IR 05000254/2022013

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Biennial Problem Identification and Resolution Inspection Report 05000254/2022013 and 05000265/2022013
ML22319A156
Person / Time
Site: Quad Cities  
Issue date: 11/17/2022
From: Robert Ruiz
NRC/RGN-III/DORS/RPB1
To: Rhoades D
Constellation Energy Generation
References
IR 2022013
Download: ML22319A156 (1)


Text

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000254/2022013 AND 05000265/2022013

Dear Mr. Rhoades:

On October 7, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Quad Cities Nuclear Power Station and discussed the results of this inspection with Mr. B. Wake, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations problem identification and resolution program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for problem identification and resolution programs.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

Three findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

November 17, 2022 If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Quad Cities Nuclear Power Station.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Quad Cities Nuclear Power Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Robert Ruiz, Chief Reactor Projects Branch 1 Division of Operating Reactor Safety Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000254 and 05000265

License Numbers:

DPR-29 and DPR-30

Report Numbers:

05000254/2022013 and 05000265/2022013

Enterprise Identifier:

I-2022-013-0007

Licensee:

Constellation Nuclear

Facility:

Quad Cities Nuclear Power Station

Location:

Cordova, IL

Inspection Dates:

August 22, 2022 to November 21, 2022

Inspectors:

Z. Coffman, Resident Inspector

T. Gardner, Physical Scientist

Z. Hollcraft, Senior Reactor Operations Engineer

C. Mathews, Illinois Emergency Management Agency

A. Nguyen, Senior Resident Inspector

A. Tran, Project Engineer

Approved By:

Robert Ruiz, Chief

Reactor Projects Branch 1

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Quad Cities Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Incorporate Vendor Recommendations into Preventative Maintenance Procedures Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green FIN 05000265/2022013-01 Open/Closed

[P.4] - Trending 71152B A self-revealed finding of very low safety significance (Green) was identified for multiple examples of the licensee failing to incorporate vendor recommendations into preventative maintenance procedures, resulting in the failure of multiple risk-significant components.

Failure to Identify and Correct a Condition Adverse to Quality Resulting in Both Trains of Standby Gas Treatment being Rendered Inoperable and Non-Functional Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000254,05000265/2022013-02 Open/Closed

[P.4] - Trending 71152B A self-revealed finding and associated non-cited violation (NCV) of very low safety significance (Green) was identified for the licensee's failure to promptly identify and correct a condition adverse to quality. Specifically, the licensee failed to take corrective actions to address identified drain line blockages and water accumulation in the main chimney, which eventually accumulated in the common discharge line of the standby gas treatment system to the point where both trains of the system could no longer fulfill their safety functions.

Failure to Follow Operations Procedures for Lowering Reactor Vessel Water Level Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000265/2022013-03 Open/Closed

[H.9] - Training 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance (Green) was identified for the licensee's failure to follow operations procedures in response to lowering reactor water level due to the 2A feedwater regulating valve (FRV)failing shut. Specifically, the licensee's alarm response procedure and abnormal operations procedure directed operators to initiate an emergency power reduction in response to the lowering reactor water level; however, the operators took different actions to try to manually control the 2B FRV. As a result, operators were driven to initiate a manual scram prior to an automatic one due to the continued lowering reactor water level.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000265/2022-002-00 LER 2022-002-00 for Quad Cities Nuclear Power Station, Unit 2, Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level 71153 Closed LER 05000254, 05000265/2022-003-00 LER 2022-003-00 for Quad Cities Nuclear Power Station, Unit 1 and 2, Both Trains of Standby Gas Treatment Inoperable due to Blockage in the Common Discharge Line 71153 Closed

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 03.04)

(1) The inspectors performed a biennial assessment of the effectiveness of the licensees problem identification and resolution program, use of operating experience, self-assessments and audits, and safety-conscious work environment.

Problem Identification and Resolution Effectiveness: The inspectors assessed the effectiveness of the licensees problem identification and resolution program in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review of the reactor core isolation cooling system.

Operating Experience: The inspectors assessed the effectiveness of the licensees processes for use of operating experience.

Self-Assessments and Audits: The inspectors assessed the effectiveness of the licensees identification and correction of problems identified through audits and self-assessments.

Safety-Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000265/2022-002-00, "Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level," ML22244A135. The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71153.
(2) LER 05000265/2022-003-00, "Both Trains of Standby Gas Treatment Inoperable due to Blockage in the Common Discharge Line," ML22244A134. The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71152B.

INSPECTION RESULTS

Assessment 71152B Based on the samples reviewed, the team concluded that the licensee's implementation of the corrective action program (CAP) was generally effective and supported nuclear safety.

Effectiveness of Problem Identification

The inspectors reviewed a large sample of issue reports, causal evaluations, audits, and NRC-identified issues to assess the licensees documentation of issues in the CAP. The inspectors ensured the issue reports were complete, accurate, and documented in a timely manner. The causal products were reviewed to ensure identification of root and contributing causes of the issues/events. The inspectors also evaluated the licensees identification of negative trends associated with human performance or equipment performance that could potentially impact nuclear safety. Finally, the inspectors reviewed NRC-identified issues to determine if prior opportunities existed to identify the problems.

Based on the samples reviewed, the team concluded that generally the licensee identified issues at a low threshold and entered these issues into the CAP. The team determined that the licensee usually entered problems into the CAP completely and accurately. However, the team noted in interviews that writing a condition report was not the default method for many when they raised safety concerns, and some individuals indicated that they had not or did not frequently write condition reports, opting to inform their supervisors instead. The team did not identify any examples of issues raised to supervision that were not captured in the CAP.

