IR 05000254/2020004

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Integrated Inspection Report 05000254/2020004 and 05000265/2020004
ML21036A002
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/04/2021
From: Kenneth Riemer
Division Reactor Projects III
To: Rhoades D
Exelon Generation Co
References
IR 2020004
Download: ML21036A002 (15)


Text

February 4, 2021

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000254/2020004 AND 05000265/2020004

Dear Mr. Rhoades:

On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Quad Cities Nuclear Power Station and discussed the results of this inspection with Mr. K. Ohr, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects

Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000254 and 05000265

License Numbers:

DPR-29 and DPR-30

Report Numbers:

05000254/2020004 and 05000265/2020004

Enterprise Identifier: I-2020-004-0065

Licensee:

Exelon Generation Company, LLC

Facility:

Quad Cities Nuclear Power Station

Location:

Cordova, IL

Inspection Dates:

October 1, 2020 to December 31, 2020

Inspectors:

J. Cassidy, Senior Health Physicist

M. Garza, Emergency Preparedness Inspector

R. Murray, Project Engineer

D. Tesar, Senior Resident Inspector

C. Mathews, Illinois Emergency Management Agency

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Quad Cities Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000254,05000265/20 20-002-00 LER 2020-002-00 for Quad Cities Nuclear Power Station, Unit 1, Main Steam Line Drain Valve Declared Inoperable Due to Improper Torque Switch Setting 71153 Closed

PLANT STATUS

Unit 1

The unit began the inspection period at full-rated thermal power, where it remained for the entire inspection period, with the exception of planned power reductions for turbine testing, scram timing testing, control rod pattern adjustments, and other short-term power reductions as requested by the transmission system operator.

Unit 2

The unit began the inspection period at full-rated thermal power, where it remained for the entire inspection period, with the exception of planned power reductions for turbine testing, scram timing testing, control rod pattern adjustments, and other short-term power reductions as requested by the transmission system operator.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 reactor core isolation cooling on October 26, 2020
(2) Turbine building closed cooling water on October 26, 2020

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the control rod drive system on October 26, 2020.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Zone 8.2.2.A, Unit 2 turbine building, elevation 572'-6", control rod drive pumps on October 19, 2020
(2) Fire Zone 8.2.7.C, Unit 1/2 turbine building, elevation 611'-6", turbine building closed cooling water area on October 19, 2020
(3) Fire Zone 11.2.3, Unit 1 reactor building, elevation 554'-0", northwest corner room - 1A core spray on October 26, 2020
(4) Fire Zone 11.3.1, Unit 2 reactor building, elevation 554'-0", southwest corner room - 2B core spray on October 26, 2020

71111.07A - Heat Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) 1A residual heat removal thermal performance test on November 30, 2020

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating test which was administered between October 13 and November 17, 2020.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed and evaluated licensed operator performance in the control room during downpower, rod pattern adjustment, and scram timing tests on October 20, 2020.
(2) The inspectors observed and evaluated licensed operator performance in the control room during downpower, rod pattern adjustment, and turbine testing on November 7, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated observation of licensed operator requalification training on October 5, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) High pressure coolant injection on November 30, 2020
(2) Core spray on December 1, 2020
(3) Turbine building closed cooling water on December 7, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Work week risk reviews and PARAGON updates on November 2, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (1 Sample)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Issue Report 4386700, "Pin-Hole Leaks 'B' HVAC [heating, ventilation, and air conditioning] System Operability," on November 30, 2020

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change 626394, "Install Bypass Switches for GRP 1 MSIV [main steam isolation valve] Isolation"
(2) Engineering Change 395100, "Replace HPCI [high pressure coolant injection]

Obsolete Temperature Indicating Switches and Thermowells"

(3) Engineering Change 621167, "RCIC [reactor core isolation cooling] Flow Controllers FIC 1(2)-1304-1 Upgrade"

