HL-4590, Special Rept 2-94-001:on 940517,fire Rated Assembly Was Inoperable for Longer than 14 Days as Result of Planned Activities.Caused by Affected Assemblies & Sealed Devices

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Special Rept 2-94-001:on 940517,fire Rated Assembly Was Inoperable for Longer than 14 Days as Result of Planned Activities.Caused by Affected Assemblies & Sealed Devices
ML20069A062
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 05/17/1994
From: Beckham J
GEORGIA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
2-94-001, 2-94-1, HL-4590, NUDOCS 9405240223
Download: ML20069A062 (3)


Text

_.

, q Georgia Power Company 40 inverness Center Parkway Post Offee Box 1295 Birmingham, Alabama 35201 Torophone 205 877-7279 m

J. T. Beckham, Jr. Georgia Power Vice Prenv.ient Nucioa.

Hatch Project ite < # + m eb/sc sywm May 17, 1994

, Docket No. 50-366 HL-4590 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Edwin 1. Ilatch Nuclear Plant - Unit 2 Special Report 2-94-001 Fire Rated Assembly Inoperablc for Greater Than 14 Days Gentlemen:

In accordance with the requirements of the Unit 2 Technical Specifications and Fire Ilazards Analysis, Georgia Power Company is submitting the enclosed special report concerning an event where a fire rated assembly was inoperable for longer than 14 days as l the result of planned activities.

If you have any questions, please contact this ofTice.

j Sincerely,  ;

& N J. T. Beckham, Jr.

JKB/cr

Enclosure:

Special Report 2-94-001 cc: Georgia l'ower comjgag Mr. II. L. Sumner, General Manager - Nuclear Plant NORMS LI.S. Nuclear Rezadatorv Commission. Washington. D.C.

Mr. K. Jabbour, Licensing Project Manager - Hatch LLS. Nuclear Rerulatory Commission Region 11 Mr. S. D. Ebneter, Regional Administrator Mr. L. D. Wert, Senior Resident inspector - Hatch .

" J 9405240223 940517 PDR ADOCK 05000366 lj G PDR t

t 7, , #

1 Enclosure Edwin I. Hatch Nuclear Plant - Unit 2 Special Report 2-94-001 Fire Rated Assembly Inoperable for Greater Than 14 Days A. Br_quirement for Report This report is required by the Plant Ilatch Unit 2 Technical Specifications, Section 6.9.2, and the Plant llatch Fire Hazards Analysis, Appendix B, Section 1.1.1. Specifically, Technical Specifications Section 6.9.2 states:

Special Reports for fire protection equipment operating and surveillance requirements shall be submitted, as required, by the Fire Hazards Analysis (FHA) and its Appendix B requirements.

FHA Appendix B, Section 1.1.1, states:

Fire-rated assemblics and sealing devices in fire rated assembly penetrations separating fire areas or separating portions of redundant systems important to' safe shutdown within a fire area shall be " OPERABLE." -

Furthennore, Action Statement (a) of Appendix B, Section 1.I'.1, allows the fire rated assembly and/or sealing devices to be inoperable provided, within I hour a continuous fire watch on at least one side of the affected assembly (s) and/or scaling .

device (s)is established, or fire detectors are verified operable on at least one side of the inoperable barrier and an hourly fire watch, patrol is established. . Action statement (b) states that, if the barrier is not returned to opeinble status within.14.

days, a special report must be submitted to the NRC within the next 30 days. On April 20,1994, fire door 2L48-2R23 had been inoperable for greater than 14 days.

B. Unit Statul_aLTirns of Event On April 20,1994, Unit 2 was in shutdown for a planned refueling outage.

C. Ds.sg.tiption i of Event This report describes an event in which a fire rated assembly was breached in a .

controlled manner to' support Unit 2 outage work and, as a result, was required to  ;

remain inoperable for more than 14 days On March 17,1994 at 1513 CDT, fire i door 2L48-2R23 was blocked open, Limiting Condition for Operation :(LCO) l 2 94-108 was entered, and an hourly fire watch was established as required by the HL-4590 E-1

__ u _

n;; : . L e Enclosure ~ '

Special Report 2-94-001 FHA, Appendix B, Section 1.1.1., action statement (a). On March 25,1994, off load of the nuclear fuel from the reactor vessel was completed and fire door 2L48-2R23 was no longer required to be operable. On ' April 14, 1994, fuel reload was initiated. On April 20, 1994, fire door 2L42-2R23 had remained inoperable for 3 longer than 14 days. The door was open from March 17,1994, until April 26,1994; i however, fuel was not in the vessel from March 25, 1994, until April 14, 1994, during which time door operability was not required.

D. Quse of the Event The fire rated assembly was breached in a controlled manner to support scheduled refueling outage work. Fire door 2L48-2R23 serves as an entrance between the Turbine Building and Reactor Building 130 foot elevation and as such is located in a high personnel traflic area. Fire door 2L48-2R23 was blocked open in a controlled manner during the Unit 2 refueling outage.

E. Analysis of Event :I In this event, Operations personnel declared fire door 2L48-2R23 inoperable on Mar.h 17,1994. Appropriate fire detectors were verified to be operable and an hourly fire watch patrol was established as required by the FHA, Appendix B,-

Section 1.1.1., action statement (a).

Since all actions required by Appendix B of the FHA were taken immediately upon declaring the door inoperable and remain in effect, it is concluded this event did not -

adversely affect nuclear safety.

F. Corrective Actions Fire door 2L48-2R23 was declared inoperable. LCO 2 94-108 was initiated, appropriate fire detectors were verified to be operable, and an hourly fire watch was established as required by the FHA, Appendix B, Section 1.1.1., - action statement (a). These actions were taken on March 17, 1994 when the door was blocked open in a controlled manner.

On April 26, 1994, fire door 2L48-2R23 was restored to operable status and LCO 2-94-108 was terminated.

IIL-4590 - E-2 i