Further, all individuals indicated that they would be willing to write condition reports, as needed. However, this gap in utilizing the corrective action program to enter issues could ultimately impact the effectiveness of the licensees ability to evaluate, resolve, and trend issues, which could potentially lead to more significant concerns. The team also noted that in some audits and self-assessments performed internally and by external organizations, including the NRC, examples were identified where condition reports were not entered into the CAP for issues. These examples further supported the gap found by the inspectors during the interviews. The licensee has taken actions to evaluate the gap in AR initiation and conduct site-wide information sharing on the importance of the CAP and how to initiate issue reports.

The inspectors determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety. However, through a review of CAP evaluations (CAPEs) and root cause evaluations for impactful equipment deficiencies and failures, the inspectors did note a potential negative trend in the licensees incorporation of vendor recommendations into site maintenance procedures. The inspectors focused on issues that caused equipment failures and the identified causes of those failures. This issue is documented in this report as a Green finding.

The team also performed a 5-year review of the reactor core isolation cooling (RCIC) system issues. As part of this review, the team interviewed engineers, reviewed the system health and maintenance rule information, and reviewed selected corrective actions and condition evaluation documents. The team concluded that issues with RCIC were identified and entered into the CAP at a low threshold and were resolved in a timely manner commensurate with their safety significance. Some equipment deficiencies/failures reviewed for this system contributed to the inspectors' identification of a potential negative trend in the licensee's incorporation of vendor recommendations into maintenance practices for the system as described in the finding referenced above.

Effectiveness of Prioritization and Evaluation of Issues The inspectors reviewed items in the CAP to ensure thorough and timely evaluation of identified issues, including disposition of operability and reportability issues. Causal products were evaluated for consideration of extent of condition and cause associated with identified root and contributing causes. These products were also reviewed for consideration of potential generic implications, common cause concerns, and evaluation of previous occurrences of issues.

Based on the samples reviewed, the team determined that licensee performance was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. The station ownership committee and the management review committee meetings were generally thorough and intrusive in reviewing issues and prioritizing actions. In addition, the team observed a healthy dialogue between the members of these committees and the members challenged each other when dispositioning issues.

In general, once a degraded or non-conforming condition was identified, the CAP directed that an equipment operability or functionality review be performed. As a result, most of the samples reviewed were evaluated appropriately and in a timely manner. However, the team did identify one example of a condition report that had a less than adequate evaluation of operability of an ASME code class valve with a pinhole leak. This issue has been determined to be a minor violation and is documented in this report.

Effectiveness of Corrective Actions

The inspectors reviewed issues in the CAP to ensure appropriate classification and prioritization of the problems resolution commensurate with the safety significance of the issue. Corrective actions were assessed to ensure they were appropriately focused to correct the problem identified and to address the root and contributing causes of significant conditions adverse to quality and conditions adverse to quality. The inspectors reviewed completion of corrective actions to validate they were completed according to the action plan, in a timely manner, and were effective at addressing the issue and preventing future issues. For NRC-identified issues, the inspectors evaluated whether prior attempts by the licensee to remedy the problems were adequate.

Based on the samples reviewed, the team determined that the licensee was generally effective in corrective action implementation. Problems identified using a root cause or other cause methodologies were resolved in accordance with CAP requirements. However, the team identified several examples where corrective actions were not fully implemented to address identified deficiencies. Based on these examples, the inspectors emphasized the importance of timely resolution of issues per a prescribed plan. The inspectors identified one example of untimely identification and resolution of an issue associated with a failure of the standby gas treatment (SBGT) system and evaluated it to be of more than minor significance. It is documented in this report as a Green NCV. The inspectors also identified two other examples of less than adequate implementation of corrective actions for identified equipment deficiencies that are described in the minor performance deficiencies below:

(1) The inspectors identified a minor performance deficiency for the licensee's failure to follow work order steps for the station blackout (SBO) equipment walkdowns. Specifically, as a result of a fire on the Unit 1 isolimiter in 2020, and based on operating experience from other sites that encountered similar failures, work order steps were added to periodic walkdowns of the SBO area to include recording decibel levels near the SBO isolimiters and inverters. This data could be then tracked and trended to identify potential degradation of the components prior to failure. From a review the inspectors conducted of the seven walkdown work orders performed between 2020 to 2022, only one set of decibel levels were recorded; even though all the work orders asked for recording decibel levels. Another fire and isolimiter failure occurred on Unit 2 in 2021. By not fully implementing the work order steps for data collection, the licensee did not effectively take corrective actions from the first failure to potentially prevent or mitigate a second failure. The licensee also did not appropriately implement those corrective actions after the second failure. The inspectors discussed this issue with the licensee and the licensee captured it in the CAP program as Action Request (AR) 4525573, "NRC PI&R ID: Walkdown Data not Recorded in Entirety." The inspectors determined it was a minor issue because the corrective actions were intended to proactively identify degradation of the isolimiter prior to failure; however, the actions on their own would not have prevented future failures. The risk consequence and impact of the SBO isolimiter failures were also very low.
(2) The inspectors identified a second minor performance deficiency for the licensees failure to follow self-imposed standards in Constellation procedure, PI-AA-125, Corrective Action Program. Specifically, corrective actions developed to address a hole in the 'B' CCST did not follow the SMARTER Criteria in the CAP procedure. The inspectors reviewed the causal evaluation for the issue and corrective action plan for addressing the identified causes. The inspectors then performed walk-downs of the CCST. It was observed that the tank caulking was cracking and missing at the interface of the tank and foundation. The inspectors questioned the licensee on the implementation of the corrective actions from the CAPE since the walkdown revealed deficiencies that should have been addressed as a result of those actions. The licensee had replaced caulking around the tank in certain areas but not as a holistic replacement in response to the event. From discussions with licensee staff, it was determined that the intent of the written corrective action plan was different than what was documented in the CAPE. Also, based on the inspectors' walkdown, the actions that were taken were not fully effective at identifying degradation of the tank caulking. The licensee captured this issue in AR 4524120, "NRC PI&R ID: Caulk Missing between 'B' CCST and Foundation," and AR 4524861, "NRC PI&R ID: Change Scope of PMRQs 166690-03 and 166691-03." The inspectors determined it was a minor issue because the identified caulking deficiencies did not have an impact to the overall structural integrity of the tank to foundation boundary.

