IR 05000254/2004005

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IR 05000254-04-005, IR 05000265-04-005 on 04/01/2004-06/30/2004 for Quad Cities Nuclear Power Station, Units 1 & 2; Event Followup
ML042030148
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 07/20/2004
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-04-005
Download: ML042030148 (36)


Text

uly 20, 2004

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000254/2004005; 05000265/2004005

Dear Mr. Crane:

On June 30, 2004, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on July 6, 2004, with Mr. Perito and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, there was one self-revealed finding of very low safety significance (Green). This finding was not subject to NRC enforcement action since the finding involved non-safety related equipment. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket Nos. 50-254; 50-265 License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 05000254/2004005; 05000265/2004005 w/Attachment: Supplemental Information

REGION III==

Docket Nos: 50-254; 50-265 License Nos: DPR-29; DPR-30 Report No: 05000254/2004005; 05000265/2004005 Licensee: Exelon Nuclear Facility: Quad Cities Nuclear Power Station, Units 1 and 2 Location: 22710 206th Avenue North Cordova, IL 61242 Dates: April 1 through June 30, 2004 Inspectors: K. Stoedter, Senior Resident Inspector M. Kurth, Resident Inspector J. House, Senior Radiation Specialist T. Ploski, Senior Emergency Preparedness Inspector R. Ganser, Illinois Emergency Management Agency Approved by: M. Ring, Chief Branch 1 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000254/2004005, 05000265/2004005; 04/01/2004-06/30/2004; Quad Cities Nuclear

Power Station, Units 1 & 2; Event Followup.

This report covers a 3-month period of baseline resident inspection and announced baseline inspections on emergency preparedness and radiation protection. The inspection was conducted by Region III inspectors and the resident inspectors. One Green finding was identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A. Inspector-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green.

A finding of very low safety significance was self-revealed when the Unit 2 main turbine and reactor automatically tripped during thrust bearing wear detector testing.

The turbine trip was a result of the licensees failure to implement the thrust bearing wear detector test program as described in the vendor manual. The inspectors determined that the licensee had modified their test program to gain efficiencies in plant operation, work control, and radiation protection. However, the licensee did not recognize that the increased efficiencies also increased the likelihood of a plant transient during thrust bearing wear detector testing.

This finding was more than minor because it was viewed as a precursor to a significant event (a transient). This finding was of very low safety significance because Unit 2 responded to the turbine trip and reactor trip as designed and all mitigating systems equipment was available following the reactor trip. The finding was not considered a violation of regulatory requirements since the main turbine thrust bearing wear detector was a non-safety related component (Section 4OA3.2).

Licensee-Identified Violations

No findings of significance were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at 85 percent power during the inspection period due to ongoing extended power uprate concerns. Operations personnel performed planned power reductions on April 25, May 30, June 19 and 20, to complete required control rod pattern adjustments, control rod scram time testing, main turbine surveillance testing, or load following.

Unit 2 also operated at or near 85 percent power due to extended power uprate concerns. On April 7 operations personnel increased Unit 2 reactor power to approximately 96 percent for additional extended power uprate data collection. Control room personnel restored Unit 2 reactor power to 85 percent after performing a load reduction and a control rod pattern adjustment. Operations personnel performed additional planned power reductions on April 1, May 23, June 19 and 20, to complete required control rod pattern adjustments, control rod scram time testing, main turbine surveillance testing, or load following.

On June 28 an Unusual Event was declared for both units due to seismic activity (4.5 magnitude on the Richter scale) in central Illinois. Although the seismic activity was not recorded by the licensees seismic monitor, or felt in the control room, security personnel reported feeling the tremor. The Unusual Event was terminated after confirming that the seismic event had no impact on plant operation, completing plant inspections, and exiting the seismic event procedure.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors performed a review of the following equipment to assess its ability to operate under adverse weather conditions:

  • Various plant heat exchangers and temperature control valves.

This review consisted of walking down in-plant and switchyard equipment with engineering personnel and interviewing operations, maintenance, and engineering personnel regarding the health of each system or piece of equipment. The inspectors reviewed condition reports, maintenance work requests and work orders, system and component health reports, and operating experience reports for potential issues that could impact the ability of this equipment to perform its function during adverse weather situations. The inspectors also reviewed any applicable operational decision making documents to ensure that continued plant operation with known material condition deficiencies was acceptable.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following risk-significant mitigating systems equipment during times when the equipment was of increased importance due to redundant systems or other equipment being unavailable:

  • 1/2 Diesel Generator Cooling Water Pump.

