementation as detailed in the enclosed report.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket Nos. 50-254; 50-265 License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 05000254/2004011; 05000265/2004011 w/Attachment: Supplemental Information

REGION III==

Docket Nos: 50-254; 50-265 License Nos: DPR-29; DPR-30 Report No: 05000254/2004011; 05000265/2004011 Licensee: Exelon Nuclear Facility: Quad Cities Nuclear Power Station, Units 1 and 2 Location: 22710 206th Avenue North Cordova, IL 61242 Dates: October 18 through 29, 2004 Inspectors: G. Wright, Team Lead K. Stoedter, Senior Resident Inspector, Quad Cities C. Brown, Resident Inspector, Clinton R. Ganser, IEMA, Quad Cities Approved by: M. Ring, Chief Branch 1 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000254/2004011, 05000265/2004011; 10/18/2004 - 10/29/2004; Quad Cities Nuclear

Power Station, Units 1 & 2; Problem Identification and Resolution Inspection The inspection was conducted by one region-based inspector, two resident inspectors and an inspector from the Illinois Emergency Management Agency. No findings of significance were identified.

Identification and Resolution of Problems In general, the licensee identified issues and entered them into the corrective action process at an appropriate level. Nuclear Oversight (NOS) assessment reports identified issues for the licensee to resolve, including issues with corrective action follow through and effectiveness.

The majority of issues reviewed were properly categorized and evaluated. In general, corrective actions reviewed were appropriately implemented and appeared to have been effective. While no findings were identified during the inspection, the team developed a number of observations.

The team observed that many condition reports or issue reports were narrowly focused.

Documentation was often weak, resulting in lack of ties between problem statements and corrective actions. The weak documentation also contributed to a lack of clarity on how the licensee arrived at corrective actions. Condition reports and assessments addressing maintenance rework or inadequate/ineffective corrective actions, did not routinely evaluate why the responsible organization had put ineffective actions in place. The team also observed that the threshold for identifying deficiencies on non-safety related systems may not be consistent with the systems contribution to the sites overall risk profile.

REPORT DETAILS

OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution

.1 Effectiveness of Problem Identification

a. Inspection Scope

The team reviewed selected documents generated over the past 2 years including:

NRC inspection report findings, selected plant corrective action documents, and trend assessments to determine if problems were being identified at the proper threshold and entered into the corrective action process. The team also conducted a focused plant walkdown of the turbine building closed cooling water (TBCCW) system to ensure that equipment problems were entered into the corrective action system. The TBCCW system was selected due to its high risk significance. The walkdown represented one semiannual sample. The corrective action documents used during the reviews are listed in Attachment 1 and were selected from the following areas:

1) Human performance 2) Inadequate corrective actions 3) Rework 4) Operator workarounds 5) Operability evaluations 6) Configuration control 7) Operating experience 8) Root cause assessments 9) Common cause assessments

.

10) Apparent cause assessments 11) Issues generated during the last three refueling outages for each unit.

b. Observations In general, the licensee identified issues and entered them into the corrective action program (CAP) at an appropriate level. The licensee appropriately used the CAP to document instances where previous corrective actions were ineffective or inappropriate.

The team conducted a detailed walkdown of selected portions of the TBCCW system to assess the licensee identification and documentation of degraded conditions within the corrective action program.

b.1 Turbine Building Closed Cooling Water (TBCCW) System Walk Down The team verified that major equipment issues identified in the system walk down, such as malfunctioning valves and pump leakage, were addressed within the licensees corrective action program. However, the team identified a relatively high number of system material deficiencies that were not identified by the licensee. These included numerous improperly secured piping supports, corrosion on system components and valves, and improper labels on air compressors. This indicated that the threshold for identifying deficient conditions was not as low as that given to a safety-related system with equal or lower risk significance. Subsequent to the walk down, the system engineer submitted issue reports (IRs) to address the teams concerns. The licensee initiated extent of condition walk downs to identify similar conditions and initiate the necessary corrective action.

b.2 Identification Threshold From December 2002 until July 2004, the licensees CAP allowed conditions adverse to quality to be documented in condition reports or maintenance work requests. In July 2004, the licensee implemented a new CAP which instituted the use of issue reports to document items adverse to quality or in need of repair. With the change, all activities are entered into the system as IRs. The IRs are reviewed daily by a team consisting of managers from the major departments. The licensees review team, with input from the various organizations, determines which course the item will take (e.g., event report, work request). The number of condition reports in the previous CAP appeared to be appropriate for a dual unit site. The number of issues being generated in the new CAP has not stabilized; about 950 items were generated in September. The teams review of CRs generated under the previous program and a small sample of items from the current system, indicated that an adequate threshold had been established for documenting issues and an appropriate prioritization system had been used.

While the licensee appeared to appropriately identify most issues, the TBCCW walkdown identified a number of deficiencies. The individual deficiencies did not directly affect the operation of the system; however, they did indicate that the licensees threshold for identifying and documenting deficiencies on the system may not be consistent with the systems risk importance. For example, the inspector identified a number of deficiencies with pipe supports, (e.g., lock nuts missing and loose fasteners).

In following up on the teams findings, a system engineer identified that responsibility for pipe supports had changed from a designated individual for all systems to each system engineer. The change was brought about by the elimination of the pipe support specialist position at the site.

b.3 Operating Experience The team reviewed a sampling of industry operating experience (OPEX) reports and concluded that the licensee was appropriately including OPEX items in the corrective action program. The team identified one example where the licensees corporate OPEX coordinator had not sent General Electric Service Information Letter (SIL) 448, Revision 2, to the site for review. The team reviewed the SIL revision and concluded that the information in the SIL had no impact on the current operation of equipment at Quad Cities. The licensee initiated IR 266809 to document the oversight by the corporate OPEX coordinator.

b.4 Identification of Issues Associated with Inadequate/Ineffective Corrective Actions or Maintenance Rework The team reviewed a sample of IRs and CRs written for inadequate or ineffective corrective actions. In general, the licensee adequately addressed the technical issue, (i.e., the issue which had not been corrected by the original corrective action). However, in almost none of the cases did the licensee address why it had not corrected the problem the first time.

- CR 216467 Ineffective ACE & ACIT Closure Problems: The CR appropriately addressed the specific issues addressed by the ACE (Apparent Cause Evaluation). The CR did not address why the organization developed an ineffective ACE. Additional discussions with the licensee identified they had assessed the cause of the problem and taken actions; however, none of that information had been included in the CR evaluation.

.2 Prioritization and Evaluation of Issues

a. Inspection Scope

The team conducted an independent assessment of the prioritization and evaluation of selected CRs generated after the 2002 problem identification and resolution inspection.

