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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217D3951999-10-13013 October 1999 Forwards Request for Addl Info Re Util 990806 Submittal on USI A-46, Implementation Methodology Used at Pilgrim Nuclear Power Station, Per GL 87-02 ML20217E1581999-10-0808 October 1999 Forwards Insp Rept 50-293/99-05 on 990726-0905.Three Violations Noted & Being Treated as Ncvs.Violations Include Failure to Assure That Design Bases Correctly Translated Into Specifications ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20212J8301999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Pilgrim Nuclear Power Station.Staff Conducts Reviews for All Operating NPPs to Integrate Performance Info & to Plan Insp Activities at Facility Over Next Six Months ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212F7871999-09-24024 September 1999 Advises That Util 990121 Application for Amend Being Treated as Withdrawn.Proposed Changes Would Have Modified Facility UFSAR Pertaining to Values for post-accident Containment Pressure Credited in Pilgrim Net Positive Head Analyses ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20212C2861999-09-16016 September 1999 Forwards SER Accepting Licensee 981123 Request for Relief RR-E1,RR-E5,RR-E6 Pursuant to 10CFR50.55a(a)(3)(i) & Request for Relief RR-E2,RR-E3 & RR-E4 Pursuant to 10CFR50.55a(a)(3)(ii) ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211H5701999-08-27027 August 1999 Forwards Insp Rept 50-293/99-04 on 990610-0725.Two Violations Identified Being Treated as non-cited Violations ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20210U7521999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opossing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U6691999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opposing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U5761999-08-18018 August 1999 Responds to Opposing Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts. Informs That for Sale,Nrc Responsible for Only Ensuring That Entergy Technically & Financially Qualified to Operate NPP ML20210U5151999-08-17017 August 1999 Forwards Notice of Withdrawal of Application for Approval of Indirect Transfer of FOL for Pilgrim in Response to .Approval No Longer Needed Since Beco Sold Interest in Pilgrim to EOI on 990713 ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216E2321999-07-26026 July 1999 Discusses GL 92-01,rev 1,suppl 1, Rv Structural Integrity. NRC Revised Info in Rvid & Releasing as Rvid Version 2 ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210E2231999-07-20020 July 1999 Discusses Arrangements Made by Dennis & M Santiago During 990615 Telephone Conversation for NRC to Inspect Licensed Operator Requalification Program at Pilgrim During Wk of 991004 ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210A9441999-07-14014 July 1999 Responds to Re Changes to Pilgrim Nuclear Power Station Physical Security Plan Identified as Issue 2,rev 14, Addendum 1,respectively.No NRC Approval Is Required IAW 10CFR54(p) ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20209G2251999-07-0909 July 1999 Forwards Insp Rept 50-293/99-03 on 990419-0609.Five Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations,Consistent with App C. Several Individual Tagging Errors Occurred ML20209C4661999-07-0707 July 1999 Forwards SE Accepting Addendum on Proposed Change in Corporate Ownership Structure Involving Entergy Nuclear Generation Co ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20196J7251999-07-0101 July 1999 Informs of Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, for Pilgrim Nuclear Power Station ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20196H2381999-06-29029 June 1999 Forwards SER Denying Licensee 980820 Request for Alternative Under PRR-13,rev 2 for Use of Code Case N-522 During Pressure Testing of Containment Penetration Piping ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20209A8761999-06-28028 June 1999 Forwards SER Authorizing Licensee 990317 Relief Request to Use ASME Code Case N-573 as Alternative to ASME Code Section XI Article IWA-4000 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 ML20195G3721999-06-0707 June 1999 Informs That Proposed Indicators Failed QA Assessments for Digital Verification,Validation & Control of Software. Proposed Mod Can Be Completed on-line ML20195B5021999-05-27027 May 1999 Provides Suppl Info to 990203 Request of Beco That NRC Consent to Indirect Transfer of Control of Util Interest in License DPR-35.Request Described Proposed Merger of Bec Energy with Commonwealth Energy Sys ML20207D4681999-05-24024 May 1999 Provides Addl Info to That Included in Beco Ltr 98-123 Dtd 981001,addressing NRC Concerns Described in GL 96-06, Concerning Waterhammer