IR 05000254/2020010

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Biennial Problem Identification and Resolution Inspection Reportt 05000254/2020010 and 05000265/2020010
ML20329A436
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 11/24/2020
From: Reimer K
NRC/RGN-III/DRP/B1
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2020010
Download: ML20329A436 (20)


Text

November 24, 2020

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000254/2020010 AND 05000265/2020010

Dear Mr. Hanson:

On October 23, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Quad Cities Nuclear Power Station and discussed the results of this inspection with Mr. K. Ohr, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects

Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000254 and 05000265

License Numbers:

DPR-29 and DPR-30

Report Numbers:

05000254/2020010 and 05000265/2020010

Enterprise Identifier: I-2020-010-0034

Licensee:

Exelon Generation Company, LLC

Facility:

Quad Cities Nuclear Power Station

Location:

Cordova, IL

Inspection Dates:

October 05, 2020 to October 23, 2020

Inspectors:

V. Petrella, Reactor Inspector

C. Mathews, Illinois Emergency Management Agency

C. Phillips, Project Engineer

A. Shaikh, Senior Reactor Inspector

D. Tesar, Resident Inspector

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Quad Cities Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities, and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program (CAP), use of operating experience, self-assessments and audits, and safety conscious work environment.

Corrective Action Program Effectiveness: The inspectors assessed the CAP's effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review of the Unit 1 turbine building closed cooling water (TBCCW) system.

  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Assessment of the Corrective Action Program

Based on the samples reviewed, the team determined that your staff's performance in each of these areas adequately supported nuclear safety.

Effectiveness of Problem Identification

Overall, the licensee was generally effective at identifying issues at a low threshold and was properly entering them into the CAP as required by station procedures. The inspectors determined issues were normally identified and captured in a complete and accurate manner in the CAP. The inspectors determined the licensee was effective at identifying negative trends that could potentially impact nuclear safety. The inspectors walked down portions of the Unit 1 TBCCW system, the Unit 1 control rod drive system, and the main control room.

The inspectors did, however, identify issues in the area of problem identification. The inspectors concluded that the CAP was not always used to its full potential. In addition, maintenance discrepancy tags were not always removed from the field for work that had been accomplished or cancelled. Maintenance discrepancy tags that are still hanging for work that has been completed or cancelled can interfere with the entry of items into the CAP.

The licensee's CAP audit completed in 2019 identified a small number of equipment and housekeeping deficiencies

(10) that were not entered into the CAP, and 33 percent of the deficiency tags reviewed (5 of 15) were found to be completed or cancelled. Maintenance department management determined that there was a process for removing tags, and no further actions were necessary. The operations department management spoke with non-licensed equipment operators and asked them to review deficiency tags periodically, as time allowed.

The maintenance audit completed in March 2020 identified a small number

(4) of CAQs items that had not been entered into the CAP. In response, the station generated a performance improvement action plan (PIAP) to provide site-wide communication and face-to-face reinforcement of CAP usage. The PIAP was completed on April 30, 2020. The effectiveness review (EFR) of the PIAP was completed in June 2020. The Safety Culture Monitoring Panel and End-of-Day Senior Leadership Team reviews determined that the efforts regarding the PIAP for issues not being entered into the CAP were effective. This was a determination based on what the site was seeing with regards to CAP documents being initiated and the efforts that had been put forth to address this trend. The maintenance audit identified that 27 percent of the deficiency tags reviewed (8 of 30) were from completed or cancelled work.

The actions associated with the deficiency tags from that audit were to issue a site-wide communication regarding proper removal of orphaned deficiency tags. This communication was to be sent out four times before the outage in April 2020 and once a month after the outage for an overall timeframe of three months. The action was marked as completed before the three months even started, and subsequently the site-wide communication was sent out only once prior to the outage.

The inspectors had identified about 15 items that had not been entered into the CAP without prompting from the resident inspectors over the last two years. The majority of these items were identified before the corrective actions were taken in April.

