IR 05000254/2021004

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Integrated Inspection Report 05000254/2021004 and 05000265/2021004
ML22033A307
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/02/2022
From: Kenneth Riemer
NRC/RGN-III/DRP/B1
To: Rhoades D
Constellation Energy Generation
References
IR 2021004
Download: ML22033A307 (26)


Text

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000254/2021004 AND 05000265/2021004

Dear Mr. Rhoades:

On December 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Quad Cities Nuclear Power Station. On January 11, 2022, the NRC inspectors discussed the results of this inspection with Mr. M. Bridges, Operations Director, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000254 and 05000265

License Numbers:

DPR-29 and DPR-30

Report Numbers:

05000254/2021004 and 05000265/2021004

Enterprise Identifier:

I-2021-004-0114

Licensee:

Constellation Nuclear

Facility:

Quad Cities Nuclear Power Station

Location:

Cordova, IL

Inspection Dates:

October 01, 2021 to December 31, 2021

Inspectors:

C. Hunt, Senior Resident Inspector

R. Baker, Senior Operations Engineer

J. Cassidy, Senior Health Physicist

Z. Coffman, Resident Inspector

M. Garza, Emergency Preparedness Inspector

C. Mathews, Illinois Emergency Management Agency

J. Neurauter, Senior Reactor Inspector

G. Roach, Senior Operations Engineer

E. Sanchez Santiago, Senior Reactor Inspector

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Quad Cities Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 The unit began the inspection period at full-rated thermal power. On October 22, 2021, the station experienced a trip of the 1B reactor recirculation pump, resulting in an unplanned downpower to approximately 35 percent. Following troubleshooting, the station returned to full-rated thermal power on October 23, 2021. For all other periods, the unit was at full-rated thermal power with the exception of short-term power reductions for control rod sequence exchanges, testing, and as requested by the transmission system operator.

Unit 2 The unit began the inspection period at full-rated thermal power, where it remained for the entire inspection period, with the exception of short-term power reductions for control rod sequence exchanges, testing, and as requested by the transmission system operator.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

On February 1, 2022, the operating license for Quad Cities held by Exelon Generation Company, LLC was transferred to Constellation Energy Generation, LLC (Constellation) as documented in the associated license amendments (ML22021B660). While some or all of the inspection documented in this report was performed while the license was held by Exelon Generation Company, LLC, this report will refer to the licensee as Constellation throughout.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)1A core spray during planned maintenance on the 1A low pressure coolant injection (LPCI) system on October 21, 2021 (2)safe shutdown makeup pump following maintenance on December 1, 2021

(3) Unit 1 reactor core isolation cooling (RCIC) during Unit 1 high pressure coolant injection (HPCI) out of service for troubleshooting on December 16, 2021

Complete Walkdown Sample (IP Section 03.02) (2 Samples)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 reactor building closed cooling water on November 3, 2021.
(2) The inspectors evaluated system configurations during a complete walkdown of the Unit 2 core spray system on November 9, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Zone 8.2.6.A, Unit 1 turbine building, elevation 595', elevator hallway, on October 21, 2021
(2) Fire Zone 11.1.3, Unit 1 HPCI room, on December 2, 2021

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) 1B residual heat removal (RHR) room on October 14, 2021

71111.07T - Heat Sink Performance Heat Exchanger (Service Water Cooled) (IP Section 03.02)

The inspectors evaluated heat exchanger/sink performance on the following:

(1)1A RHR heat exchanger (1-1003A)

(2) Unit 1 emergency diesel generator heat exchangers (1-6661-A/B)

Ultimate Heat Sink (IP Section 03.04) (1 Sample)

(1) The ultimate heat sink, specifically Sections 03.04.c and 03.04.e were completed.

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating test and biennial written examinations administered from October 4, 2021 through November 11, 2021.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examinations administered from October 4, 2021 through November 11, 2021.

Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating tests administered from October 4, 2021 through November 11, 2021.

Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated operators in the simulator during an annual licensed operator evaluation on October 19, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (4 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Unit 0 emergency diesel generator on October 13, 2021 (2)24/48V battery charges on October 20, 2021 (3)480V switchgear on November 1, 2021
(4) Unit 1 feedwater control on December 10, 2021

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) E-2 certification meeting and risk management for work week 10/04/2021 on October 4, 2021
(2) E-2 certification meeting and risk management for work week 10/25/2021 on October 13, 2021
(3) Unit 1 emergency diesel generator (EDG) troubleshooting on October 15, 2021 (4)1/2 EDG cooling water pump high vibration on October 18, 2021 (5)1B reactor recirculating pump trip on October 22, 2021

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Action Request 4447816, "Degraded 1/2 EDG Air Inlet Silencer"
(2) Action Request 4450943, "1B RHRSWP [residual heat removal service water pump]

Vault Cooler Return Line UT Results"