in Reactor Bldg Closed Cooling Water Sys ML20195B9051999-05-20020 May 1999 Forwards Completed Renewal Applications for Listed Operators.Without Encls ML20206J4901999-05-0606 May 1999 Forwards Completed License Renewal Application,Including Forms NRC-398 & 396 for Sc Power,License OP-6328-3 ML20206P0711999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee, for K Walz,License SOP-10886-1.Encl Withheld IAW 10CFR2.790(a)(6) ML20206D3621999-04-27027 April 1999 Informs NRC That Final Five Sys self-assessments Required to Fulfill Commitment Made in 980828 Response to Insp Rept 50-293/98-04 Were Completed on 990422.Completion Was Delayed by High Priority Refueling Outage 12 Preparatory Work ML20205R9871999-04-21021 April 1999 Forwards Affidavit of JW Yelverton of Entergy Nuclear Generation Co Supporting Request for Withholding Info from Rept on Audit of Financial Statements for Year Ended 971231. Pages 16 & 18 of Subj Rept Also Encl ML20207B0891999-04-20020 April 1999 Forwards e-mail Message from Constituent,J Riell Re Y2K Compliance of Nuclear Power Plant in Plymouth,Massachusetts. Copy of Article Entitled Nuke Plants May Not Be Y2K Ready Also Encl ML20206A2741999-04-16016 April 1999 Dockets Encl Ltr Which Was Sent to AL Vietti-Cook Re Condition of Approval of Transfer of License & License Condition for DPR-35.Encl Resolves Issues Between Attorney General of Commonwealth of Massachusetts & Applicants ML20205P9131999-04-16016 April 1999 Submits Applicant Consent to Listed Condition of Approval of Transfer of License & License Condition for License DPR-35 & Affirmatively Request That NRC Adopt Listed Language in Order ML20205P9271999-04-16016 April 1999 Withdraws Motion for Leave to Intervene & Petition for Summary Or,In Alternative,For Hearing.Requests That NRC Adopt Condition of Approval of Transfer of License & License Condition Agreed to Beco & Entergy Nuclear Generation Co ML20205Q9231999-04-15015 April 1999 Forwards Proprietary & non-proprietary Addl Info in Support of Request to Transfer of Plant FOL & Matls License to Entergy Nuclear Generation Co.Proprietary Info Withheld,Per 10CFR2.790 ML20205P9631999-04-15015 April 1999 Provides Attachments a & B in Support of Request for Transfer of Plant Operating License & NRC Matl License from Beco to Entergy Nuclear Generation Co as Submitted in Ref 1. Info Provided in Response to Request at 990413 Meeting ML20205H9281999-04-0707 April 1999 Requests Withdrawal of Uwua Locals 369 & 387 Unions Joint Intervention in Listed Matter ML20205F3731999-04-0202 April 1999 Submits Addl Info Provided in Support of Request for Transfer of Pilgrim Nuclear Power Station Operating License & Matls License.State of Ma Order Authorizing Divestiture & Copy of Financial Arrangement Encl ML20204H3771999-03-26026 March 1999 Informs That Local 387,Utility Workers Union of America,AFL- Cio Voted to Approve New Contract with Entergy Nuclear Generation Co & Voted to Accept Boston Edison Divestiture Agreement ML20205D4231999-03-24024 March 1999 Forwards Decommissioning Funding Rept for Pilgrim Nuclear Power Station,In Accordance with 10CFR50.75(f)(1) 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARBECO-90-108, Forwards Anticipated Operator Licensing Exam Schedule Requested by Generic Ltr 90-07, Operator Licensing Natl Exam Schedule,1990-09-12012 September 1990 Forwards Anticipated Operator Licensing Exam Schedule Requested by Generic Ltr 90-07, Operator Licensing Natl Exam Schedule, ML20059D6641990-08-30030 August 1990 Forwards Revised Emergency Plan Implementing Procedures,Per 10CFR50,App E,Section V.W/O Encl ML20059D6791990-08-30030 August 1990 Notifies That Two Remaining Actions for Implementation of SPDS at Plant Complete,Per .Spds Procedures Modified,Identifying Sampling Panel C-19 Return Valves to Operator BECO-90-100, Advises That Valve MO-1001-50 Cannot Be Shown to Meet 30-day Mission for PASS in post-accident Environ Due to Elevated Radiation Dose Rates.Util Currently Developing Solution to Allow PASS to Meet 30-day Availability Requirement1990-08-27027 August 1990 Advises That Valve MO-1001-50 Cannot Be Shown to Meet 30-day Mission for PASS in post-accident Environ Due to Elevated Radiation Dose Rates.Util Currently Developing Solution to Allow PASS to Meet 30-day Availability Requirement BECO-90-102, Forwards Fitness for Duty Program Performance Data for Jan- June 19901990-08-23023 August 1990 Forwards Fitness for Duty Program Performance Data for Jan- June 1990 BECO-90-095, Informs That Kn Taylor Permanently Reassigned to Nuclear Training Dept as of 900717.Taylor Will Remain in Position Which Does Not Require License Certification1990-08-0808 August 1990 Informs That Kn Taylor Permanently Reassigned to Nuclear Training Dept as of 900717.Taylor Will Remain in Position