IR 05000282/2014008

From kanterella
Revision as of 15:09, 28 January 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
IR 05000282-14-008, 05000306-14-008; on 04/14/2014 - 06/03/2014; Prairie Island Nuclear Generating Plant, Units 1 and 2; Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications
ML14162A593
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 06/11/2014
From: Daley R C
Engineering Branch 3
To: Davison K
Northern States Power Co
Alan Dahbur
References
IR-14-008
Download: ML14162A593 (19)


Text

June 11, 2014

Mr. Kevin Davison Site Vice President Prairie Island Nuclear Generating Plant Northern States Power Company, Minnesota 1717 Wakonade Drive East Welch, MN 55089

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 EVALUATIONS OF CHANGES, TESTS, AND EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000282/2014008; 05000306/2014008

Dear Mr. Davison:

On June 3, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed inspection report documents the inspection results which were discussed on May 1, 2014, with Mr. S. Sharp, Site Operation Director, and on June 3, 2014 with Mr. J. Mathew, Design Engineering Manager, and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The NRC inspectors documented one finding of very low safety significance (Green) in this report. This finding was determined to involve violations of NRC requirements. However, because of its very low safety significance and because the issue was entered into your Corrective Action Program, The NRC is treating the issue as Non-Cited Violation (NCV) in accordance with Section 2.3.2 of the NRC Enforcement Policy. Additionally, a licensee identified violation is listed in Section 4OA7 of this report. If you contest the subject or severity of the Non-Cited Violation you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector office at the Prairie Island Nuclear Generating Plant. In addition, if you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Prairie Island Nuclear Generating Plant. In accordance with Title 10, Code of Federal Regulations (CFR), Section 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60

Enclosure:

Inspection Report 05000282/2014008; 05000306/2014008

w/Attachment:

Supplemental Information cc w/encl: Distribution via LISTSERV Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos.: 50-282; 50-306 License Nos.: DPR-42; DPR-60 Report Nos.: 05000282/2014008; 05000306/2014008 Licensee: Northern States Power Company, Minnesota Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2 Location: Welch, MN Dates: April 14 through June 3, 2014 Inspectors: A. Dahbur, Senior Reactor Inspector, Lead J. Gilliam, Reactor Inspector S. Sheldon, Senior Reactor Inspector D. Szwarc, Senior Reactor Inspector Approved by: Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety 1

SUMMARY OF FINDINGS

IR 05000282/2014008, 05000306/2014008; 04/14/2014 - 06/03/2014; Prairie Island Nuclear Generating Plant, Units 1 and 2; Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications. This report covers a two-week announced baseline inspection on evaluations of changes, tests, and experiments and permanent plant modifications. The inspection was conducted by Region III inspectors. One finding was identified by the inspectors. The finding was considered Non-Cited Violation (NCV) of NRC regulations. The significance of most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Cross-cutting aspects were determined using IMC 0310, "Aspects Within the Cross Cutting Areas." Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated July 9, 2013. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5, dated February 2014.

A. NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a finding of very low safety significance and associated NCV of the Prairie Island Nuclear Generating Plant Facility Operating License Condition 2.C.(4) for the licensee's failure to implement the requirements as specified in the Fire Protection Program (FPP) for impaired safe shutdown equipment. Specifically, the licensee failed to establish appropriate compensatory measures when they identified lack of coordination between DC panel fuses and upstream panels supply fuse under fault conditions for several safe shutdown power supplies. The licensee replaced all miss-coordinated fuses and entered the issue into their Corrective Action Program. The performance deficiency was determined to be more than minor because the finding was associated with the Mitigating Systems cornerstone attribute of Protection Against External Factors (Fire) and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to fire events prevent undesirable consequences (i.e., core damage). Specifically, the failure to establish compensatory measures for lack of fuse coordination degraded the defense and depth element of the

Fire Protection Program. The finding represented a low degradation and therefore the inspectors determined that the finding screened as having very low safety significance (Green) in Task 1.3.1 of IMC 0609, Appendix F. The inspectors determined that the finding had a cross-cutting aspect in the area of Human Performance, Procedure Adherence for the licensee's failure to follow instructions as specified in Procedure FP-E-CAL-01 "Calculations." [H.8] (Section 1R17.2(b)(1))

B. Licensee-Identified Violations

Violations of very-low-safety significance or Severity Level IV that were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's Corrective Action Program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.