Effectiveness of Prioritization and Evaluation of Issues

The inspectors determined the licensee was effective at prioritizing and evaluating issues.

Most issues were evaluated appropriately in accordance with station procedures and addressed at levels commensurate with their safety significance. Root, potential, and contributing causes were identified for issues as required. The proper level of consideration was taken for extent of cause and condition, generic implications, and evaluation of previous occurrences. The inspectors determined the Management Review Committee meetings and the Station Ownership Committee meetings were thorough and maintained a high standard for evaluation quality. Members of the two committees were prepared and engaged. The committee members discussed selected issues in sufficient detail and challenged each other regarding proposed conclusions and recommendations.

The inspectors also completed an in-depth review of issue reports and work orders for a 5-year time period for the Unit 1 TBCCW system.

Effectiveness of Corrective Actions

The inspectors concluded the licensee was generally effective in developing corrective actions that were appropriately focused to correct the identified problem and to address the root and contributing causes for significant conditions adverse to quality to preclude repetition. The licensee completed these corrective actions in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue. For NRC-identified issues, the inspectors determined the licensee assigned actions were effective and timely.

Assessment 71152B Operating Experience and Self-Assessments and Audits Observations

Based on the samples reviewed, the team determined that licensee performance in the use of operating experience, self-assessments, and audits adequately supported nuclear safety.

Use of Operating Experience

Overall, the inspectors concluded operating experience was adequately evaluated for applicability and appropriate actions were implemented in an effective and timely manner to address lessons learned as needed. Relevant industry operating experience was disseminated across the various departments and was used at the station for activities such as pre-job briefs and daily meetings. The inspectors also verified the use of operating experience in formal CAP products such as root cause evaluations and apparent cause evaluations was appropriate and adequately considered.

Self-Assessments and Audits

Based on the results of the inspection, the inspectors determined the licensee was effective at performing self-assessments and audits to identify issues and enhancement opportunities at an appropriate low level, properly evaluated those issues, and resolved them commensurate with their safety significance. The self-assessments and audits reviewed were accurate and thorough. The inspectors concluded these audits and self-assessments were completed by personnel knowledgeable in the subject area. Issues identified were entered into the CAP as required by procedures. The inspectors also determined that findings from the CAP self-assessment were generally consistent with the inspectors assessment.

Assessment 71152B Assessment of Safety Conscious Work Environment

The inspectors found no evidence of challenges to the licensees safety-conscious work environment. Licensee personnel appeared willing to raise nuclear safety concerns through at least one of several means available.

The inspectors held scheduled interviews with eight individuals from various departments and experience levels to assess their willingness to raise nuclear safety issues. Information obtained during the interviews indicated an environment was established where licensee personnel felt free to raise nuclear safety issues without fear of retaliation. Licensee personnel were aware of and generally familiar with the CAP and other processes, including the Employee Concern Program and the NRCs allegation process, through which concerns could be raised. In addition, a review of the types of issues in the Employee Concern Program indicated licensee staff were appropriately using the CAP to identify issues. The inspectors did not observe and were not provided any examples where there was retaliation for the raising of nuclear safety issues. Documents provided to the inspectors regarding surveys and monitoring of the safety culture and safety conscious work environment generally supported the conclusions from the interviews.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 23, 2020, the inspectors presented the biennial problem identification and resolution inspection results to Mr. K. Ohr, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

ALARA Plans

QC-02-19-0807

TB BLDG Moisture Separator/Steam Reheater Activities

(Q2R25)