Which Does Not Require License Certification BECO-90-092, Forwards, Decommissioning Funding Rept, Per 10CFR50.33(k) & 50.75(b)1990-07-26026 July 1990 Forwards, Decommissioning Funding Rept, Per 10CFR50.33(k) & 50.75(b) ML20044B3111990-07-11011 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Corrective Actions Include Replacement of Transmitters Identified in Suspect Lots & Implementation of Surveillance Program ML20044A7891990-06-19019 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Table Listing Status of Each Issue Encl ML20043D7181990-05-31031 May 1990 Advises That Response to NRC 900426 Safety Evaluation Re Util 880804 & 890619 Responses to Generic Ltr 88-01 Will Be Sent on 901115 ML20043A8211990-05-15015 May 1990 Notifies of Change of Senior Operator Status for Cj Martin, Per 10CFR50.74.CJ Martin Will No Longer Participate in Licensed Operator Requalification Training Program ML20042F2211990-05-0101 May 1990 Advises That Scheduled Completion of SPDS Human Factors Validation Activities Scheduled for 900630 & Sys Availability Test by 900731 ML20043B3881990-05-0101 May 1990 Responds to Violations Noted in Insp Rept 50-293/90-05. Corrective actions:82 Excess Flow Check Valves Installed & Operability of Valves Verified by Performing Surveillance Testing ML20012F5601990-04-0202 April 1990 Responds to Generic Ltr 89-13 Re Svc Water Sys Problems Affecting safety-related Equipment.Util Instituted Biofouling Control Program in 1982 & Program Has Been Effectively Implemented at Plant & Complies W/Generic Ltr ML20012F3631990-03-30030 March 1990 Requests Temporary Waiver of Compliance from Requirements of Tech Spec Table 3.2.C-1, APRM Upscale Rod Block in Startup & Refuel Modes to Avoid Unnecessary Delay in Critical Path Surveillance Testing ML20012C6501990-03-15015 March 1990 Responds to Generic Ltr 90-01 Re Request for Voluntary Participation in NRC Regulatory Impact Survey.Completed Questionnaire for Applicable Areas Delineated in Survey Encl ML20012D1931990-03-15015 March 1990 Forwards Proposed Scope & Objectives of Annual Exercise 90-04-B Scheduled for 900618 Per Lazarus 890609 Ltr, Emergency Exercise Objective & Scenerio Guidelines. Exercise Will Test & Evaluate Util EPIPs ML20012C7191990-03-14014 March 1990 Forwards Explanation of Errors in 890707 Application Re Corrective Action Plan & Advises That Errors Do Not Affect Technical Basis on Which Exemption Granted.Util Corrective Action Plan Remains Unchanged ML20011F5381990-02-26026 February 1990 Responds to Violations Noted in Insp Rept 50-293/89-12 on 891002-1119.Corrective Actions:On 891109,operations Personnel Directed,Via Night Orders,To Be More Diligent W/ Tagout Documentation & Boundary Tagging Clarified ML20011F2301990-02-23023 February 1990 Notifies of Change in Status of Senior Licensed Operator. DW Gerlits Terminated Senior Reactor Operator License on 900201 But Will Retain Position as Senior Sys & Safety Analysis Engineer ML20006G1411990-02-23023 February 1990 Advises That Tj Mcdonough Reassigned Effective 900126. Individual Will No Longer Participate in Licensed Operator Requalification Training Program ML20011F6521990-02-21021 February 1990 Forwards Inservice Insp Plan for 1990 mid-cycle Spring Outage for Facility.Augmented Insp Will Be Performed for Three IGSCC Category a Welds Using Guidance in Generic Ltr 88-01 & Criteria in NRC Bulletin 88-08,Suppl 3 ML20011F4481990-02-20020 February 1990 Forwards Revised Operability Evaluation of Salt Svc Water Pumps for Plant.Evaluation Concludes That Salt Svc Water Pumps Operable & Requirements of Tech Spec 3.5.B.1 for Pumps Met ML20006G0051990-02-20020 February 1990 Forwards Update to long-term Plan,In Accordance W/Section V.A of Plan for Long-Term Program. Util Implementing Plant Betterment Mods & Activities ML20011E7551990-02-0909 February 1990 Requests Temporary Relief from Tech Spec 4.7.A.2.b.1.d, Limiting Condition for Operation. ML19354E7661990-01-23023 January 1990 Responds to NRC Bulletin 89-002, Stress Corrosion Cracking of High Hardness Type 410 Stainless Steel Bolting in Anchor Darling.... Review Determined That No Subj Anchor Darling Swing Check Valves or Similar Valves Installed at Facility ML20011F4441990-01-19019 January 1990 Forwards Operability Evaluation Re Salt Svc Water Pumps P208 B,C,D & E,Per 900117 Telcon.Evaluation Concluded That Salt Svc Water Pumps P208 B,C,D & E Operable & Tech Spec 3.5.B.1 Requirements Met ML20006A0761990-01-15015 January 1990 Forwards Executed Amend 10 to Indemnity Agreement B-48 ML20006A2591990-01-15015 January 1990 Responds to Generic Ltr 89-10, Safety-Related Motor- Operated Valve Testing & Surveillance. Util Will Develop Program to Enhance Maint,Analysis & Testing Already Conducted on motor-operated Valves ML20005G7701990-01-11011 January 1990 Discusses