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 Issue dateTitleTopic
ML20086G3716 October 1975Environ RO 75-21:on 750926,all Cooling Towers Removed from Svc.Caused by High Mud Content in River Water.Cooling Towers Returned to Svc After Mud Content Decreased
ML20086G37426 September 1975Environ RO 75-19:on 750916,cooling Tower C Inoperable.Caused by Failure of Wooden Distribution Header.Leak Repaired & Tower Returned to Svc
ML20086G40924 September 1975Environ RO 75-18:on 750914,second Fan on Cooling Tower C Failed.Cause Under Investigation.Fan Returned to Svc W/O Excessive Vibration
ML20086G41210 September 1975Environ RO 75-17:on 750831,significant Leak on Cooling Tower a Lift Pump Packing Gland Required Removal of Pump from Svc. Caused by Failure of Supports for Lift Pump Lower Guide Bearing.Corrective Action to Be Determine After DismantlingPacking leak
ML20086G4158 September 1975Environ RO 75-16:on 750829,cooling Tower B Lift Pump Tripped.Caused by Plugging of Lubricating Water to Pump Shaft.Lift Pump Lubricating Water Filter & Flow Switch Cleaned & Returned to Svc
ML20086G41625 July 1975Environ RO 75-13:on 750716,two Cooling Towers Simultaneously Inoperative.Caused by Setpoint Drift in Flow Switch of Lift Pump Lube Water Supply Line.Faulty Vibration Switch Replaced & Fan Restarted
ML20086H91127 June 1975Environ RO 75-12:on 750619,second Cooling Tower Removed from Svc within Allowable 48 H Maint Period.Caused by Failure of Banding Around Distribution Header Which Resulted in Blowout of Portion of Wooden Structure
ML20086H91627 June 1975Environ RO 75-11:on 750618,second Cooling Tower Removed from Svc within Allowable 48 H Maint Period.Caused by Failure of Banding Around Distribution Header Which Resulted in Blowout of Portion of Wooden Structure
ML20086H92123 May 1975Environ RO 75-10:on 750513,second Fan Lost on Cooling Tower B.Caused by Worn Motor Bearings.Bearings on Motor Replaced & Fan Returned to Svc
ML20086H92918 May 1975Environ RO 75-9:on 750508,radioactivity in Critical Pathway Exceeded Design Objective.Caused by Wind Blowing at Lower Elevation in Direction of Facility.No Corrective Actions Required
ML20086H93728 April 1975Environ RO 75-8:on 750416,second Fan Lost on Cooling Tower C.Caused by Worn Motor Bearings.Fan D Drive Train Completed & Returned to Svc.Fan a Motor Removed,Bearing Replaced & Motor Returned to Svc
ML20086H9424 April 1975Environ RO 75-7:on 750327,second Fan Lost on Cooling Tower C.Caused by Several Small Fitting Leaks in Oil Lines.All Leaks Repaired
ML20086H94511 March 1975Environ RO 75-6:on 750301,second Fan Lost on Cooling Tower C.Caused by Motor Bearing Oil Seal Failure.Fan H Motor Replaced
ML20086H9507 March 1975Environ RO 75-5:on 750226,impingement of Fish in Excess of Min Reporting Limit Noted.Caused by Abnormally High River Flow.No Corrective Action Required
ML20086H95923 February 1975Environ RO 75-4:on 750213,excessive Usage of Alum & Sodium Hydroxide Noted,Resulting from Large Demineralizer Water Requirements of Preoperational Flush Program.Mods to Condensate Return Sys Planned
ML20086H96221 February 1975Environ RO 75-3:on 750211,second Fan Lost on Cooling Tower C.Caused by Loosening or Fracture of Mounting Bolts.Fan F Will Be Returned to Svc as Soon as Conditions Permit.Fan D Awaiting New Shaft Bearing Box Prior to Repair
ML20086H9647 February 1975Environ RO 75-2:on 750128,second Fan Lost on Cooling Tower A.Caused by Electrical Motor Failure.Fan Motor Replaced
ML20086K2073 February 1975Environ RO 75-1:on 750124,second Fan Lost on Cooling Tower C & Cooling Tower a Lift Pump Removed from Svc.Caused by High Vibration.Fan Vibration Trips Reset & Fan Operated Satisfactorily