The assessment included a review of the category assigned, the operability and reportability determinations, the extent of condition evaluations, the cause investigations, and the appropriateness of assigned corrective actions. Other attributes reviewed by the team included the quality of the licensees condition trending and the corresponding corrective actions. In addition, one member of the team attended a management meeting to observe the licensees assessment of IRs. This review included the controlling procedures and selected records of activities. In addition, the team conducted interviews with cognizant licensee personnel.

The team reviewed previous NRC inspection reports and associated corrective action documents to verify that identified issues were appropriately characterized and entered into the CAP.

The team likewise reviewed the licensees efforts to capture industry operating experience (OPEX) issues in the CAP. Documents reviewed included the licensees assessment of industry operating event reports, NRC, and vendor generic notices.

b. Observations The team verified that, in general, issues reviewed through the CR/IR process were properly categorized and evaluated. However, the team had several observations regarding the quality of the evaluations as follows:

b.1 Overview of Prioritization and Evaluation Process The team identified several items where narrowly focused assessments missed opportunities to identify broader causes and to determine complete corrective actions for specified causes. For example:

- CR 138696; Low Pressure Coolant Injection Inoperable due to Failure to Reset Isolation Logic Following Surveillance Testing, dated January 9, 2003. This condition report was written when operations personnel discovered a residual heat removal valve which did not operate as expected during testing. The licensee determined that the valve did not operate as expected due to the presence of a Group II containment isolation signal which had not been reset during surveillance testing conducted on December 18, 2002. The failure to reset the containment isolation logic was caused by an inadequate procedural development and review process which did not ensure that a step to reset the logic was placed in the procedure before the procedure was issued for use. The corrective actions to prevent recurrence included reviewing the other logic tests to identify any similar discrepancies, revising any deficient procedures, and revising the applicable surveillance procedures to include visual verification that the logic had been reset. However, the corrective actions to prevent recurrence did not address the deficient procedural development and review process.

- CR 154716; Valve 2-1001-43A will not Open from the Control Room, dated April 24, 2003, and CR 169407; Troubleshooting of Valve 2-1001-43A Should Have Been Better Documented, dated July 29, 2003. Condition Report 154716 was initiated when shutdown cooling suction valve 2-1001-43A could not be opened from the control room. The team reviewed this condition report and identified several examples where the licensee had failed to follow procedure (see the Non-Cited Violation documented in Inspection Report 50-254/2003009; 50-265/203009). These failures resulted in several human performance issues including failing to initiate a work request when required, performance of troubleshooting activities before developing a formal troubleshooting plan, use of repetitive cycling to resolve equipment deficiencies, and using equipment cycling results as a basis for continued operability. In addition, the team identified that even though CR 154716 had received numerous supervisory reviews, no one had recognized that the root cause of the valves failure to stroke had not been addressed. The team reviewed the licensees corrective actions for this issue and found that the actions were very narrowly focused. Specifically, the licensee addressed the deficiencies in the work request and troubleshooting plan initiation by conducting additional training. However, none of the other deficiencies documented in the inspection report were addressed.

- CR 130676, 1B Fuel Pool Pump Failure to Start. The CR documented a problem where a fuel pool pump failed to start. An associated work request (WR) identified that the pump had not been properly wired. The WR & CR resulted in the wiring being corrected; however, it did not address why the pump wasnt tested after the activities which had resulted in the errant wiring.

IR 266075 was written to follow up on this issue.

- CR 166557, HPCI MO 2-2301-03 valve possible leak by. The CR identified that a high pressure coolant injection (HPCI ) steam valve was leaking into the HPCI room sump. The evaluation of possible leakpaths through the valve documented on the CR was very good . The CR stated that the sump high level alarms were coming in once to twice per day; however, no further evaluation was performed. In response to the teams questions, the licensee determined that the normal frequency of the alarm was once every 3 to 4 days, this indicated that the operators missed an opportunity to identify the leakage 2 to 3 days earlier.

The operators did verify that the alarm cleared within an appropriate amount of time, but did not send anyone to investigate the situation. The HPCI steam valve has had a history of leakage which may have desensitized the operators to the alarm.

- IR 143666, White residue found at 480V MCCs aux contacts. The IR documented potential dried grease on CR105X auxiliary contacts. The extent of condition investigation found similar white powdery residue on 22 additional auxiliary contact assemblies. Appropriate actions were taken to correct the identified conditions and a preventive maintenance activity to grease the auxiliary contact assemblies was established. However, the team noted that the periodicity of the preventive maintenance activity was 6 years when one of the auxiliary contact assemblies (CR-143005, ECCS Keep Fill Pump motor unexpectedly shut off) had failed after only 4 years of operation. When the team questioned the appropriateness of the 6 year periodicity, the licensee stated that the period was in accordance with industry guidance for critical breakers and that the dried powder was a precursor to dried grease and did not indicate that binding was imminent. The licensee also noted that the corrective actions were being monitored under the licensees SHIP [system health indicator program]

actions. The licensee did not directly address the failure of the one breaker in evaluating its surveillance periodicity.

- CR 132397, Failed Time Delay Relay. On April 5, 2001, the under voltage permissive time delay relay for the emergency diesel generator loading onto 4kV Bus 24-1 failed routine bench calibration check following removal from its installed location. The calibration check was performed to confirm proper relay timing and operation before operations surveillance QCOS 6500-10. The team reviewed the operability evaluation for CR 132397 and the root cause report, CR Q2001-01049, for the cause of the relay failure. The team found the root cause investigation to be very comprehensive. The documentation detailed an excellent case for an improper solder joint which allowed slight wire movement causing electrical discontinuity as the failure mechanism. However, the operability evaluation for CR 132397 was not as thorough.

The operability evaluation appeared to default to the possibility that removing the relay for bench testing caused the relay coil wire to be moved, resulting in the relays failure. While the team concluded that the licensees assessment was plausible, the team was unable to identify where the licensee had considered and investigated other possibilities (e.g., work in the cabinet during routine system maintenance activities, that could have caused the relay to fail). The lack of a thorough assessment of alternative causes for the relays failure, reduced the teams confidence that the relay had been operable prior to its removal from the circuit. Despite the lack of a convincing case that the relay had not failed while in-service, the team could not positively conclude that the operability evaluation was incorrect -- only that it was based on weak logic and a possible scenario for the time of failure. The team noted that the relay was replaced immediately after it was discovered to be failed and the operability surveillance test successfully completed.