Revised Schedule for Operability & Availability of Spds,Per 891221 Notification to Nrc.Rev Necessitated by Software Problems Affecting 891231 Schedule Projected in Util 890710 Ltr ML20005G7451990-01-11011 January 1990 Provides Bases for Environ Qualification of Instrumentation Monitoring Effluent Radioactivity & Status of Standby Power Per Reg Guide 1.97,Rev 3 & Generic Ltr 82-33 ML20005G8061990-01-11011 January 1990 Advises That Commitment to Complete Enhancements of Control Panels as Part of Dcrdr,Per NUREG-0737,Item I.D.1 by Oct 1989 Not Met.All Three Panels at Simulator Enhanced & Installation of Revised Meter Scales in Progress ML20005F0761990-01-0404 January 1990 Forwards Revised Inservice Test Program in Response to Generic Ltr 89-04.List of Inservice Test Program Relief Requests Previously Submitted & Acceptable,Per Generic Ltr 89-04,encl ML20005E5601989-12-29029 December 1989 Certifies That Util Has Established Fitness for Duty Program That Meets Requirements of 10CFR26.Drug & Alcohol Level Screening Match Rule Imposition & Implementation Will Be Effective on 900103 ML20042D4821989-12-26026 December 1989 Responds to Violations Noted in Insp Rept 50-293/89-10. Corrective Action:Radiological Section Standing Order 89-09 Issued Allowing Only Radiological Supervisors to Exercise Locked High Radiation Area Door & Key Control ML20011D6851989-12-14014 December 1989 Forwards Response to Generic Ltr 89-21, Request for Info Re Status of Implementation of USI Requirements. ML20011D1631989-12-14014 December 1989 Forwards Pilgrim Nuclear Plant Station Final Assessment Rept, Summarizing Results of self-assessments & Evaluations Conducted Throughout Implementation of Plant Restart Plan & Power Ascension Program ML19325F2751989-11-10010 November 1989 Responds to NRC Bulletin 88-010,Suppl 1, Nonconforming Molded-Case Circuit Breakers. Util Installed H2/02 Analyzers Procured in 1980 & Therefore Exempt from Bulletin Requirements ML19327C0911989-11-0606 November 1989 Forwards Response to Suppl 3 to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. Since cyclic- Thermal Heatup/Cooldown Not Present in Piping,Failure Due to Cyclic Thermal Fatigue Will Not Occur ML19325E8581989-11-0101 November 1989 Discusses Litigation Before FERC Re Plant.Util Will Undertake Review of Matls Developed by Opposing Parties in Proceedings.Required Repts Will Be Submitted to NRC After Reportability Has Been Determined ML19325E5251989-10-27027 October 1989 Responds to Generic Ltr 88-20,Suppl 1,describing Plan for Completing Individual Plant Exam for Severe Accident Vulnerabilities.Performance of Level 1 PRA Based on Current Plant Design & Operation Intended ML19325E5661989-10-27027 October 1989 Response to Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. Revised Inservice Testing Program Which Will Include Statement of Conformance to Technical Positions Will Be Submitted by 891215 ML19324B8191989-10-25025 October 1989 Informs That C Leonard & J Stokes Reassigned to Positions Which Do Not Require License Certification Effective 891003 & 891020,respectively ML19327B2291989-10-20020 October 1989 Responds to Generic Ltr 89-07 Re Power Reactor Safeguards Contingency Planning for Surface Vehicle Bombs.Changes Made to Contingency Plan,Per 10CFR50.54.Plan Withheld (Ref 10CFR73.21) ML19325E0981989-10-20020 October 1989 Responds to NRC Re Violations Noted in Insp Rept 50-293/89-07.Corrective Actions:Terminal Block Replaced, post-work Functional Test of Ref Temp Switches Performed & Procedure Tp 88-78 Revised to Correct Relay Numbers BECO-89-142, Responds to NRC Re Violations & Proposed Imposition of Civil Penalty from Insp Rept 50-293/89-95. Corrective Action:Two Responsible Util Operators Suspended Because Breakers Incorrectly Positioned for Test1989-09-22022 September 1989 Responds to NRC Re Violations & Proposed Imposition of Civil Penalty from Insp Rept 50-293/89-95. Corrective Action:Two Responsible Util Operators Suspended Because Breakers Incorrectly Positioned for Test BECO-89-144, Requests Interim Approval for Relief from Testing of RHR Sys Valves 63 & 64 Until Refueling Outage 8 Scheduled for 9103151989-09-22022 September 1989 Requests Interim Approval for Relief from Testing of RHR Sys Valves 63 & 64 Until Refueling Outage 8 Scheduled for 910315 BECO-89-135, Forwards Util Anticipated OL Exam Schedule,Per 890706 Generic Ltr 89-12 Request1989-09-11011 September 1989 Forwards Util Anticipated OL Exam Schedule,Per 890706 Generic Ltr 89-12 Request BECO-89-131, Forwards Tech Spec Figures 6.2-2 & 6.2-1,replacing Title of Director of Nuclear Engineering W/Title of Station Director & Adding New Title of Vice President of Nuclear Engineering1989-09-0505 September 1989 Forwards Tech Spec Figures 6.2-2 & 6.2-1,replacing Title of Director of Nuclear Engineering W/Title of Station Director & Adding New Title of Vice President of Nuclear Engineering BECO-89-129, Submits Addl Info Re 890707 Request for Exemption from Certain Containment Leakage Testing Requirements of 10CFR50. Plant mid-cycle Maint Outage,Previously Scheduled for Oct 1989,has Been Rescheduled for Spring 19901989-09-0101 September 1989 Submits Addl Info Re 890707 Request for Exemption from Certain Containment Leakage Testing Requirements of 10CFR50. Plant mid-cycle Maint Outage,Previously Scheduled for Oct 1989,has Been Rescheduled for Spring 1990 1990-09-12