Assessment 71152B The inspectors reviewed the licensees operating experience program to ensure items are adequately evaluated for applicability, and applicable lessons learned are communicated to appropriate organizations and implemented as appropriate.

Based on the samples reviewed, the team determined that licensee's performance in the use of operating experience was generally effective. The licensee screened industry and NRC operating experience information for applicability to the station. When applicable, actions were developed and implemented to prevent similar issues from occurring. Operating experience lessons learned were communicated and incorporated into plant operations. The team observed the information being used in daily activities, such as pre-job briefs, as well as issue reviews and investigations. The team did not identify any concerns in this area.

Assessment 71152B The inspectors reviewed a sample of completed self-assessments and audits conducted by licensee personnel, corporate personnel, the nuclear oversight group, and external organizations. The products reviewed included assessments of each of the cornerstone areas and CAP specific items.

Based on the samples reviewed, the team determined that the licensee's performance of self-assessments and audits was generally effective. The licensee performed department self-assessments and nuclear oversight audits throughout the organization on a periodic basis. These self-assessments and audits were generally effective at identifying issues and enhancement opportunities at an appropriate threshold. The self-assessments and audits reviewed by the team identified issues that were not previously known, including issues within the CAP itself. The team did not identify any concerns in this area.

Assessment 71152B The team interviewed approximately 75 individuals that had varying roles and levels of responsibility within the organization. These interviews included a conversation with the sites employee concerns program manager. The team also observed the most recent nuclear safety culture review meeting and reviewed minutes from prior meetings. Finally, the team reviewed the results from the 2021 employee organizational health survey and internal audits/assessments of the sites safety culture. The team focused their questions on individuals willingness and ability to identify issues, freedom from potential retaliation for raising safety concerns, effectiveness of the CAP at resolving issues, and individual involvement and drive to ensure proper resolution of issues.

The team did not identify any impediment to the establishment of a safety conscious work environment. Individuals felt free to raise safety concerns at all levels and through various avenues without fear of retaliation. If issues were not resolved appropriately, individuals would advocate for proper resolution as needed. The staff interviewed believed that operational issues and issues with high safety significance were being appropriately addressed in a timely manner.

As mentioned in the Identification section of this report, the team noted in interviews that writing a condition report was not the default method for many when they raised safety concerns, in those cases opting to notify their supervisor instead. While some individuals indicated that they had not or did not frequently write condition reports, all individuals indicated that they would be willing to write condition reports, as needed. This gap in directly utilizing the corrective action program appeared to have roots in previous negative experiences in the CAP, a belief that issues could be resolved timelier and effectively outside of the process, and potentially a lack of support/advocacy for issues once they were outside of the individuals immediate realm of influence. This information was discussed with licensee management for further consideration in the sites efforts to address the identified gap in issue report initiation.

Failure to Incorporate Vendor Recommendations into Preventative Maintenance Procedures Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green FIN 05000265/2022013-01 Open/Closed

[P.4] - Trending 71152B A self-revealed finding of very low safety significance (Green) was identified for multiple examples of the licensee failing to incorporate vendor recommendations into preventative maintenance procedures, resulting in the failure of multiple risk-significant components.

Description:

During the 2022 Problem Identification and Resolution biennial team inspection, inspectors reviewed three examples of equipment failures and assessments that determined causes of the issues were a failure to ensure vendor recommendations were properly incorporated into preventative maintenance plans and procedures.

During a self-assessment of the instrument air system conducted in December 2020, the licensee identified that a vendor recommended action to replace the drain solenoid for the 1/2 B instrument air compressor was not incorporated into the maintenance program.

During a Unit 2 RCIC flow rate test on March 12, 2021, the pump tripped on mechanical overspeed. The cause was determined to be failure to consider vendor recommendations in the replacement frequency of the electronic governor - mechanical (EG-M).

On July 4, 2022, the Unit 2A feedwater regulating valve (FRV) failed closed resulting in a manual scram. The root cause was foreign material in the hydraulic oil in the valve servo. The licensee discovered that vendor recommendations for particulate concentration in oil additions and for replacement of the in-line filters were not incorporated into the maintenance program.

Constellation procedure ER-AA-200, Preventative Maintenance Program, Revision 6, step 4.3.3 states that "in order to help develop the Maintenance Strategy, [performance centered maintenance] PCM templates are developed by the [corporate subject matter expert] CSME based on...vendor recommendations...." Further, step 4.3.4 states that "it is the responsibility of the [site subject matter expert] SSME or Strategic Engineer to ensure that there is an effective Maintenance Strategy for all Critical and Non-Critical Components based on...vendor recommendations...." For all these examples, the licensees failure to incorporate vendor recommendations into the maintenance procedures for the equipment led to specific component failures.