2

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events and Mitigating Systems

1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications

.1 Evaluations of Changes, Tests, and Experiments

a. Inspection Scope

The inspectors reviewed eight safety evaluations performed pursuant to Title 10, Code of Federal Regulations (CFR) 50.59 to determine whether the evaluations were adequate and that prior NRC-approval was obtained as appropriate. The inspectors also reviewed fourteen screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if: the changes, tests, and experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required; the safety issue requiring the change, tests or experiment was resolved; the licensee conclusions for evaluations of changes, tests, and experiments were correct and consistent with 10 CFR 50.59; and the design and licensing basis documentation was updated to reflect the change. The inspectors used, in part, Nuclear Energy Institute (NEI) 96 07, "Guidelines for 10 CFR 50.59 Implementation," Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, "10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments." This inspection constituted eight samples of evaluations and fourteen samples of screenings and/or applicability determinations as defined in IP 71111.17 04.

b. Findings

No findings of significance were identified.

.2 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed six permanent plant modifications that had been installed in the plant during the last three years. This review included in-plant walkdowns for portions of the modified emergency Diesel Generators D1 and D2 starting air systems; verified actions to open batteries rooms doors as specified in procedures; Control Room Envelope and the connected Aux Building drains and the HELB Doors in Unit 2 Turbine Building Relay Room. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if: the supporting design and licensing basis documentation was updated; the changes were in accordance with the specified design requirements; the procedures and training plans affected by the modification have been adequately updated; the test documentation as required by the applicable test programs has been updated; and post-modification testing adequately verified system operability and/or functionality. The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report. This inspection constituted six permanent plant modification samples as defined in IP 71111.17 04.

b. Findings

(1) No Compensatory Measure were established for Lack of Fuses Coordination associated with Safe Shutdown Power Supplies

Introduction:

The inspectors identified a finding of very low safety significance (Green) and associated NCV of the Prairie Island Nuclear Generating Plant Facility Operating License Condition 2.C.(4) for the licensee's failure to implement the requirements as specified in the Fire Protection Program for impaired safe shutdown equipment. Specifically, the licensee failed to establish appropriate compensatory measures when they identified lack of electrical coordination between DC panel fuses and upstream panels supply fuses under fault conditions for several safe shutdown power supplies. The licensee replaced all miss-coordinated fuses and entered the issue into their Corrective Action Program.

Description:

On November 02, 2010, during a revision to ENG-EE-012, 125 Volts DC System Coordination Study, electrical coordination issues were identified in which non-selective fuse coordination existed between a DC panel fuses and the upstream fuses to the panels. The non-selective coordination was shown to exist for high values of current which would only be expected under fault conditions. The circuits identified were as follows: PNL 131-11, PNL 131-13, PNL 131-18, PNL 131-19, PNL 171-1, PNL 171-2, PNL 181-1, PNL 181-2, PNL 231-13, PNL 231-18, PNL 231-19, PNL 271-1, PNL 271-2, PNL 281-1,and PNL 281-2. This issue was documented in the Corrective Actions Program as AR 01256681. Complete review and verification of ENG-EE-012 Revision 1 under EC 16914 was completed on February 01, 2011 and confirmed that mis-coordination identified in the parent AR remained present. An evaluation of fuse replacement options was performed under AR 01256681 assignment, which developed recommended replacement fuse sizes/types to achieve coordination. Fuse replacements and selections were performed under ENG-EE-012, Revision 2 per EC 18289. All work orders for fuse replacement were completed by November 16, 2013. During the inspectors' review of the engineering changes and corrective actions associated with this issue, the inspectors questioned if this issue was reviewed by the Fire Protection Program group. Specifically, the inspectors were concerned if the effect of lack of fuses coordination on the safe shutdown power supplies and the safe shutdown analysis (SSA) were evaluated during the licensee's review and if any compensatory measures were established. In response to the inspectors' concern, the licensee indicated that no Fire Protection Engineers' review was performed for this issue and hence no compensatory measures were established during the non-compliance time frame. The licensee entered the inspectors' concern into their Corrective Action Program as AR 01428822 and identified that at the time of AR 01256681 issuance, the SSA Calculation GEN-PI-026, Revision 5D was the analysis of record. At that time there was no documented use of ENG-EE-012 as an input to GEN-PI-026, however, Calculation GEN-PI-026 provided the basis for fuse coordination for several power supplies credited in the SSA. The failure to properly identify Calculation ENG-EE-012 as an input to Calculation GEN-PI-026 resulted in a potential impact on the SSA with no review by the FFP Engineer. The licensee entered the inspectors' concern into their Corrective Action Program as AR 01428822 and planned to update GEN-PI-026 to include ENG-EE-012 as an input; verify that the SSA contains all required inputs to validate the output of the analysis; determine why ENG-EE-012 was not used as an input to GEN-PI-026; and issue actions to resolve any identified process weakness