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- t BOSTON E'Ois O N COMPANY B00 BOYLSTON STREET GOSTON, MASSACHUSETTS O2199 J. EDWARO HOWARO January 27, 1987 BECo 87-015 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 License DPR-35 Docket 50-293
Subject:
Request for Emergency Relief from Technical Specification 4.7.B.2.a Control Room High Efficiency Air Filtration System
References:
- 1) BECo Letter #87-007, dated January 19, 1987, " Proposed Technical Specification Change to Section 4.7.B.2.a"
- 2) NRC Letter to Boston Edison dated January 7, 1975
- 3) BECo Letter to NRC dated May 1, 1975
Dear Sir:
This letter requests emergency relief from Technical Specification (Tech Spec) 4.7.B.2.a while our Tech Spec change (Reference 1) is being processed.
' Relief is required by January 31, 1987 in order to support fuel off-load at i Pilgrim Station.
Emergency relief is requested because the Tech Spec required surveillance is overly conservative and unachievable even when the system performs as designed. At this time the system is physically operable, can perform its intended safety function and yet is unable to pass the surveillance test as currently specified.
Our research into the origin of this surveillance requirement has led us to conclude that it was incorrectly incorporated into the Tech Spec probably due
{ to an undetected typographical error (see enclosure). Since it's receipt, the surveillance has been met only with great difficulty and by utilizing a 110%
fan flow tolerance on the design flow rate (1000 cfm).
The NRC resident inpsector and plant personnel believed a Tech Spec change requested in August 1985 would address this problem. This Tech Spec change referred to involved the same section of the Tech Spec but did not address
- this issue. Accordingly, we did not recognize the continued existence of this problem until late December 1986.
Recognizing the impending fuel movement date, we pursued all available avenues of compliance to avoid requesting relief. We tested and retested the system, making adjustments and replacing components. We also considered the O
8701300123 870127 QO PDR ADOCK 05000293 1)1 P PDR
BOSTON EDISON COMPANY January 27, 1987 U.S. Nuclear Regulatory Commission Page 2 re-scheduling of fuel movement. However, our attempts proved to be unsuccessful.
One avenue which we are continuing to explore is to perform a temporary modification under 10CFR50.59. This would enable the system to pass the test and would negligibly reduce design margin. While this is allowable, in our judgement, emergency relief is preferred to the temporary modification because ,
it does not unnecessarily change the configuration of the plant to resolve an I administrative error.
Should the Tech Spec problem not be resolved, the impact on the outage is twofold:
- 1. delay fuel movement which results in additional delays of other outage tasks that cannot begin until fuel is removed from the vessel, and
- 2. replacement of fuel costs of approximately 300 thousand dollars per day could total in excess of 13 million dollars.
Additional information and justification for this request is enclosed.
No interim compensatory measures are required while the Tech Spec change is being processed because the system is fully operational and meets its design basis. It cannot, however, be qualified against overly restrictive criteria currently in the Tech Spec.
The system exists to protect control room personnel in the event of a radiological event; its presence or absence therefore has negligible impact on the external environment. Emergency breathing apparatus is available as a back-up measure to ensure control room habitability. The change does not create undue risk, and will not endanger life or property because the change will serve to ensure proper system operability.
Reference 1 provided the information necessary to conclude no significant hazards considerations exist and included revised Tech Spec pages.
Mr. Robert Hallisey, Director Radiation Control Program, Mass. Dept. of Public Health was contacted on January 26, 1987 and apprised of the contents of this letter, the January 19, 1987 letter, and the circumstances involved in this issue.