(3) Action Request 4448022, "Required Flow Not Met for RCIC High Disch Press Condition"
(4) Action Request 4460893, "Low Switchyard Voltage"
(5) Action Request 4464185, "U1 HPCI Gland Exhauster Tripped"
(6) Action Request 4466003, "Pin-Hole Leaks Found at Weld for 0-5799-381 'B' HVAC

[heating, ventilation, and air conditioning] Train"

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the following post-maintenance test (PMT) activities to verify system operability and functionality:

(1)

'B' control room emergency ventilation system PMT following planned work window on October 7, 2021

(2) Unit 1 EDG following planned outage and voltage regulator troubleshooting on October 15, 2021 (3)1/2 diesel generator cooling water pump PMT after an emergent work window on October 19, 2021

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1)recirculation single loop operation on October 22, 2021

(2) Unit 2A loop LPCI and containment cooling modes of RHR non-outage logic test on October 27, 2021 (3)standby liquid pump flow rate test on November 29, 2021

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) The inspectors evaluated the following maintenance and testing of the alert and notification system:

2019 PNS System Maintenance Report

2020 PNS System Maintenance Report

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the emergency preparedness organization.

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program.

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Walkdowns and Observations (IP Section 03.01) (7 Samples)

The inspectors evaluated the following radiation detection instrumentation during plant walkdowns:

(1)portable ion chamber dose rate instruments "Ready for Use" at the entrance to the radiologically controlled area (2)extendable Geiger-Mueller dose rate Instruments "Ready for Use" at the entrance to the radiologically controlled area (3)personnel contamination monitors used at the exit of the radiologically controlled area (4)small article contamination monitors used at the exit of the radiologically controlled area

(5) Shepherd Model 89 box calibrator used to perform functional checks of portable dose rate instruments (6)portable Geiger-Mueller frisker "Ready for Use" at the main access facility (7)personnel gamma portal monitor used to exit the main access facility

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage, &

Transportation

Radioactive Material Storage (IP Section 03.01)

The inspectors evaluated the licensees performance in controlling, labeling, and securing the following radioactive materials:

(1) Inspectors evaluated the licensees performance in controlling, labeling, and securing radioactive materials.

Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)

The inspectors walked down the following accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality:

(1) Inspectors walked down accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality.

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

The inspectors evaluated the following characterization and classification of radioactive waste:

(1) The inspectors evaluated the licensees characterization and classification of radioactive waste shipment QC-19-080.
(2) The inspectors evaluated the licensees characterization and classification of radioactive waste shipment QC-20-074.

Shipping Records (IP Section 03.05) (4 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through a record review:

(1) Radioactive Waste Shipment QC-20-074; Radioactive Material, Type B(U) package, UN2916; Dewatered Reactor Water Cleanup Resin
(2) Radioactive Waste Shipment QC-20-075; Radioactive Material, Type B(U) package, UN2916; Dewatered Reactor Water Cleanup Resin
(3) Radioactive Waste Shipment QC-20-076; Radioactive Material, Type B(U) package, UN2916; Dewatered Reactor Water Cleanup Resin
(4) Radioactive Waste Shipment QC-19-080; Radioactive Material, low specific activity (LSA-II), UN3321; Filters and Activated Material

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS07: High Pressure Injection Systems (IP Section 02.06)===

(1) Unit 1 (October 1, 2020 through September 30, 2021)
(2) Unit 2 (October 1, 2020 through September 30, 2021)

MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)

(1) Unit 1 (October 1, 2020 through September 30, 2021)
(2) Unit 2 (October 1, 2020 through September 30, 2021)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (October 1, 2020 through September 30, 2021)
(2) Unit 2 (October 1, 2020 through September 30, 2021)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (October 1, 2020 through September 30, 2021)
(2) Unit 2 (October 1, 2020 through September 30, 2021)

EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12) (1 Sample)

(1) Unit 1 (July 1, 2020 through September 30, 2021)

Unit 2 (July 1, 2020 through September 30, 2021)

EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13) (1 Sample)

(1) Unit 1 (July 1, 2020 through September 30, 2021)

Unit 2 (July 1, 2020 through September 30, 2021)

EP03: Alert and Notification System (ANS) Reliability Sample (IP Section 02.14) (1 Sample)

(1) Unit 1 (July 1, 2020 through September 30, 2021)

Unit 2 (July 1, 2020 through September 30, 2021)

71152 - Problem Identification and Resolution (PI&R)

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in breakdown in corrective action program (CAP) and work control programs leading to latent issues that might be indicative of a more significant safety issue on November 8, 2021.