The inspectors utilized the valve and breaker checklists listed at the end of this report to verify that the components were properly positioned and that support systems were configured as required. The inspectors examined the material condition of the components and observed equipment operating parameters to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and condition reports associated with each system to verify that those documents did not reveal issues that could affect the equipment inspected. The inspectors also used the information in the appropriate sections of the Updated Final Safety Analysis Report to determine the functional requirements of the systems.

b. Findings

No findings of significance were identified.

.2 Complete Walkdown

a. Inspection Scope

During the weeks of May 17 and 31, 2004, the inspectors performed a complete walkdown of the accessible portions of the Unit 1 and 2 residual heat removal service water systems. The residual heat removal service water systems were selected due to their high safety-significance and risk-significance. The inspection consisted of the following activities:

  • a review of plant procedures (including selected abnormal and emergency procedures), drawings, Technical Specifications, and the Updated Final Safety Analysis Report to determine the proper system alignment and the systems licensing basis;
  • a review of outstanding maintenance work requests to determine items in need of repair;
  • a review of outstanding or completed temporary and permanent modifications to the system; and
  • an electrical and mechanical walkdown of the system to verify proper alignment, component accessibility, availability, and condition.

The inspectors also reviewed selected issues documented in condition reports to verify that the issues were appropriately addressed.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors performed routine walkdowns of accessible portions of the following risk significance fire zones:

  • Fire Zone 6.1.B - Unit 1 Turbine Building Battery Switchgear Room;
  • Fire Zone 8.1 - Turbine Oil Storage Area;
  • Fire Zone 8.2.2.1 - Unit 2 Control Rod Drive Pump Area;
  • Fire Zone 8.2.7.E - Unit 2 Turbine Building North Mezzanine Floor;
  • Fire Zone 8.2.8.E - Unit 2 Turbine Building Main Turbine Floor; and
  • Fire Zones 8.2.10 and 14.1.1 - Unit 1 Turbine Building Fan Floor.

The inspectors verified that transient combustibles were controlled in accordance with the licensees procedures. During a walkdown of each fire zone, the inspectors observed the physical condition of fire suppression devices and passive fire protection equipment such as fire doors, barriers, penetration seals, and coatings. The inspectors also observed the condition and placement of fire extinguishers and hoses against the Pre-Fire Plan fire zone maps.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors conducted an annual review of the licensees external flooding procedures and analyses. The review included discussing the information with operations, maintenance, engineering, and security personnel to confirm that the actions could be accomplished within the time specified in the documents; verifying that flooding-related equipment was readily available, in the specified location, appropriately labeled, and in good material condition; ensuring that preventive maintenance tasks on external flooding related equipment were completed; and verifying that flooding problems entered into the corrective action program were adequately addressed.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

On April 19 and June 14, 2004, the inspectors observed operations crews in the simulator. The April 19 scenario consisted of a reactor pressure vessel instrument failure, the loss of Motor Control Center 15-2, a steam leak inside containment, an anticipated transient without scram, and the need to flood the reactor pressure vessel.

In the June 14 scenario, operations personnel were challenged by a simulated circulating water system rupture, the loss of the feedwater system, the loss of all high pressure injection systems, and the need to emergency depressurize the reactor vessel in order to restore water level.

The inspectors evaluated crew performance in the areas of:

  • clarity and formality of communications;
  • ability to make timely actions in the safe direction;
  • prioritization, interpretation, and verification of alarms;
  • procedure use;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • group dynamics.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:

The inspectors verified that the crews completed the critical tasks listed in the above scenarios. The inspectors verified that the evaluators effectively identified crews requiring remediation and appropriately indicated when removal from shift activities was warranted. Lastly, the inspectors observed the licensees critique to verify that weaknesses identified during these observations were noted by the evaluators and discussed with the respective crews.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees handling of performance issues and the associated implementation of the maintenance rule (10 CFR 50.65) to evaluate maintenance effectiveness for the systems listed below:

  • Source Range and Intermediate Range Monitoring Instrumentation (Function Z0750); and

These systems were selected based on them being designated as risk significant under the maintenance rule; being in increased monitoring (maintenance rule category a(1) group); or due to a work practice, reliability, or common cause issue that impacted system performance.

