ML17340B149

From kanterella
Revision as of 14:56, 14 September 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-033/01T-0:on 791101,NSSS Vendor Identified & Corrected Input Error in Two LOCA Analyses.Caused by Use of Incorrect Method.Procedures Revised
ML17340B149
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 11/15/1979
From: SCHOPPMAN M A
FLORIDA POWER & LIGHT CO.
To:
FLORIDA POWER & LIGHT CO.
Shared Package
ML17340B144 List:
References
LER-79-003-01T, LER-79-3-1T, NUDOCS 8105050087
Download: ML17340B149 (2)


Text

~(I~I I'e(etoowpj'err&o gkgs Ar'krA,~'p~~4..'i'~ovdkj'rpI err'~'ILYRo wplo gl,Clio erA prr.o4vrA NAC RORh1 S88 P 77I LICENSEE EVENT REPORT U S NUCL erAR REGULATORY COA1LrlISSION 1 CON'T~O l a'0 19LSAS 8 PAIIIT oR TYPS ALL Aeaul Reo INROAiULTIQNI I 5 10 I.>>-I OO~I>>I@~Q 9 L:CZ.'rsea COOS I.ICZNSZ NloMASR 15 L'cz.4sa Tvps Ja ST~T sa'Q~ll I'ao, al OOCXATPIVMSZR aa 5>av NTO*Te IS RSPCRTO*TZ so LP'ENT OSSCRIPTIQN rLNO PROSArSI S CONSRCUGi4CSS Qlo The NSSS vendor has identified and corrected an in ut error in each of two~o2 A i nn'bl t Ir Pi n'he LOCA anal ses for the 22K and the 25/steam enerator tube lu in'evels~OS r rr r in the 22 anal sis resulted in a reduction of the maximum allowable F from 2.10 to 1.90.Both units have~ol less than 22'X steam enerator tube lu in.~Oa~po 1 SY STANDI CAUSS CAVSZ CQVP, VALVe COOS COOS SUSCCOS CCMPON ZNT COOS sUScoo j svacoae iu'4 QrQ i&0~r'0 I OQ OQQ 7 a 9 Io 11 Ig I'5 I 9 zo SZCUSNTI*I.

OCCVRIIZNCK'SPORT RSVISIQN'PPIAQ SVfNT YeAR RCPORT'IO.

Coca YP4~NO.Qir ro'~71 0+~03 I 3+e II}JjJ~T Q~IILI'1 I I 1'14 18 I I 15 Sa Sl ACTICN PVTVlle SPP4C.SNVTOOYIN*T.ACNMSNT 4PRQA PrllrMS COMP.COVPCNZNT TAKZN ACTIO"I C:I PLANT.MSTIoOO IIOURS Q22 SUSMOTTSO PCRrPYU0.S JPPIJSrl r oANV P AC'Vr PI PR I!'oQooQ IrrQ rrroo~!"'rrQ LorQ QI0 oJoQrQS CWUSS OKSCRIPTIQr4 aNO CORRGur lve ACTIOr4S Q27 o Both units are now o eratin with a revised F limit and a T.S.chana~ro osal will be formall submitted.

Root cause and addi t action are discussed in the attachment.

CZ3 ACTIVITY CONT 4T~oIZLZASSQ OI RZLSASZ AMQU:ITQP ACTIVITY QSS s~Z Q22~ZQSA NA I 1 IO I I AA PeRSONNZL aXPOSVR4$.4UMSZPI TYP4 OSSCRIPTICN Q>L0000Or rQr~2QIr N 7 S 1'l 11 IS P4RSONNZI, INIL;RIS1~~~QA LCSS QP Col QAMACZ O PACIUTv 2~YPS OZSCRIPTION 9+Z'A2 NA 7 8 1'o PVSLIC: iY:ssveo QSSORI pT:cN GS)~NIQ<<NA In As NASZL OR PrlePAIISR N.A.Scho man I a 9 PACILI.Y~2p u TNCQ CP Si*'IUS"i POPISH CTIISH STATUS~QISCQVZHV r00~rQ~IO l1 l1 AA 45 OISCCVAAVOSSCRIPTICN QS2 NSSS notification LCC*TIQN OP RZLZASZ OSS NA ao NRC USK ONI Y 88 58 lo PNONs: 305 552-3802 82.oiono<++

p C,~~'REPORTABLE OCCURRENCE 250-/9-33 LICENSEE EVENT REPORT PAGE T!l0 Additional Cause Descri tion and Corrective Actions: There are two methods which utilize pressure drops for input to SATAN computer.code calculations.

One is a standard technique and the other is used for steam'enerator tube plugging analyses when only the tube plugging input is changed.Since the 22X analvsis involved an updated hot assembly flow area input to SATAN (unrelated to tube plugging), the first method should have been used.However, since the 22K analysis was a"tube plugging" analvsis, the second method was inadvertently used.eolith respect to the 2SX analysis, a value for power in the hot assembly that was input to the SATAN calculation was 3/too low.In order to assure that a similar error will not occur in the future, the following revisions to the NSSS v'endor's procedures are being implemented.

a.Automated cross checks of current input data with those of a previous analysis (or analysis for a similar olant)will be requir ed (while it is now only recommended).

Safeguards Engineering Standards dealing with SATAN pressure drops will be revised to include a cautionary sta tement about the impact of data changes on the methods used.4 c.A standard for steam generator tube plugging analysis will be written.