ML17338A270

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LER#78-014/03L-0 on 781002:condensate Storage Tank(Cst)Fell to 182,000 Gallons Because of Water Demand Increase for Steam Generator Blowdown Resulting from Cation Resin Bed Regeneration.Cst Filled After Resin Bed Regeneration
ML17338A270
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 10/02/1978
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML17338A269 List:
References
LER-78-014-03L-01, LER-78-14-3L-1, NUDOCS 7811080150
Download: ML17338A270 (1)


Text

S'e N4C FORM CES l7 77l LICEIMSEE EVERT REPORT U.S NUCLEAR REGULATORY C MMISSION[oaij l 3 CCN'T 0 I I 0 l 2'0 (PLEASE PRINT OR TYPe AI.L RKCUIRED INFORMATION)

I FI L T PISI4IQ2 I I-OIO IOIOIO I-IO 9 UCENSEE COOS>4'5 UCSNSENUMdda S~~I~~0"'".*'Il<'0 rr'ID~O~r>0 50 41 OOCKer NVMSEa da 49 EVENT CATE lS ac~IIT CATE 30 EVENT OHCRIPTION

'NO PROSABL CONScCUENCSS QIO For a eriod of about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> durin unit startu the Condensate Stora e~03 Tnk CST ntain d s hn h 8 o r ima lv 8 00 n.P bli he 1th and~04 safet was not affected.The onl effect of havin a reduced volume in 0 I: SYSTeM CAUSS CAVSE COMP,'ALVE COOS C OE 548CCOE CCMPONENT COOS SVSCOOE SVSCCOE S LJS LUS~S mre ale l 4 9 10 I I 13 18 19 Z0 SECUENTIAI OCCUaaEINCE aEPONT aEVISION LSSIAO EVENTYS&a AEPOAT NO.COOS TYPE NO.Qrr rr'crrr~78~~01 14~~Lp)~~L'~p EI ZZ 36 33 39 30 33 AcTIcu gvTUAE Eppcc.5NUTccwu ATTACNMENT NPROA PIIIMEC MP.'OMPONENT TAICEN ACTIO'I CN PLANT METNCO 40445'Q svsMITTzo pcaMYUB.$'JppLIEa MANvpA Ua 4 Irsrlrrs 1lrs burrs~r Ies LEs Ir's Irrr'"s 34 6 SI 41 42~4 41 CAUS-DESCRIPTION AND CORRECTIVE ACT)ONS Q27 0 After re air of condenser leaks the water treatment lant was shutdown to~09~~0 a nces of this: t are numbered 250-78-4 251-78-250-78-13 8 251-78-13.

allow re ener ation of cation resin beds.Water demand for steam enerator i h f w m nt lant out ut re-'han th T.S.3.8.1.c limit.Fill-)b d r eneration.

a P 4CILI.Y 3~ATVS'I PCNER~cc METIIOO OP OWERSTA'rrS

~OISCOVERY~AQSI 44 45 NA NA DD7 L'JS IILLLIIIS~

7 a 10 IS IS 44 ACTIVITY CONTENT 9'ELEASEO CI'ELEASE AMOUNT OF ACTIVITY QSS.Q-l~l I zlQ~~zQ2 NA l 3 IO I I p'EasoNNEL Expcsvads NvMSEa.YPE ESCRIPTICN Q9 o'OLZJGr 3 3 lt I2 IS P!AscuuEL INIUaIES NI'Msda-ESCRIP YICNQAI a~i~llQAO CIsccvERY odscaIpTICN Q>2 0 erator Observation LOCATION OP aELEASE QSS NA 30 3 3 2 I)I I I'3'SS OP ca OAMACS TO PACILITY~A-.YP~OESCalPTION

~Q42:0 PrJSLIC:~.33430 sdscaIptlcN Qd~uuO:0 F P 4 R.A.Scho oman NA 30 30 NRC I'Sc ONI Y dd 89 ,NONe..305 552-3802 789.;OS o l S-0