The inspectors assessed system performance and maintenance work practices by reviewing system health reports, condition reports, apparent cause reports, root cause reports, common cause reports, functional failure determinations, and corrective action effectiveness reviews. The validity of system specific maintenance rule performance criteria was evaluated by comparing the performance criteria to probabilistic risk assessment and industry performance information. Lastly, the inspectors reviewed the licensees maintenance rule scoping by comparing the scoping information to the design basis.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the documents listed in the List of Documents Reviewed section of this report to determine if the risk associated with the activities listed below agreed with the results provided by the licensees risk assessment tool. In each case, the inspectors conducted walkdowns to ensure that redundant mitigating systems and/or barrier integrity equipment credited by the licensees risk assessment remained available. When compensatory actions were required, the inspectors conducted inspections to validate that the compensatory actions were appropriately implemented.

The inspectors also discussed emergent work activities with the shift manager and work week manager to ensure that these additional activities did not change the risk assessment results. The activities inspected included:

  • Work Week April 5 through 10, including planned maintenance on the Unit 2 residual heat removal system and the 2B reactor building closed cooling water system;
  • Work Week April 12 through 16, including planned vibrational testing of the reactor protection system reactor water level instrumentation;
  • Work Week May 3 through 7, including planned maintenance on the Unit 2 emergency diesel generator and diesel generator cooling water pump;
  • Work Week May 10 through 14, including planned maintenance on the Unit 1 125 Vdc system and the Unit 1 station blackout diesel generator;
  • Work Week May 17 through 22, including planned maintenance on the Unit 2 high pressure coolant injection system and the 2A reactor building closed cooling water system; and

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Evolutions

.1 Extended Power Uprate Testing and Data Collection

a. Inspection Scope

On April 7, 2004, the licensee momentarily increased Unit 2 reactor power from 85 percent (100 percent power level prior to extended power uprate) to 96 percent to collect plant data for an extended power uprate vibration analysis. The data collected included various vibration readings on systems and components, pressure and flow readings from various steam and water systems, reactor vessel water level readings, and moisture carryover information. The inspectors observed portions of the operators performance during the power ascension to verify that the appropriate procedures were prescribed and implemented. In addition, the inspectors verified that the operators completed several surveillance test procedures at the increased power levels.

b. Findings

No findings of significance were identified.

.2 Seismic Event

a. Inspection Scope

On June 28, 2004, at 1:10 a.m. (CST) a seismic event of magnitude 4.5 occurred in central Illinois. Although the operators did not feel the seismic activity in the control room, the earthquake was felt by security personnel. As a result, the shift manager declared an Unusual Event in accordance with Emergency Action Level HU4, Natural or Destructive Phenomena Inside the Protected Area. During the time of the seismic event both units were operating at 85 percent power.

The inspectors responded to the station and verified that operators implemented the appropriate procedures and conducted plant walkdowns to verify that no earthquake damage had occurred. Security personnel performed visual inspections outside the vital area and identified no damage. The inspectors also conducted site walkdowns, both inside and outside the vital area, and independently verified no observable earthquake damage.

The shift manager terminated the Unusual Event after confirming that the seismic event had no impact on plant operation, completing the plant inspections, and exiting the seismic event procedure.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors assessed the following operability evaluations or condition reports associated with equipment operability issues:

  • 1A Core Spray System Minimum Flow Valve Did Not Perform as Expected (Condition Report 208670);
  • Minimum 345 kV Switchyard Voltage Not Modeled in State Estimator Program (Condition Report 212837).

The inspectors reviewed the technical adequacy of the evaluations against the Technical Specifications, Updated Final Safety Analysis Report, and other design information; determined whether compensatory measures, if needed, were taken; and determined whether the evaluations were consistent with the requirements of LS-AA-105, Operability Determination Process, Revision 0.

In addition, the inspectors reviewed selected issues that the licensee entered into its corrective actions program to verify that identified problems were being entered into the program with the appropriate characterization and significance.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds

a. Inspection Scope

The inspectors assessed the following three operator workaround issues to determine the potential effects on the functionality of the corresponding mitigating systems:

  • OWA 04-008, Unit 2 Station Blackout Diesel Generator has extremely poor voltage control; and
  • Cumulative Review of all Operator Workarounds.