Corrective Actions: For the instrument air system, the licensee created a corrective action to incorporate replacement of the drain solenoid into the maintenance work order.

For the RCIC pump, the licensee immediately replaced the EG-M and restored system operability. Another corrective action was initiated to update the PCM template to replace the EG-M within the vendor recommended frequency.

For the 2A FRV, the licensee replaced the valve internals and initiated corrective actions to update their preventative maintenance program to incorporate the vendor's recommended oil particulate values for oil changes and replacing the in-line filters on a specific frequency.

Corrective Action References: AR 4347896, AR 4509196, AR 4408543

Performance Assessment:

Performance Deficiency: The failure to incorporate vendor recommendations into preventative maintenance procedures was a performance deficiency. Specifically, Constellation procedure ER-AA-200, Preventative Maintenance Program, Revision 6, step 4.3.4 contains guidance "to ensure that there is an effective Maintenance Strategy for all Critical and Non-Critical Components based on...vendor recommendations..." However, an effective maintenance strategy, including incorporating vendor recommendations into equipment maintenance templates, was not implemented for the instrument air system, the Unit 2 RCIC EG-M, and the 2A FRV to prevent equipment failures.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, in this finding, an example was identified for the failure to replace the EG-M for the RCIC pump in the vendors recommended time frame, which affected the reliability of that system to respond to initiating events.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the issue using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, and determined that this finding was of very low safety significance, or Green. In the RCIC example, the degraded condition did represent a loss of the PRA function of a single train technical specification (TS) system, however, it was not lost for greater than its TS-allowed outage time.

Cross-Cutting Aspect: P.4 - Trending: The organization periodically analyzes information from the corrective action program and other assessments in the aggregate to identify programmatic and common cause issues. Specifically, the licensee failed to identify a trend, from an aggregate review and analysis of corrective action program evaluations and other assessments, of not incorporating vendor guidance into their preventative maintenance strategies.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Identify and Correct a Condition Adverse to Quality Resulting in Both Trains of Standby Gas Treatment being Rendered Inoperable and Non-Functional Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000254,05000265/2022013-02 Open/Closed

[P.4] - Trending 71152B A self-revealed finding and associated non-cited violation (NCV) of very low safety significance (Green) was identified for the licensee's failure to promptly identify and correct a condition adverse to quality. Specifically, the licensee failed to take corrective actions to address identified drain line blockages and water accumulation in the main chimney, which eventually accumulated in the common discharge line of the standby gas treatment system to the point where both trains of the system could no longer fulfill their safety functions.

Description:

On July 4, 2022, Quad Cities Unit 2 scrammed due to a transient in the feedwater system. In response to the scram, the standby gas treatment (SBGT) system automatically started on low reactor water level (as designed). However, the operators noted degraded and oscillating flow on the discharge side of the in-service train. Operators manually started the redundant train and it also indicated degraded and oscillating flow. Both trains were declared inoperable and unavailable, which led to Units 1 and 2 entering 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> limiting condition of operation (LCO) action statements that subsequently led to both units entering 12-hour shutdown LCOs.

During this time, operations conducted troubleshooting that identified a partial blockage in the 24-inch common discharge line from both trains of SBGT to the main chimney. The main chimney drain lines were also identified to have blockages. Data trending showed improved system performance once all the blockages were removed to the point where system flows returned to within the required technical specification (TS) flow values. The SBGT subsystems were declared operable after successful surveillance runs were performed (within the 12-hour shutdown window). The licensee also completed an operability evaluation to assess the condition of water accumulation in the common discharge line. This engineering change (EC 637081) was approved and included compensatory and corrective actions to:

1) remove the identified main chimney drain line blockages; 2) return to a monthly SBGT surveillance frequency to monitor the system operation for potential degradation (changed from every 6 months prior to the event); and 3) added a step to the surveillance procedure to collect data on the SBGT system flow damper position, which would provide indication of margin to the TS required flow rate and correlate to water accumulation in the discharge line.

In response to this event, the licensee conducted a root cause evaluation to determine the cause(s) of the water accumulation in the SBGT common discharge line. As described above, the SBGT system consists of two trains (the 1/2A and 1/2B) that share a common 24-inch discharge line that runs underground to the main chimney. Initial troubleshooting efforts identified that a partial blockage in the 24-inch common discharge line existed due to water intrusion and that blockage was the cause of the degraded system flow. Water intrusion into the SBGT system 24-inch common discharge line was determined to potentially come from two sources: 1) condensation from the main chimney area; or 2) groundwater intrusion from a flaw in the wall of the buried common discharge line pipe section. A review of historical condition reports and work orders identified multiple instances of water build-up in the main chimney due to main chimney drain line blockages with CRs dating back to 2004, and 2005. At that time, there were no work orders created or conducted to document draining of the main chimney drain lines. In 2010, work orders were created to fix the drain line blockages and the identified structural integrity issues with the main chimney that allowed water intrusion but those were never completed. Additionally, there was no initiation of periodic inspection/cleaning of these drain lines between 2010, and July 2022, when the lines had to have blockages removed as part of the response to the July 4 event. It was not recognized that not addressing the drain line blockages for prolonged periods of time would allow for the condensation occurring in the main chimney to be a significant contribution of water to the SBGT discharge line. The licensee concluded that the most likely source of the water intrusion for this event was slow accumulation of water from the main chimney area into the SBGT common discharge line.