Very truly yours, TAV/ns f%J Enclosure l cc: see next page i
BOSTON, EDISON COMPANY January 27, 1987 U.S. Nuclear Regulatory Commission Page 3 cc: Mr. John A. Zwolinski, Director BWR Project Directorate #1 Division of Licensing Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, DC 20555 Dr. Thomas E. Murley Regional Administrator Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, PA 19406
Enclosure to BECo Letter 87-015 dated, January 27, 1987 DISCUSSION:
The intent of the existing Tech Spec surveillance 4.7.B.2.a is to ensure that filter cartridges in the control room high efficiency air filtration system are clean and unrestricted. To ensure this a differential pressure measurement is taken at design flow rate and compared to the surveillance test limit. The existing limit is too restrictive in that the acceptance criterion of 3" of water at 1000 cfm can only be achieved with the application of the i 101 fan flow tolerance found in Tech Spec 3.7.B.2.d. This has been our procedural practice since the incorporation of 4.7.B.2.a into Pilgrim's Tech Specs. The history of how these acceptance criteria came about lends credence to the fact that this is not a technical issue but merely administrative.
In a letter dated January 7,1975, ( Attachment 2) the NRC requested BECo to augment the Limiting Conditions for Operation (LCO) and Surveillance Requirements related to installed filter systems. These additional LC0's and Surveillances were considered necessary in order to ensure high confidence that the systems will function reliably, when needed, at a degree of efficiency equal to or better than that assumed in the accident analyses.
Accompanying this letter was a set of model Tech Specs for guidance in what the NRC would consider acceptable. For Control Room Air Treatment Systems, the model Tech Specs recommended an acceptance criteria of less than 6" of water at system design flow rate. BECo responded by proposing an acceptance criteria of less than 9.5" of water at 1000 cfm (Attachment 3).
Our notes from a series of telephone conversations between BECo and NRC management indicate that less than 8" of water at 1000 cfm was an acceptable change to our initial proposal of less than 9.5" of water. When the amendment was issued (Amendment 42 dated May 12, 1980) the wording specified less than 3" of water at 1000 cfm. No material can be found on our docket concerning the origin of the 3". This probably was a typographical error. Amendment 42 was necessary for startup from Refuel Outage #4. The surveillance was conducted and passed with the procedural acceptance criteria of 1 10% fan flow. This acceptance criteria of Tech Spec 3.7.B.2.d was assumed to be inherent to the 1000 cfm of Tech Spec 4.7.B.2.a. Plant startup occurred on May 21, 1980.
BECo continued to utilize this assumption, but meeting this specification has been difficult and marginal.
Absent the NRC granting this emergency relief fuel movement could be delayed.
This would effectively derate Pilgrim for whatever period of time it takes to process the change in the normal fashion (i.e., DL Operating Procedure 228).
Delaying fuel movement would result in additional delays of other outage tasks that cannot begin until fuel is removed from the vessel. The external expertise needed to perform these tasks has been pre-arranged and is available for a specified period of time only. Re-scheduling this work would depend
O upon their flexibility in changing commitments already made elsewhere in the Industry. Examples of the tasks which would be jeopardized are:
- Relocation of the Reactor Water Level reference legs outside the drywell to eliminate heatup induced level errors
- - Analog Trip System Installation to improve reliability and eliminate RPS System challenges
- Reactor Vessel Dry Tube Inspection / Replacement (SIL 409)
- In-Vessel Instrument Line Inspection (SIL 420)
- Installation of Hydrogen Water Chemistry Probe.
i Fuel unloading is scheduled to commence on January 31, 1987 and will take
, between 10 and 30 days to complete. Recognizing this date could shift slightly due to unforeseen circumstances, we will keep the NRR Project Manager
- apprised on a daily basis.
Attachments: 1) BECo Letter #87-007, dated January 19, 1987, " Proposed Technical Specification Change to Section 4.7.B.2.a"
- 2) NRC Letter to Boston Edison dated January 7, 1975 1 3) BECo Letter to NRC dated May 1, 1975 i
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10CFR50.90 BOSTON EoisDN COMPANY B00 BovLsTON STREET BOSTON. MASSACHUSETTS 02199 J. EDWARD HOWARD vess pia. sos v January 19, 1987 BECo 87-007 Propo:ed Change 87-01 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 License DPR-35 Docket 50-293 Proposed Technical Specification Change to Section 4.7.B.2.a
Dear Sir,
Pursuant to 10CFR50.90, Boston Edison hereby proposes the attached modification to Appendix A of Operating License No. DPR-35. This modification revises the acceptance criteria for flow and filter train differential pressure for the Control Room High Efficiency Air Filter System (CRHEAF). The proposal is made to reduce overly restrictive criteria, the strict interpretation of which prevents the system from being considered operable.