The team also identified an oversight in the licensees evaluation process for addressing items identified by the NRC as Non-Cited Violations. The NRCs Enforcement Manual indicates that a Severity Level IV violation can be dispositioned as a Non-Cited Violation as long as the licensee has placed the violation into their corrective action program to address recurrence. The Enforcement Manual also states for Non-Cited Violations: At the time a violation is closed in an inspection report, the licensee may not have...begun the process to identify the root cause and develop action to prevent recurrence. The team identified that the licensees corrective actions for Non-Cited Violations were generally appropriate. However, the licensees CAP procedure does not include steps to ensure that the root cause of each Non-Cited Violation was identified and that corrective actions to prevent recurrence were implemented. The licensee initiated IR 268389 to address this oversight.

b.2 Trending Program The team reviewed how the licensees trending activities, noted below, interfaced with the CAP Component Maintenance Optimization Corrective Maintenance Unexpected Maintenance Rule Equipment Reliability System Health Indicator Program Component Health Indicator Program Instrument Trending The team also observed use of the engineering work station program used by system engineering to monitor system performance. The Engineering Work Station program gathered information from a number of sources including the plant computer and non-licensed operator rounds for evaluation by the system engineer. The system also allowed the engineer to input values or formulas with provisions for notifying the engineer when the specified conditions have been met or exceeded. This feature allowed for almost real-time monitoring of system parameters. The program also allowed the engineers at all Exelon sites to share information with their counterparts.

The team noted good coordination between the various trending programs and the CAP.

However, the team also noted that the trending program relies on individuals to identify the trends, with the computers only holding and sorting the information. With the exception of the Engineering Work Station program, noted above, the licensee did not use computers to flag potential trends or problems.

The team performed an in-depth examination of the licensees instrument set-point and calibration trending program as a follow-on to an observation made in the previous problem identification and resolution inspection. The team found that the licensee had corrected the difficulty in trending instrument performance, specifically, the current data base was comprehensive and was reviewed quarterly for any developing trends. The team noted one possible weakness in that the initial CR, where a trend was noted, was closed separately from an additional CR initiated to identify the trend. The team noted that a more clearly defined documentation trail would have the trend tracked as a corrective action to the initial CR. On October 29, 2004, the licensee initiated IR 268311, Possible Enhancement to IR Processing, to assess the trend identification process

.3 Effectiveness of Corrective Action

a. Inspection Scope

The team reviewed past inspection results, selected CRs, root cause reports, and common cause evaluations to verify that corrective actions, commensurate with the safety significance of the issues, were specified and implemented in a timely manner.

The team evaluated the effectiveness of corrective actions. The team also reviewed the licensees corrective actions for Non-Cited Violations (NCVs) documented in NRC inspections in the past 2 years.

b. Observations In general, the licensees corrective actions for the sample reviewed were appropriate and appeared to have been effective. The team noted that the licensee appropriately used the CAP to document instances where previous corrective actions were ineffective or inappropriate.

.4 Documentation

a. Inspection Scope

The team independently assessed the thoroughness of the licensees documentation to determine whether the documents could stand on their own or required additional inputs.

If additional information was necessary, the team also assessed the availability of the information.

b. Observations In general, the team found the licensees documentation practices associated with the corrective action program to be weak.

b.1 In several instances, the team was only able to successfully understand the licensees actions because key individuals recalled details of what had occurred and, more important, why it occurred. The team noted that this documentation weakness left the licensee vulnerable to the loss of key information. For example:

- OPEX Item 171244 was initiated to perform a review of NRC Information Notice 2002-29, Design Problems in Safety Functions of Pneumatic Systems. The licensees review stated that no actions were needed as the information in the notice was similar to that included in Generic Letter 88-14, Instrument Air Supply Problems Affecting Safety-Related Equipment. While this was true, it was not apparent that the licensee considered physical or operational changes in the pneumatic systems between 1988 and 2002 which could have resulted in the information included in Information Notice 2002-29 having increased applicability at the station. The team discussed this OPEX item with the responsible engineering personnel and found that a full review of pneumatic system performance had been performed. However, this review was not documented.

- CR 144464, "Concerns with CAPR closure and EFR for ECCS venting." While containing valuable information, the CR did not identify clearly what the inadequacies were, what the procedural changes were, or how the corrective actions addressed the inadequacies. Initial discussions with the licensee identified they were unable to address the deficiencies. The teams questions were appropriately addressed only after a discussion with the individual who wrote the document.

- A number of CRs (e.g., 161395, 171039, 175517, 183316) identified inadequate assessments or evaluations and indicated that the evaluation had been returned to the originator along with comments. The CRs neither itemized the specific problems with the documents nor addressed the cause for the deficiencies.

Without detailed information in the CR, it is difficult to identify whether CAs were being effective or if repeat failures were continuing to occur.

b.2 The team also identified a number of CRs involving human performance where from the documentation, it did not appear that the individual had been interviewed regarding the error. The failure to interview individuals associated with issues limits an assessments ability to identify broader corrective actions.

- CR 158648 1/2-5599-Y valve operator air supply hooked up in reverse. The CR documented what had occurred and evaluated the extent of condition. The CR did not identify whether the mechanics who connected the air lines backwards had been interviewed. Further, the CR did not address potential knowledge deficiencies which may have led to the problem. In answering the teams questions, the licensee indicated that potential knowledge deficiencies were addressed in a subsequent CR written on a similar performance error.

.5 Safety-Conscious Work Environment (SCWE) Assessment

a. Inspection Scope

The team conducted interviews with plant staff to assess whether there were impediments to the establishment of a SCWE. During the interviews, the team used Appendix 1 to Inspection Procedure 71152, Suggested Questions for Use in Discussions with Licensee Individuals Concerning PI&R Issues, as a guide to gather information and develop insights. The team also discussed the implementation of the Employee Concerns Program (ECP) with the plants ECP Coordinator.

b. Observations Plant staff interviewed did not express any concerns regarding the safety conscious work environment. The staff was aware of and generally familiar with the corrective action program. During the interviews, the team found that the plant staff was generally unfamiliar with the process to use for initiating an anonymous issue report. However, the plant staff felt that the option of anonymous issue reports was not needed since they were comfortable documenting potential safety issues. The licensee staffs unfamiliarity with anonymous issue reports was provided to licensee management for information.

The licensee initiated IR 267841 on this issue and provided a site-wide communication to ensure that everyone was knowledgeable on the methods available to generate anonymous issue reports.