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1) Standby gas treatment post-maintenance testing QCOS-7500-05, -06, -07 on October 22, 2020
(2) Station blackout diesel quarterly on October 29, 2020
(3) Unit 2 emergency diesel generator following 12-year preventive maintenance on November 5, 2020
(4) QCOS 1400-1, "'B' Core Spray Pump Flow Rate Test," on November 16, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) QCOS 1000-04, "RHR [residual heat removal] Service Water Pump 'B' Flow (IST),"

on October 22, 2020

FLEX Testing (IP Section 03.02) (1 Sample)

(1) Emergency portable pump (B.5.B/FLEX) on November 7, 2020

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors completed an evaluation of submitted emergency action level and emergency plan changes on December 2, 2020. This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (2 Samples)

The inspectors evaluated:

(1) Chemical, spill, anticipated transient without scram, loss of torus level on October 20, 2020
(2) Emergency preparedness drill - contaminated injured man on December 9,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS07: High Pressure Injection Systems (IP Section 02.06)===

(1) Unit 1 (10/01/2019-09/30/2020)
(2) Unit 2 (10/01/2019-09/30/2020)

MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)

(1) Unit 1 (10/01/2019-09/30/2020)
(2) Unit 2 (10/01/2019-09/30/2020)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (10/01/2019-09/30/2020)
(2) Unit 2 (10/01/2019-09/30/2020)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (10/01/2019-09/30/2020)
(2) Unit 2 (10/01/2019-09/30/2020)

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)

(1) Unit 1 (10/01/2019-09/30/2020)
(2) Unit 2 (10/01/2019-09/30/2020)

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1)

(10/01/2019-09/30/2020)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1)

(04/01/2019-09/30/2020)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (2 Samples)

The inspectors reviewed the licensees corrective action program for potential adverse trends in:

(1) Elevated offgas flow and radiation monitor adjustments on November 9, 2020, that might be indicative of a more significant safety issue.
(2) Control rod drive hydraulic accumulator unit trend review on December 14, 2020, that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Partial)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1)

(Partial)

Issue Report 4371385, "[Unit] 1C RHRSW [residual heat removal service water] Seal Cooling Line Break," follow-up on December 9, 2020

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs): LER 2020-002-00 for Quad Cities Nuclear Power Station, Unit 1, Main Steam Line Drain Valve Declared Inoperable Due to Improper Torque Switch Setting

(1) LER 2020-002-00, Quad Cities Nuclear Power Station, Unit 1, Main Steam Line Drain Valve Declared Inoperable Due to Improper Torque Switch Setting (ADAMS Accession No. ML20315A447). The inspection conclusions associated with this LER are documented in NRC Integrated Inspection Report 05000254; 05000265/2020003 under Inspection Results Section

INSPECTION RESULTS

Observation: Follow-Up of Residual Heat Removal Service Water Low Pressure Pump Seal Line Break 71152 As documented in NRC Integrated Inspection Report 05000254; 05000265/2020003, the inspectors noted that on September 23, 2020, the licensee generated Issue Report 4371385, "Documenting a Seal Cooling Line Leak from the Unit 1C RHRSW Pump." The inspectors walked down the pump on the same day and noted that the seal cooling line had sheared at a union elbow joint. Additionally, the inspectors noted the piping at the elbow was completely blocked with debris and/or corrosion products and discussed with the licensee. The licensee documented the as found conditions in Issue Report 4371588, "As Found Condition of 1C RHRSW Pump Seal Cooling Line Leak," on September 23, 2020. The inspectors performed additional inspection activities to review the licensee's causal evaluation, and corrective actions associated with this issue during this inspection period as indicated in NRC Integrated Inspection Report 05000254; 05000265/2020003.

The inspectors reviewed the work group evaluation associated with Issue Report 4371385 as well as the documented response from the vendor regarding the loss of seal water flow to the RHRSW pump low pressure seals. In addition, inspectors reviewed the actions from Issue Reports 4371385 and 4371588.

All actions from Issue Report 4371588 are documented as complete with no issues identified.

Actions from Issue Report 4371385 are in progress with extent-of-condition work orders generated and scheduled for completion during the next available work windows for each of the remaining RHRSW pumps. In addition, Action Item 02 to evaluate the need for scheduled preventive maintenance on the low-pressure pump seal lines is in progress and scheduled for completion on January 21, 2021.

