/03L-0 on 781102:reactor Maximum Cooldown Rate of 100 Degrees F Exceeded During Reactor Auto Scram & Vessel Depressurization.Caused by Personnel Error;Personnel Have Been Admonished| ML20148P415 |
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| Site: |
Hatch  |
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| Issue date: |
11/20/1978 |
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| From: |
Baxley S GEORGIA POWER CO. |
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| To: |
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| Shared Package |
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| ML20148P410 |
List: |
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| References |
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| LER-78-063-03L-01, LER-78-63-3L-1, NUDOCS 7811280220 |
| Download: ML20148P415 (2) |
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LER-1978-063, /03L-0 on 781102:reactor Maximum Cooldown Rate of 100 Degrees F Exceeded During Reactor Auto Scram & Vessel Depressurization.Caused by Personnel Error;Personnel Have Been Admonished |
| Event date: |
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| Report date: |
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| 3661978063R03 - NRC Website |
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hEFO41 OAl E LJ ot semPTiod AND s'HOULL.E CONSEQUEr:CLS h cvt 70 j l Reactor maximum cooldoun ra te _ of 100 degrys F Per_ lLQUEJIU_.cyceeded on *,'cL_2.._.1928 ]
of,; [ Due to injection of condensate water into reactor vessel followinq a reactor scram I
gj l from rated pressure, reactor pressure decreased di,Lq_t?_mjn_timbjnn seals supplied I
o ;,,,, by nuclear steam to below condensate booster pump pressure and allowed condensate l
o g,, l water to be injected into reactor vessel through feeduater lines, resulting in a cool-1 o,; ; doen rate of 119 degrees F. in a one hour period.
Reactor r1SIV's were closed and j
gi injection of condensate water to vessel stopped, reactor coolant temocratures (con ' t )J B D
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SYSif fA CAU3E
CAUSE
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43 44 47 AUSE DESCRIPTloN AND COnHECTIVE ACTsoN3 h i l o'] [ During reactor auto scram and vcM dopycssuri7atiartj.Lerconnal allowed confersnto I
TlT) I water to be injected into Reactor vessel when pressure decrmsed bninw condebte 1
73 g j booster purp discharge pressure, thus causino rapid croldewn of Reactor coolant i
,j,j[ temperature.
Personnel have been cauticned about reactor nrossure decrexes bolo r I
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Edwin 1. Hatch Power O caxies, ceorsie 31sia Reportable Occurrence f! umber:
50-366/1978-63 l
' Event Description Con't were back within limits in-15 minutes.
Evaluation of occurrence by reactor engineering confirmed that due to evaluatien of other temperatures indications for overall reactor coolant systems and by o');erving rccctor vessel metal temperatures (Delta T's) that no significant stress occurred'io reactor vessel or coolant systems.
There were no personnel injuries or overexposure or any release of radioactive materials to the environs as a result of this occurrence.
Cause Description Con't
^
and to observe pressure decrease and level increase very closely in transient conditions to prevent exceeding reactor cooldcun rates.