During these inspections, the inspectors reviewed the technical adequacy of the workaround documentation against the Updated Final Safety Analysis Report and other design information to assess whether the workaround conflicted with any design basis information. The inspectors compared the information in abnormal or emergency operating procedures to the workaround information to ensure that the operators maintained the ability to implement important procedures when needed. Multiple entries into the corrective action program were also reviewed to ensure that the operator workarounds had been entered into this process.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post maintenance testing activities listed below during the inspection period:

  • The performance of QCOS 6600-10, 1/2 Diesel Vent Fan Auto-Transfer Logic Test, following planned maintenance on the Unit 1/2 emergency diesel generator;
  • The performance of MA-MW-773-045, Nuclear Operational Analysis Department High Potential Testing, following replacement of the Unit 2 main power transformer;
  • The performance of QCOS 1400-01, Quarterly Core Spray System Flow Rate Test, following corrective maintenance on the 1A core spray system;
  • The performance of QCOS 6600-06, Diesel Generator Cooling Water Pump Flow Rate Test, following preventive maintenance on the Unit 2 diesel generator cooling water pump.

For each post maintenance activity selected, the inspectors reviewed the Technical Specifications and Updated Final Safety Analysis Report against the maintenance work package to determine the safety function(s) that may have been affected by the maintenance. Following this review the inspectors verified that the post maintenance test activity adequately tested the safety function(s) affected by the maintenance, that acceptance criteria were consistent with licensing and design basis information, and that the procedure was properly reviewed and approved. When possible, the inspectors observed the post maintenance testing activity and verified that the structure, system, or component operated as expected; test equipment used was within its required range and accuracy; jumpers and lifted leads were appropriately controlled; test results were accurate, complete, and valid; test equipment was removed after testing; and any problems identified during testing were appropriately documented. The inspectors also performed a condition report word search to ensure that issues identified during the performance of post maintenance testing were being entered into the corrective action process as appropriate.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed surveillance testing activities and/or reviewed completed surveillance test packages for the tests listed below:

The inspectors verified that the structures, systems, and components tested were capable of performing their intended safety function by comparing the surveillance procedure or calibration acceptance criteria and results to design basis information contained in Technical Specifications, the Updated Final Safety Analysis Report, and licensee procedures. The inspectors verified that each test or calibration was performed as written, the data was complete and met the requirements of the procedure, and the test equipment range and accuracy were consistent with the application by observing the performance of the activity. Following test completion, the inspectors conducted walkdowns of the associated areas to verify that test equipment had been removed and that the system or component was returned to its normal standby configuration.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed documentation for the following temporary configuration change:

  • Temporary Modifications 348495 (Unit 1) and 348461 (Unit 2); Installation of Turbine Thrust Bearing Wear Detector Trip Bypass Circuitry.

The inspectors assessed the acceptability of this temporary configuration change by comparing the 10 CFR 50.59 screening and evaluation information against the Updated Final Safety Analysis Report and Technical Specifications. The comparisons were performed to ensure that the new configuration remained consistent with design basis information. The inspectors reviewed the modification to ensure that installation instructions were clear, the modification would operate as expected, modification testing was appropriate, and that operation of the modification did not impact the operability of any interfacing systems. The inspectors also reviewed condition reports associated with the temporary modification process to ensure that previously identified problems were not repeated.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

.1 Review of Simulator Drill

a. Inspection Scope

The inspectors observed an operations crew perform an emergency preparedness simulator drill on April 19. The focus of the inspection activities was to note any weaknesses or deficiencies in the drill performance, ensure that the licensees evaluators noted the same items, and verify that the licensee entered these items into their corrective action program. The inspectors placed emphasis on observations regarding event classification, notifications, protective action recommendations, and site evacuation and accountability activities. As part of this inspection, the inspectors reviewed the simulator scenario listed at the end of this inspection report and attended the licensees drill critique.

b. Findings

No findings of significance were identified.