Corrective Action

Documents

AR 1184855

IRSF BLDG has Leaking Water Shields

03/07/2011

AR 1312050-01

Reoccurring AT to Refill IRSF Water Shields

01/11/2012

AR 1502141

NOS ID: Long Term Storage for Lead Blankets

04/15/2013

AR 1529867

Clean Water Act 316(B) Final Rules Delayed to Nov. 4, 2013

06/27/2013

AR 2579025

TBCCW HX Outlet Temperature Low on Rounds

10/29/2015

AR 2662555

1B TBCCW Heat Exchanger North Cover Leak

04/28/2016

AR 2669114

NRC ID'd: MO 2-2399-40 Overthrust Event Human

Performance

06/13/2016

AR 2696077

TI 1-3840-3 On 912-1 is Reading 5 Degrees Higher Than

Local

07/23/2016

AR 3177044

Document the Power Labs Failure Analysis Report of the

Failed Servo and Lockup Solenoid Valves

08/06/2019

AR 3998478

Unit 1 RCIC Failed Surveillance

05/10/2017

AR 4003656

1A EHC TBCCW TCV Slow to Respond

04/27/2017

AR 4072162

Unit 1 HPCI did Not Trip during QCOS 2300-05

11/07/2017

AR 4097431

SA: NRC RP Occupational ALARA Planning and Controls

01/26/2018

AR 4098275

Self-Assessment: Operator Fundamentals

01/29/2018

AR 4098310

Self-Assessment: Configuration Control Program

01/29/2018

AR 4103500

Cover Missing from TI 1-3841-36H

01/18/2018

AR 4114303

EO ID: Hydrolase or Block Floor Drain that is Causing

Contamination

03/13/2018

AR 4117193

Improper Control of Safeguards Information

03/09/2018

AR 4123777

2A RFP Vent Fan Discharge Damper Closed on Fan Start

04/06/2018

AR 4136242

Assignment #87 Station OPEX Review of IRIS 467286 from

Monticello for Applicability

01/31/2020

AR 4136242

Assignment #88 Station OPEX Review of IRIS 451474 from

Peach Bottom for Applicability

2/12/2020

AR 4145668

Unit 1 MSV #1 did Not Initiate 10 Percent Close RPS Signal

06/09/2018

AR 4154544

Air Leak on U1 TBCCW Expansion Tank LCV PRV

07/10/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4156181

U2 EDG Elevated Temps During Monthly Load Test

07/16/2018

AR 4161195-99

Performance Analysis

2/20/2020

AR 4167051

Need Update to PM WO SFP Level

08/24/2018

AR 4168927

Rear Sight Aperture Missing

08/30/2018

AR 4170951

PAF Enter 1 Turnstile Releases with no Badge Usage

09/07/2018

AR 4171765

MO-1-1001-7C May Not Open During Mode 3 LOCA

09/11/2018

AR 4177502

Performance of Contact Verifications on Output Breaker 7-8

with Output Breaker 6-7 Open Caused Unit SCRAM Due to

Turbine-Generator Load Reject

11/01/2018

AR 4180286

Emergency Light Battery Pack Low Conductance

10/04/2018

AR 4180321

CRD Exercises in Q1F66 Found New CRDM to be Repaired

10/04/2018

AR 4186613

Assignment #13 Perform Level 3 OPEX Evaluation

01/31/2019

AR 4187996

REC Assignment Not Created for Strength from SRPT

4099106-04

10/26/2018

AR 4188055

Incorrect Assignment Types and Event Codes Used in DEF

ARS

10/26/2018

AR 4189054

Tamper Seal Tape Missing on SBO DCS Applications Panel

10/29/2018

AR 4194729

PORC Minutes Not Submitted Within 30 Days

11/14/2018

AR 4194732

PORC Action Item Documentation of Approval Deficiency

11/14/2018

AR 4196555

RRP Seal MGMT ER-AA-3006 Implementation Deficiencies

11/20/2018

AR 4201822

Review of QDC FRV Lockups Trend

2/10/2018

AR 4202301

EO ID: 3 DPM Leak on TBCCW to 1A IAC SOL. Bypass

Valve

2/12/2018

AR 4206618

Expired Capacitors in Inventory

2/29/2018

AR 4208594

EP - Siren Failures (QC08, QC18, QC26, QC31)