Analysis:

The inspectors determined that the failure to establish compensatory measures was contrary to the Prairie Island Nuclear Generating Plant License Condition associated with the Fire Protection Program and was a performance deficiency. Specifically, the licensee failed to establish compensatory measures as specified in Procedure F5 Appendix K for lack of fuse coordination associated with safe shutdown power supplies. The performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of Protection Against External Events (Fire) and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the failure to establish appropriate compensatory measures degraded the defense and depth element of the Fire Protection Program. In accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase I - Initial Characterization of Findings," Table 3, the inspectors determined that the finding affected the implementation of the administrative controls of the FPP. Therefore, screening under IMC 0609, Appendix F, "Fire Protection Significance Determination Process," was required. The inspectors determined that the finding represented a low degradation because the compensatory measures were only associated with lack of coordination between fuses for safe shutdown power supplies and not because of hot work or other fire protection impairment. Therefore, the inspectors determined that the finding screened as having very-low-safety significance (Green) in Task 1.3.1 of IMC 0609, Appendix F. This finding had a cross-cutting aspect in the area of Human Performance, Procedure Adherence for the licensee's failure to follow instructions as specified in Procedure FP-E-CAL-01 "Calculations," which is the governing procedure for preparing, reviewing, and managing configuration control of calculations and analysis. Specifically, the licensee failed to identify and review the SSA when updated Calculation ENG-EE-012 because the SSA did not reference the calculation as an input. [H.8].

Enforcement:

Prairie Island Nuclear Generating Plant facility Operating License Condition 2.C.(4), for both Units 1 and 2, required the licensee to implement and maintain in effect all provisions of the approved Fire Protection Program as described in the Updated Safety Analysis Report (USAR). Procedure F5 Appendix K was a written procedure which covered Fire Protection Program implementation in that the procedure provided functional requirements, compensatory action, surveillance requirements, and reporting requirements of Fire Protection systems. Procedure F5 Appendix K, Section 7.20, stated, in part, if a fire protection-related system, structure, or component (SSC) not addressed in Section 7.0 is determined to be impaired, appropriate compensatory measures shall be determined by the Fire Protection Program Engineer and their basis documented in a CAP. Contrary to the above, from February 1, 2011 through November 16, 2013, the licensee failed to implement the approved Fire Protection Program as specified in Procedure F5, Appendix K, Section 7.2. Specifically, the licensee failed to establish appropriate compensatory measures for lack of fuse coordination associated with safe shutdown power supplies. The licensee entered this issue into their Corrective Action Program as AR 01428822 and planned to revise affected calculations and resolve any identified process weaknesses. Because this violation was of very-low-safety significance and it was entered into the licensee's Corrective Action Program, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000282/2014008-01; 05000306/2014008-01, No Compensatory Measure were established for Lack of Fuses Coordination associated with Safe Shutdown Power Supplies).

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed several corrective action process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations of changes, tests, and experiments. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the to this report.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary On May 1, 2014, the inspectors presented the inspection results to Mr. S. Sharp, and on June 3, 2014, to Mr. J. Mathew and other members of the licensee staff.

The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material reviewed during the inspection was returned to the licensee staff.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) or Severity Level IV was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as an NCV. The licensee identified a Severity Level IV violation of 10 CFR 50.59, (Changes, Tests, and Experiments," for the failure to demonstrate in a written evaluation that prior NRC-approval was not required for changes made to an accident analysis. Specifically, the licensee incorrectly concluded in written Evaluation 1102, "Waste Gas Tank Rupture Dose Analysis," Revision 0 that higher activity levels and dose rates at the Exclusion Area Boundary and Low Population Zone associated with extended plant life due to license extension did not result in a more than minimal increase in the consequences of an accident previously evaluated in the UFSAR. The performance deficiency was determined to be more than minor because it was associated with the Radiation Safety cornerstone attribute of program and process and affected the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. The inspectors determined the violation was of Severity Level IV because the associated finding was of very low safety significance (Green) as there was no actual radioactive material release. The licensee entered this issue into their Corrective Action Program as AR 1417573 and AR 1427150 and intended to submit a license amendment request for review by the NRC. ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

