ML20101J453

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Special Rept 96-01:on 960218,RM-A1 Taken Out of Svc Due to Failure of Detector to Respond to Check Source.Replacement Detector from Stores & Bench Calibrate.Expects to Return RM-A1 to Svc Prior to Restart from Refueling Outage
ML20101J453
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 03/26/1996
From: Hickle B
FLORIDA POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
3F0396-21, 3F396-21, 96-01, 96-1, NUDOCS 9604010436
Download: ML20101J453 (2)


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l Florida Power CORPORATION cw rever una a mum March 26, 1996 3F0396-21 i

I U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D. C. 20555

Subject:

Special Report 96-01 i l

Dear Sir:

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Attached is Special Report 96-01 which is submitted in accordance with the Florida Power Corporation Nuclear Operations Off-Site Dose Calculation Manual, Table 2-3, Action 29.

Should there be any questions, please contact this office.

Sincerely, LL n 82 ke B. J. Hickle, Director Nuclear Plant Operations l BJH/RLM Attachment xc: Regional Administrator, Region II NRR Project Manager Senior Resident Inspector 9604010436 960326 DR ADOCK0500g2 CRYSTAL RIVER ENERGY COMPLEX: 15760 W Power Line St . Crystal River, Florida 34428-6708 . (904) 795-6486 A Florida Progress Company ,

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'9 SPECIAL REPORT 96-01 0FFSITE DOSE CALCULATION MANUAL REQUIRED RADIATION MONITOR UNAVAILABLE FOR GREATER THAN SEVEN DAYS This Special Report provides information concerning the reactor building purge i exhaust high range radiation monitoring instrumentation (RM-A1).

On February 18, 1996, Florida Power Corporation's (FPC) Crystal River Unit 3 (CR- ,

3) was in MODE 4 (H0T SHUTDOWN) at 0% power for a refueling outage. At 1851, RM-Al was taken out of service due to failure of the ietector to respond to the check source. At that time, Offsite Dose Calculation Manual (0DCM) table 2-3 Action #29 was entered which requires instrument restoration to service within seven days or submission of a Special Report within the next thirty days. As of March 26, 1996, the instrument has not been restored to service.

A Special Report outlines the actions taken, the cause of the inoperability, and -

the plans and schedule for restoring the system to OPERABLE status.

Troubleshooting efforts indicate the detector failed to exhibit a linear response to a calibration source. A replacement detector will be obtained from stores and bench calibrated. If this unit is not acceptable, parts will be used to make a ,

uorking detector. It is expected the RM-Al will be restored to service prior to i restart from the refueling outage, currently scheduled for April 17, 1996.

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