None of the individuals interviewed expressed any reluctance to identify plant safety issues. However, only a few of the people interviewed readily identified the use of the Employee Concerns Program as an alternative method for raising a concern. While most individuals favored the ease of use of the new system, some individuals indicated they were not adept at using the computer system to initiate an item into the corrective action program. In all cases, these workers stated that they would ask for assistance in initiating an IR. None of the workers interviewed appeared reluctant to identify safety issues or bring them to the attention of the NRC if they felt it was necessary. They did say they would go through their supervisor first and use the alternate methods if they needed to do so.

4OA6 Management Meetings

.1 Exit Meeting Summary

The team presented the inspection results to Mr. R. Gideon and other members of licensee management in an exit meeting on October 29, 2004. The licensee acknowledged the observations presented and indicated that no proprietary information was provided to the team.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

Individuals Contacted

Licensee:

J. Bartlet Operations Training Manager

W. Beck Regulatory Assurance Manager

T. Bell On Line Work Center Manager

D. Craddick Electrical Maintenance Superintendent

T. Fuhs Regulatory Assurance

R. Gideon Plant Manager

D. Hieggelke Nuclear Oversight Manager

D. Kallenbach Radiation Protection Superintendent

J. ONeil Corrective Action Program Manager

M. Perito QC/Operations Manager

C. VanDenburgh Engineering

NRC:

M. Kurth NRC Quad Cities Resident Inspector

Acronyms Used in the Report

ACE Apparent Cause Evaluation

ACIT Action Item

CAPR Corrective Action to Prevent Recurrence

CFR Code of Federal Regulations

CR Condition Report

DRP Division of Reactor Projects

ECCS Emergency Core Cooling System

ECP Employee Concerns Program

EFR Effectiveness Review

HPCI High Pressure Coolant Injection

IEMA Illinois Emergency Management Agency

IR Issue Report

NCV Non-cited violation

OPEX Operating Experience

SCWE Safety Conscious Work Environment

SIL Service Information Letter

TBCCW Turbine Building Closed Cooling Water

Documents Reviewed

Human Performance Related Condition Reports

Ar Number Ar Subject Origination Date

00134002 MRule: ECCS Room Coolers 20021204

00134318 Improper respirator installed in SCBA used for fire drill 20021206

00135466 Vibration of Steam lines may risk test tap line to break 20021212

00136195 IMPROPER USE OF BOUNDING FOR 1A RHR HX

OPEVAL ISSUE 20021217

00137008 Late CR initiation to evaluate U1 HPCI venting results 20021220

00137396 Sheet Metal Screw Installation Causes Electrical Arc 20021227

00140164 Valve Found Already Closed And Tagged During C/O

First Hang 20030119

00141008 Compensatory action for Op Eval 105454-08 not

implemented 20030124

00144309 Due date of PMID 33784-01 beyond interval for late

due date 20030212

00145840 Air Supply to Regulator for AOV 2-3507-A Isolated 20030223

00147691 Failed PMT for New Valve 20030306

00150278 Inadvertent RCIC Trip Throttle Valve trip & unplanned LCO 20030322

00151852 Unit One Emergency Diesel Generator Trip Checks 20030401

00152430 Operability Determination Actions Inappropriately Closed 20030404

00156029 2Bcrd motor oil drain plug found loose on running pump 20030428

00158648 1/2-5599-Y valve operator air supply hooked up in reverse. 20030513

00164026 "B" Core Spray Loop Air venting investigation results 20030619

00164221 3-VALVE MANIFOLD MISPOSITION 20030620

00164355 Wrong valve opened when recircing 2B Cond Phase

Separator 20030622

00181083 Improper Verification Practices 20031015

00182811 Apparent incorrect pressure indicator calibrated. 20031024

201012 Orifice plates for RO and FE installed reversed (EC24429) 20040211

202221 Venture electricians working on equipment not out

of service 20040217

205444 NOS ID'd equipment staged in electrical cabinet 20040302

205639 Potential containment breach 20040302

205695 Contractor Tools Stored in Electrical Panel (Q2R17 OLL) 20040303

205740 EC# 24553 Components Not Installed Per Approved

Design 20040303

206505 Water pressure encountered when unbolting north

H2 cooler 20040305

209409 RV 2-3607 Leaks 60 dpm After System Placed In Service 20040319

211163 Inoperable CRD Accumulator During Scram Timing 20040326

211425 HCU 22-15 113 valve found out of position 20040329

211881 Rework - CS Rm Cooler Temp Switch cal'd to

incorrect data 20040330

211966 Hand Tools Found Stuffed in Cable Tray 20040331

221700 Red Window in Engineering Technical Rigor Fundamental 20040517

223488 Appendix R Not Addressed in OpEval 220863 20040525

225847 FME In Electrical Cabinets 20040604

256816 North Main Control Room Door #329 Difficulties Closing 20040925

Root and Common Cause Analyses

00138696 2-1001-29A immediately reclosed when opened

during testing 20030109

00138737 Flammables not being properly stored 20030109

00139325 Leak in line 1-1043B-14"-L Approx 1 Gal per Minute 20030114

00140818 NOS identified apparent trends in RCR themes 20030123

00151852 Unit One Emergency Diesel Generator Trip Checks 20030401

00152094 Challenges to Radwaste shipping activities 20030403

00158786 Two Corrective Actions Not Entered for CR 152884 20030514

00159607 Pressure boundry leakage from 2" Rx head vent line 20030520

00159864 Inability to cool upper elevations for Rx disassembly 20030521

00162091 FP DRILL PERFORMANCE DEFICIENCIES 20030605

00162743 Dresden CAPCo Identifies Adverse Trend in EPU

Modifications 20030611

00164026 "B" Core Spray Loop Air venting investigation results 20030619

00170142 MSL hi flow instrument drift - reportable 20030804

00170378 Trend of CR's dealing with reactor pressure >1005 psig 20030805

00172349 Review of July CAP data identifies a potential trend 20030820

00179578 Review of Chemistry CAP data identifies a potential trend 20031006

00181022 Security Safety FASA Recommendations 20031015

00181083 Improper Verification Practices 20031015

00197277 CCA needed for External Identified CRs 20040123

00198137 INOP D/W Rad Monitor due to BAD SOLDER JOINT ON

RIS 2-2419-A 20040129

202476 Human performance errors 20040218

208111 Q2R17 OLL U-2 Refuel Bridge experienced "Hoist Tube

Hangup" 20040312

209752 Site CR Trending CC Document Quality as Issue 20040321

211724 Unexpected U2 reactor scram during turbine weekly testing 20040330

216684 Untimely Initiation of Condition Reports by Engineering 20040423

216941 Common Cause for SRM/IRM outage problems 20040426

222787 Initiate Planned CCA for Unplanned Modification Revisions 20040521

235678 OOT, DPIS 1-0261-2M, TREND CODE B2 20040713

240264 Ineffective CAPR For Main Steam Line Flow Switch

Root Cause 20040730

240494 OOT, 1-263-111A, 1-263-111C, TREND CODE B2 20040730

243058 Operations Human Error Prevention Fundamental Id'd

As Yellow 20040810

255735 E-3 Walk Down Identified Additional Parts Required. 20040922

Operating Experience Condition Reports

00136898 GE SIL 646 Target Rock SRV failed to fully open 20021220

00141461 GE SC 03-01, Additional material concerns for TIP valve

qualification 20030128

00145346 Complete SOER 2002-03 Recommendations 20030220

00148037 NER DR-03-001, Rev1, High Flow Control Line After

Load Drop 20030307

00151777 GE SIL 448R1 GE AK/AKR breaker lube OPEX 20030401

00156575 NER KS-03-006, Corrective actions for 2002 plant events 20030430

00164755 NRC GL 2003-01, Control Room Habitability, OPEX 20030625

00168622 NER QC-03-047, Inadvertent Opening of PORV and

Manual Scram 20030722

00171244 NRC IN2002-29 Des Problems in Sfty Functions of

Pneu Sys 20030812

00171258 NRC IN2002-34 Fail Of Sfty-Related Circ Break Aux Switch 20030812

00174867 NER KS-03-016 Red, Scram Due To Inadequate SSPV

Disposition 20030909

00175971 SME Review Of NER DR 03-096, MOV Stroke Time Issues 20030916

00179572 NRC, IN 2003-18, GE SBM Control Switches W/Defective

Cam 20031006

200024 NER DR-04-006 Red U3 Reactor Scram- Turbine Oil

Cooler Trsfr 20040206

200989 SER 6-03 Cooling Water System Debris Intrusion 20040211

202720 Sme Review Of Ner Dr-04-009, Water In Hpci Steam

Line /Scram 20040219

219125 Sme Review Of Oe-18201, Hydrogen Found In Srv

Downcomers 20040506

227149 INPO SEN 249 Worker Injured Removing Water Box Cover 20040609

254371 NER LI-04-067 Red Unit 1 Thermal Power Exceeded By

.2-.4 percent 20040918

NRC Item Related Condition Reports

205862 Wrong oil in the 2A Core Spray motor upper and lower

resrvr. 20040303

222870 SSDR not updated with max. torus temp. with HPCI

running 20040521