ML20086K21821 November 1974Environ RO 74-C-1:on 741112,instrument Valves Associated w/PS-2-55C & PS-2-55D & Bypass Valves Associated W/Excess Flow Valves 3-2-3-11 & 3-2-33 Found in Improper Positions. Cause Unknown.Investigation in Progress
ML20086K23421 December 1974Environ RO 74-10:on 741211,effluent from Suspended Solids Settling Basin & Sewage Plant Exceeded Environ Tech Spec Limit.Cause Unknown.Sampling Procedure Not Performed So Accurate Determination of Suspended Solids Impossible
ML20086K25520 December 1974Environ RO 74-9:on 741210,effluent from Settling Basin Exceeded Environ Tech Spec Limits.Caused by Gate Between Sections of Settling Basin in Closed Position.Basin Isolated & Cause of High Turbidity Investigated
ML20086K25812 December 1974Environ RO 74-7:on 741202,Units 2 & 3 Operated at 20% Power W/Only One Cooling Tower in Operation.Caused by Failure of Two Straps on Water Distribution Header on Cooling Tower A. Straps Replaced & Cooling Tower Returned to Svc
ML20086K2619 December 1974Environ RO 74-6:on 741129,fan F on Cooling Tower C Failed. Cause Unknown.Motor from Fan F Relocated to Fan C.Work Continuing on Repair Operations on Fan F
ML20086K2808 October 1974Environ RO 74-3:on 740928,oil Noted in Conowingo Pond.Caused by Broken Oil Boom.Underwater Technics Deployed Emergency Oil Booms to Contain Oil Near Shoreline & Pumped Out Entrapped Oil.River Completely Cleaned
ML20086K28115 July 1974Environ RO 74-2:on 740705,cooling Tower Inoperable for Period in Excess of 48 H.Caused by Excessive Vibration. Vibration Readings Taken to Determine Applicability of Present Motors
ML20086K30221 December 1974Environ RO 74-8:on 741211,during Cooling Tower Maint,Only One Cooling Tower in Svc.Caused by Requirement to Perform Preventive Maint.No Corrective Action Necessary
ML20086K30514 November 1974Environ RO 74-5:on 741104,cooling Tower Availability Found Not in Accordance W/Tech Specs.Caused by Pump Suction Bell & Lower Guide Bearing Becoming Detached.Corrective Actions to Be Determined After Investigation
ML20086K30812 November 1974Environ RO 74-4:on 741102,cooling Tower a Removed from Svc for Emergency Maint.Caused by Lower Outboard Section of Screen Plugged W/Pebbles & Debris.Screens Repaired & Reinstalled
ML20086K87711 June 1974Environ RO 74-1:on 740601,oil Noted in Plant Discharge Canal North of Intake Structure.Caused by Separator Receiving 100% Oil & Discharging Total Oil Flow Into Storm Sewer. Oil Booms Deployed
ML20086R51725 July 1995Special Rept:On 950630,determined That Number 12 Cylinder on E-1 D/G Had Lower than Normal Operating Temps During Surveillance Test.Caused by Failure of Fuel Oil Injector Pump.Injector Pump Replaced & Satisfactorily Tested
ML20087H25114 August 1995Special Rept:On 950726,non-valid Failure of E-3 EDG Occurred Due to Dead Spot on E-3 EDG Motor Operated Potentiometer (MOP).E-1 & E-3 EDG Mops Will Be Replaced W/New Type Mop During Future Mod Outages
ML20092M17522 September 1995Special Rept:On 950726,valid Failure of E-3 EDG Occurred Due to Dead Spot on Potentiometer Which Affected E-3 EDG Controller Output signal.E-3 EDG Returned to Operable Status Following Motor Operated Potentiometer Replacement
ML20093F19521 September 1984RO MM-3-03:on 840823,routine Surveillance Testing Indicated Three Moisture Sensors in Recirculation Sys Moisture Monitoring Sys Functioning Improperly.Cause Not Determined. Hourly Monitoring Being Performed
ML20094F44523 July 1984RO MM-3-01:on 840622 & 25,moisture Sensors in Recirculation Sys Moisture Monitoring Sys Functioned Improperly.Cause Unknown.Drywell Sump Collection Sys Monitored Hourly Until Next Outage