The strict interpretation is also in conflict with vendor design information.
Should you wish further information on this submittal, please contact us.
Very truly yours,
! PMK/ns Attachment 0
One Original and 37 Copies Commonwealth of Massachusetts)
County of Suffolk )
! Then personally appeared before me, J. E. Howard, who, being duly sworn, did
! state that he is Vice President - Nuclear Engineering and Quality Assurance Department of Boston Edison Company and that he is duly authorized to execute and file the submittal contained herein in the name and on behalf of Boston Edison Company and that the statements in said submittal are true to the best of his knowledge and belief.
My commission expires: /3ddy. dL /988 _
'(
L DATE V NOTARY UBLIC
$ a 4 ee next page . ~
BOSTON EDISCN COMPANY Ja-nuary 19, 1987 ,
J.S. Nuclear Regulatory Commission Page 2 cc: U.S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, PA 19406 Senior P.RC Resident Inspector Pilgrim Nuclear Power Station Robert M. Hallisey, Director Radiation Control Program Mass. Dept. of Public Health .
150 Tremont Street F-7 Boston, MA 02111 1
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Proposed Change to Technical 50ecifications Proposed Change Reference is made to Pilgrim Station Operating License No. DPR-35, page 1588 Sec tion 4.7.8.2.a. This currently states:
At least once every 18 months the pressure drops across each combined filter train shall be demonstrated to be less than 3 inches of water at 1000 cfm.
This will be changed to provide 6 inches of water pressure drop and a 107.
tolerance to the flow rate, and shall state, in part: "
... less than 6 inches of water at 1000 cfm or the calculated equivalent."
Reason for Change .
The change is proposed to allow flexibility in surveilling the Control Room High Efficiency Air Filtration (CRHEAF) system. The existing 1000 cfm is too restrictive in that no tolerance is specified, therefore strict compliance requires a flow rate of exactly 1000 cfm. This is contrary to common operating practice in that it does not provide for small variations in the system, the atmosphere, or measuring at any particular surveillance. .
The "3 inches of water" pressure drop is very restrictive when applied to the combined filter train, as currently required. A review of vendor design information indicates that 3 inches of differential pressure is the vendor recommended action point for changeout for each HEPA filter. Each filter train consists of a prefilter, two HEPA filters, a charcoal adsorber, and heaters, all of which contribute to differential pressure. When 3 inches is applied to the combined HEPA filters it is overly restrictive vis-a-vis the vendor recommended criteria, i.e., filters should be either tested separately to 3 inches or less, or the differential pressure raised to 6 inches or less for the combined filter train.
Safety Considerations The addition of a " calculated equivalent" to the CRHEAF acceptance criteria is in keeping with the standard engineering and operating practice of providing tolerance in measuring HVAC system flow performance, and allows the procedural
.! use of a performance curve with flow rates bounded by TS 3.7.B.2.d.
The changing of the differential pressure criterion to 6 inches of water is i acceptable for the following reasons:
o The summation of vendor recommended action levels for all components in each filter train gives a total differential pressure of approximately 8 inches of water; o The maximum vendor allowed differential pressure across any one HEPA
. unit is 8 inches of water; o The expected value for the summation of component differential pressures for a filter train with new filter media is approximately 3.75 inches of water; l
Therefore, a value of 6 inches of water across the combined filter train components is conservative because it will prompt action before any single HEPA would reach its maximum. and before the vendor recommended level for the combined filter train is reached.
This proposed change has been reviewed by and approved by the Operations Review Committee and reviewed by the Nuclear Safety Review and Audit Committee.
Supporting Information and No Significant Hazards Conditions Analyses The proposed change provides a tolerance to the test success criteria for CRHEAF by allowing the use of a procedural curve relating differential pressure to 1000 cfm as bounded by TS 3.7.B.2.d. The change also raises the differential pressure criteria to 6 inches from 3 inches of water.
The Code of Federal Regulations,10CFR50.91 requires that at the time a licensee requests an amendment, it must provide to the Commission its analysis 4 using the standards in 10CFR50.92, about the issue of no significant hazards consideration. Therefore, in accordance with 10CFR50.91 and 10CFR50.92 the following analysis has been performed.
- 1. Operating Pilgrim Station in accordance with the proposed amendment will not involve a significant increase in the probability or consequences of an accident previously evaluated.