Corrective Actions: The licensee cleared the water accumulation in the 24-inch common discharge line and the blockages and drained water from the main chimney drain lines. The licensee also completed the operability evaluation for continued assurance of operability of the system with compensatory measures in place. Additional corrective actions included performing periodic checks of the main chimney drains to remove what is currently considered the primary source of water to the SBGT discharge line. The second corrective action was to identify and isolate any source of water intrusion into the SBGT underground discharge line. Further corrective actions included a periodic inspection and removal of water from the SBGT system underground section of the common discharge line to the main chimney and enhancements to the SBGT surveillance procedures.

Corrective Action References: AR 4509198, Both Trains of SBGT not Producing Required Flow

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to identify and correct a condition adverse to quality associated with drain line blockages and water accumulation in the main chimney, which eventually accumulated in the common discharge line of the SBGT system, was a performance deficiency. Specifically, the failure to correct the condition led to the slow accumulation of water from the main chimney area into the SBGT common discharge line and affected the safety function of both trains of the system.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the SSC and Barrier Performance attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, failure to identify and correct water accumulation in the SBGT common discharge line led to emergent inoperability and non-functionality of the system when it was required to perform in service.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the issue using IMC 0609, Appendix A, Exhibit 3, Barrier Integrity Screening Questions, and determined that this finding was of very low safety significance, or Green, by answering yes to section D, Control Room, Auxiliary, Reactor, or Spent Fuel Pool Building, question 1, does the finding only represent a degradation of the radiological barrier function for theSBGT system? The degradation of the SBGT system for this issue could not have resulted in a potential substantial overexposure and was not expected to have an impact on the large early release frequency (LERF).

Cross-Cutting Aspect: P.4 - Trending: The organization periodically analyzes information from the corrective action program and other assessments in the aggregate to identify programmatic and common cause issues. Specifically, the licensee failed to identify a potential trend of degradation and issues related to the structural integrity of the main chimney. The inspectors identified multiple condition reports and work orders that were generated in the corrective action program from 2004, to the event in 2022 that documented degraded structural integrity of the main chimney and drain lines. The work orders that were generated for the condition reports were still open at the time of the event to address the identified deficiencies. Also, sufficient data was not collected during the surveillance runs of the SBGT system to identify a degraded trend in the system performance. This was noteworthy during this time frame because the surveillance test frequency was extended from monthly to every 6 months with no additional monitoring or data collection mechanisms in place to assure the surveillance frequency change was appropriate.

Enforcement:

Violation: Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected.

Contrary to the above, from September 2004 until July 4, 2022, the licensee failed to promptly identify and correct a condition adverse to quality. Specifically, the licensee failed to take corrective actions to address water intrusion into the SBGT line from the identified drain line blockages and water accumulation in the main chimney, which eventually accumulated in the common discharge line of the SBGT system to the point where both trains of the system could no longer achieve its technical specification required flow rates. This was revealed when the system was automatically actuated in response to a plant transient.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Minor Violation 71152B Minor Violation: The inspectors identified a minor violation for the licensees failure to follow Constellation procedure, OP-AA-108-115, Operability Determinations. Specifically, while reviewing condition report AR 4432559 for a pinhole leak on the 2-1402-72, Unit 2 core spray keep fill discharge valve, the inspectors noted that the component was determined to be operable but non-functional. The licensee determined the ECCS keep fill system could not perform its function because the identified leak on the valve was unisolable. However, the licensee only considered the effect this would have on the core spray system operability and did not appropriately review the operability of the valve, an ASME code class component, per the applicable ASME code requirements. Constellation procedure, OP-AA-108-115, Operability Determinations, Attachment 3, establishes the requirements for conducting operability determinations. This attachment specifically provides guidance for conducting operability reviews of code class components when various structural integrity issues are identified. In response to the identified leak, the licensee did enter the applicable LCOs (per the TRM) to conduct repairs to the valve that day.

Screening: The inspectors determined the performance deficiency was minor. The inspectors determined the performance deficiency was minor. Specifically, the inspectors screened the performance deficiency in accordance with Inspection Manual Chapter 0612, Appendix B, and despite the operability evaluation screening the component as operable, the system was still promptly isolated and declared inoperable under TRM requirements for the ECCS keep fill system. The valve was repaired and restored to operable within the LCO-allowed outage time.

The licensee entered this issue into their CAP as AR 4527063, NRC PI&R ID Issue Report 4432559 Operability Basis.

Enforcement:

Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires in part that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, the licensee failed to follow procedure OP-AA-108-115, Operability Determinations, when assessing a leak on the Unit 2 core spray keep fill discharge valve, 2-1402-72. This failure to comply with 10 CFR 50, Appendix B, Criterion V, constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Failure to Follow Operations Procedures for Lowering Reactor Vessel Water Level Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000265/2022013-03 Open/Closed

[H.9] - Training 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance (Green) was identified for the licensee's failure to follow operations procedures in response to lowering reactor water level due to the 2A feedwater regulating valve (FRV)failing shut. Specifically, the licensee's alarm response procedure and abnormal operations procedure directed operators to initiate an emergency power reduction in response to the lowering reactor water level; however, the operators took different actions to try to manually control the 2B FRV. As a result, operators were driven to initiate a manual scram prior to an automatic one due to the continued lowering reactor water level.