.2 Review of Emergency Preparedness Pre-Exercise

a. Inspection Scope

The inspectors observed the licensees emergency preparedness pre-exercise from the simulator and technical support center. The scenario began with a water hammer in the 1B residual heat removal room. The scenario then progressed and included a reactor water cleanup system leak, main turbine high vibrations, the failure of the reactor to scram, and a failure of the 1C main steam line to isolate. The inspectors assessed the accuracy and timeliness of emergency classifications, notifications, and protective action recommendations by observing personnel performing these activities, ensuring that the classifications were made in accordance with the licensees emergency action levels, and reviewing the notification and protective action recommendation forms. Emergency preparedness personnel initiated Issue Report 229597 to document an unsuccessful emergency classification opportunity. The inspectors also observed the licensees critique to ensure that items identified by the inspectors were also identified by the licensee.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors examined the licensees physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within the spent fuel or other storage pools. This included discussions with cognizant licensee representatives. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 High Risk Significant, High Dose Rate, High Radiation Area and Very High Radiation

Area Controls

a. Inspection Scope

The inspectors evaluated the controls that were in place for special areas that had the potential to become very high radiation areas during certain plant operations including traversing in-core probe operations. Discussions were held with radiation protection supervisors to determine how the required communications between the radiation protection group and other involved groups would occur beforehand in order to allow corresponding timely actions to properly post and control the radiation hazards. This review represented one sample.

b. Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable Planning And Controls (71121.02)

.1 Declared Pregnant Workers

a. Inspection Scope

The inspectors reviewed dose records of declared pregnant workers for the current assessment period to verify that the exposure results and monitoring controls employed by the licensee complied with the requirements of 10 CFR 20.1208. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and Special Reports related to the as low as is reasonably achievable (ALARA) program since the last inspection to determine if the licensees overall audit programs scope and frequency for all applicable areas under the Occupational Cornerstone met the requirements of 10 CFR 20.1101(c). This review represented one sample.

The inspectors verified that identified problems were entered into the corrective action program for resolution, and that they had been properly characterized, prioritized, and resolved. This included dose significant post-job (work activity) reviews and post-outage ALARA report critiques of exposure performance. This review represented one sample.

Corrective action reports related to the ALARA program were reviewed and staff members were interviewed to verify that follow-up activities had been conducted in an effective and timely manner commensurate with their importance to safety and risk using the following criteria:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions;
  • Resolution of non-cited violations tracked in the corrective action system; and
  • Implementation/consideration of risk significant operational experience feedback.

This review represented one sample.

The inspectors also determined that the licensees self-assessment program identified and addressed repetitive deficiencies and significant individual deficiencies that were identified in the licensee's problem identification and resolution process. This review represented one sample.

b. Findings

No findings of significance were identified.

2PS2 Radioactive Material Processing and Transportation (71122.02)

a. Inspection Scope

The inspectors reviewed shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness for a shipment of 14 drums of radwaste. The inspectors verified that the receiving licensee was authorized to receive the shipment package. The inspectors observed radiation worker practices to verify that the workers had adequate skills to accomplish each task and to determine if the shippers were knowledgeable of the shipping regulations and whether shipping personnel demonstrate adequate skills to accomplish the package preparation requirements for public transport with respect to NRC Bulletin 79-19 and 49 CFR Part 172 Subpart H. This review represented one sample.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Cornerstones: Initiating Events, Mitigating Systems, and Emergency Preparedness Reactor Safety Strategic Area

a. Inspection Scope

The inspectors sampled the licensees performance indicator submittals for the periods listed below. The inspectors used the performance indicator definitions and guidance contained in Revision 2 of Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, to verify the accuracy of the performance indicator data. The following nine performance indicators were reviewed:

Unit 1

  • Safety System Functional Failures (June 2003 through April 2004), and
  • Safety System Unavailability for the Emergency Alternating Current Power System (June 2003 through April 2004).

Unit 2

  • Safety System Functional Failures (June 2003 through April 2004), and
  • Safety System Unavailability for the Emergency Alternating Current Power System (June 2003 through April 2004).

Common

  • Alert and Notification System (October 2002 through December 2003),
  • Emergency Response Organization Drill Participation (October 2002 through December 2003), and
  • Drill and Exercise Performance (October 2002 through December 2003).

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are included in the list of documents reviewed which are attached to this report.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors interviewed licensee personnel and reviewed licensee system health reports, common cause analyses, trending reports, quality assurance assessment reports, performance indicators, maintenance rule assessments, maintenance backlog lists, and corrective action backlog lists to identify trends that might have indicated the existence of a more significant safety issue which may have been documented outside of the normal corrective action program.

b. Findings

No findings of significance were identified.

