ML18227A400

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Attached April, 1976, Operating Status Reports for Turkey Point Unit Nos. 3 & 4 and St. Lucie Unit No. 1
ML18227A400
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 05/07/1976
From: Schmidt A
Florida Power & Light Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18227A400 (15)


Text

NRC FORM 195 U.S. NUCLEAR REGULATORY MISSION (2-761 50-25~25 335 FILE NUMBER NRC DISTRIBUTION FQR PART 50 DOCKET MATERIAL MONTHLY REPORT USNRC FRoM:Flordia Power. 8 Lioht Co. DATE OF OOCUMENT Miami, Flordia 5-7-76 A.D. Schmidt OATE RECEIVEO CJLETTE R GNOTORIZEO INPUT FORM NUMBER OF COPIES RECEIVEO

)OORIQINAL X3 UN C LASS IF I E O 0 COPY OESCRIPTION LET~re TRANS THE FOLLOWING: MONTHLY REPORT FOR A PLANT & COMPONENT OPERABILITY &

AVAILABILITY'HISREPORT TO BE USED IN PREPARING GRAY BOOK BY PLANS &

OPERATIONS'LANT gONOg REMOVE .

NAME: Turkey PT. ¹ 3 8 4 ZCKXO<<<DGED:

St. Lucie ¹ 1 FOR ACTION/INFORMATION MIPC W CYS FO AC ON INTERNAL D IST RI BUTION PD BRANCH CHIEF L EXTERNAL DISTRIBUTION CONTROL NUMBER

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. ~ .O. BOX 013I00, MIAMI, FLORIDA 3310I Regufatoty il 1 FLORIDA POWER Ei LIGHT COiVIPAiIY Office of Management Xnformation and Program Controls U. S. Nuclea'r Regulatory Commission Washington, D. C. 20555 Gentlemen:

Attached are the, April, 1976 Operating Status Re for Turkey Point, Unit Nos. 3 and 4 and St. Lucie Unit No. 1.

Very truly yours, Or DOCKfyg0 U

D. chmidt Vice President Power Resources VTC/pm Attachments cc: Mr. Norman C. Moseley Jack R. Newman, Esquire H E L ii I N G B LI I L 0 P L0 R I O A

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APPENDIX B AVERAGE DAILY DNZT POWER LEVEL DOCKET No. 50 250 DNIT Turkey Point Unit No.

~ ~ DATE Hay 5, 1976 COPNLETED BY V.

xoNTB April 1976

~ DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAZIY POWER LEVEL (YRc-Nct) (Nwc-Nct) 1 662 17 2 661 18 663

! 670 19 658

~

4 667 20 660 664 21 661 6 665 .22 580 7 663 23 650 8 664 649 9 669 25 623 673 26 650 11 384 '27 649 12 634 28 13 662 29 645 660 30 571 15 623 16 487 NOTE- Daily average power level .

greater than 666 hlHe due to cooler condenser cooling water.

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APPENDIX C OPERATING DATA REPORT P~

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POCEE1'O. 2() -

UNIT Turkey Point Unit No. 3 DATE)iay 52 1976 COMPLETED BY V.T. Chilson TELEPHONE (305) 552 - 3830.

'PERATING STATUS S ~

1. REPORTING PERZODQ001 76 04 01 GROSS HOURS ZN REPORTZNG PERIOD: 719.0>

THROUGH 2400 76 04, 30 PAN. DEPEND. CA. ACYYY (NN -N it: 88

3. POWER LEVEL TO WHICH RESTRICTED (ZF ANY) (MWc-Nct):

4~ REASONS FOR RESTRICTION (ZF ANY):

I

'I THIS MONTH YEAR TO DATE CUMULA ZVE 5~ NUMBER OF HOURS REACTOR WAS CRZTZCALA ~ 718.4 . 2p643.4 '3,923.6

6. REACTOR RESERVE SHUTDOWN BOURDON' ~ ~ ~ ~

15.4 18.6

7. HOURS GENERATOR ON LINE..... ~ ............ 717.9 2,600.8 22,970.8 0 128(IT R-SERVE SHU Doiv14 HOURS ~ ~ ~ 15.4 8..

9 GROSS SEE)II!AD ENERGY GEEEIIAYED (ISIS)..... 15299161 ~87 87 IANNA

10. GROSS ELECTRICAL E11ERGY GENERATED (MWH).. 481 830 1 793,370 13,808,606 NET ELECTRICAL ENERGY GENERATED (MWH).. . 4572957 lp7032726 13p0592488
12. REACTOR SERVICE FACTOR ~ ~ 99 ' . 91 ' 80.1 13 REACTOR AVAILABILITYFACTOR...... ~ .. .... 99 9 91.1
14. UNIT SEPVZCE FACTOR.. . ....... .... .. 99.8 89. 6 76.9 Ui)1ZT AVAZAZLITY 7 FACTORP ~ ~ ~

