05000321/LER-2002-001, Re Manual Reactor Scram Inserted Because of High Hydrogen Content in the Off Gas System

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Re Manual Reactor Scram Inserted Because of High Hydrogen Content in the Off Gas System
ML020930076
Person / Time
Site: Hatch 
Issue date: 03/26/2002
From: Sumner H
Southern Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
HL-6211 LER-02-001-00
Download: ML020930076 (6)


LER-2002-001, Re Manual Reactor Scram Inserted Because of High Hydrogen Content in the Off Gas System
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv), System Actuation
3212002001R00 - NRC Website

text

Lewis Sumner w

Southern Nuclear Vice President Operating Company, Inc.

Hatch Project Support 40 Inverness Parkway Post Office Box 1295 Birmingham, Alabama 35201 Tel 205.992.7279 Fax 205 992.0341 A

SOUTHERNNO COMPANY Energy to Serve Your World March 26, 2002 Docket No. 50-321 HL-621 1 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Edwin I. Hatch Nuclear Plant -Unit 1 Licensee Event Report Manual Reactor Scram Inserted Because of High Hydrogen Content in the Off Gas System Ladies and Gentlemen:

In accordance with the requirements of 10 CFR 50.73(a)(2)(iv), Southern Nuclear Operating Company is submitting the enclosed Licensee Event Report (LER) concerning a manual reactor scram inserted because of high hydrogen content in the off gas system.

Respectfully submitted, H. L. Sumner, Jr.

OCV/eb Enclosure: LER 50-321/2002-001 cc:

Southern Nuclear Operating Company Mr. P. H. Wells, Nuclear Plant General Manager SNC Document Management (R-Type A02.001)

U.S. Nuclear Regulatory Commission, Washington, D.C.

Mr. L. N. Olshan, Project Manager - Hatch U.S. Nuclear Regulatory Commission. Region II Mr. L. A. Reyes, Regional Administrator Mr. J. T. Munday, Senior Resident Inspector - Hatch Institute of Nuclear Power Operations LEREventsginpo.org makucinjmginpo.org

Abstract

On 02/08/2002, at 2252 EST, Unit 1 was in the Run mode at 27% rated thermal power (746 CMWt). At that time, the Reactor Protection System (RPS) was manually actuated to facilitate placing the Main Condenser mechanical vacuum pump in service. Prior to the reactor shutdown, on 02/08/2002, at approximately 2100 EST, degraded operation of the Main Condenser Off Gas Recombiner System had resulted in high hydrogen in the Off Gas.

Procedure 34AB-N62-001-lS (FAILURE OF RECOMBINER AND CONTROL OF SUSTAINED COMBUSTION IN THE OFF GAS SYSTEM) was entered at about 2100 EST and licensed personnel proceeded to reduce reactor power from 100 percent rated thermal power beginning at about 2105 EST. Per the procedure, the in-service Steam Jet Air Ejector was removed from service at about 2200 EST due to Off Gas Hydrogen concentration reaching approximately 4%. Unit 1 was scrammed to facilitate placing the mechanical vacuum pump in service for maintaining the Main Condenser as the heat sink. The lowest Reactor Water Level during the scram was approximately 165 inches above the top of the active fuel (7 inches above instrument zero) this was above any ESF actuation settings. Therefore, no automatic ESF actuations were received and none were required. There was no Reactor Pressure increases during the scram. Reactor pressure following the reactor shutdown did not exceed the pre-event level of 1035 psig.

The cause of the event was component failures that resulted in blocked drain lines in the off gas system. The blocked drain lines caused the recombining action to degrade resulting in high hydrogen in the off gas system.

Corrective actions included restoring the off gas system drain lines.U.S. NUCLEAR REGULATORY COMMISSION

(-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER (6)

PAGE 3 YEAR SEQUENTIAL REVISION YEAR NUMBER Edwin I. Hatch Nuclear Plant - Unit 1 05000-321 2002 001 00 2 OF 5 TEXT (If more space is required, use additional copies of NRC Forn 366A) (17)

PLANT AND SYSTEM IDENTIFICATION

General Electric -Boiling Water Reactor Energy Industry Identification System codes appear in the text as (EIIS Code XX).

DESCRIPTION OF EVENT

On 02/08/2002, at 2252 EST, Unit 1 was in the Run mode at 746 CMWT (27 percent rated thermal power). At that time, the Reactor Protection System (RPS, EIIS Code JC) was manually actuated to maintain the Main Condenser (EIUS Code Q) as the heat sink.