4OA3 Event Followup

.1 (Closed) Licensee Event Report 05000265/2004-002-00: Axial Flaws Detected in

Recirculation Piping During Inservice Inspection. During a March 2004 Unit 2 refueling outage, the licensee identified two axial indications during an inservice inspection of reactor recirculation weld 02B-S7. These indications were identified due to the licensees chemical decontamination of the reactor recirculation piping which removed a crud layer and made the indications visible. Due to the axial orientation of the indications, the licensee was unable to evaluate the indications for continued service using Article IWB-3000 of Section XI to the American Society of Mechanical Engineers Code. As a result, a two-layer weld overlay was applied to the indications in accordance with Code Case N-504-2. The application of this code case for the repairs of axial indications was previously endorsed by the Nuclear Regulatory Commission in Regulatory Guide 1.147, Revision 13, Inservice Inspection Code Case Acceptability Section XI, Division 1. The licensee performed inservice inspections of other similar welds and did not identify any other indications. This issue was not subject to NRC enforcement since a violation of NRC requirements did not occur.

.2 (Closed) Licensee Event Report 05000/2004-003-00: Unit Trip from Turbine Trip during

Thrust Bearing Wear Detector Testing.

Introduction:

A Green finding was self-revealed when Unit 2 automatically tripped during main turbine thrust bearing wear detector testing. The finding was not considered a violation of regulatory requirements since the main turbine thrust bearing wear detector was a non-safety related component.

Description:

On March 30, 2004, Unit 2 was in operation at 680 megawatts electric (MWe) after completion of Refueling Outage Q2R17. During the outage, all three low pressure turbines were disassembled and reassembled to allow the turbine buckets to be replaced. After completion of the work a number of post maintenance tests were performed. In particular, the turbine thrust bearing wear detector system was tested using QCOS 5600-10, Unit 2 Weekly Turbine Generator Tests. As the operators were implementing the surveillance, an inadvertent turbine trip occurred which caused a reactor trip. All of the control rods inserted and the plant responded as designed.

The licensee determined that multiple changes in site work practices resulted in increasing the probability of a turbine trip and a reactor trip during thrust bearing wear detector testing. In particular, the instrument maintenance department had three procedures for calibrating and testing the thrust bearing wear detector. The procedures consisted of an initial adjustment (performed at zero percent power), an intermediate adjustment (performed at approximately 25 percent power), and a final adjustment (performed at greater than 80 percent power). Over time several procedure revisions were implemented which resulted in incorporating some of the initial adjustment procedure steps into the intermediate adjustment procedure. As a result, the initial adjustment procedure was no longer used. The inspectors were informed that the final adjustment procedure was also used infrequently because it required personnel to complete procedural steps inside the turbine shield wall which resulted in significant personnel dose.

The inspectors determined that while the licensee had implemented multiple procedure revisions to gain efficiencies in several areas, the licensee had not recognized that these changes also increased the probability of a plant transient during thrust bearing wear detector testing. For example, the original thrust bearing wear detector testing as described in the vendor manual consisted of three parts for specific reasons. The initial adjustment was performed at zero percent power such that gross adjustments to the thrust bearing wear detector setpoints could be made without any impact on plant operation. The intermediate adjustment was performed at approximately 25 percent because a turbine trip would not cause a reactor trip at this power level. Lastly, the final adjustment phase was implemented to make any fine adjustments to the thrust bearing wear detector setpoints that may have been needed and included instructions for inhibiting a potential turbine trip. Conversely, on March 30, the licensee performed the intermediate adjustment with Unit 2 operating at approximately 70 percent power without implementing appropriate measures to minimize a turbine trip or a reactor trip.

Analysis:

The inspectors determined that the failure to appropriately implement thrust bearing wear detector calibration and testing procedures was more than minor because it was a precursor to a significant event (a transient). The inspectors also determined that this finding should be evaluated in accordance with Inspection Manual Chapter 0609, Significance Determination Process, because the finding was associated with the increase in the likelihood of an initiating event. The inspectors conducted a Phase 1 Significance Determination Process screening and determined that this finding was of very low safety significance (Green) because it did not contribute to:

(1) the likelihood of a primary or secondary system loss of coolant accident initiator,
(2) both the likelihood of a reactor trip and that mitigation equipment or functions would not be available,
(3) the likelihood of a fire or internal/external flood, or
(4) an increase in the initiating event frequency of events described in the individual plant examination of external events or other existing plant-specific analyses (FIN 050000265/2004005-01).
Enforcement:

This finding was not subject to NRC enforcement because the thrust bearing wear detector and associated equipment are non-safety related components.