ML20096F49014 August 1984RO-MM-3-02:on 840715,surveillance Test Revealed Malfunctioning of Moisture Sensors in Recirculation Sys Moisture Monitoring Sys.Cause Unknown.Hourly Monitoring of Drywell Sump Collection Initiated Until Next Outage
ML20111B47510 May 1996Special Rept:On 960422,vent Stack Wide Range Gas Radiation Monitor Sys Was Removed from Svc for Planned Mod.Field Survey Teams Would Be Dispatched to Monitor Radioactive Effluents as Defined in Plant Emergency Plan
ML20115H01117 July 1996Special Rept:On 960703,main Stack Wide Range Gas Radiation Monitor Sys Removed from Svc for Planned Mod.Sys Expected to Be Returned to Svc by 960830 After Mod Work Completed
ML20115H76817 July 1996Special Rept:On 960603,Unit 2 Vent Stack Wide Range Gas Radiation Monitor Sys Removed from Svc for Planned Mod.Sys Subsequently Returned to Svc on 960701.Mod Replaced
ML20125E3103 January 1980R0 2-80-1/1P:on 800103,drywell Ventilation Isolation Valve Was Fully Open at Time When Valve Should Have Been Limited to 37 Degree Opening.Caused by Lack of Proper Control to Maintain Valve at Less than 37 Degree Opening
ML20126A60311 January 1980RO 2-80-2/1P on 800110:leak Testing on ADS Safety Relief Valve Air Supply Piping Identified Check Valves in Piping Exhibiting Through Leakage in Reverse.Caused by Inappropriate Design.Unit 2 Shut Down for Piping Insp
ML20126B17521 January 1980RO 2-80-3/1P:on 800119,Units 2 & 3 of Offgas Radiation Monitoring Sys Were Determined out-of-svc Due to Low Radiation Monitor Readings.Caused by Plugging of Gas Metering Flow Control Valve at Unit 3 & by Operator Error
ML20126B4235 March 1980Ro:On 800305,during Automatic Switching of Emergency Power Sources,Emergency 480 Volts Power Source Did Not Recover. Cause Under Investigation.Breaker E-334 Manually Closed
ML20126H32023 March 1981RO 2-81-19/1P:on 810320,re-evaluation of Concrete Block Walls Identified Four Walls Which Were Unstable Under Effects of Obe.Caused by Const or Design Error.Addl Restraints Will Be Designed & ImplementedOperating Basis Earthquake
Earthquake
ML20126H3311 April 1981RO 2-81-22/1P:on 810331 During Feed & Bleed Operation, Drywell Chilled Water Closed Cooling Sys Inadvertently Drained to Normal Waste Drain Sys.Release Terminated Upon Discovery.Further Investigation Planned
ML20126H3341 April 1981RO 2-81-23/1P:on 810401,three Drywell Pressure Transmitters Valved Out of Svc During Refueling Outage.Cause Under Investigation.Valves Opened Upon Discovery.Operability of Other Instruments Verified
ML20126L14420 May 1981RO 2-81-32/1P:on 810520,w/units in Shutdown Condition, re-evaluation of Concrete Block Walls Identified Four Walls Unstable Under Effects of Tornado Depressurization & Cardox Injection.Caused by Const or Design Error
ML20147C20811 January 1988Special Rept:On 871216,planned Release of Liquid Radwaste from Laundry Drain Tank B Made W/O Being Treated as Described in Limiting Condition of Operation 3.8.B.4.Caused by Procedural Deficiency.Procedure Revised
ML20147G1533 March 1988Ro:On 880302,both Fire Pumps Became Inoperable When Breaker E-224 for Motor Driven Fire Pump Tripped.Diesel Driven Fire Pump Taken Out of Svc for Maint on 880301.Caused by Failure of Bus E-22 Undervoltage Relay.Temporary Jumpers Installed
ML20153B31016 March 1988Special Rept:On 880302,E-224 440-volt Emergency Load Ctr Supply Breaker Tripped Open,Removing Power Supply for Motor Driven Fire Pump.Caused by Failure of Undervoltage Relay on E-22 Bus.Failed Relay Replaced
ML20153B46816 March 1988Revised Special Rept Re Diesel Driven Fire Pump out-of-svc for More than Tech Spec Limit of 7 Days.On 871111,diesel Driven Fire Pump Declared Inoperable.Probably Caused by Battery Failures.Surveillance Procedure Revised