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its CAP related to the following issues:

(1)1-4899-121 on October 26, 2021 (2)inadvertent isolation of Unit 2 RCIC during surveillance testing on December 12,

INSPECTION RESULTS

Minor Performance Deficiency 71152 Minor Performance Deficiency: On October 26, 2021, the inspectors identified a performance deficiency where the licensee had failed to perform leakage testing on the 1B core spray room floor drain ball valve, 1-4899-121, in accordance with surveillance procedure QCOS 0020-04, Reactor Building Floor Drain Sump Ball Valve Leakage Testing. Valve 1-4899-121 is a non-safety related, normally closed valve, credited with preventing a flooding event in the Torus area, or an emergency core cooling system corner room, from propagating to adjacent areas. The licensee performs the qualitative leakage test outlined in QCOS 0020-04 every 2 years to verify acceptable performance. The last successful completion of the QCOS 0020-04 on valve 1-4899-121 was performed July 12, 2018, as documented in Work Order 4591143. During the subsequent surveillance performed under Work Order 4878780 on July 8, 2020, the licensee documented two issues in the CAP concerning the surveillance and ultimately listed the surveillance as Complete - Portions UNSAT-Credit Predefined, in accordance with the licensees surveillance program requirements. One of those issues, captured in Action Request 4355514, documented that step H.3 of QCOS 0020-04, for performing the leakage test on valve 1-4899-121, was not performed due to concerns over the valve having a history of being difficult to operate. Actions out of Action Request 4355514 included scheduling Work Order 1769615 to replace the valve prior to the surveillance late date of January 10, 2021. However, prior to work being performed, the work order was inadvertently rescheduled to July 2022.

The licensee captured the issue in the CAP under Action Request 4455921 and performed a work group evaluation which revealed several breakdowns in the work control process that led to the leakage test being missed. Additionally, the licensee performed an extent of condition review over twenty-four months of corrective action documents to identify any other work orders meeting similar criteria of having a partial failure of surveillance requirements and did not identify any additional issues. The inspectors reviewed the licensee's evaluation and determined that the actions generated were adequate given the safety significance of the system.

Screening: The inspectors determined the performance deficiency was minor. Specifically, the inspectors determined that failing to perform a leakage test on valve 1-4899-121 in accordance with QCOS 0020-04 was a performance deficiency. Upon discovery, the licensee satisfactorily performed the applicable portions of QCOS 0020-04 for valve 1-4899-121 on October 26, 2021. Therefore, the performance deficiency is being treated as minor in accordance with IMC 0612, Appendix E, Examples of Minor Issues, dated January 1, 2021, Example 1.b.

Observation: Repeat Inadvertent Isolation of Reactor Core Isolation Cooling During Surveillance Testing 71152 On September 8, 2021, while performing MA-QC-IM-1-13201, Unit 2 RCIC Low Reactor Pressure Isolation Calibration and Channel Functional Test, step 5.8.2, to isolate and vent pressure switch 2-1360-9D, the Unit 2 RCIC unexpectedly isolated. This was the second instance of Unit 2 RCIC unexpectedly isolating during the performance of MA-QC-IM-1-13201, with the previous instance occurring on June 8, 2021, documented in the CAP under Action Request 4428172. Following the first occurrence, the licensee conducted a work group evaluation and determined that there was inadequate procedural guidance to validate the as-found state of all four RCIC low reactor pressure isolation switches prior to the testing of each individual switch. Validating that all four switches are in a normal alignment prior to cycling an individual switch would eliminate the potential for satisfying the one-of-two taken twice isolation logic should a switch fail to reset following testing. Actions were created from Action Request 4428172 to draft the necessary procedure revision to eliminate the vulnerability. The draft revision was completed on June 21, 2021, and the action was marked completed in the CAP. Prior to implementing the revised procedure, however, the licensee identified additional issues which resulted in the procedure remaining in a draft status. No additional action tracking items were opened in the CAP to track resolution of the issues. Additionally, the date for implementing the new procedure revision was extended from August 19 to October 1, 2021. The licensee did not recognize that the next scheduled performance of MA-QC-IM-1-13201 was September 8, 2021. None of the licensees work planning processes, or work practices in the field, such as pre-job briefs and operating experience reviews, identified that the desired changes to the procedure had not been implemented. As a result, the licensee inadvertently isolated the Unit 2 RCIC system while performing the surveillance for a second time. The licensee documented the second inadvertent isolation and associated work group evaluation in the CAP under Action Request 4445201.

The inspectors noted that for both occurrences of inadvertent isolation, the RCIC system was procedurally declared inoperable to support the surveillance testing prior to the commencement of the testing; therefore, other sources of reactor vessel high pressure injection were protected and available per the licensees procedures. The inadvertent isolation of RCIC placed the associated containment isolation valves in their safety-related position, and the overall system unavailability time incurred during each event was minimal.

Additionally, the inspectors verified that the intended changes to surveillance procedure MA-QC-IM-1-13201 were completed on November 9, 2021.

The inspectors did not identify any findings or violations in this sample.