The licensee initiated Condition Report 211724 to document this event. Corrective actions were to design and install a permanent modification to disable the turbine trip circuitry during future thrust bearing wear detector testing. The licensee has also suspended further thrust bearing wear detector testing until the modification is installed.

The inspectors determined that the suspension of this test was acceptable since the probability of a transient due to the failure to perform thrust bearing wear detector testing was low, the test was performed as part of the licensees turbine warranty, and the test was not required by any NRC regulations.

4OA5 Other Activities

Temporary Instruction 2515/156, Offsite Power System Operational Readiness

a. Inspection Scope

The inspectors reviewed licensee maintenance records, event reports, corrective action documents and procedures, and interviewed the station engineering, maintenance, and operations staff to collect data necessary to complete Temporary Instruction 2515/156.

This review was conducted to confirm the operational readiness of the offsite power systems in accordance with NRC requirements such as Appendix A to 10 CFR Part 50, General Design Criterion 17; Criterion XVI of Appendix B to 10 CFR Part 50; the Technical Specifications; 10 CFR 50.63; 10 CFR 50.65 (a)(4), and licensee procedures.

Specifically, the inspectors reviewed the licensee's procedures and processes for ensuring that the grid reliability conditions were appropriately assessed during periods of maintenance in accordance with 10 CFR 50.65 (a)(4). The inspectors also assessed the reliability and grid performance through a review of historical and current data to verify compliance with 10 CFR 50.63, Technical Specifications, and General Design Criterion 17. Lastly, the inspectors assessed the licensee's implementation of operating experience that was applicable to the site as well as corrective action documents to ensure issues were being identified at an appropriate threshold, assessed for significance, and appropriately dispositioned.

b. Findings

No findings of significance were identified. Based on the inspection, no immediate operability issues were identified. In accordance with Temporary Instruction 2515/156 reporting requirements, the inspectors transmitted the required temporary instruction data to the headquarters staff for further analysis. The licensee was asked to assess their readiness for summer operation by addressing three key questions. The licensee responded to the questions by stating that an agreement was in place to ensure that they were informed if the electrical grid was stressed to the point that a scram of either unit would result in inadequate post-trip switchyard voltages. This agreement included the required voltage range and the post-scram electrical load from each unit that would be expected to be connected to the electrical grid. In addition, the agreement required that post-trip voltages be calculated every few minutes.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. M. Perito and other members of licensee management at the conclusion of the inspection on July 6, 2004. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • Access control to radiologically significant areas, the ALARA planning and controls program, and the radioactive material processing and transportation program with Mr. R. Gideon on May 20, 2004.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Tulon, Site Vice President
R. Gideon, Plant Manager
R. Armitage, Training Manager
W. Beck, Regulatory Assurance Manager
G. Boerschig, Engineering Manager
J. DeYoung, Emergency Preparedness Specialist
T. Hanley, Maintenance Manager
D. Hieggelke, Nuclear Oversight Manager
K. Leech, Security Manager
S. McCain, Corporate Emergency Preparedness Manager
K. Moser, Chemistry/Environ/Radwaste Manager
K. Ohr, Acting Radiation Protection Manager
M. Perito, Operations Manager

Nuclear Regulatory Commission

M. Ring, Chief, Reactor Projects Branch 1
L. Rossbach, Project Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000265/2004005-01 FIN Failure to Appropriately Implement Turbine Thrust Bearing Wear Detector Calibration and Surveillance Testing Procedures

Closed

05000265/2004005-01 FIN Failure to Appropriately Implement Turbine Thrust Bearing Wear Detector Calibration and Surveillance Testing Procedures
05000265/2004-002-00 LER Axial Flaws Detected in Recirculation Piping During Inservice Inspection
05000265/2004-003-00 LER Unit Trip from Turbine Trip During Thrust Bearing Wear Detector Testing

LIST OF DOCUMENTS REVIEWED