Description:

On July 4, 2022, at 1:03 a.m. Quad Cities Unit 2 was operating at 100 percent power when the 2A feedwater regulating valve (FRV) failed in the fully closed position, causing a lowering reactor vessel water level. The FRV is designed with a lock-up function that prevents it from moving in the event of a failure based on position demand/deviation. However, that function has a time delay, and the valve was fully closed before the lock-up occurred. Main control room operators took manual control of the feedwater system and attempted to raise reactor water level with the 2B FRV to try to maintain it above the automatic low-level scram setpoint. Approximately 55 seconds later, reactor vessel water level reached the lower limit set by the operations response procedure and directed by the unit supervisor. Subsequently, operators initiated a manual scram. All control rods inserted, and the reactor shutdown. The licensee reported this event to the NRC under Event Notification 55975 and Licensee Event Report 2022-002-00. The licensee replaced affected components of 2A FRV and returned the unit to power on July 6, 2022.

The licensee conducted a root cause evaluation for this event. The root cause of the FRV failure was foreign material partially or completely blocking the hydraulic oil flow internal to a servo valve inside the FRV. A contributing cause to this failure was determined to be failure of the control room operators to perform an emergency power reduction in response to the lowering reactor vessel water level. This emergency power reduction could have reduced reactor power rapidly enough to a level that could be maintained with just one FRV (the 2B in this case). This particular failure mechanism of the FRV, going fully closed without locking up first, was previously unrecognized as a possible failure mode by the licensee. Because of that, through post-transient data review and interviews, it was identified that operators were unfamiliar with diagnosing the event properly as it presented itself. This led them to not take the appropriate actions to mitigate the transient within the time frame available before the transient became unrecoverable and a manual scram was required.

As part of reviewing the licensees event report and the root cause evaluation, the inspectors reviewed the operators actions during the event to determine if they were appropriate and if there were any human performance issues that contributed to the event. The main control room received alarm, Reactor Vessel Low Level, after the 2A FRV went fully closed. Quad Cities alarm response procedure, QCAN 901(2)-5, F-8, Reactor Vessel Low Level, is the operations implementing procedure for steps to respond to this alarm. The operator actions in this procedure provide reactor scram criteria (if level cannot be maintained >11), direct operators to validate the low-level alarm is valid (level is actually <26), and then reduce reactor recirculation pump speeds (emergency down power) as necessary to try to maintain level between 11 and 44. From the inspectors review of the information, the operators appeared to not reference this alarm response procedure and move directly into the abnormal operating procedure for the conditions present. Quad Cities procedure, QCOA 0201-09, Reactor Low Water Level, directs operators to perform the following Immediate Operator Actions:

C.1 Perform one or more of the following actions, based on assessment of the situation:

  • Transfer from 3-element to 1-element control.
  • Place online feedwater regulators in MANUAL to control Reactor water level.

C.2 Initiate Emergency Power Reduction as necessary to maintain Reactor water level between +11 inches and +44 inches.

In this transient, the operators only attempted to control reactor water level through manual control of the remaining FRV (2B). When this transient was modeled in the Quad Cities simulator post-event, an emergency power reduction could have reduced reactor power to within the capacity of a single FRV and prevented a reactor scram if performed within 30 seconds of the first alarm.

Corrective Actions: To address the contributing cause of operator performance, the licensee revised abnormal operating procedure, QCOA 0201-09, to place the step to reduce power first in the immediate actions section. The licensee also revised operator training to include similar scenarios and emphasize the importance of reducing power.

Corrective Action References: AR 4509196, 2A FRV Failed Close, Unit 2 Manual Scram Inserted on Low Reactor Water Level

Performance Assessment:

Performance Deficiency: The failure to follow the steps of the alarm response procedure and the abnormal operating procedure to perform an emergency power reduction in response to lowering reactor vessel water level was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the failure of operators to initiate an emergency power reduction in response to the 2A FRV failing closed resulted in the necessity to manually scram the reactor due to lowering water level.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the issue using IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, and determined that this finding was of very low safety significance (Green) because although it caused a scram, it did not also result in the loss of mitigating equipment.

Cross-Cutting Aspect: H.9 - Training: The organization provides training and ensures knowledge transfer to maintain a knowledgeable, technically competent workforce and instill nuclear safety values. Specifically, this failure mechanism of the FRV, going fully closed without locking up first, was previously unrecognized as a possible failure mode by the licensee. Because of that, operators misdiagnosed this event by not properly assessing all available indications. This led them to not take the appropriate actions to mitigate the transient within the time frame available before the transient became unrecoverable and a manual scram was required.

Enforcement:

Violation: Quad Cities Technical Specification Section 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 5 addresses Procedures for Abnormal, Off-normal, or Alarm Conditions.

The licensee established Quad Cities alarm response procedure QCAN 901(2)-5, F-8, Reactor Vessel Low Level, Revision 11, to address plant conditions associated with a low water level in the reactor vessel. This includes Step 3 which directs operators to reduce reactor recirculation pump speeds as necessary to try to maintain water level between 11 and 44 prior to reaching the level threshold for initiating a manual scram. Quad Cities abnormal operating procedure QCOA 0201-09, Revision 28 (in effect at the time), Step C.2 of the Immediate Operator Actions section, also directs operators to initiate an emergency power reduction as necessary to maintain reactor water level between 11 and 44.