Observation: Unresolved Issues Lingering in the Corrective Action and Work Control Programs 71152 The inspectors identified eight instances where either the CAP or the work control program failed to resolve non-risk significant conditions adverse to quality. Specifically, inspectors noted several instances of due dates for actions to resolve outstanding issues being extended multiple times, including instances where due dates were scheduled past important equipment milestones like surveillance late dates, with no tangible actions being taken to resolve the issue. Additionally, inspectors noted instances of corrective work orders being closed with no work being done to address the degraded condition, degraded conditions being assessed as not significant but then allowed to continue to degrade without monitoring, and work arounds being proceduralized to cope with long-standing unresolved degraded conditions. Examples include:

1. 1/2 trackway door degradation (Action Requests 4139659, 4193055, 4344543,

4441840, and 4443482)

2. 1B core spray corner room ball valve 1-4899-121 degradation (Action Requests

4202399, 4355514, and 4455921)

3. Unit 2 RCIC inadvertent isolation (Action Requests 4428172, 4428864, and 4445201)

4. condensate demineralizer backwash valves issues (Action Requests 4455639,

4456408, and 4456344)

5. room cooler hanger in the 1A RHR corner room (Action Requests 4441227, 2486975,

and 2599169)

6. Unit 1 and Unit 2 station black out diesel isolimiter fires (Action Requests 4310554,

4319365, and 4399868)

7. 1/2 'A' fire diesel level switch (Action Requests 4443776 and 2541024)

8. Fire protection valve 1-4199-39 corrosion (Action Requests 4132135 and 4441227)

Issues not being resolved due to poor planning, administrative errors, and lack of ownership have the potential to undermine the effectiveness of the sites corrective action and work control programs. Inspectors noted that while the issues identified were non-risk significant individually, collectively, the issues represented a breakdown of the sites problem identification and resolution safety culture trait as discussed in NUREG-2165, Safety Culture Common Language, published March 2014. The licensee captured the inspectors' observation in the CAP under Action Request 4461856.

The inspectors did not identify any findings or violations in this sample.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 11, 2022, the inspectors presented the integrated inspection results to Mr. M. Bridges, Operations Director, and other members of the licensee staff.

On September 28, 2021, the inspectors presented the radiation protection inspection results to Mr. D. Griffiths, Acting Plant Manager, and other members of the licensee staff.

On November 12, 2021, the inspectors presented the biennial licensed operator requalification program inspection results to Mr. B. Wake, Site Vice President, and other members of the licensee staff.

On November 16, 2021, the inspectors presented the review of annual licensed operator requalification program testing inspection results to Mr. S. Sullivan, Senior Operations Instructor, and other members of the licensee staff.

On December 3, 2021, the inspectors presented the EP program inspection results to Mr. D. Griffiths, Plant Manager, and other members of the licensee staff.

On December 14, 2021, the inspectors presented the triennial heat sink inspection results to Mr. B. Wake, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