00182811 Apparent incorrect pressure indicator calibrated. 20031024

205892 Wrong oil in the 2B Core Spray motor upper and lower rsrvr.20040303

223815 (SSDI) Potential to Drain the Torus on Failure of RCIC Line 20040526

00167725 Missed Opportunity - Corrective Action Program 20030715

00171034 Past Operability not Addressed for 1B RHRSW Pump Leak 20030811

00181040 Cable Tabulation Dwgs contain Incorrect Service

Description 20031015

00182702 Deficiency Identified in Calculation QDC-0000-E-0853, R/0 20031024

00185418 Flood Protection Alarm PM Review is Needed 20031107

00189928 Additional Corrective Action Prudent for CR 110756

(RHRSW Screens) 20031210

00190069 1A RHR HX Repair Not Included in the Sec. XI R/R Prog. 20031210

00190175 RHRSW Pump Cubicle Cooler tube plugging limit in UFSAR 20031211

200169 CCST Heaters--use of increased monitoring as

compensatory ac 20040206

205146 Load rating for Hoist found greater than support structure. 20040301

220295 QCOA 1300-02 Has Error for Maintaining

RCIC </= 400gpm 20040511

220460 SSDI Walkdown Identified Incorrect TOL Setting 20040512

220546 Operations Procedures lists old ITS limits for Rx Lo-Lo Lvl 20040512

220748 Cal QDC-1300-E-021 apparent omission 20040513

221078 RCIC Operation w/ App R torus pressure not well

documented 20040514

222543 SSMP Motor Start Limitations 20040520

222713 SSDI Issue RCIC Operation During an Appendix R Fire 20040521

223638 SSDI RCIC/CS Rm Temp Switch Locations Do Not

Match UFSAR 20040525

224355 Wrong Vendor letter used for engineering reference 20040528

243264 Non-conservative technical specifications requirement 20040810

247298 Error Discovered In SRV Discharge Flange Calculation 20040825

254931 Qcos 5750-04 Test Acceptance Criteria 20040920

254936 Maintenance Procedures Lack Some Acceptance Criteria 20040920

00194680 Identifying Non-Conservative Technical Specifications 20040112

Configuration Control Condition Reports

00134855 Feed Water Pump Low Suction Pressure 20021210

00135995 Bkr For Mcc 27-1 Cub F1 Found To Be Wrong Size For

Application 20021216

00144400 Fit-Up Anomalies Id'd For 1a Rhr Ht Exchanger Floating

Head 20030213

00145867 Valve 1-4799-824 Not Installed Per Drawing 20030224

00151852 Unit One Emergency Diesel Generator Trip Checks 20030401

00155349 Received RFP Suction Low Pressure Alarms 20030423

00155624 Several Hundred Calculation Revisions "Inprog" In

Passport 20030424

00157697 Qcop 6000-4 Not Revised Post Epu 20030507

00158439 Insufficient Oil Placed Into 2a Serv Wtr Motor Upper Bearing 20030512

00160467 3c ERV Pilot Valve Independently Cycles When Operated 20030525

00161015 QCOP 5600-04 Not Revised For Unit 1 Epu

Conditions 20030529

00162743 Dresden CAPCO Identifies Adverse Trend In EPU

Modifications 20030611

00163226 Station Vent System Controlled Drawings Need Major

Revision 20030613

00166134 FASA Supplement - Permanent Plant Modification 20030703

00167422 Offgas Glycol System Discrepancies 20030714

00175380 Piping Clamps Missing From Various Crd System Pipes. 20030911

00176455 Overload Heater Size Drawing Issues 20030919

00180661 Loss Of HPCI Room Cooler Fan On Appendix K And Eq 20031013

00182969 HRSS Line Broken Loose From Pipe Hangers. 20031026

00184538 Fw Discharge Pipe Hanger Fastener Falls To Floor In

Rfp Room 20031103

00187652 Classification Change From Non-Safety To Safety-Related 20031121

00188277 Ec 337692 Specified Torque Valves Exceeded Yield Of

U-Bolt 20031126

00188306 Inadequate Input Verification For Calculation Qc-10q-301 20031126

00188668 New Xl-3 System Is Safety Hazard. 20031201

00190175 RHRSW Pump Cubicle Cooler Tube Plugging Limit In

UFSAR 20031211

00194651 EC 341397 Scope Increase Due To Voltage Drop Concerns 20040112

00196677 Incorrect Trip Settings For Epn 2-6900-26-2b 20040121

201118 GE Identifies Potential HPCI Design Issues 20040211

202451 Irregularities While Performing Ec 341370 20040218

206203 Rx Vessel Bottom Drain Temperature Continuing Trend 20040304

207872 Existing Overload Heater Size Do Not Match Drawing. 20040312

212087 EC 24424 Requires Revision For The Unit 2 Edg 20040331

215791 Unplanned Revisions To Ec 23918 Ups/Battery Room Hvac 20040419

218406 Print 4e-2679f Shows The Wrong Size Transformer

In MCC 29-2 20040503

219901 Dwgs Identify Ss Piping Replacements Never Installed 20040510

221865 Pressure/Temperature Curves Non-Conservative 20040518

222787 Initiate Planned Cca For Unplanned Modification Revisions 20040521

231212 Nrc Uri 04-002-01 Concerning Mssv Setpoint Drift 20040624

233191 Pipe Support Clamp On Sw Line To 1-5746-A With No

Hangar Att 20040701

234471 "As Found" Circuit Breaker Size Does Not Match

Plant Drawing 20040708

236208 Potential Breaker Sizing Issue In Cubicle 20040715

237095 Ec Eval. 347941 Used To Implement A Configuration

Change 20040719

237204 System Function Changed Without 50.59 Screening

Review 20040719

239516 Power Changes Due To Which Feedwater Pumps

(Rfp) Are Running 20040728

239545 Im Work Order 00584879-01 Cancelled In Error. 20040728

245512 Pm Completed On Breaker 603 Instead Of

Breaker 607 20040818

247373 Fail Open Valve Installed Instead Of A Fail Close

Valve. 20040825

Rework Condition Reports

00149922 Gross EHC leak during attempt to return 2A EHC

pump 20030320

00186069 1-0203-3D steam leak at flange 20031112

00132066 Wrong Splice Kits Installed on 250V Cables 20021118

00147691 Failed PMT for New Valve 20030306

00160405 PMT Failure on WO579144-01 20030524

00166787 Unit 1 CIV #3 EHC leak 20030709

00169754 Reactor level indication 20030731

00172229 Failed Pmt For WO #586281 (2-3201-A 2A

RFP Min Flow) 20030819

00182424 Torus High Level Switches 20031022

00196997 OOT, (LT 1-1641-5A) Trend Code =B4 20040122

201012 Orifice plates for RO and FE installed

reversed (EC24429) 20040211

216730 Water in sensing lines (rework) 20040423

00130676 1B Fuel Pool pump failed to start. 20021107

00132857 Oil Mist From Concrete Piping

Repair To Ground 20021122

00135932 Flow blockage in NORMAL lineup for Gen Thermal Gas

Analyzer 20021216

00139873 Failed PMT for Work Order 98131574 20030117

00154484 Auto Start Relay (ASR) for 1/2 EDG Lost Continuity 20030417

00158353 High vibration on the OV2 Fan due to bearing degradation 20030512

00183900 Wrong parts reserved for valve overhaul 20031030

Operations Configuration Control & Closed Level 1 & 2 CRs

00126235 RHR logic electric lead disconnected 20021007

00137908 2A Recirc MG set scoop tube inadvertent reset 20030102

00138149 H2/ O2 Monitor System Control Switch Found in OFF

Position 20030105

00140164 Valve Found Already Closed And Tagged During C/O First

Hang 20030119

00150278 Inadvertent RCIC Trip Throttle Valve trip & unplanned LCO 20030322

00151220 Valve position differences between QOM, procedure and

P&ID 20030328

00159607 Pressure boundary leakage from 2" Rx head vent line 20030520

00161345 CAM System Alarms 20030531

211163 Inoperable CRD Accumulator During Scram Timing 20040326