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| 05000366/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000366/LER-1978-006-03, /03L-1 on 780724:average Drywell Temp Exceeded Limit of 135F as Set Forth in Tech Specs 3.6.1.7.Caused by Stratification of Air Temp in Drywell | /03L-1 on 780724:average Drywell Temp Exceeded Limit of 135F as Set Forth in Tech Specs 3.6.1.7.Caused by Stratification of Air Temp in Drywell | | | 05000321/LER-1978-008-01, /01T-0 on 780209:during Steady State Power Operation,Test Valve Found to Be Broken Off.Cause Unknown. Valve Repaired.Investigation Under Way | /01T-0 on 780209:during Steady State Power Operation,Test Valve Found to Be Broken Off.Cause Unknown. Valve Repaired.Investigation Under Way | | | 05000321/LER-1978-008, Forwards LER 78-008/01T-0 | Forwards LER 78-008/01T-0 | | | 05000366/LER-1978-020, Has Been Voided | Has Been Voided | | | 05000366/LER-1978-023, Forwards LER 78-023/01L-1 | Forwards LER 78-023/01L-1 | | | 05000366/LER-1978-026-03, Mechanical Penetrations in Oil Room Floor & in Wall of 600-volt Switchgear Room 2D Found W/O Fire Penetration Seals.Caused by Personnel Determining Seals Unnecessary.Seals Installed | Mechanical Penetrations in Oil Room Floor & in Wall of 600-volt Switchgear Room 2D Found W/O Fire Penetration Seals.Caused by Personnel Determining Seals Unnecessary.Seals Installed | | | 05000321/LER-1978-027, Forwards Updated LER 78-027/03X-1 | Forwards Updated LER 78-027/03X-1 | | | 05000321/LER-1978-027-03, Hanger E11-RHR-H97 on RHR Svc Water Outlet from Heat Exchanger Found Broken. Caused by Sheared Support Rod & Disengaged Saddle Bolt. Switch Replaced | Hanger E11-RHR-H97 on RHR Svc Water Outlet from Heat Exchanger Found Broken. Caused by Sheared Support Rod & Disengaged Saddle Bolt. Switch Replaced | | | 05000366/LER-1978-030, Forwards LER 78-030/03L-0 | Forwards LER 78-030/03L-0 | | | 05000366/LER-1978-030-03, /03L-0:on 780910,RHR Valves Failed to Close After Being Fully Opened.Temporary Fix Set Until Vendor Can Supply Permanent Fix.Followup Rept Will Be Issued | /03L-0:on 780910,RHR Valves Failed to Close After Being Fully Opened.Temporary Fix Set Until Vendor Can Supply Permanent Fix.Followup Rept Will Be Issued | | | 05000366/LER-1978-031, Forwards LER 78-031/01T-0 | Forwards LER 78-031/01T-0 | | | 05000366/LER-1978-031-01, /01T-0:on 780915,during Shutdown,Core Spray Piping Hangers 2E21-CS-H6 & 2E21-CS-H92 in Core Spray Suction Lines Found to Lack Strength for Load.New Hangers Installed.Caused by Use of Incorrect Drawing | /01T-0:on 780915,during Shutdown,Core Spray Piping Hangers 2E21-CS-H6 & 2E21-CS-H92 in Core Spray Suction Lines Found to Lack Strength for Load.New Hangers Installed.Caused by Use of Incorrect Drawing | | | 05000366/LER-1978-032-03, /03L-0:on 780916,continuous Fire Watch Not Established at Unsealed Conduit.When Failure Was Recognized, Continuous Fire Watch Immediately Established.Shift Foreman Supervisors Made Aware of Conditions to Prevent Recurrence | /03L-0:on 780916,continuous Fire Watch Not Established at Unsealed Conduit.When Failure Was Recognized, Continuous Fire Watch Immediately Established.Shift Foreman Supervisors Made Aware of Conditions to Prevent Recurrence | | | 05000366/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000366/LER-1978-033-03, /03L-0:on 780915,during Plant Startup,Drywell Pressure Exceeded 0.75 Psig Tech Spec Limit | /03L-0:on 780915,during Plant Startup,Drywell Pressure Exceeded 0.75 Psig Tech Spec Limit | | | 05000366/LER-1978-034-03, /03L-0:on 780917,electrical Cables for Fire Dampers Between Generator & Battery Rooms Found Improperly Routed.Cables Rerouted | /03L-0:on 780917,electrical Cables for Fire Dampers Between Generator & Battery Rooms Found Improperly Routed.Cables Rerouted | | | 05000366/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000366/LER-1978-035, Forwards LER 78-035/03L-0 | Forwards LER 78-035/03L-0 | | | 05000366/LER-1978-035-03, /03L-0:on 780914,weekly IRM Procedure HNP-2-3052 Not Completed within Tech Spec Time Interval.Caused by Personnel Oversight | /03L-0:on 780914,weekly IRM Procedure HNP-2-3052 Not Completed within Tech Spec Time Interval.Caused by Personnel Oversight | | | 05000366/LER-1978-037, Forwards LER 78-037/01T-0 | Forwards LER 78-037/01T-0 | | | 05000366/LER-1978-037-01, /01T-0:on 780920.diesel Generator Control Logic Identified Potential Problem Which Could Exist Under LOCA or Losp.Caused by Design Discrepancy in Generator.Design Change Request Initiated | /01T-0:on 780920.diesel Generator Control Logic Identified Potential Problem Which Could Exist Under LOCA or Losp.Caused by Design Discrepancy in Generator.Design Change Request Initiated | | | 05000366/LER-1978-038-03, /03L-0:on 780920,during Review of Commitments to Nrc,Discovered That Fire Team Training Not Conducted.Team Members Will Review Procedures by 781104 | /03L-0:on 780920,during Review of Commitments to Nrc,Discovered That Fire Team Training Not Conducted.Team Members Will Review Procedures by 781104 | | | 05000366/LER-1978-038, Forwards LER 78-038/03L-0 | Forwards LER 78-038/03L-0 | | | 05000366/LER-1978-039, Forwards LER 78-039/03L-0 | Forwards LER 78-039/03L-0 | | | 05000366/LER-1978-039-03, /03L-0:on 780921,discovered Drywell Airlock Door Seals Not Inspected Every 72 H While Multiple Entries Performed.Surveillance Performed & Completed on 780921 | /03L-0:on 780921,discovered Drywell Airlock Door Seals Not Inspected Every 72 H While Multiple Entries Performed.Surveillance Performed & Completed on 780921 | | | 05000366/LER-1978-040-03, /03L-0:on 78092,switch 2B21-n010C Setpoint Found Higher than 200f.Caused by Drift of Temp Switch.Switch Recalibr | /03L-0:on 78092,switch 2B21-n010C Setpoint Found Higher than 200f.Caused by Drift of Temp Switch.Switch Recalibr | | | 05000366/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000366/LER-1978-041, Forwards LER 78-041/03L-0 | Forwards LER 78-041/03L-0 | | | 05000366/LER-1978-041-03, /03L-0:on 78092,setpoint of Valve 2B21-N013C Found Higher than 200 F.Caused by Setpoint Drift.Switch Recalibr | /03L-0:on 78092,setpoint of Valve 2B21-N013C Found Higher than 200 F.Caused by Setpoint Drift.Switch Recalibr | | | 05000321/LER-1978-043, Forwards LER 78-043/03L-1 | Forwards LER 78-043/03L-1 | | | 05000321/LER-1978-043-03, /03L-1 on 780609:procedure HNP-1-3902,Safety Relief Valve Functional Test Tried Unsuccessfully on 2 Solenoids.One Failed Due to Bent Plunger;Other Failure Due to Plunger Not Properly Secured to Actuating Springs | /03L-1 on 780609:procedure HNP-1-3902,Safety Relief Valve Functional Test Tried Unsuccessfully on 2 Solenoids.One Failed Due to Bent Plunger;Other Failure Due to Plunger Not Properly Secured to Actuating Springs | | | 05000366/LER-1978-043-03, /03L-0:on 780923:CRD Hatch Cover Removed & Both Personnel Air Lock Doors Opened.Leak Tests Not Completed in Specified Time Period.First Incident Caused by Jamming of Inner Personnel Air Lock Door | /03L-0:on 780923:CRD Hatch Cover Removed & Both Personnel Air Lock Doors Opened.Leak Tests Not Completed in Specified Time Period.First Incident Caused by Jamming of Inner Personnel Air Lock Door | | | 05000366/LER-1978-043, Forwards LER 78-043/03L-0 | Forwards LER 78-043/03L-0 | | | 05000366/LER-1978-044, Forwards LER 78-044/03L-0 | Forwards LER 78-044/03L-0 | | | 05000366/LER-1978-044-03, /03L-0:on 780923,during Startup & Power Ascension Testing,Drywell Pressure Exceeded Tech Spec Limit