05000366/LER-1978-006-03, /03L-1 on 780724:average Drywell Temp Exceeded Limit of 135F as Set Forth in Tech Specs 3.6.1.7.Caused by Stratification of Air Temp in Drywell

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/03L-1 on 780724:average Drywell Temp Exceeded Limit of 135F as Set Forth in Tech Specs 3.6.1.7.Caused by Stratification of Air Temp in Drywell
ML20147C262
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/28/1978
From: Thomas Greene
GEORGIA POWER CO.
To:
Shared Package
ML20147C249 List:
References
LER-78-006-03L, LER-78-6-3L, NUDOCS 7812180205
Download: ML20147C262 (1)


LER-1978-006, /03L-1 on 780724:average Drywell Temp Exceeded Limit of 135F as Set Forth in Tech Specs 3.6.1.7.Caused by Stratification of Air Temp in Drywell
Event date:
Report date:
3661978006R03 - NRC Website

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a 121 [ During tho' heatup plateau of Unit 2. Startup Testing the average drywell temperature g exceeded the. limit of 1350 F as set forth in Tech. Specs. Section 3.6.1.7.

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] Following reactor shutdown on 7-27-78 an investigation by Bechtel Power Corporation iO Li j il g and Georgia Power Company personnel revealed stratification of air temoeratures in thet g i rywell.

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