At 2252 EST on February 8, 2002 the reactor was scrammed at approximately 27% RTP and the Main Turbine subsequently tripped. Per off gas system recorder lN62R602 the point 1 temperature in the Recombiner lN62AOOlA began falling from 320'F to 220'F between 1700 EST and 1730 EST. Between 1700 EST and 1900 EST both points 2 and 3 began falling from 600'F to 400'F on the same recorder lN62R602. At 1930 EST point 2 had fallen to 220'F and Off Gas Hydrogen levels began increasing per recorder1N62R603 at 1935 EST. At 2045 EST point 3 had fallen to 220'F. Per GE SIL 150 Revision 2 Supplement 3, the minimum temperature of 250'F must be maintained to have a dry catalyst surface for gas to gas catalyst contact and to have an adequate catalyst reaction rate constant in the Recombiner. At 2045 EST operators were directed to drain the Preheater (lN62BOO1A, EIIS Code WF) and to check the Electric Boiler (1N62D530, EUS Code WF) with the purpose of correcting the problems associated with the Recombiner. Operators found the Electric Boiler, (EIIS Code WF) flooded and pressurized to about 280 psig.

At about 2100 EST procedure 34AB-N62-00I -1 S (FAILURE OF RECOMBINER AND CONTROL OF SUSTAINED COMBUSTION IN THE OFF GAS SYSTEM) was entered and a power reduction began at 100% RTP at about 2105 EST. The Steam Jet Air Ejector (SJAE, EIIS Code SH) was removed from service at about 2200 EST due to Off Gas Hydrogen concentration reaching approximately 4%. Unit 1 was scrammed to facilitate placing the Main Condenser mechanical vacuum pump in service for maintaining the Main Condenser as the heat sink. The lowest Reactor Water Level during the scram was approximately 7 inches above instrument zero and since that level was above any Engineered Safety Features (ESF) actuation settings, none were received.

The RPS actuation resulted in a rapid insertion of all control rods. As expected, following a reactor scram, void collapse occurred in the reactor core region resulting in a reduction of reactor water level. The lowest level reached during the transient was seven inches above instrument zero (165 inches above the top of the active fuel). The "B" Reactor Feedwater Pump (RFP, EIIS Code SJ) restored water level to normal. Additionally, the reactor pressure did not exceed the pre-event level of 1035 psig.U.S. NUCLEAR REGULATORY COMMISSION (1-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER (6)

PAGE (3) llYEAR lSEQUENTIAL I REVISION I

YEAR INUMBER Edwin I. Hatch Nuclear Plant - Unit 1 05000-321 2002 001 --

00 3 OF 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

CAUSE OF EVENT

This event was the result of component failures. There are six drain lines on the Off Gas system (EIIS Code WF) between the third stage Steam Jet Air Ejector and Catalytic Recombiners (lN62AOOlA and lN62AOO1B). One of these drain lines is unique to the Catalytic Recombiner 1N62A00lB that was not in service during this event. The drain line that is unique to the Catalytic Recombiner IN62AOO 1A that was in service was functioning as designed.

However, the four drain lines on the Off Gas system between the third stage Steam Jet Air Ejector and the Preheater (IN62B00 A) were isolated due to various component failures. Each one of these drain lines has a drain pot that fills with water that actuates a level switch that in turn actuates a one inch solenoid operated valve to open and drain the line. Per the GE SWL 150 Revision 2 Supplement 1, "the system is designed to provide superheated (dry) steam to the recombiner. If the steam entering the recombiner is wet, water collects on the catalyst, inhibiting the recombining action. This results in an uncombined hydrogen/oxygen mixture passing through the recombiner with a constant increase in the hydrogen concentration in the system downstream from the recombiner." Per GE SEL 150 Revision 2 Supplement 3, "smaller sized drains are susceptible to plugging, thereby causing loss of recombination due to catalyst wetting." Although the Unit 1 drain lines are only one inch in diameter and the SIL recommends two inches, plugging was not the cause of this event. However, four of the five drain lines became isolated which resulted in the same consequences as a plugged line.

One drain line (containing valve 1 N62F 13 3A) was concluded to be isolated due to the solenoid valve being in the de-energized closed position and unable to open prior to the event. Two of the drain lines (containing valves 1N62F 1 33B and IN62F0 1 5A) were concluded to be isolated due to their solenoid valves being in the de-energized closed position and unable to open prior to the event and the inability of the valves' level switches (lN62N057B and lN62N056A) to actuate at the appropriate setpoint. One drain line (containing valve 1N62F01 SB) was concluded to be isolated due to the inability of the valve's level switch (IN62N056B) to actuate at the appropriate setpoint.