of 0.75 Psig for 30 Minutes.Caused by Temp Increase While Running HPCI | /03L-0:on 780923,during Startup & Power Ascension Testing,Drywell Pressure Exceeded Tech Spec Limit of 0.75 Psig for 30 Minutes.Caused by Temp Increase While Running HPCI | | | 05000366/LER-1978-045, Forwards LER 78-045/03L-0 | Forwards LER 78-045/03L-0 | | | 05000366/LER-1978-045-03, /03L-0:on 780923,while Running HPCI Sys,Torus Water Temp Rose to 106 F.Caused by RHR Svc Water Pump Cooling Water Relief Valve Stuck Partially Open.Valve Cleaned,Checked & Reinstalled | /03L-0:on 780923,while Running HPCI Sys,Torus Water Temp Rose to 106 F.Caused by RHR Svc Water Pump Cooling Water Relief Valve Stuck Partially Open.Valve Cleaned,Checked & Reinstalled | | | 05000321/LER-1978-046-01, /01T-1 on 780616:w/reactor in Startup & Hot Standby,Testing of Excess Flow Check Valve B31-F040A Revealed Unacceptable Leakage of 4.2 Gph.Cause Unknown.Trash May Have Been on Seat & Been Lost During Valve Removal | /01T-1 on 780616:w/reactor in Startup & Hot Standby,Testing of Excess Flow Check Valve B31-F040A Revealed Unacceptable Leakage of 4.2 Gph.Cause Unknown.Trash May Have Been on Seat & Been Lost During Valve Removal | | | 05000366/LER-1978-046-03, /03L-0:on 780926,rated Flow W/Two Pumps Running in Loop 1 Could Not Be Achieved for Either Loop of RHR Svc Water Pump.Caused by Damaged Cavitrol V Trims & 10 Inch Fisher Valves | /03L-0:on 780926,rated Flow W/Two Pumps Running in Loop 1 Could Not Be Achieved for Either Loop of RHR Svc Water Pump.Caused by Damaged Cavitrol V Trims & 10 Inch Fisher Valves | | | 05000366/LER-1978-046, Forwards LER 78-046/03L-0 | Forwards LER 78-046/03L-0 | | | 05000366/LER-1978-047, Forwards LER 78-047/03L-0 | Forwards LER 78-047/03L-0 | | | 05000366/LER-1978-047-03, /03L-0:on 780926,HNP-2-3054 of APRM Surveillance Signed Off During Run Mode at 174 Mwt Due to Personnel Misunderstanding.Personnel Instructed to Adhere to Schedule | /03L-0:on 780926,HNP-2-3054 of APRM Surveillance Signed Off During Run Mode at 174 Mwt Due to Personnel Misunderstanding.Personnel Instructed to Adhere to Schedule | | | 05000366/LER-1978-049, Forwards LER 78-049/03L-0 | Forwards LER 78-049/03L-0 | | | 05000366/LER-1978-049-03, /03L-0:on 781009,reactor Water Level Indicator 2C82-R005 Had Continuous Reading Higher than +60 Inches. Caused by Level Indicator Transmitter 2C82-N005 Piped in Backwards & Bad Amplifier | /03L-0:on 781009,reactor Water Level Indicator 2C82-R005 Had Continuous Reading Higher than +60 Inches. Caused by Level Indicator Transmitter 2C82-N005 Piped in Backwards & Bad Amplifier | | | 05000366/LER-1978-050, Forwards LER 78-050/03L-0 | Forwards LER 78-050/03L-0 | | | 05000366/LER-1978-050-03, /03L-0:on 781017,w/reactor in Run Mode,Standby Plant Svc Pump Lights Found Inoperable.Caused by Water in Starter Box.Low Pressure Pulled moisture-laden Cool Air Into Diesel Bldg Pullbox | /03L-0:on 781017,w/reactor in Run Mode,Standby Plant Svc Pump Lights Found Inoperable.Caused by Water in Starter Box.Low Pressure Pulled moisture-laden Cool Air Into Diesel Bldg Pullbox | | | 05000366/LER-1978-051-03, /03L-0 on 781017:during Startup Testing While Calibrating APRM High Flux Scram Setpoints,Discerned That Trip Setpoints Were Set in Excess of Reg Guide Criteria. Caused by Deficiency in Procedures | /03L-0 on 781017:during Startup Testing While Calibrating APRM High Flux Scram Setpoints,Discerned That Trip Setpoints Were Set in Excess of Reg Guide Criteria. Caused by Deficiency in Procedures | | | 05000366/LER-1978-051, Forwards LER 78-051/03L-0 | Forwards LER 78-051/03L-0 | | | 05000366/LER-1978-053, Forwards LER 78-053/03L-0 | Forwards LER 78-053/03L-0 | |
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