AR 4463030

EOID: SSMP Local Flow Controller Indicates 43 GPM

11/24/2021

1304-ED01

RCIC Piping - Reactor Bldg

M-33

Diagram of Reactor Building Closed Cooling Water Piping,

Sheet 1

2/23/1997

Drawings

M-70

Diagram of Safe Shutdown Make-Up Pump System

09/11/1999

QCOP 0050-17

Flex RCIC Room Cooler Lineup

QCOP 2900-01

Safe Shutdown Makeup Pump System Preparation for

Standby Operation

QCOS 1300-21

RCIC Keep Fill Valve Lineup Verification

71111.04

Procedures

QCOS 1400-10

Core Spray Operability Verification

FZ 11.1.3

Fire Zone 11.1.3: Unit 1 HPCI Room

71111.05

Fire Plans

FZ 8.2.6.A

Unit 1 TB 595'-0" Elev. Hallway

June 2012

Corrective Action

Documents

AR 4355298

1B RHR Room Floor Drain Valve Failed QCOS 0020-04

07/08/2020

Engineering

Changes

EC 394543

Perform a Technical Evaluation of QCOP 0020-04

QCOS 0020-04

Reactor Building Floor Drain Sump Ball Valve Testing

71111.06

Procedures

QCTS 0810-10

Reactor Building Internal Flood Barrier Surveillance

Calculations

8001688-EVAL-1

Analysis and Performance of Weigmann & Rose Heat

Exchanger

2/25/2011

AR 1416480

Godwin Pump Performance Not Routinely Checked

09/21/2012

AR 1418982

Godwin Pump Relocation

09/27/2012

Corrective Action

Documents

AR 3959076

Unit 2 SW Strainer Basket Needs Replaced

01/04/2017

AR 4466331

NRC UHS - Potential Observation for QCMPM 4400-11

2/13/2021

AR 4466341

NRC UHS-Potential Minor Violation and Observation for 1A

RHR

2/13/2021

Corrective Action

Documents

Resulting from

Inspection

AR 4466353

NRC UHS - Observation for Portable Diesel Pump

Documentation

2/13/2021

EC 346690

1A RHR HX Tube Plugging Criteria

71111.07T

Engineering

Changes

EC 362215

Maximum Tubes That Can Be Fouled DGHXs

001

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

EC 381002

Evaluation of EDG HX Flow Rate for Functional Impact

EC 387980

Determine Tube Fouling Limit for Weigmann & Rose Diesel

Generator Heat Exchangers

EC 632531

Piping Line 1-3958-6" Through Wall Leak

8001699-EVAL-1

Analysis and Performance of Weigmann & Rose Heat

Exchange

05/22/2012

Engineering

Evaluations

EA 498197

Eddy Current Final Examination Report

04/2021

ER-AA-340

GL 89-13 Program Implementation Procedure

ER-AA-340-1001

GL 89-13 Program Implementation Instructional Guide

Procedures

ER-AA-340-1002

Service Water Heat Exchanger Inspection Guide

WO 1217059

MM Replace Strainer Basket with Smaller Mesh

01/11/2011

WO 1264291

OP QCOS 1000-29 RHR HX Thermal Performance Test

2/18/2011

WO 1847561

Engineering Inspection of Service Water Strainer

2/20/2017

WO 4678906

1A RHR HX Thermal Performance Test

2/01/2020

WO 4682727

Open/Inspect Diesel Generator Heat Exchanger 1-6661-A

03/24/2019

WO 4682732

Open/Inspect Diesel Generator 'B' Heat Exchanger

03/24/2019

WO 4761428

Demonstrate the Capability of Godwin Pumps

09/08/2021

WO 4855344

Simulate Response to Lock and Dam 14

11/06/2020

WO 4916927

2A Circulating Water Intake Bay Inspection

03/03/2020

WO 4916928

1A CW Bay Inspection

03/09/2020

WO 4964720

EWP Trash Rake Annual

10/07/2020

WO 5076298

2A Traveling Screen Inspection

03/03/2021

WO 5087540

Trash Rake Annual Maintenance

10/06/2021

WO 5104170

RHR Service Water Bay Inspection

04/27/2021

WO 5107917

Intake Canal Sounding Readings

05/10/2021

WO 5131326

2A Traveling Screen Inspection

08/30/2021

Work Orders

WO 835123

Eddy Current Test 1A RHR HX

05/06/2009

71111.11A

Miscellaneous

Requalification

Program Annual

Testing Summary

Results

Licensed Operator Annual Examination Performance

Records for 2021

11/12/2021

AR 4388149-04

Pre 711111.11 Focused Self-Assessment

09/21/2021

71111.11B

Corrective Action

Documents

AR 4412991

Unexpected 1/2 Scram on Unit 1

03/31/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Post Event

Testing

Unit 1 Main Generator Trip/Scram - Simulator Comparison

08/26/2019

Post Event

Testing

Unit 1 Hydrogen Water Chemistry (HWC) Trip - Simulator

Comparison

09/09/2021

Scenario Based

Testing Report

SBT for Quad Cities 2021 Initial License NRC Exam

Scenario 4, Rev 2

11/10/2020

Scenario Based

Testing Report

SBT for Quad Cities 2021 LORT NRC Exam Scenario 00-01,

Rev 24

07/12/2021

Scenario Based

Testing Report

SBT for Quad Cities 2021 LORT NRC Exam Scenario 00-22,

Rev 14

08/07/2021

Simulator

Certification Test

44% Power Simulator Steady State Test Q1C27

04/01/2021

Simulator

Certification Test

75% Power Simulator Steady State Test Q1C27

04/01/2021

Simulator

Certification Test

100% Power Simulator Steady State Test Q1C27

04/05/2021

Simulator

Certification Test

Simulator Real Time Test Q1C27

04/06/2021

Simulator

Transient Test

TR-01

Manual Reactor Trip Q1C27

04/07/2021

Simulator

Transient Test

TR-03

Simultaneous Closure of All Main Steam Isolation Valves

Q1C27

04/08/2021

Simulator

Transient Test

TR-04

Simultaneous Trip of All Reactor Recirculation Pumps

Q1C27

04/08/2021

Engineering

Evaluations

Simulator

Transient Test

TR-08

Maximum Sized Reactor Coolant System Rupture Combined

with Loss of Offsite Power Q1C27

04/08/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Simulator

Transient Test

TR-10

Simultaneous Closure of All Main Steam Isolation Valves

Combined with a Stuck Open Safety/Relief Valve (Inhibit

Actuation of High Pressure ECCS) Q1C27 Simultaneous

Closure of All Main Steam Isolation Valves Combined with a

Stuck Open Safety/Relief Valve (Inhibit Actuation of High

Pressure ECCS) Q1C27

04/07/2021

21 NRC Exam

Crew-D

RO Written Exam

11/05/2021

21 NRC Exam

Crew-D

SRO Written Exam

11/05/2021

Attendance

Records

Licensed Operator Continuous Training Attendance Records

20-2021

Exam Scenario

00-01

Simulator Scenario Guide

Exam Scenario

00-13

Simulator Scenario Guide

Exam Scenario

00-18

Simulator Scenario Guide

Exam Scenario

00-22

Simulator Scenario Guide

LP-0050-01

Job Performance Measure

LP-4100-01

Job Performance Measure

LP-6620-01

Job Performance Measure

LP-6900-01

Job Performance Measure

LS-0700-02

Job Performance Measure

LS-1100-02-A

Job Performance Measure

LS-1400-02

Job Performance Measure

LS-2300-03-A

Job Performance Measure

LS-6600-03

Job Performance Measure

Medical Records

Licensed Operator Medical Records (Various)