J. Hallenbeck, Site Engineering Director
S. Sharp, Site Operation Director
N. Haskell, Corporate Engineering Director
H. Butterworth, Nuclear Oversight Manager
J. Kivi, Employee Concern Program Manager
B. Rogers, Procurement. Manager
W. Partridge, Mechanical Design Engineering
S. Kerus, Procurement Supervisor
I. Nordby, Regulatory Assurance
J. Mathew, Design Engineering Manager
R. Schaefer, Design Engineering Supervisor
D. Vincent, Regulatory Assurance
H. Storgen, Site Engineering
B. Wegner, Mechanical Design Engineering Nuclear Regulatory Commission
G. Shear, Director, Division of Reactor Safety

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened/Closed

05000282/2014008-01
05000306/2014008-01 NCV No Compensatory Measure were established for Lack of Fuses Coordination associated with Safe Shutdown Power Supplies (Section 1R17.2(b)(1))

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort.
Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. 10
CFR 50.59 EVALUATIONS Number Description or Title Date or Revision 1085 Manual Actions Required to Maintain Battery Room Temperatures Revision 2 1088 Auxiliary Feedwater Increased Flow to SG due to Recirculation Line Flow Meter Install Revision 0 1095 Revised Steamline Break Containment Response Analysis of Record for Unit 2 Revision 0 1096 Relay Rom Integrity Test Revision 0 1102 Waste Gas Tank Rupture Dose Analysis Revision 1 1103 Control Room Envelope Special Test Revision 0 1105 Unit 2 MSLB Containment Response with RSGs Revision 0 1107 Revised LOCA Containment Response Analysis for Unit 1 and Unit 2 Revision 0
10
CFR 50.59 SCREENINGS Number Description or Title Date or Revision 3682 D1 and D2 Starting Air AOV Replacement August 6, 2012 3692 Installation of Orifice Flow Meter on Unit 1, 11 TD AFWP Recirculation Flow Path Revision 0 3700 Temp Procedure Changes Required to Support
OPR 1266815-02 Compensatory Measures Revision 4 3729 Replacement of 1NR-45 and 2NR-45 Recorders Revision 1 3780 Fuse Setpoint Change to Improve Coordination Revision 0 3865 Temporary Change to Operations Procedure 2C14, "Component Cooling System - U2", Relative to Phase II Cooldown of the Unit 2 Reactor Coolant System (RCS) December 9, 2011 3878 Delete Technical Requirements Manual 3.7.2 "Diesel Driven Cooling Water Pumps" January 23, 2012 3882 Revise Diesel SPs to Ensure EDG Breaker Auto-Closure Revision 0 3890
RCE 1297439- Revise USAR and T.S. Bases Revision 1 3966 Scaffold Building August 14, 2012
10
CFR 50.59 SCREENINGS Number Description or Title Date or Revision 3984 STPT Change for Bus 26 Fuses Revision 0 4019 Unit 1 4KV Safegaurd Protective Relay Setting and Coordination Revision 1 4143 Compensatory Measures in Support of
OPR 01266815-02 Revision 5 Revision 0 4277 Revise Frequency of the Turbine Stop Valve Disc Surveillance Revision 0 4372 Revision to
SPC-EG-011, "D1/D2 Emergency Diesel Generator Fuel Oil Day Tank Level Switch Setpoints" Revision 0
CORRECTIVE ACTION PROGRAM DOCUMENTS ISSUED DURING INSPECTION Number Description or Title Date or Revision
01427150 Required LAR not Entered into CAP April 16, 2014
01427356 FU/26-16 Safety Class April 17, 2014
01427512 EC Refers to Deleted Procedure April 18, 2014
01427521 Battery Room Heatup
OPR 01265904-01 April 18, 2014
01428822
ENG-EE-012 Updated without Evaluation of Impact on SSA April 29, 2014
01428934 2014 50.59/ Mod Insp: Eval 1103 Statement Not Justified April 30, 2014
CORRECTIVE ACTION PROGRAM REVIEWED Number Description or Title Date or Revision
01343661 D5 HT Cooling Temps High during
SP 2093 July 2, 2012
01348833 D5 HT Cooling Temps High during
SP 2093 August 20, 2012
01050237 Bases for AFW Pump Low Discharge Pressure Switches June 15, 2012
01417573 50.59 Evaluations 1102 and 1074 Have Incorrect Conclusion February 5, 2014
01256681 Non-Selective Fuse Coordination in
ENG-EE-012 November 01/2010