01/07/2019

AR 4209429

AVB-4 Leaking Fluid

01/09/2019

AR 4209656

AVB 4 Leaking Fluid - Vegetable Oil

01/09/2019

AR 4209855

SA ID - Vendor Audit Records Missing from EDMS

01/10/2019

AR 4213355

1A RHR Pump in IST Alert Range

01/23/2019

AR 4217114

Active Vehicle Barrier #4 Leaking Fluid

2/04/2019

AR 4217557

Unit 1 HPCI Failed to Roll During QCOS 2300-27 Due to

Blown Fuse

03/08/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4222485

EO ID: Standby 1A TBCCW Discharge PI Indicates High

2/22/2019

AR 4226091

Humidity in the TSC is High

03/04/2019

AR 4226971

Long Term Storage Area >90 Days for Temp Shielding

Equipment

03/06/2019

AR 4226980

Long Term Storage Area >90 Days for Temp Shielding

Equipment

03/06/2019

AR 4228629

IMD Requires New Test Equipment

03/12/2019

AR 4230952

Assignment #15 Perform OPEX Review of NRC IN 2019-01

05/10/2019

AR 4232297

Q1R25 - Higher than Expected Radiological Conditions

03/18/2019

AR 4232533

Q1R25 IVVI CS Piping 3P4D Weld New Indication

03/24/2019

AR 4234066

Long Term Storage Area for Lead Blankets

03/28/2019

AR 4235173

QC RP Candidate for Elevation

04/19/2019

AR 4235745

Error Found in Quarterly ODCM Permit for 3rd Qtr 2018

04/02/2019

AR 4237923

Manual Action 50.59/Calculation Different from EC

04/23/2020

AR 4241135

NOS ID: TSC HVAC Mod was Not Assessed by EP

04/18/2019

AR 4241139

NOS ID - PA Speaker Testing Not Completed in 2018

04/18/2019

AR 4244824

2-1301-20 HPCI CCST Suction Check Valve Leaks

By/Hangs Up

04/30/2019

AR 4244924

Follow Up to IR 4235745

04/30/2019

AR 4246921

EO ID: Leak on SS Mesh Hose to 1C RFP Outboard Seal

Cooling

05/07/2019

AR 4250774

EDMS Record Turned Over with Incorrect Title

05/21/2019

AR 4250843

EO ID'D 1A TBCCW Pump Disch PI is Vibrating Excessively

05/22/2019

AR 4250933

1A TBCCW Oil Leak

05/22/2019

AR 4254547

Unit 1 HPCI did Not Trip Locally During QCOS 2300-13

06/05/2019

AR 4256218

NRC IN 2019-02: EDG Excitation System Diode Failures

06/12/2019

AR 4259342

Diesel Fuel Self-Assessment Deficiency

06/25/2019

AR 4259835

FAC OE - 2018 Indian Point HP FWH Leak (INPO ICES

  1. 444436)