~

~ ~ ~ ~ ~

~ ~ ~ ~

. 'aa.8 15'6.

U11ZT CAPACITY FACTOR (Using MDC)......... 66.8

17. UNIT CAPACITY FACTOR (Using Design YÃc).. 84.7 63.1
18. UNIT FORCED OUTAGE RATE. ~ ...... .. ~ ~ ~ .~~~ 0.1 0.2 3 '

19 ~ SHUTDOWNS SCHEDULED OVER NEXT,6 MONTHS (TYPE, DATES AND DURATION 0 EACH):

Refueling, Maintenance, and Inspection.". - October 4 through-Novcnber 1(, 1976' 20 'F SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP.

21i UNITS IN TEST STATUS (PRIOR TO CONA(ERCZAL OPERATION): FORECAST ACHIEVED P

ZNZTZAZ CRITICALITY

~

INITIAL ELECTRICITY

~, ~ COMMERCIAL OPERATION i, ~ ~

<NOTE Changed to D.S.T.E on hpril 25, 1976 i

'1) ~psott VNIT SHUTDOWNS AND POWER REDUCAIONS UNIT NAME Turkev Point Unit Nft At EQUIPHEttT FAILURE (EXPLAIN)

Bt MAItlT, OR TEST . DATE )9m 5, 1976 Ct FZFUEl ItlG ~

Dt PEGVLATORY RESTRICTION COMPLETED BYV.T. Chilson Et OPERATOR TRAINING AND LICEtlSE EXAMINATION (305) 552 3830 Ft ADHItlISTRATIVE TELEPHON.

! G. OPERATIONAL ERROR (EXPLAIN) ARRORP xcars~ar[1 1976 Ht OTHER (EXPLAIN) l

, (2) METHOD HETHOD OF 1 t MANUAL TYPE SHUTTING DOWN 2t MANUAL SCRAM Ft FORCED DURATION THE REACTOR OR 3t AUTOMATIC SCRAM NO. DATE St SCHEDULED (HOURS) REASON(1) REDUCING POWER(2) CORRECTIVE ACTIONS Cottt(EttTS 4t OTHER (EXPLAIN) 08 76-04-1 A Load on Unit No. 3 was reduced to approximately 258 1(Ye (45 0 R.P.) to locate and repair condenser tube leak.

(Non-Nuclear System) 09 76-04-1 A Load on Unit No. 3.ttas reduced to approximately 215 1$ (e to locate and repai'e condenser tube leak.

(Non-Nuclear System) 10 76-04-2 F Reactor trip caused by removing undervoltage time delay relay frost service. on operating unit, in error.

Corrective. action taken'included installing large signs identifying each relay cabinet and associated unit number.

scauasy: 'Unit No. 3 operated at approximately 109 9 R.p. except for reactor trip on April 22 and load reductions to repair condenser tune ledks on April 1'1 and 16, 1976.

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APPENDIX C OPERATING DATA REPORT DOCKET NO 50 - 251 UNIT.Tur):ey Point Unit No. 4 REPORT M)NTH Anril 1976 DATEV~y 5, 1976 COMPLETED BY V.T. Chilson TELEPHONE (305) 552 - 3830.