218906 Discovered 1-1901-12,Fuel Pool Gate Drain Vlv Close 20040505

Operator Work Arounds

227718 Review RCIC system Design and Licensing Basis 20040611

00146146 Rising offgas levels unit 1 20030225

00133579 1B1 heater normal LCV tripping due to Flash Tank high

level 20021201

00136806 2A MSDT level indication (LI 2-3541-59A) is pegged high. 20021219

00141665 SJAE Rad Monitors elevated (Ref. CR 146146) 20030129

00076147 Q2001-02891 - System modification creates excess entries 20010917

00102082 Low Flow Feedwater Reg Oscillations 20020403

00129665 2B3 Heater Trip 20021031

00138067 CNMT H2/O2 MON Torus Sample Line Heat Trace

Temperature 20030103

00156214 Offgas Sample parameters > Action Lvl One for Failed Fuel 20030428

00161391 1B RR MG Set Voltage Regulator Volts/Hertz 20030601

00193417 Rework on FT 0-7541-1B, continues to act erractic 20040105

207287 Toxic Gas Analyzer false high concentration inops CREVs 20040310

00101668 U-2 Digital FWLC response during shutdown 20020330

00131422 Service Air Back-Up Valve Auto Open 20021113

00142151 Low Flow FRV oscillations 20030130

00142500 Feedwater Low Flow Feed Regulator valve 20030201

00148161 Low flow frv cable loose causing erratic operation of valve 20030308

00148469 NOS ID'd no CRs written for frequent alarms from

HCU 26-39 20030311

00193621 CCST Heaters Reliability 20040106

210224 OOT, (0-7541-1B), TREND CODE = (B3) 20040323

244262 Owa Review For Defeating Rcic Suction Vlv Swap Logic 20040813

Operability CRs

00132397 Agastat Time-Delay Relays -Coil Lead Solder Connection

Issue 20021120

00138067 CNMT H2/O2 MON Torus Sample Line Heat Trace

Temperature 20030103

00143666 White residue found at 480V MCCs aux contacts 20030209

00148103 Moore Type SCT signal converters/isolators design

problem 20030307

00179235 Potentially non-conservative pressure temperature curves 20031003

223815 (SSDI) Potential to Drain the Torus on Failure of RCIC Line 20040526

235997 Installed Transformer Does Not Match

Print #4e-1438j 20040714

00105454 GE Part 21 Notification SC 02-05 20020426

00126208 Missing bolt on cplg guard 20021007

00159950 1-1001-43A follow up to CR 159693 20030521

00186375 Main Steam SRVDL Flange Rating Lower Than

Max Pressure 20031113

221865 Pressure/Temperature Curves Non-Conservative 20040518

00159693 Failure of 1-1001-43A to fully stroke 20030520

Outage Related CRs

00095024 LLRT on 2-0220-1 valve exceeded its Required Action

limit 20020213

00094984 LLRT,MSIV exceeded the allowable leakage limit of

< 46 scfh 20020213

00095044 LLRT on 2-0220-2 valve exceeded its admin Alarm Limit 20020213

208828 Unplanned TS Entry, CREVs Inop 20040317

00097303 Deficiencies in DG2 PT compt of aux cubicle at Bus 24-1 20020228

00095273 EHC Discharge pressure switch OOT 20020215

00095515 Out of tolerance 20020217

00095554 Line 2-3009A-1" as-found wall thickness below

minimum wall. 20020217

00095557 LLRT Failed on valve 2-1301-64, would not hold pressure. 20020217

00095798 Bus 24-1 UV relay found Out of Tolerance 20020219

00095965 2-2301-45 failed leak test QCOS 2300-19. 20020220

00096226 LLRT on 2599-4B exceeded its Admin Limit 20020221

00096239 LLRT on 2-2599-5A exceeded its Administrative limit 20020221

00097628 Found 1-1459B out of tolerance while performing

qcis 1400-03 20020304

204106 APRM #6, TB #3 has Multiple Discrepancies 20040225

204737 OOT, Relay 2-6701-21-1 (AC) 20040227

204739 OOT, Relay 2-6701-21-1 (AD) 20040227

205670 Bus 26 4kV Feed Breaker "A" phase relay OOT 20040303

205671 2-203-1D 2B switch out of tech spec allowable value 20040303

205672 Bus 26 4kV Feed Breaker "C" phase relay OOT 20040303

207572 Found loose wire in plug for drywell rad monitor 2-2419B. 20040310

208197 TIP Tubing Missing Clamps Undervessel 20040313

208205 LPRM 4041B Failure 20040313

208870 LPRM 56-25D failed downscale 20040317

211248 2B DW Rad Monitor 2-2419B Reading Downscale 20040327

Q1998-04844 Discovered localized wall pitting HPCI

suction during ISI 11/07/1998

Q1998-04863 PS 1-5641-124 Out of Tolerance 11/08/1998

Q1998-04887 HPCI switches found Out of Tolerance 11/09/1998

Q1998-04894 Turbine Trip PS 1-5650-100A found Out

of Tolerance 11/09/1998

Q1998-04937 RCIC temperature switches (2) as funds

were Out of Tolerance 11/11/1998

Q1998-04942 DPIS 2-302-52 found Out of Tolerance 11/12/1998

Q1998-05035 Condenser low vacuum switch found Out

of Tolerance 11/15/1998

Q1998-05036 Relay 287-121B time delay fund slightly Out

of Tolerance 11/15/1998

Q1998-05051 LS 1-5441-34A Out of Tolerance 11/16/1998

Q1998-05084 Instrument failure 11/17/1998

Q1998-05117 Out of Tolerance 11/18/1998

Q1998-05133 As found date OOT 11/18/1998

Q1998-05158 Trip Out of Tolerance 11/19/1998

Q1998-05200 PS 1-263-37b found Out of Tolerance 11/21/1998

Q1998-05207 HPCI flow loop calibration found Out

of Tolerance 11/21/1998

Q1998-05220 Out of Tolerance 11/23/1998

Q1998-05290 Out of Tolerances found during QCIS 0200-01 11/25/1998

Q1998-05305 Out of Tolerance (per IMD Administrative

Guidance) while performing QIP 263-1 11/26/1998

Q1998-05318 Transmitter Out of Calibration 11/28/1998

Corrective Action Program Process Coded CRs

00136710 Delay in Condition Report Issuance after Problem

Identified 20021219

00136729 Identified problem reporting 20021219

00137020 Corrective Action Assignment completed inappropriately 20021220

00139529 CR 132067 closed without completion of recommended

action 20030115

00140355 NOS ID'd RCR on B14-1 fuse drawer didn't address

CR 132496 20030121

00140371 MRC Rejected RP Root Cause Report 20030121

00140818 NOS identified apparent trends in RCR themes 20030123

00144464 Concerns with CAPR closure & EFR for ECCS venting 20030213

00145305 Dried grease at Dresden/Quad aux contacts-Untimely

response 20030219

00145609 Investigation Timeliness Needs Improvement 20030221

00146496 NOS Identified Untimely Corrective Actions 20030227

00146791 NOS identified ineffective freeze seal 20030228

00146799 NOS id'd problems with Effectiveness Review 95542-07 20030228

00146878 Corrective Action AT Assignment 00143607-04 Overdue 20030228

00147253 ACE Assignment 142318-01 Rejected by MRC 20030303

00149149 QRT Grade 3 for ACE 101650-01 20030314

00152154 Corrective action items from CR149922 not initiated 20030403

00152972 Action Tracking Item Overdue 20030408

00153078 NOS identified trend codes not updated after ACE

performed. 20030409

00153101 CR 89176 CAPR Action Not as Directed 20030409

00153525 Soer 02-4 FASA for SCWE at Quad Cities- Objective 4 20030411

00156697 NOS rated site CAP implementation as ineffective for

2003Q1 20030501

00157332 NOS "Ineffective Performance" CR Not Timely 20030505

00160946 NOS IDd CR processing quality issues - supervisory

reviews 20030529

00161395 EACE 154698 Receives MQRT Grade of "D" 20030601

00161396 ACE 150851 Receives MQRT Grade of "D" 20030601

00161503 ACE 150278 Receives MQRT Grade of "D" 20030602

00161528 NOS ID'd CR not written for test failure and TS entry 20030602