06/27/2019

AR 4262718

EP-Loss of Off-Site Communication

07/08/2019

AR 4266776

HPCI Not Disabled for Fire Areas TB-III And TB-I

07/24/2019

AR 4269822

PAF Enter 1 Turnstile will Not Release

08/06/2019

AR 4270068

Pre-Access Facility Entry Turnstile Number 1 Failed Test

08/07/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4281772

PJR QC-01-19-0054DW Inboard MSIV Overhaul

09/24/2019

AR 4283563

TRNG - Self-Assessment Gaps in NISP-TR-01 Form

Completion

09/30/2019

AR 4285721

Emergency Lighting Needs Added to Aux Electric Room

10/07/2019

AR 4287032

Unable to Perform PMT AO 0-4199-315, CR HVAC AFU Fire

FP VLV

10/11/2019

AR 4289588

4.0 Critique U1 Downpower

10/21/2019

AR 4291738

Water Found in Control Room HVAC Air Filtration Unit

10/27/2019

AR 4292644

Results of 2019 Self-Assessment Check-In Critical CTRL

Docs

10/30/2019

AR 4292671

Unable to Drain via 1-3999-240B

10/30/2019

AR 4292718

Operation Training Issue Matrix Update

10/30/2019

AR 4295378

Perform Update to ODCM at Next Major Revision

11/07/2019

AR 4296750

Configuration Control Self-Assessment Deficiency

11/13/2019

AR 4297293

SRPT Def - Issues with Actions Under IR 4168791

11/14/2019

AR 4297327

SRPT Def: REC Not Created for Strength in SRPT

4197601-04

11/14/2019

AR 4297380

SRPT Def: EFR Assignments Not Created under RCR

4177502-05

11/14/2019

AR 4297427

SRPT Def: Issues with ECAP 4187243

11/14/2019

AR 4298489

SRPT Def: Issues with ECAP 4217557-04

11/19/2019

AR 4298851

ALARA FASA Deficiency #1 - Post Job Review Not

Completed

11/20/2019

AR 4298854

ALARA FASA Deficiency #2 - WIP Admin Errors

11/20/2019

AR 4299103

SPRT Def: Issues with CAPE 4248635-12

11/21/2019

AR 4299841

1B TBCCW HX Requires Additional Maintenance

11/25/2019

AR 4300537

Plant Emergency Siren Breaker Trip During Surv

11/29/2019

AR 4301424

Cyber Security Lessons Learned - SFAQ 17-04

2/04/2019

AR 4301425

Cyber - System Assessment Requires Revision

2/04/2019

AR 4301427

Missing Signature on IT-AA-101-1502-F-01 for Log QDC-

001-19

2/04/2019

AR 4301428

Missing Initial and Date on DTE Inventory PM Packages

2/04/2019

AR 4301429

Missing Pages in EDMS Scans of Cyber Incident Forms

2/04/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4301430

Cyber - Required Recurring Task Periods Exceeded

2/04/2019

AR 4301431

Incorrect Document Number in EDMS

2/04/2019

AR 4301436

Cyber - SA 04204131 Deficiency 1

2/04/2019

AR 4301438

Cyber - SA 04204131 Deficiency 2

2/04/2019

AR 4301439

Cyber - SA 04204131 Deficiency 3

2/04/2019

AR 4301441

Cyber - SA 04204131 Deficiency 4

2/04/2019

AR 4301443

Cyber - SA 04204131 Deficiency 5

2/04/2019

AR 4302034

Trigger IR - Chemistry 3 Month Decline

2/06/2019

AR 4304392

SA ID: Objective Evidence Report Quality Deficiencies

2/17/2019

AR 4304402

SA ID: Objective Evidence Reports Require Clarification

2/17/2019

AR 4304891

1A TBCCW HX Requires Additional Maintenance

2/17/2019

AR 4308635

EO-ID 1C RFP Outbd Seal Cooling Jacket Leak

01/08/2020

AR 4309332

Preparation for NRC Problem Identification and Resolution

(PI&R) Inspection

AR 4312994

Inadequate Progress in Resolving Site Obsolescence Issues

01/27/2020

AR 4315832

19-003 SA Deficiency-FLS Peer Group

2/06/2020

AR 4318507

EP-Siren Failure (QC26, QC40)

2/17/2020

AR 4319267

Explosive Detector #2 Shows Detector Flow Warning

2/19/2020

AR 4321646

HPCI ECAP 4217557 Corrective Action Implementation Error 02/26/2020

AR 4322001

Assignment #3 Station OPEX Review of IRIS 469506 From

Cook for Applicability

04/24/2020

AR 4322001

Assignment #26 Station OPEX Review of IRIS 474860 from

Columbia for Applicability

07/10/2020

AR 4322001

Assignment #31 Station OPEX Review of IRIS 479210 from

Davis-Besse for Applicability

08/03/2020

AR 4322036

Unit 0 250 Battery Charger Resistor Replacements

2/27/2020

AR 4324285

TSC HVAC Air Conditioning

03/05/2020

AR 4327228

Viking Boxes 11 and 12 Failed Test

03/17/2020

AR 4327972

NSMART Array Battery Failures

03/19/2020

AR 4330099

FME 480V Breaker N015 Lockwasher Issue

03/27/2020

AR 4330737

ERV 2-0203-3D Relief Valve did Not Actuate

03/30/2020

AR 4332194

Elevated Dose Rates on Both U2 Core Spray Lines DW 640'