'PERATING STATUS 1>> REPORTING PERIOD: 0001t 76E 04E01 GROSS HOURS ZN REPORTING PERIOD 2>> CURRENTLY AUTHORIZED POWER LEVEL (MWt):2 200 t):

~

HAE OEPESO. CAPACATY (H'A -H ~bt 3 POWER LEVEZ TO WHICll RESTRZCTED (IF ANY) (MWc-Nct):

4~ REASONS FOR RESTRICTION '(ZF ANY) t THIS MONTH YEAR TO DATE CUMULATIVE 5 NUMBER OF HOURS REACTOR WAS CRITICAL..... 410. 5 ~ 2,411.0 18,056.9 6~ REACTOR RES..RVD SHUTDO)AAJ HOURS. ~ ~ ~ ~ ~ ~ ~ ~ ~ ~

117.1 7~ HOURS GENERATOR ON IZNE... ~ . ~ . ... . ~

408.7 2,370.5 172 084. 2 8 UNIT RESERVE SHUTDOWN HOURS. ~ ~ ~ .~ ~ ~ ~

. , E. GROSS TIIEIIHllA El)ERCY GEIIERATEG (HHII)..... 87~233 ~51 5 759 35 784 395

10. GROSS ELEC"RZCAL ENERGY G NERATED (MwH) 275,701 1,661,601 11,640,678

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NET ELECTRICAL ENERGY GENERATED (M'A>>H) ~

2615 336 lt 580r 280 lit038S 9 0 12>> FLECTOR SERVICE FACTOR>> ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ >> ~ ~ 57.1 . 83.1 76.6 13 'EACTOR AVAILABILITYFACTOR. ~ ~ ~ ~ ~ ~ ~ .2 ' ~

57.1 83.1 77. 1 14 ~ UNIT SERVICE FACTOR ~ ~ ~ ~ ~ >> ~ ~ ~ ~ ~ ~ ~ ~ ~ >> 56.8 81.7 72.5 15: UNIT AVAZAZLITYFACTOR.. >>' ~ . >>. ~ >>

~ 56.8 81.7 72.5

16. UNIT CAPACITY FACTOR (Using MDC)......... 54.6 65.0- 71.3
17. UNIT CAPACITY FACTOR (Using Design MWc) .. 52.4 78.6 67. 6 18 'NIT FORCED OUTAGE RATE. ~ . >>>> ~ . >> ~ ~ . ~ . 2.4 3.4 19>> SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS .(TYP, DATE AND DURATION OF EACH):

NONE Ht 20 ~,'F SHUTDO'tJN AT END OF REPORT PERIOD,. ESTIMATED DA E OF STARTUP:

21. UNITS ZN TEST STATUS (PRIOR TO COJDKRCZAL OPERATION): FORECAST ACHIEVED INITIALCRITICALITY

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~ INITIALELECTRICITY

~ COJO(ERCZAL OPERATION JJ NOTE: Changed to D.S.T.'n April 25; 1976

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APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DocFET No. 50 - 251

. mtzT Turkey point Unit No. 4 DATE May 5, 1976.

coNPLETED BY v T chilson TELEPHoNE (305) 552 3830

) oNTH APril 1976 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER'EVEL (MWc-Nct) (MWc-Nct) 662 599 661 18 648 19

\ 4 419 20 662 21 658 660 23 DDI. g4 25 10 672 26 660 '27 12'3 660 28 657 14 657 30 15 664 16 660 NOTE: Daily average power level greater than 666 ))We due to cooler condenser cooling water;

(1) REASO)t UNIT SHUTDOWNS AND 'PCWER RSDUCiIONS UNIT ttA>tE Turkey Point Unit No. I, Ai EQTUIPMENT FAILURE (EXPLAIN)

E: MAIttT. OR TEST DATE b'av 5P 1976 Ct FSFUELING D: PZGULATORY RESTRICTION COMPLFTED DY V.T. Chilson Et OPERATOR TRAIttIttG AttD LICENSE EXAMINATION Ft ADMItIISTRATIVE TELEPHONE(305) 552- 3830 Oi"ERATIONAL ERROR (EXPLAIN) ANPOAT MONTN APril 1976 G:

HL OTHER (EXPLAIN)

(2) F iHOD METHOD OP 1: MAttUAL TYPE StlUTTING DOWN 2: MANUAL SCRAM F: FORCED DURATION Tt!E REACTOR OR 3c AUTOMATIC SCRAM NO DATE Sy SCHEDULED (<<oURs) REASON(1) REDUCING POWER(2) CORRECTIVE ACTIOttS/CON(EttTS 44 OTHER (EXPLAIN) )

09 6-04-03 Load on Unit No. 4 v7as reduced to approxictately 250 )(t(e to perforct periodic tost of turbine nain stean stop, reheat stop, and reheat intercept valves.