11/08/2021

NF-AB-130-1400

Cycle Management Report Generation - Quad Cities 1

(Q1C27)

Miscellaneous

Remediation

Records

21 Annual Operating Test JPM Evaluation Results Form A

- Remediation for Failure of 1 JPM

10/01/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Simulator Work

Request Listing

List of All Open SWR Items

11/09/2021

Simulator Work

Request Listing

List of All SWR Items Closed Since Previous Biennial Requal

Inspection

11/09/2021

SRO-28

Job Performance Measure

TQ-AA-155-F04

Individual Simulator Evaluation Forms for 2021 Annual

Operating Test - Crew D-All Operators

TQ-AA-155-F05

Crew Simulator Evaluation Forms for 2021 Annual Operating

Test - Crew D

TQ-AA-306-F02

Simulator Review Board Minutes - Semi-Annual

08/31/2021

TQ-AA-306-F02

Simulator Review Board Minutes - Semi-Annual

01/28/2021

TQ-AA-306-F02

Simulator Review Board Minutes - Semi-Annual

08/18/2020

OP-AA-105-102

Active License Tracking Logs for 2nd and 3rd Quarter 2021

for Crew D Personnel

TQ-AA-150

Operator Training Programs

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-155-F106

Simulator Evaluation - Shift Manager Competency

Standards

TQ-AA-155-F107

Simulator Evaluation - STA or IA Competency Standards

TQ-AA-155-F108

Simulator Evaluation - Individual Competency Standards

TQ-AA-155-F109

Simulator Evaluation -Crew Competency Standards

TQ-AA-201

Exam Security and Administration

TQ-AA-306

Simulator Management

Procedures

TQ-QC-201-0113

Simulator Examination Security Actions Checklist

Simulator Work Request 136132

Simulator Crash during Scenario LOCT-1001

06/04/2020

Simulator Work Request 136528

OPRM Bypass Switches

11/11/2020

Simulator Work Request 137058

Q1C27 Recirc Drive Water Flow Update

05/21/2021

Work Orders

Simulator Work Request 137222

EC 621164 Update HPCI Simulator Controller

07/23/2021

71111.12

Corrective Action

AR 4371339

Received 902-5 G-1 (24/48 Batt Charger 2A/2B Circuit Fail)