One drain line (containing valve IN62F 126A) was concluded to be open and draining as required prior to the event.

REPORTABILITY AND SAFETY ASSESSMENT

This report is required pursuant to 10 CFR 50.73(a)(2)(iv) because a condition occurred which required a manual actuation of an engineered safety feature. Specifically, the Reactor Protection System was manually actuated as a conservative action that was not part of a pre-planned normal reactor shutdown.

The Reactor Protection System is designed to automatically shutdown the reactor by rapidly inserting the control rods into the reactor core when sensed parameters exceed predetermined setpoints. One of the parameters sensed is a Main Turbine trip or Turbine Stop Valve (TSV, EIIS Code TA) closure at greater than a nominal 28 percent rated thermal power. A trip of the Main Turbine (i.e., closure of the TSVs) with the reactor at power results in a reactor pressure transient and a reactivity transient. The reactor pressure vessel and the reactor core are designed with ample margin to withstand these transients; however, when a turbine trip is anticipated conservative actions should be taken to manually shut down the reactor to avoid or lessen the transient. An automatic trip of the Main Turbine occurs on Main Condenser low vacuum to preclude damage to the Main Turbine and the Main Condenser due to an over-pressure condition.

In this event, an automatic turbine trip was not imminent; however, the RPS was manually initiated to facilitate placing the mechanical vacuum pump in service, thus preserving the main condenser as a heat sink. The reactor I'U.0.

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0W (1-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL REVISION I

YEAR NUMBER Edwin I. Hatch Nuclear Plant - Unit 1 05000-321 2002 001 00 4 OF 5 TEXT (if more space is required, use additional copies of NRC Form 366A) (17) pressure remained at the pre-event level of 1035 psig. As expected following the scram, void collapse occurred in the reactor core region resulting in a reactor water level transient. The lowest level reached during the transient was seven inches above instrument zero (165 inches above the top of the active fuel) before level was restored by the "B" RFP. Therefore, the reactor pressure vessel was not subjected to any abnormal pressure transients and the fuel was adequately covered during the event.

Based on this analysis, it is concluded that this event did not adversely impact nuclear safety.

CORRECTIVE ACTIONS

The IN62F133A and 1N62F133B solenoid valves were replaced. The lN62FO15A solenoid coil was replaced. The IN62N056B level switch for the IN62F01 SB drain line was repaired. The IN62N056A and IN62N057B level switches for the IN62F01 5A and 1 N62F 133B drain lines will be replaced during the spring 2002 refueling outage.

An interim corrective action has been established to require manually stroking the drain valves open with the control switch periodically (four of the six valves are stroked daily and two of the six drain valves are stroked weekly). An evaluation of the system will be performed to determine the reliability of the drain lines and the components associated with the drain lines by 6/01/2002. This evaluation will determine if the interim actions will continue to be necessary.

ADDITIONAL INFORMATION

No systems other than those described in this report were affected by this event.

There were no previous similar events in the last two years in which the reactor was manually scrammed because of Hydrogen concentration in the off gas system.

Master Parts List Number: IN62F133A and IN62F133B Type: Offgas Preheater Drain Solenoid Valves Manufacturer: Laurence Vendor Code (VPN): L087 EHS System Code: WF EUS Component Code: SLV Root Cause Code: X Reportable to EPIX: Yes IIU.S. NUCLEAR REGULATORY COMMISSION (1-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER (6)

PAGE (3)

YEAR lSEQUENTIAL REVISION l

YEAR INUMBER Edwin I. Hatch Nuclear Plant - Unit 1 05000-321 2002 001 00 5 OF 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

Master Parts List Number: lN62F01 5A Type: Offgas Preheater 1 A Shell Drain Solenoid Valve Manufacturer: Laurence Vendor Code (VPN): L087 Model: 506WA44PSSWS EUS System Code: WF EIIS Component Code: LSV Root Cause Code: X Reportable to EPIX: Yes Master Parts List Number: IN62N056A and IN62N056B Type: Offgas Preheater 1 B Shell Drain Float Level Switches Manufacturer: Robertshaw Vendor Code: R290 Model: SL-326-AlX EUS System Code: WF EIS Component Code: LS Root Cause Code: X Reportable to EPIX: Yes Master Parts List Number: lN62N057B Type: Condensate In Process line Float Level Switch Manufacturer: Robertshaw Vendor Code: R290 Model: SL-326-A2X EIIS System Code: WF EUS Component Code: LS Root Cause Code: X Reportable to EPIX: Yes