(Non-Nuclear System)

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T 10 6-04-18 310.3 Unit No. 4 was rewed frost service for scheduled refueling, tcaintenance, and inspections. (Nuclear and Non-Nuclear Systems) d I ~ ee I

'slrwxtar Unit No. 6 operated at appioximately 100 t n p u.nt.il unit wiis removed frau service for refueling, maintenance, and inspections on April 16, 1976, except for load reduction for p'eriodic turbine valve test on April 3, 1976.-

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APPENDIX C OPERATING DATA REPORT DOCKET NO 50 - 335 UNIT.St. Lucie Unit No. 1 DATE Hay 5, 1976 COMPLETED BY V.T. Chilson TELEPHONE (305) 552 3830 OPERATING STATUS

~

1~ REPORTING PERIOD:MOls 76E 04s01 GROSS HOURS ZN REPORTING PERZOD: 719 0" THROUGH 2400, 76 04 30 MAX DEPEND CAPIACIAY OIAAI'e Net): n

' POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net)

REASONS FOR ASTRICTION '(ZF ANY):

THIS MONTH YEAR To DATE CUMULATIVE

5. IIOHEER OE H!IOIIS REACZOR HAS CRZ'ZZCAR..

6 REACTOR RESERVE SHUTDOWI4 HOURS os ~ ~

7~ HOURS GENERATOR ON LINE .. ~ .~ o ~ .~

0 9 GROSS THERMAL'NERGY GENERATED (Ã&) E ~ .

)0. GROSS ELECTRICAL E'.EERGY GENEPATED (YiÃ(l)

NET ELECTRICAL ENERGY GENERATED (MWH)

12. REACTOR SERVICE FACTOR. ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ,' ~ ~ ~ ~ ~ ~ N/A N/A N/A
13. REACTOR AVAZLABZLZTYFACTOR...... .... ~ o
14. UNIT SERVICE FACTOR.
15. UNIT AVAILABILITYFACTOR........ ~ .~.
16. UNIT CAPACITY FACTOR (Using MDC).........
17. UNIT O'APACITY FACTOR (Using Design MWe)..

18 'NIT FORCED OUTAGE RATER ~ .. ~ ~ .~ . ~.

19 ~ SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):

20. 'F SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

21 UNITS IN TEST STATUS (PRIOR TO COitVERCZAL OPERATION) FORECAST ACHIEVED INITIAL CRITICALITY April'ZS, 1976 INITIALELECTRICITY COWKRCIAL OPERATION

~ HOTE: Changed to DST on April 25, 1976

APPENDIX B AVERAGE DAILY ONIT POWER LEVEL DOCKET NO.

. DNIT St. Lucie Unit No. 1

~ ~ DATE Na 5, 1976 COiMLETED BY V. T. Chilson HONT)f ~~<)~

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER ZEVEL (NWc-Nct) (HWc-Nct) 17 18 19

( 4 20 21 23 24 -0>>

25 10 26

'27 12

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28 13 29 30 15 l6

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APPEllDZX D DOCKET NOe (1) REASON UNIT SHUTDOWNS AtlD POWER REDUCAZONS UNIT NAME St. Lucie Unit No. 1 As EQUZPME'tT FAILURE (EXPLAIN)

Bs MAZttT. OR TEST ~ DATE )/ay 5, 1976 Cs Fml'UELItlG Ds PXGULATORY RESTRICTIOil COMPLETED BYV.T. Chilscn Es OPERATOR TRAINING AND LICEtlSE EXAMINATION TELEPHONE ~305) 552 - 3S30 Fs ADMItlISTRATZVE REPORT MONTH A)>rfl 1976 C: OPERATIONAL ERROR (EXPLAIN)

Hs OTHER (EXPLAIN)

(2) METttOD METHOD OF 1s HiQlUAL TYPE SHUTTING DOWN 2: MAtlUAL SCRAM Fs FORCED DURATION THE REACTOR OR 3s AUTOeMATZC SCRAM DA.TE Ss SCHEDULED (HOURS) REASON (1) REDUCINC POWER(2) CORRECTIVE ACTIONS COMMEtlTS 4 2 OTllER {EXPLAZtl) l N/A secants 'Unit No. 1 achieved initial criticality at 8:30 a.m. April 22, 1976.

Low power physics test program in progress.

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