04/02/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4333529

Emergency Light Pack 76H Trickle Charger Light is Out

04/07/2020

71152B

Corrective Action

Documents

AR 4333651

Unit 2 Refuel Bridge Main Hoist Load Cell Abnormal

Indication

04/08/2020

AR 4335536

B Control Room HVAC RCU Feed Breaker Tripped

05/21/2020

AR 4335890

QC-02-20-00906 Cavity Decon Post-Job Review

04/15/2020

AR 4345208

Unable to Rack in 2A RHRSW Pump Breaker

05/22/2020

AR 4345774

250V DC Essential Battery Undervoltage

05/26/2020

AR 4346037

U1 DGCW Piping Inspection

05/27/2020

AR 4348113

Facilities Maintenance Backlog of Security Work Requests

06/04/2020

AR 4348145

U2 HPCI Check Valve Response During QCOS 2300-11

06/04/2020

AR 4348762

U1 HPCI Service Water Strainer High D/P

06/08/2020

AR 4349586

2D Corrosion on U2 250VDC Safety Batteries

06/11/2020

AR 4349840

ECCS Keep Fill Check Valve Stuck Closed

06/11/2020

AR 4350112

2B RBCCW Pump Shaft Seal Leaking Oil

06/13/2020

AR 4350838

MO 1-3301-C Found with Extruding Gasket

06/17/2020

AR 4351170

EMD Group 1 Fire Seal Discrepancies

06/18/2020

AR 4351382

U2 TBCCW Temperature Irregularities

06/19/2020

AR 4351484

Greater than 25 Percent of ILT 20-1 Candidates Screen as

At-Risk

06/19/2020

AR 4352084

U1 1-5802 Oil Analysis Indicates out of Spec Oil Samples

06/23/2020

AR 4352191

Unit 2 QCIS 1600-10-QAI Lessons Learned

06/23/2020

AR 4352572

Hydrogen Leak Detected in 2252-7 Cabinet

06/25/2020

AR 4353049

2B RHRSW LP Pump OB Seal Leak

06/26/2020

AR 4354219

Disch Press Gage Reading Higher than Suct Press

07/01/2020

AR 4357863

PI&R CAP Invest Issues Identified During Self-Assessment

07/20/2020

AR 4358063

Gap Under India 2 Gate does Not Meet Security

Requirements

07/21/2020

AR 4358195

Security OPEX - Failure of OC Canister Seal

07/22/2020

AR 4358541

DEP was Not Counted in the Month Completed

07/23/2020

AR 4358551

DEP Opportunity Not Counted in the Month it was Performed

07/23/2020

AR 4358557

Q1R26 - Torus Vapor Phase Recommended Coating Repairs 07/23/2020

AR 4358559

ERO Participation Credit Given in Error

07/23/2020

AR 4360860

EP Historical Demonstration Criteria Failure

08/04/2020

AR 4363713

EP Containment Hydrogen from Simulator Not Accurate in

TSC

08/11/2020

AR 4366400

NCV 20-002, CLSR PKG - Failed 3D ERV Event

08/31/2020

AR 44344520

NCV 20-001, CLSR PKG - CREVs AFU PMT Not Performed

Event

05/20/2020

CA 4187243-28

Implement Revision to QCOS 6500-09 and QCOS 6500-10

to Math TIC #3490, to Open the Knife Switches Prior to

Relays Testing

2/14/2019

CAPE 04117193

Improper Control of Safeguards Information

03/20/2018

CAPE 4330737-

ERV 2-0203-3D did Not Actuate

04/24/2020

CAPE 5328207

LPCI Swing Bus (MCC 28/29-5) did Not Transfer QCOS

6700-02

04/30/2020

ECAP 4163086-