1396827
CD-34180 and
CD-34145 are Potentially Leaking by September 14, 2013
1396327 Re-test of CRE per
SP 1449 was Unsatisfactory September 11, 2013
1396183
SP 1449- Tracer Gas Test of Control Room, Sec 7.2- Test #1 September 10, 2013
1336304 50.59 Screening not Completed prior to EC Approval May 3, 2013
1333310 Safety Evaluation 1080 requires Revision/ April 11, 2012
CORRECTIVE ACTION PROGRAM REVIEWED Number Description or Title Date or Revision Cancellation
1346715 Two TMODs not Documented as required August 1, 2012
1392548 Unacceptable Preconditioning used to Meet TS 5.5.16 August 6, 2013
1299415 D1/D2 Tachometer Indicator Noise Susceptibility August 15, 2011
1348744
SV-2 Pressure did not Meet the Criteria for Closure
August 19, 2012
01333297 Fuse and Drawing Descrepancy on Bus 26 Cubical 16 April 11, 2012
DRAWINGS Number Description or Title Date or Revision
NF-39222 Flow Diagram Feedwater & Aux Feedwater Unit 1 Revision 82
MODIFICATIONS Number Description or Title Date or Revision
EC 17465 Install Flow Meters On 11 Turbine Driven Auxiliary Feedwater Pump Recirculation Line Revision 0
EC 9521 D1 and D2 Starting Air AOV Replacement Revision 0
EC 12156 Lower Setpoints for 1R-12 and 1R-22 per Special Outage and Calculation Revision 1
EC 18020 D1/D2 TACH Generator to Speed Switch Cable Replacement Revision 1
EC 22872 Evaluation of AFW Room Heatup with no Coolers Revision 0
PROCEDURES Number Description or Title Date or Revision
ST 1449 Tracer Gas Test of Control Room No Loop Seal
Revision 0
TCR 027B
OPR 1265904 and Associated CAP Compensatory Measures
Revision 27
SP 1449 Tracer Gas Test of Control Room
Revision 0 C18.1 Engineered Safeguards Equipment Support Systems Revision 37
OTHER DOCUMENTS Number Description or Title Date or Revision SPCR 2649 D5 Engine 1 HT Cooling Water Outlet High Temp Switch January 12, 1994 SPCR 2650 D5 Engine 1 HT Cooling Water Outlet High High Temp Switch January 12, 1994 SPCR 2651 D5 Engine 2 HT Cooling Water Outlet High Temp Switch January 12, 1994 SPCR 2652 D5 Engine 2 HT Cooling Water Outlet High High Temp Switch January 12, 1994
SPC-AF-006 AFW Pump Minimum Recirculation Flowmeter Uncertainty Revisions 1, 1A, 1B
WO 484032 D1 Diesel Generator 6 Month Fast Start Test March 10, 2014
ENG-ME-779 AFW Pump Low Discharge Pressure Switch Revision 0
ENG-ME-374 Tracer Gas Inleakage Testing of the Control Room Revision 0
WO 446200 Perform Relay Room Leakage Test for CO2 Calculation Revision 1
OPR 01265904-01 Operability Recommendation Revision 1
List of Acronyms Used ADAMS Agencywide Document Access Management System AR Action Request BWR Boiling Water Reactor CFR Code of Federal Regulations CS Core Spray DC Direct Current EDG Emergency Diesel Generator EPRI Electrical Power Research Institute FPEE Fire Protection Engineering Evaluation IMC Inspection Manual Chapter IP Inspection Procedure IR Inspection Report LER Licensee Event Report LOCA Loss of Coolant Accident LOOP Loss of Off-site Power MCC Motor Control Center MSO Multiple Spurious Operation NCV Non-Cited Violation NEI Nuclear Energy Institute NFPA National Fire Protection Association NPSH Net Positive Suction Head NRC Nuclear Regulatory Commission PARS Publicly Available Records RHR Residual Heat Removal RPV Reactor Pressure Vessel SDP Significance Determination Process SFP Spent Fuel Pool SSC Systems, Structures, and Components SSD Safe Shutdown SRV Safety Relief Valve TAF Top of Active Fuel USAR Updated Safety Analysis Report
K. Davison -2- In accordance with Title 10, Code of Federal Regulations (CFR), Section 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely, /RA/
Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket Nos.
50-282; 50-306 License Nos.
DPR-42;
DPR-60 Enclosure: Inspection Report 05000282/2014008; 05000306/2014008 w/Attachment:
Supplemental Information cc w/encl:
Distribution via