Contrary to the above, on July 4, 2022, the licensee failed to implement either Step 3 of QCAN 901(2)-5, F-8, or Step C.2 of QCOA 0201-09 to initiate an emergency power reduction in response to lowering reactor vessel water level. As a result, operators needed to initiate a manual scram for Quad Cities Unit 2 based on reactor water level continuing to lower.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 7, 2022, the inspectors presented the biennial problem identification and resolution inspection results to Mr. B. Wake, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1015222

Main Stack Leaking - Icicle Formation South Side

01/12/2010

2633585

OPEX Review - Confined Space

03/01/2019

2710067

Dresden Station Blackout Failure Analysis Report

Applicable to QDC

08/30/2016

318706

Chimney has Water Leaking Out

03/30/2005

4030236

Base AR for Operating Experience Reviews

2017-2019

4104474

QDC Review of Hatch OE, 4kV Breaker Failed to Close

2/15/2018

4116642

U2 1C Inboard MSIV Slow to Close during QCOS 0250-04

03/19/2018

280384

NOS Finding: FP Surveillance Program

09/18/2019

4301438

Cyber Security Workflows and Additional Steps

2/04/2019

4310554

U1 SBO Isolimiter Fire

01/16/2020

22001

Base AR to Review Operating Experience

20-2025

24419

Intentionally Abbreviated Maint. on U1 HPCI Converter

03/06/2020

4335396

Unit 2 Main Generator Negative Sequence

04/14/2020

4356663

NOSA-QDC-20-09 QDC External Event and Emergency

OPS Audit

09/07/2020

4359448

NOS ID: Detached Conduit Support on East Ext. RB Wall

by SBO

07/28/2020

4359461

NOS ID: Oil Leak on 2A SBO DG Engine Near Lube Oil

Strainer

07/28/2020

4359474

NOS ID: Oil Leak from Engine Head Cover on U2 SBO DG

07/28/2020

4359480

NOS ID: Oil Leak on 2A SBO DG Engine Near Turbo Filter

Assembly

07/28/2020

4368333

Unit 2 RCIC Pump Trip during Flow Rate Test

09/09/2020

4369686

NRC Information Notice 2020-02 FLEX Diesel Operational

Challenges

09/15/2020

4380192

No Response to Quad EP NRC Practice Exercise

Feedback

10/28/2020

4391803

NRC IN 2020-04: Fire Protection Main Yard Buried Cast

Iron Piping Failures

2/17/2020

71152B

Corrective Action

Documents

4395536

Issues Identified During Installation of U2 Tip 2

01/12/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4396932

Ineffective Effectiveness Review from EFR 4280384-21

01/07/2021

4399868

Unit Two Station Blackout Isolimiter Fire

03/05/2021

4408543

Unit 2 RCIC Overspeed during Quarterly Surveillance

03/12/2021

4410299

Trip of the Reserve Auxiliary Transformer, T-12, during

Q1R26

03/19/2021

4410615

'B' Contaminated Condensate Storage Tank NDE Results

03/22/2021

4411301

NRC Inspector Questions Related to Carousel

03/24/2021

23071

NRC Information Notice 2021-01: Design Bases Lessons

Learned for Power Operated Valves

05/11/2021

28172

RCIC Isolated during Performance of MA-QC-IM-1-13201

06/08/2021

4432559

Pinhole Leak on the Core Spray 2-1402-72 Valve

06/30/2021

4435864

NOSA-QDC-21-05 Quad Cities Corrective Action Program

Audit

10/18/2021

4438662

NRC ID: Broken Locking Pin on Bottom of Door to U2 EDG

08/03/2021

4439282

NRC ID: Update to IR 4438662

08/04/2021

4445201

RCIC Isolation during Performance of MA-QC-IM-1-13201

09/08/2021

4466003

Pinhole Leaks Found at Weld for 0-5799-381 'B' HVAC

Train

2/11/2021

4479617

1/2 Emergency Diesel Generator Cooling Water Pump Not

Starting

2/21/2022

4486861

Unit 1 Fuel Failure

03/23/2022

4506342

1/2 EDGCWP Failed to Swap to Bus 18 from Bus 28

06/19/2022

4509196

2A FRV Failed Close, Unit 2 Manual Scram Inserted on

Low Reactor Water Level

07/04/2022

4509198

Both Trains of SBGT Not Producing Required Flow

07/04/2022

4517997

1-1705-16A Fuel Pool Rad Monitor Trending Upward

08/21/2022

4518521

Unable to Remove Cap on Line 2-10546B-1-L

08/24/2022

4518524

Unable to Achieve Full Isolation on 2B RHRSW Pump

08/24/2022

4518585

U2 TIP Machine 2 Channel 7 Failure to Insert to Top of

Core

08/24/2022

4518621

EO ID: RB Vents Outlet Isolation Valve Open Light Out

08/24/2022

4518783

NRC NCV 2022-002-01 IR Not Initiated for ERV

08/25/2022

4518872

EO ID: Light Pack Stuck in Fast Charge Mode

08/25/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4519031

'A' Fire Diesel Day Tank Level FAS Failure

08/26/2022

4519640

EO ID: Door 21, Aux Electric Room to Trackway, Knob

Loose

08/30/2022

23409

1B FRV Actual Position vs. Demand Position Deviation

09/10/2022

24991

Improper RP Self Brief Performed for Non-Self-Brief Area

09/27/2022

24081

NRC PI&R ID Functional Basis Improvement Opportunities

09/22/2022

24120

NRC PI&R ID: Caulk Missing Between 'B' CCST and

Foundation

09/22/2022