09/22/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4383979

FME: 2B RB Supply Fan Breaker Bus 28 Cub 3B Failure

11/12/2020

AR 4411809

1C RB Exhaust Fan Auto Trip

03/26/2021

AR 4420973

2C TB Exhaust Fan Did Not Trip When Taken to Trip

05/03/2021

AR 4425369

1B FWRV Positioner Hunting in Auto and Manual at Full

Power

05/24/2021

AR 4447978

1/2 EDG Governor Shutdown Solenoid Not Replaced In

YR PM

09/22/2021

Documents

AR 4448310

Unable to Start Unit 1/2 EDG Following Maintenance

09/24/2021

Drawings

M-15

Feedwater Regulating Valve Actuator Piping

08/17/2001

EC 363145

Electrical Maintenance Requirements for 12 Year Diesel

Inspection

2

Engineering

Changes

EC 633283

PCTCC to Crosstie 24 VDC Chargers per QOP 6900-10

000

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-440

Emergency Diesel Generator (EDG) Reliability Program

OP-AA-107-F-01

Risk Screening Mitigation Plan

2

Procedures

SA-AA-116-2124

Job Hazard Analysis

009

Work Orders

WO 5155256

FNI Troubleshoot 1B FWRV 1-0642-B

05/24/2021

AR 4450656

PARAGON Error with HREs Not Reported as Action Green

10/04/2021

AR 4451409

Issues Occurred During 1F Cond Demin Return to Service

10/07/2021

AR 4453139

Unit 1 EDG Volt Regulator Not Responding

10/15/2021

AR 4453291

Cannibalize Limit Switches for U1 EDG MRV

10/15/2021

AR 4453721

U0 DGCW Outboard Bearing Degradation

10/18/2021

Corrective Action

Documents

AR 4454877

1B ASD Trip

10/22/2021

Corrective Action

Documents

Resulting from

Inspection

AR 4453255

RA24 NRC Question on Protected Equip During U1 EDG

Window

10/15/2021

71111.13

Procedures

OP-AA-108-114

Post Transient Review

QDC-1300-M-

0800

Pressure Drop Through RCIC Discharge Piping to Reactor

Vessel

71111.15

Calculations

QDC-2900-M-

0472

Determination of Pressure Required at PI-1/2-2941-8 for

Safe Shutdown Makeup Pump System Injection Under Safe

Shutdown Conditions

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4447816

Degraded 1/2 EDG Air Inlet Silencer

09/21/2021

AR 4448022

Req'd Flow Not Met for RCIC High Disch Press Condition

09/22/2021

AR 4450943

1B RHRSWP Vault Cooler Return Line UT Results

10/05/2021

AR 4456336

U1 RCIC Failed to Achieve Required Flow

10/27/2021

AR 4456930

U1 RCIC Troubleshooting Findings

10/29/2021

AR 4460893

Low Switchyard Voltage on 11/13

11/15/2021

AR 4464185

U1 HPCI Gland Exhauster Tripped

2/01/2021

AR 4464449

4.0 Critique for QCOS 2300-05

2/02/2021

AR 4464484

HPCI Condensate Pump 1-2304 Failed to Start

2/03/2021

Corrective Action

Documents

AR 4466003

Pin-hole Leaks Found at Weld for 0-5799-381 'B' HVAC

Train

2/11/2021

AR 4391077

Use of OP-AA-108-115 for Alternate Methods

2/18/2020

Corrective Action

Documents

Resulting from

Inspection

AR 4465397

NRC Question on U1 HPCI PRA Availability

2/08/2021

Drawings

Drawing M-22

Diagram of Service Water Piping Diesel Generator Cooling

Water

AB

EC 339445

Seismic Evaluation of Degraded DG 1 & 2 Air Turning Box

Supports (CR 126770)

EC 352027

ENS Notification Retraction Justification - Unit 1 HPCI Signal

Converter Trouble Alarm During IST HPCI Run

10/26/2004

EC 375711

Seismic Review of Replacement EDG Inlet Silencer (Turning

Box)

EC 399724

Provide New State Estimator Setpoints Based on Percent

Voltage Drop

000

EC 635127

Evaluation of 1/2 EDG Air Turning Box Degraded Condition

EC 635700

N-513 Evaluation at the CREVS 1/2-5799-381 Inlet Valve

Engineering

Changes

QDC-2300-M-

0433

Quad Cities HPCI Room Thermal Analysis Loss of Gland

Seal System

Operability

Evaluations

635719

CR HVAC Train B Piping Line 0-57479-2.5" Leak AT

1/2-5799-381

QCMMS 6600-06

Emergency Diesel Generator Twelve Year Preventive

Maintenance Inspection

Procedures

QCOA 6000-03

Low Switchyard Voltage

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

QCOS 1300-05

RCIC Pump Operability Test

QCOP 6600-25

Unit 1 Diesel Generator Start Up

QCOS 5750-02

Control Room Emergency Filtration System

QCOS 5750-04

Quarterly Testing of Control Room HVAC System Valves

and Dampers

Procedures

QCOS 6600-06

Diesel Generator Cooling Water Flow Rate Test

71111.19

Work Orders

WO 5186605

(LR) Diesel Generator Load Test (IST)

10/04/2021

QCOS 0202-09

Recirculation Single Loop Operation Outage Report

QCOS 1000-43

Unit 2 'A' Loop LPCI and Containment Cooling Modes of

RHRS Non-Outage Logic Test

71111.22

Procedures

QCOS 1100-07

Standby Liquid Control Pump Flow Rate Test

AR 4393998

EP-Siren Failure QC41

01/05/2021

AR 4399757

EP-Siren Failure QC14, QC34)

2/02/2021

AR 4401007

EP-Siren Failure (QC28)

2/08/2021

AR 4405958

EP-Siren Failures (QC19)