The inspectors reviewed the work group evaluation and vendor response associated with Issue Report 4371385. The inspectors requested clarification of statements in the work group evaluation. All questions have been resolved with no additional concerns identified.

The inspectors did identify that the low-pressure seal water piping was not included in the aging management program, the preventive maintenance program, nor were there steps included in the scheduled scope of work to disassemble, clean or inspect the low-pressure seal water piping. The inspectors did not identify any violations of procedural or regulatory requirements during this review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On December 31, 2020, the inspectors presented the integrated inspection results to Mr. K. Ohr, Site Vice President, and other members of the licensee staff.
  • On December 16, 2020, the inspectors presented the licensed operator annual exam inspection results to Mr. R. Ramsay, Operations Training Manager, and other members of the licensee staff.
  • On December 17, 2020, the inspectors presented the IP 71114.04 exit meeting inspection results to Mr. D. Moore, Senior Manager - Emergency Preparedness, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Procedures

QCOP 0300-01

CRD System Startup and Operation

QCOP 0300-02

CRD System Shutdown

QCOP 1300-01

RCIC System Preparation for Standby Operation

QCOP 3800-02

Unit 1 TBCCW System Operation

QCOP 3800-03

Unit 2 TBCCW System Operation

QOM 1-3800-01

Unit 1 TBCCW Valve Checklist

QOM 2-3800-01

Unit 2 TBCCW Valve Checklist

71111.05

Fire Plans

FZ 11.2.3

Unit 1 RB 554'-0" Elev. NW Corner Room - 1A Core Spray

November

2011

FZ 11.3.1

Unit 2 RB 544'-0" Elev. SW Corner Room - 2B Core Spray

October

2013

FZ 8.2.2.A

Unit 2 Turbine Building, Elevation 572'-6", Control Rod Drive

Pumps

October

2019

FZ 8.2.7.C

Unit 1/2 Turbine Building, Elevation 611'-6", Turbine Building

Closed Cooling Water Area

October

2019

71111.07A Work Orders

WO 4678906-01

1A RHR HX Thermal Performance Test

11/30/2020

71111.12

Corrective Action

Documents

IR 4299841

1B TBCCW Hx Requires Additional Maintenance

11/25/2019

IR 4304891

1A TBCCW Hx Requires Additional Maintenance

2/17/2019

IR 4306910

Abnormal Pressure on Keepfill During 2A Core Spray

Surveillance

2/30/2019

IR 4329527

2-3 C-4 Core Spray Pump 'A' High Seal Leakage Alarm

Received

03/25/2020

IR 4333976

Q2R25 As-Left LLRT on HPCI MO 2-2301-5 Exceeds Alert

04/09/2020

IR 4337637

Light to Moderate Corrosion Observed During HPCI

Walkdown

04/22/2020

IR 4347201

EO ID's Excessive No Flow Time During HPCI Venting

06/01/2020

IR 4348145

U2 HPCI Check Valve Response During QCOS 2300-11

06/04/2020

IR 4349837

Unexpected 2B Core Spray Header Low Pressure Alarm

06/11/2020

IR 4350782

U2 HPCI Room Temp High

06/16/2020

IR 4360041

Suspected Crack/Flange Leak in 2B Core Spray Floor Drain

07/30/2020

IR 4363378

U2 HPCI TG MGU Signal Converter Display Not Functioning

08/15/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

IR 4367470

U2 HPCI Check Valve Response During QCOS 2300-11

09/04/2020

IR 4371330

EO ID: 2B TBCCW Pump Oil Leak

09/22/2020

71111.15

Corrective Action

Documents

IR 4386700

Pin-Hole Leaks Found at Weld for 0-5799-381 'B' HVAC

Train

11/27/2020

Engineering

Changes

EC 633107

N-513 Evaluation for Line 1/2-57479-2 1/2" Through-Wall

Leak

Operability

Evaluations

Op Eval 633095

CR HVAC 'B' Train Piping Line 0-57479-2 1/2" Through-Wall

Leak

Procedures

OP-AA-108-115

Operability Determinations (CM-1)

71111.18

Engineering

Changes

EC 395100, Rev.