U1 MSV 1 RPS Limit Switch did Not Initiate 10 Percent RPS

Close Signal

09/20/2018

ECAP 4187243-

Undervoltage Trip of Bus 13-1 During QCOS 6500-09

11/29/2018

ECAP 4254019-

Pump Failed to Start During QCOS 1000-04

06/03/2019

ECAPE 3990038

MSIVs 1-0203-1B, 1-0203-1D, 1-0203-2C and 1-0203-2D

Closure Times Exceeded the Maximum Technical

Specification Limit of 5 Seconds

04/11/2019

ECAPE 4116642

MSIVs 2-0203-1A and 2-0203-1C Closure Times Exceeded

the Maximum Technical Specification Limit of 5 Seconds

04/11/2019

ECAPE 4266776

HPCI Not Disabled for Fire Areas TB-III and TB-I

09/05/2019

EFR 14

Effectiveness Review for CR 4116642

05/21/2020

EFR 3291738-17

Effectiveness Review for Actions to Address the Failure to

Perform A PMT on the B CREVs

05/21/2020

PIAP AP-2020-22

Issues Not Being Entered Into CAP

06/25/2020

RCR 4160631

Unit 1 Resin Intrusion Event

09/21/2018

RCR 4274286

Water Intrusion on the "A" Isolated Phase Bus Duct Near the

Unit Auxiliary Transformer Caused

10/04/2019

RCR 4335396

Quad Cities Unit 2 Trip Due to Cut Wire in Generator

Protection Circuit

05/29/2020

Corrective Action

Documents

Resulting from

Inspection

AR 4375043

NRC PI&R ID'd: Action Created with the Wrong Reference

10/07/2020

AR 4375899

NRC PI&R ID'd: MA-AA-716-026 Requirements Not

Followed

10/11/2020

AR 4377638

NRC PI&R ID's WO Cancellation Notes Require More Detail

10/19/2020

AR 4377760

NRC PI&R ID'd: TBCCW System Walkdown Results

10/19/2020

AR 4378340

NRC PI&R ID'd: Typo Identified in Self-Assessment

4097431-04

10/21/2020

AR 4378372

NRC PI&R ID'd: 1B TBCCW HX Inspection Frequency

Incorrect

10/21/2020

AR 4378394

NRC PI&R ID'd: ELP 45F Labeling Enhancement

10/21/2020

AR 4378416

NRC PI&R ID: CAP Not Used to Full Potential

10/21/2020

AR 4378570

NRC PI&R ID: MREQ 4323765-02 Closure Issues

10/22/2020

AR 4378880

IEMA ID: Trends on Remediation Well

10/23/2020

Miscellaneous

Heat Exchanger Inspection Report for 1A TBCCW

2/27/2016

Heat Exchanger Inspection Report for 1B TBCCW

11/22/2019

Heat Exchanger Inspection Report for 1A TBCCW

2/17/2019

CFAM

CFAM Monthly Performance Summary - OR-PI

March 2019

CFAM

CFAM Monthly Performance Summary - OR-PI

March 2020

CFAM

CFAM Monthly Performance Summary - OR-PI

May 2020

CFAM

CFAM Monthly Performance Summary - OR-PI

June 2019

CFAM

CFAM Monthly Performance Summary - OR-PI

September

2019

CFAM

CFAM Monthly Performance Summary - OR-PI

December

2018

NOSA-QDC-19-

Corrective Action Program Audit Report

NOSA-QDC-19-

Radiation Protection Audit Report

NOSA-QDC-20-

Chemistry Audit Report

Procedures

MA-AA-716-026

Station Housekeeping/Material Condition Program

15, 17, 18

RP-AA-550-1001

Hot Spot Tracking

71152B

Self-Assessments AR 04096589

Pre-2018 NRC Emergency Preparedness Graded Exercise

Baseline Inspection