03/02/2021

AR 4415846

EP-Siren Failure QC41

04/12/2021

Corrective Action

Documents

AR 4441394

Review for Potential Trend Siren Motor Failures

08/18/2021

71114.02

Miscellaneous

PNS System Maintenance Report

2019 and

20

AR 4339630

Operations Staffing Less Than Minimum Per QAP 0300-03

04/30/2020

AR 4349596

Operations Staffing Less Than Minimum Per QAP 0300-03

06/11/2020

AR 4363327

Operations Staffing Less Than Minimum Per QAP 0300-03

08/15/2020

Corrective Action

Documents

AR 4413261

RP Went Below Minimum Staffing for 33 Minutes

04/01/2021

71114.03

Miscellaneous

Emergency Response Organization (ERO) Augmentation

Drill Reports

2019-2021

AR 4324167

Emergency Preparedness Audit Report

04/22/2020

AR 4325357

EP 1Q20 PI Drill Facility and Equipment Issues

03/10/2020

AR 4325364

EP 1Q20 PI Drill TSC Demonstration Criteria Failure

03/10/2020

AR 4325368

EP 1Q20 PI Drill TSC Performance Issues

03/10/2020

AR 4325384

EP 1Q20 PI Drill OSC Demonstration Criteria Failure

03/10/2020

AR 4325388

EP 1Q20 PI Drill OSC Performance Issues

03/10/2020

AR 4341971

2nd Quarter OSC EP Inventory Results

05/08/2020

71114.05

Corrective Action

Documents

AR 4362851

QDC-EP-2020-NRC-CORP-EOF-Failed Objective

08/13/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4363571

NARS Communication DC Failure During ERO Graded

Exercise

08/17/2020

AR 4363578

Scenario Control Message Issues from NRC Graded

Exercise

08/17/2020

AR 4363581

EP 2020 NRC Exercise TSC Demonstration Criteria Failure

08/17/2020

AR 4363585

EP NRC Exercise TSC Demonstration Criteria Failure

08/17/2020

AR 4363590

EP NRC Graded Exercise OSC Demonstration Criteria

Failure

08/17/2020

AR 4363592

EP NRC Graded Exercise OSC Demonstration Criteria

Failure

08/17/2020

AR 4363593

EP NRC Graded Exercise OSC Demonstration Criteria

Failure

08/17/2020

AR 4363710

EP Speakers From OSC/ TSC to MMD Break Area Failed

08/17/2020

AR 4363713

EP Containment Hydrogen from Simulator Not Accurate in

TSC

08/17/2020

AR 4367047

QDC-EP-2020-NRC-CORP-EOF-Other Issues

09/02/2020

AR 4367061

QDC-EP-2020-NRC-CORP-JIC-Other Issues

09/02/2020

AR 4392392

21 Pre-NRC Emergency Preparedness Baseline

Inspection

06/30/2021

AR 4410803

1st Quarter ERO Drill Performance

03/22/2021

EP-AA-1000

Standardized Radiological Emergency Plan

EP-AA-1006

Radiological Emergency Plan Annex for Quad Cities Station

Miscellaneous

EP-AA-1006

Addendum 3

Emergency Action Levels for Quad Cities Station

71124.05

Procedures

RP-AA-700-1240

Operation and Calibration of the Canberra ARGOS-5

Personnel Contamination Monitor

AR 4338167

NOS ID: Radwaste Shipping Packages

04/24/2020

AR 4411473

Waste Shipment Manifests

03/25/2021

Corrective Action

Documents

AR 4435171

21 Low Level Waste Project Lessons Learned

07/15/2021

Part 37 Security Plan for the Protection of Category 1 and

Category 2 Quantities of Radioactive Material

N-AN-RP-

10CFR37

Exelon 10 CFR Part 37 Physical Protection of Category 1

and Category 2 Quantities of Radioactive Material

71124.08

Miscellaneous

N-AN-SY-

Protection of Radioactive Material at Quad Cities Generating

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PART37

Station - Part 37 Training

QCCP 0100-12

Chemistry

Department

Special

Evaluation

Beta Smear LLD Determination

03/17/1998

SRRS: 2B.127

Source Inventory Page; Semi-Annual Source

Leak Test Report

05/25/2021

TRM 3.7.g

Sealed Source Contamination

AR 4205154

Radwaste Material Condition

2/12/2019

Self-Assessments

AR 4389672

Radioactive Solid Waste Processing and Radioactive

Material Handling, Storage, and Transportation, 71124.08

10/07/2021

QC-19-080

Filters and Activated Material

10/14/2019

QC-20-074

Dewatered Reactor Water Cleanup Resin

09/15/2020

QC-20-075

Dewatered Reactor Water Cleanup Resin

09/22/2020

Shipping Records

QC-20-076

Dewatered Reactor Water Cleanup Resin

09/29/2020

NRC Performance Indicator Data; Emergency Preparedness

- Alert and Notification System

3rd Quarter

20 through

3rd Quarter

21

NRC Performance Indicator Data; Emergency Preparedness

- ERO Participation Drill

3rd Quarter

20 through

3rd Quarter

21

NRC Performance Indicator Data; Emergency Preparedness

- Drill/Exercise Performance

3rd Quarter

20 through

3rd Quarter

21

71151

Miscellaneous

QC-MSPI-05

Quad Cities MSPI Basis Document

AR 4355514

QCOS 0020-04 Complete with Portions UNSAT

07/08/2020

AR 4428172

RCIC Isolated During Performance of MA-QC-IM-1-13201

06/08/2021

Corrective Action

Documents

AR 4445201

RCIC Isolated During Performance of MA-QC-IM-1-13201

09/08/2021

71152

Corrective Action

Documents

AR 4455921

NRC-Identified Documentation Discrepancy for

QCOS 0020-04

10/26/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Resulting from

Inspection

AR 4461856

NRC Observation of Non-Technical Unintended

Consequences

11/18/2021

Miscellaneous

QDC-38110

PowerLabs Report: Failure Analysis of Switch, Pressure,

to 180 PSIG, Rated at 250 VAC

Procedures

MA-QC-IM-1-

201

Unit 2 RCIC Low Reactor Pressure Isolation Calibration and

Channel Functional Test

6