001

Replace HPCI Obsolete Temperature Indicating Switches

and Thermowells

04/03/2019

EC 621167, Rev.

000

RCIC Flow Controllers FIC 1(2)-1340-1 Upgrade

01/08/2020

EC 626394, Rev.

000

U-2 Install Bypass Switches for -59" Group 1 MSIV Isolation

2/03/2019

Work Orders

WO 1529963

Replace U2 HPCI TIS 2-2341-3B

09/02/2020

WO 1731449

Failed Instrument, TIS 2-2341-2B

09/02/2020

WO 4943032

Install Bypass Switches for GRP 1 MSIV Isolation 626394

04/16/2020

71111.19

Procedures

QCOS 1400-01

Core Spray System Flow Rate Test

QCOS 1400-10

Core Spray Operability Verification

QCOS 6600-42

Unit 2 Emergency Diesel Generator Load Test

QCOS 6600-45

Unit 2 Diesel Generator Timed Start Test

QCOS 6620-01

SBO DG 1(2) Quarterly Load Test

QCOS 7500-05

SBGTS Monthly Operability Test

QCOS 7500-06

SBGTS Power Operated Valve Test

QCOS 7500-07

SBGT System 24-Month Operability Test

71111.22

Procedures

OP-AA-201-010-

1001

Mitigating Strategies Equipment Expectations

QCOS 1000-04

RHR Service Water Pump Operability Test

Work Orders

WO 5085804

(Flex) Emergency Portable Pump (B.5.B/Flex)

11/07/2020

71114.04

Corrective Action

Documents

IR 4325295

Perform an Impact Review of EAL Revisions for EOP/SAMG

Revision 4

03/10/2020

IR 4328154

EP FAQ EAL Change License Amendment Implementation

03/20/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Actions

IR 4329864

NOS ID: Revise Standardized Emergency Plan

03/26/2020

IR 4334253

Emergency Plan: CDAM 50.54(q) Potential Deficiencies

04/09/2020

Miscellaneous

Eval No. 19-29

Exelon Nuclear Standardized Radiological Emergency Plan

09/04/2019

Eval No. 19-65

Exelon Nuclear Standardized Radiological Emergency Plan

09/06/2019

Eval No. 19-79

Various Station Emergency Plan Annexes

11/08/2019

Eval No. 19-80

On-Shift Staffing Assessments

11/08/2019

Eval No. 20-28

EALs for Quad Cities Station

03/24/2020

71151

Miscellaneous

CY-QC-120-720,

Actual Dose Data - Unit 1

April 2019 -

September

20

CY-QC-120-720,

Actual Dose Data - Unit 2

April 2019 -

September

20

LS-AA-2090

Monthly Data Elements for NRC ROP Indicator - Reactor

Coolant System (RCS) Specific Activity

October

2019 -

September

20

SP-AA-3000,

A

Site Performance Indicator Information

October

2019 -

September

20

71152

Corrective Action

Documents

IR 4317442

U1 MCR Received Alarm 901-3 D2 Offgas High Radiation

2/13/2020

IR 4318180

U1 MCR Received Alarm 901-3 D2 Offgas High Radiation

2/15/2020

IR 4353803

Unexpected Receipt of 901-3 D-2 (Offgas High Rad)

06/30/2020

IR 4356753

901-D2 Offgas High Radiation Alarm

07/14/2020

IR 4358010

Offgas Rad Monitor Setpoint Need Adjusted

07/21/2020

IR 4363085

Unexpected Offgas High Radiation Alarm

08/14/2020

IR 4371385

U1C RHRSW Pump Seal Line Leak

09/23/2020

IR 4371588

As Found Condition of 1C RHRSW Pump Seal Cooling Line

Leak

09/23/2020

IR 4383062

Offgas Rad Monitor Setpoints Need Adjusted

11/08/2020

IR 4383559

'B' CREV HVAC AHU Motor Overload

11/11/2020

IR 4389289

2D RHR Pump Breaker Auxiliary Contracts High Resistance

2/09/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

CY-QC-170-301

Offsite Dose Calculation Manual (ODCM) Special

Distribution (Change SRRS ID Number to 2C.110 Before

Archiving)

14