08/16/2018

AR 04187211

Foreign Material Exclusion Self-Assessment

2/12/2019

AR 04321425

IP 71130-04 Equipment Performance, Testing/Maintenance

and IP 71151 Performance Indicator

05/08/2020

AR 04321453

Review of Power Reactor Target Sets

07/06/2020

AR 4250900

Engineering Design Control Audit Report

07/24/2019

AR 4341665

Engineering Programs Audit Report

06/24/2020

NOSA-QDC-18-

Security Programs Audit Report

01/30/2018

NOSA-QDC-18-

Emergency Preparedness Audit Report

04/25/2018

NOSA-QDC-19-

Security Programs Audit Report

2/06/2019

NOSA-QDC-19-

Emergency Preparedness Audit Report

04/24/2019

NOSA-QDC-20-

(AR 4308359)

Maintenance Functional Area Audit Report

03/11/2020

NOSA-QDC-20-

Security Programs Audit Report

2/05/2020

NOSA-QDC-20-

Emergency Preparedness Audit Report

04/22/2020

RP SRPT

4097382-04

Radwaste and Radioactive Material Handling, Storage, and

Transportation

10/05/2018

RP SRPT

4097431-04

NRC RP Occupational ALARA Planning and Controls

RP SRPT

4118048-04

Post-Accident Gaseous Effluent Monitoring (NUREG 0737)

2/18/2018

RP SRPT

4197601-04

NRC RP Exposure Controls, Airborne Inspections

05/02/2019

RP SRPT

4198147-13-03

Radiation Protection Dosimetry

01/03/2020

RP SRPT

4198941-13-03

Radiation Protection Instrumentation

11/14/2019

71152B

Self-Assessments RP SRPT

4199090-13-03

2019 ALARA (Site Review)

11/20/2019

RP SRPT

207564-04

NRC RP - Rad Monitoring Instrumentation Inspection

07/16/2019

RP SRPT

207574-04

NRC RP - Solid Waste Processing, Handling, Storage, and

Transportation Inspection

10/22/2019

SRPT 4082073-

Condensate Chemistry

01/04/2019

SRPT 4096570-

Self-Assessment and Benchmark Compliance

SRPT 4098275-

Operator Fundamentals

10/31/2018

SRPT 4184143-

Diesel Fuel Oil

07/02/2019

SRPT 4184154-

Lab Safety - Hygiene

2/19/2019

SRPT 4205175-

Clearance and Tagging

2/27/2019

SRPT 4206027-

Radioactive Effluents Control Program/Radiological

Environmental Monitoring Program/Radiation Monitoring

(RECP/REMP)

06/04/2019

SRPT 4228697-

Off-Year NRC PI&R Assessment of the Corrective Action

Program

SRPT 4259948-

Project Legacy - CY Mid-Project Update

09/10/2019

SRPT 4337229-

Chemistry Supervisory Oversight

06/24/2020

Work Orders

WO 1845827-03

Op Work Instructions to Stroke 0-4199-315, Fire WTR to

Charcoal Filts AO

WO 1857843

(LR) TBCCW System Walkdown By System Engineer

11/16/2015

WO 1930650

(LR) TBCCW System Walkdown By System Engineer

09/22/2016

WO 4630031

(LR) U1 TBCCW System Walkdown

07/18/2017

WO 4687313-01

HPCI CCCST Suction CK VLV Disassemble & Inspect

04/06/2020

WO 4718695

(LR) U1 TBCCW System Walkdown

03/16/2018

WO 4848232-01

T/S and Repair Trip of Bus 13-1

03/21/2019

WO 4940878

(LR) TBCCW System Walkdown

11/01/2019

WO 5014005

(LR) TBCCW System Walkdown

06/23/2020