24723

NRC PI&R ID: Insufficient Detail to AMP B.1.20

Walkdowns

09/26/2022

24861

NRC PI&R ID: Change Scope of PMRQs 166690-03 and

166691-03

09/27/2022

25573

NRC PI&R ID: Walkdown Data Not Recorded in Entirety

09/29/2022

25854

NRC PI&R ID: Safety Culture Assessments Not in

Passport

09/30/2022

26462

Cracking in Weather Seal Between B CCST and

Foundation

10/03/2022

Corrective Action

Documents

Resulting from

Inspection

27063

NRC PI&R ID: Issue Report 4432559 Operability Basis

10/05/2022

M-22

Diagram of Service Water Piping Diesel Generator Cooling

Water

AB

M-3215

System Pressure Test Walkdown Isometric Residual Heat

Removal Service Water System

M-50 Sheet 1

Diagram of the Reactor Core Isolation Cooling Piping

M-51

Diagram of Radioactive Waste Disposal Piping Sheet 1

M-78

Diagram of Core Spray Piping

BK

Drawings

PMID 1846210-2

Intercooler Solenoid Valve

Presentation - Importance of the Corrective Action

Program (CAP)

08/04/2022

QDC-0-2022-0153

Risk Assessment - FRV Servo Valve Vulnerability

QDC-0-2022-0156

Simple Issue Risk Assessment - FRV Hydraulic Skid

Particulate

Repair/Replacement

Plan

ASME Section XI Repair Replacement Plan Per

ER-AA-330-009 for the RHR System Piping

Miscellaneous

System Health

Unit 1 and Unit 2 Reactor Core Isolation Cooling System

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Report

Vendor

Recommendation

00035167-01

RCIC EG-M Control Box

VTIP 0355, Volume

Digital EHC, GEK 111030

4017529

NRC Concerns Associated with 1-0203-2D MSIV Actuator

06/01/2017

4392826

Minor Freon Leak from 0-5799-2152 RCU Charging

Connection

2/30/2020

630927

Evaluate the Effect of the High Pressure Coolant Injection

(HPCI) Signal Converter Span Shift on the Output to the

Motor Gear Unit

634416

U1 HPCI Failed to Achieve 5000 GPM at Elevated

Discharge Pressure (1220 PSIG) during Performance of

QCOS 2300-27, Step H.63

635854

HPCI Booster Pump Recirc Line 2-23108B-1/2" Through

Wall Leak

EC 619951

Evaluate the Possible Drift in Closure Timing of

MSIV 1-0203-2D

0-3

EC 621198

Outboard MSIVs May Experience Slower Closure Times

EC 632531

Piping Line 1-3958-6" Through Wall Leak

& 1

EC 635781

N-513 Evaluation for Line 2-23018B-1/2" Through Wall

EC 636103

Low Thickness Readings on the RHRSW 1-1001-65D LP

Discharge Elbow

& 1

Operability

Evaluations

EC 637081

Water Accumulation in SBGT 24-inch Common Discharge

Line

CC-AA-101

Engineering Change Requests

CC-AA-103-1001

Design Resource Manual

CC-AA-204

Control of Vendor Equipment Manuals

CC-AA-256-103

Cyber Security Requirements for Disposal of Digital Based

Systems or Components

ER-AA-200

Preventative Maintenance Program

Procedures

OP-AA-101-113-

1001

Station Event Free Clock (EFC) Program

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-108-115

Operability Determinations (CM-1)

PI-AA-115

OPEX Review of ICES

PI-AA-115-1003 Att

Quad City Review of ICES

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

PI-AA-125-1006

Investigation Techniques Manual

PI-AA-126-1001-F-

Self Assessment

QCAP 1500-01

Administrative Requirements for Fire Protection

QCOA 0201-09

Reactor Low Water Level

QCOS 1300-05

RCIC Pump Operability Test

QCOS 6600-43

Unit 1/2 Emergency Diesel Generator Load Test

WA-AA-106

Work Screening and Processing

WC-AA-101

Online Work-Control Process

WC-AA-106

Work Screening and Processing

WC-AA-120

Preventative Maintenance (PM) Database Revision

Requirements

4357127

Self-Assessment: Chemistry Instrumentation

2/11/2020

4363906

Instrument Air System Self-assessment and Audit

01/22/2021

4386034

Self-Assessment: Off-Year NRC PI&R Assessment of the

CAP

10/29/2021

4388149

Pre 71111.11

10/21/2021

4393127

Self-Assessment Clearance and Tagging

11/18/2021

4393132

Reactivity Management Performance

09/30/2021

4393721

Self-Assessment: Foreign Material Exclusion Program

2/17/2021

4439785-12

Biennial Fleet Safety Culture Assessment - Quad Cities

Station

10/15/2021

Self-Assessments

4468590

Pre-PI&R Readiness Assessment

06/30/2022

Work Orders

1301851

Main Chimney Leaking-Clean Drain Line

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1302969

Action Recommended to Address the Water in the

Chimney

1357005

Drain Line from Chimney Loop Seal is Blocked

4771766

Ops PMT for U2 Tip Detector for Machine #2

2/03/2022

4888781

CCST External Inspection

5102022

Pin Hole Leaks 0-5799-381 B HVAC Train

215080

OPS PMT Repair Leak in Line 2-23108B-1/2"

08/03/2022

OP-AA-103-102-

1001

Strategies for Successful Transient Mitigation

QCAN 901(2)-5 F-8

Reactor Vessel Low Level

71153

Procedures

QCOA 0201-09

Reactor Low Water Level

28