00161792 Corrective Action not performed due to cancellation of

WO 20030604

00162160 QRT Grade 3 for ACE 148822-01 20030605

00163851 Corrective action entered that MRC did not approve 20030618

00164210 ACE 152803 Receives MQRT Grade of "D" 20030620

00166557 HPCI MO 2-2301-3 possible leak by 20030708

00167058 Station response to venting issues challenges

investigation 20030710

00167281 NOS Rated Site Corrective Action Program Ineffective 20030711

00167442 Priority for CRs not properly identified 20030714

00167972 MRC rejected ACE 20030717

00168928 NRC NCV 03-05-02 - Inadequate CA for a

Preconditioning Issue 20030724

00171039 EACE 127687 Receives MQRT Grade of "D" 20030811

00171042 EACE 145402 Receives MQRT Grade of "D" 20030811

00172936 NOS ID'd: Outage Lessons Learned Database 20030825

00175517 ACE 137396 Receives MQRT Grade of "D" 20030912

00176282 NOS ID: Weakness in a Root Cause Analysis 20030918

00177029 EACE Rejected by MRC 20030923

00177583 Unsatisfactory Closure of CR 174617 20030925

00178914 CR 143866 - Two Corrective Actions not Assigned

Upon Closure 20031002

00179144 Engineering RCR expectations not met 20031003

00180371 Inadequate information to complete corrective actions 20031010

00180678 CCA CAP Performance Indicator Yellow 20031013

00181086 Apparent Cause Administrative Deficiencies (CR) 20031015

00181949 Untimely CR Initiation 20031020

00183316 ACE 131050 Receives MQRT Grade of "F" 20031010

00186434 FASA Deficiency - Ineffective Corrective Action 20031113

00196512 PI for Median Age of CA is Red 20040120

00197277 CCA needed for External Identified CRs 20040123

201217 Corrective Action AT closed without all actions

performed 20040212

216467 Ineffective ACE and ACIT closure problems 20040422

216684 Untimely Initiation of Condition Reports by Engineering 20040423

227203 Cr Initiation Not Always Timely For Some Areas 20040609

227259 Nos Id D: Mrff Cr Processing Issues 20040609

227368 Site Wide Trending Not Consistently Used To Improve

Performance 20040610

239314 Cr210037 Corrective Action Incomplete 20040727

240264 Ineffective Capr For Main Steam Line Flow Switch

Root Cause 20040730

244665 Evaluation For Ir 232361 Does Not Exist In Passport 20040816

246150 Potential Problem With The Timely Routing Of Irs

To Ops 20040820

Additional Items Reviewed

NRC Information Notice 2002-29; Design Problems in Safety Functions of Pneumatic

Systems; dated October 15, 2002

General Electric Service Information Letter 448; Maintenance and Lubricants for GE

Type AK/AKR Circuit Breakers; Revision 2

ENG-04-07; Quad Cities June 2004 Quarterly System Health Indicators; dated July 22,

2004

NRC Generic Letter 88-14; Instrument Air Supply System Problems Affecting

Safety-Related Components; dated August 8, 1988

Commonwealth Edisons Response to Generic Letter 88-14; dated February 6, 1989

Maintenance Rule Performance Criteria Information for Function Z0012-01; Provide

Internal Flood Protection for the Reactor Building; dated October 22, 2004

Common Cause Analysis 209720; Analysis of the Trend in Work Practice Work

Instructions Coded Condition Reports Attributed to Maintenance; dated June 27, 2004

Common Cause Analysis 209752; Engineering Document Quality; dated July 28, 2004

CC-AA-103-2001; Setpoint Change Control; Revision 1

ESPT Continuing Training Course 04TESCT; Operability Determination; Revision 1

List of Camera Used for ALARA Purposes; dated October 26, 2004

Operating Experience Item 129522; Review of General Electric Technical Information

Letter 1360-2, EHC Power Supply Inspections; dated September 23, 2002

Operating Experience Item 136842; Review of General Electric SC02-22, Potential

Non-Conservatism in Small Steam Line Break Analysis Assumptions for Mark I

Containment Equipment Qualification; dated January 19, 2003

Operating Experience Item 136898; Review of General Electric Service Information

Letter 646, Target Rock Safety Relief Valve Failure to Fully Open; dated January 29,

2003

Operating Experience Item 141461; Review of General Electric SC03-01, Additional

Material Consideration for TIP System Ball and Shear Valve Qualifications; dated

June 16, 2003

Operating Experience Item 148037; Review of Nuclear Event Report DR-03-001, High

Flow Control Line Following Load Drop; dated April 4, 2003

Operating Experience Item 156575; Review of Nuclear Event Report KS-03-006,

Fleet-Wide Actions for Operating Events from 2002; dated August 26, 2003

Operating Experience Item 171258; Review NRC Information Notice 2002-37, Failure

of Safety-Related Circuit Breaker External Auxiliary Switches at Columbia Generating

Station; dated January 5, 2003

Operating Experience Item 174867; Review of Nuclear Event Report KS-03-007,

Inadequate Disposition of Single Point Vulnerability Results; dated October 1, 2003

Operating Experience Item 175971; Review of Nuclear Event Report DR-03-096,

Stroke Time Issue with High Pressure Coolant Injection Pump Discharge to

Condensate Storage Tank Motor Operated Valves; dated October 27, 2003

Operating Experience Item 179572; Review NRC Information Notice 2003-18, General

Electric SBM Control Switches with Defective Cam Followers; dated March 30, 2004

Operating Experience Item 200024; Review of Nuclear Event Report DR-04-006, Unit 3

Reactor Scram While Transferring Main Turbine Lube Oil Cooler; dated April 20, 2004

Operating Experience Item 202720; Review of Nuclear Event Report DR-04-009, Water

Entered Into the High Pressure Coolant Injection Steam Line Following a Scram; dated

March 31, 2004

Operating Experience Item 254371; Review of Nuclear Event Report LI-04-067, Unit 1

Thermal Power Exceeded by 0.2 - 0.4 Percent; dated September 21, 2004

P & ID, 21, Diagram of Turbine Building Closed Cooling Water System (Unit 1)

QOM, 1-3800-01, Rev. 8, U1 TBCCW Valve Check List

TBCCW System Engineering Notebook Index and Sample of Notebook

List of OPEN Work Orders and Work Requests for TBCCW System

Common Cause Analysis, CCA 203885-19 (Local Leak Rate Test Failures Affect Refuel

Outage Performance)

Issue Reports Submitted as a Result of the Team Observations

IR 00265130; Trapeze Type Piping Support Nut and Locknut Not Engaged

IR 00265397; Surface Corrosion on Pump Flanges/Hardware

IR 00265505; Valve Has Residue On/Near Packing Gland

IR 00265625; U-1 TBCCW Expansion Tank LCV Air Line Vibrates

IR 00265729; TBCCW Piping Hanger Issues in Crib House

IR 00266695; Valve has Residue on/Near Packing Gland

IR 00266711; TBCCW Pipe Hanger Issues in U-2 Crib House

IR 00266714; Pipe Support U-Bolts Lose or Missing, U-1 CRD Level

IR 00266734; U-1 RFP U-Bolt Pipe Supports Have Loose/Missing Jamb Nuts

IR 00266747; U-2 RFP U-Bolt Pipe Supports Have Loose/Missing Jamb NutsAR

266778; TBCCW Valves & Gauges for 1A IAC Have SW System EPNS

AR 00266814; TBCCW Valves Have 3900 System EPNS & SW and DW System

Names

IR 00266891; TBCCW Valves/Gauges Have 3900 System EPNS & Noun Names

IR 00267665; Extent of Condition From Pipe Support/Hanger Issues Found

24