05000321/LER-1979-082, Updated LER 79-082/03X-2:on 790825-27,attempt to Perform RCIC Pump Operability Procedure Unsuccessful When Turbine Failed to Trip Upon Manual Signal.Caused by Burned Out Turbine Trip Actuator Coils & Binding Assembly

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Updated LER 79-082/03X-2:on 790825-27,attempt to Perform RCIC Pump Operability Procedure Unsuccessful When Turbine Failed to Trip Upon Manual Signal.Caused by Burned Out Turbine Trip Actuator Coils & Binding Assembly
ML20070A747
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/23/1982
From: Tipps S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20070A705 List:
References
LER-79-082-03X, LER-79-82-3X, NUDOCS 8212090341
Download: ML20070A747 (1)


LER-2079-082, Updated LER 79-082/03X-2:on 790825-27,attempt to Perform RCIC Pump Operability Procedure Unsuccessful When Turbine Failed to Trip Upon Manual Signal.Caused by Burned Out Turbine Trip Actuator Coils & Binding Assembly
Event date:
Report date:
3212079082R00 - NRC Website

text

NRC FORM 366 U. S. NUCLE ATJ RE'; ULATORY COMMISSION (7 7h

  • UPDATE REPORT - PREVIOUS

, LICENSEE EVENT REPORT REPORT DATE 11/2/82 CONTROL BLOCK: l l l l l (PLEASE PRINT CR TYPE ALL RELUllED INFC.MATION) 7 o

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'I 8 60 61 DOCKET NUMBER 68 69 EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h O 2 lOn August 25, 1979, with Unit 1 at hot standby, an attempt to perform t-h d O 3 l"RCIC PUMP OPERABILITY" procedure was unsuccessful when the turbine l O 4 l failed to trip upon manual signal. On August 27, 1979, the turbine trio 1 I O l s i land throttle valve again failed to respond to a trip signal. The RCIC l O s Isystem was declared inoperable. This event is contrary to T.S.3.5.E.1. Al l0l7]l7-day LCO was initiated as per Tech. Specs. 3.5.3.E.2. The health and I l O ;g i l safety of the public were not affected by this non-repetitive event. I DE CODE SUBC E COMPONENT CODE SUBCOdE SU F 0 9 l Cl El@ [Ej@ [_B_j @ lV l A l L lV l E l X l@ [_Ej@ (_Dj @

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g lThe August 25, 1979, failure was due to burned out turbine trip actuatorI i i l coils. The burned out coils were replaced. The system was satisfactorily I

, , l tested and returned to service. The August 27, 1979, failure was caused I

, ., lby binding in the spring cylinder assembly. The spring cylinder assembly l

, , lwas replaced and the valve tested satisfactorily and returned to servicd 7 8 9 80 ST S  % POWER OTHER STATUS ISC RY DISCOVERY OESCRIPTION i 5 (G_j @ l0l0l0l@l NA l l3J@l Surveillance Test l A TIVITY CO TENT RELEASED OF RELEASE LOCATION OF RELE ASE i o Lz_1@ ' LtJ@l AMOUNT NA OF "

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