The CRHEAF creates a positive pressure in the Control Room, using air from which it has filtered out radiciodine and particulates. Currently, TS 4.7.B.2.a requires that at least once every 18 months a pressure drop of less than 3 inches of water be demonstrated across the filters at a flow rate of 1000 cfm. TS 3.7.B.2.d requires that CRHEAF fans operate within 1000 cfm 1107.. The system is designed to provide a positive Control Room pressure if the fans can provide a flow rate of 900 to 1100 cfm and the filters are not plugged. Vendor information indicates that filter
- degradation from plugging is indicated by a differential pressure of 3 inches or greater of water across each HEPA filter. Therefore, when j measured across two HEPA filter elements, and the rest of the CRHEAF a
components which create differential pressure, a differential of less than 6 inches of water demonstrates that HEPA plugging has not reached action levels. Hence, if the fans can generate 900 to 1100 cfm to satisfy 3.7.B.2.d, and has a pressure drop across the filter trains less than 6 inches at 1000 cfm or the calculated equivalent, sufficient flow exists to provide a positive pressure in the Control Room. Therefore, the purpose of the CRHEAF as a mitigator of the results of an accident will not be i
impaired by this proposed change. Hence, allowing the differential pressure of 6 inches of water 1000 cfm to be established at flow rates between 900 and 1100 cfm in conformance with a calculated procedural acceptance curve will not involve a significant increase in the probability or consequences of an accident previous!'y analyzed.
i
- 2. Operating Pilgrim Station in accordance with the proposed amendment will not create the possibility of a new or different kind of accident from any i
accident previously evaluated.
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The purpose of CRHEAF is to mitigate the consequences of certain accidents by filtering out radiciodines and particulates from air which is then used to maintain a positive pressure in the Control Room. The amendment allcws a tolerance by allowing a calculated value, based on 6 inches of water at 1000 cfm to be used for demonstrating that the filter train elements are not plugged. The flow range for the calculated value is 900 - 1100 cfm, determined by existing TS 3.7.8.2.d.
The change to 6 inches of water from 3 is in compliance with vendor information. The change of these criteria therefore is consistent with the design and fan capabilities of the system, and does not degrade the system's ability to perform its designed function of providing positive pressure in the Control Room with filtered air; therefore, operating Pilgrim in accordance with the proposed change will not create the possibility of a new or different kind of accident from any accident ,
previously evaluated.
- 3. Operating Pilgrim Station in accordance with the proposed amendment will not involve a significant reduction in the margin of safety.
The proposed change does not reduce the CRHEAF's ability to perform its designed function of creating a positive pressure in the Control Room with filtered air. Hence, accident analysis which take credit for CRHEAF as a mitigator are not affected and the safety margin remains the same.
Therefore, the operation of Pilgrim in accordance with the proposed amendment to TS 4.7.B.2.a will not involve a significant reduction in the margin of safety.
Schedule of Change This change will become effective immediately following approval by the Commission.
Fee Determination Pursuant to 10CFR170.12(c) an application fee of $150.00 is appropriate. The fee will be provided under a separate cover letter in the near future.
. 3.7.B (Continued) 4.7.B (Continued)
- 2. Control Room High E'ficiency Air 2. Control Room High Efficiency Air Filtration System Filtration System
- a. Except as specified it a. At least once every 18 months Specification 3.7.B.2. Delow, the pressure drop across each both trains of the Control Room combined filter train shall be High Efficiency Air Filtration demonstrated to be less than 6 System used for the processing inches of water at 1000 cfm or of inlet air to the control room the calculated equivalent.
under accident conditions and the diesel generator (s) required b. (1.) The tests and analysis for operation of each train of of Specification the system shall be operable 3.7.B.2.b shall be whenever secondary containment performed once every 18 integrity is required and during months or following fuel handling operations. painting, fire or chemical release in any ,
- b. (1.) The results of the inplace ventilation zone cold DOP tests on HEPA communicating with the filters shall show 199% system while the system DOP removal. The results is operating.
of the halogenated hydrocarbon tests on (2.) Inplace cold DOP testing charcoal adsorber banks shall be performed after shall show 199% each complete or partial halogenated hydrocarbon replacement of the HEPA removal when test results filter bank or after any are extrapolated to the structural maintenance initiation of the test. on the system housing which could affect the (2.) The results of the HEPA filter bank bypass laboratory carbon sample leakage.
analysis shall show 195%
methyl lodide removal at a (3.) Halogenated hydrocarbon velocity within 10% of testing shall be system design, 0.05 to performed after each 0.15 mg/m' inlet methyl complete or partial lodide concentration, 170% replacement of the R.H., and 1125'F. charcoal adsorber bank or after any structural
- c. From and after the date that one maintenance on the train of the Control Room High system housing which Efficiency Air Filtration System could affect the is made or found to be incapable charcoal adsorber bank of supplying filtered air to the bypass leakage.
control room for any reason, reactor operation or refueling (4.) Each train shall be operations are permissible only operated with the during the succeeding 7 days. heaters in automatic for If the system is not made fully at least 15 minutes operable within 7 days, reactor every month.
- Conditional Relief granted from this (5.) The test and analysis of LCO for the period February 5, 1982 Specification to startup for cycle 6. 3.7.8.2.b.(2) shall be performed after every 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of system operation.
Amendment No. 158B hb {d -